|
---|
Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 ML20204H7131999-03-17017 March 1999 Safety Evaluation Concluding That NNECO Provided Adequate Justification for Deviations from RG 1.97,Rev 2, Recommendations,For Instrumentation Monitoring CST Level & Containment Area Radiation at Mnps Unit 2 ML20204C9441999-03-10010 March 1999 Safety Evaluation Denying Licensee Request for License Amend to Revise Frequency of Certain SRs for Electrical Power Sys ML20207L2631999-03-0505 March 1999 Safety Evaluation Supporting Amend 104 to License DPR-21 ML20207L5961999-02-22022 February 1999 Safety Evaluation Concluding That Code Requirements,Which Require 100 Percent Volumetric Exam of RPV flange-to-shell, Impractical to Perform to Extent Required & That Alternative Provide Reasonable Assurance of Structural Integrity ML20203D7601999-02-11011 February 1999 Safety Evaluation Supporting Millstone 1 Certified Fuel Handler Training & Retraining Program ML20196B0501998-11-24024 November 1998 Safety Evaluation Re Licensee 960213 Submittal of 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant,Unit 2 ML20155K1981998-11-0909 November 1998 Safety Evaluation Re Application of leak-before-break Status to Portions of Safety Injection & Shutdown Cooling Sys ML20195B8711998-11-0909 November 1998 Safety Evaluation Approving Revised Evaluation of Primary Cold Leg Piping leak-before-break Analysis for Plant ML20155C3781998-10-30030 October 1998 SER Denying Amend to Allow Changes to Fsar.Nrc Found That NNECO Had Not Considered Diversity Provided by Switch in Control Room That Removes Power to 1 of 2 MOV in SDC Sys Flow Path in Evaluation of High Low Pressure Design ML20155C8441998-10-29029 October 1998 Safety Evaluation Accepting Licensee Proposal to Withdraw ATWS Test Commitment ML20238F2781998-08-27027 August 1998 SER Related to Proposed Rev 20 to Northeast Utilities Quality Assurance Program Topical Rept for Millstone Nuclear Power Station,Units 1,2 & 3 ML20237D5001998-08-20020 August 1998 SER Approving Code Case N-389-1, Alternative Rules for Repairs,Replacements,Or Mods,Section Xi,Div 1 ML20236U7051998-07-22022 July 1998 Safety Evaluation Granting All Requests for Relief W/Exception of Requests RR-89-17 (Authorized for Class 1 Sys Only) & RR-89-21.Requests RR-13 & RR-14 Will Be Addressed in Separate Evaluation ML20236K6971998-07-0101 July 1998 SER Accepting Third 10-year Interval Inservice Insp Program Plan,Rev 2 & Associated Request for Relief & Proposed Alternatives for Plant,Unit 2 ML20236K3531998-07-0101 July 1998 Safety Evaluation Supporting Amend 218 to License DPR-65 ML20249C2541998-06-24024 June 1998 Safety Evaluation Accepting Proposed Rev 19 to NNECO QAP Topical Rept & Amended Through 980609.Informs That NNECO Exception to Provisions in Paragraph 10.3.5 of Constitutes Temporary & Acceptable Alternative ML20248J0031998-06-0404 June 1998 Safety Evaluation Accepting Millstone Nuclear Power Station Emergency Plan ML20248M2991998-06-0202 June 1998 Safety Evaluation Approving Application Re Restructuring of Central Maine Power Co by Establishment of Holding Company ML20248C4131998-05-26026 May 1998 SER of Individual Plant Exam of External Events Submittal on Millstone Nuclear Power Station,Unit 3 ML20217M4181998-04-30030 April 1998 Suppl Safety Evaluation Accepting Licensee RCS Pressure & Heat Removal by Containment Heat Removal Sys post-accident Monitoring Instrumentation ML20216G7921998-03-13013 March 1998 Safety Evaluation Authorizing Proposed Alternative to Check Valve Obturator Movement Requirements of OM-10 for SIL Accumulator Outlet for Listed Check Valves ML20203E8521998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(f) for Performing Required Inservice Testing of Certain Class 2 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E9341998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(g) for Performing Required Exams for Certain Class 1 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E2441998-02-0909 February 1998 Safety Evaluation Accepting Re Approval of Realistic,Median Centered Spectra Generated for Resolution of USI-A-46 ML20198R9941998-01-13013 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Millstone Nuclear Power Station,Unit 3 ML20202H7461997-12-10010 December 1997 Safety Evaluation Accepting Licensee Position That Correction of AC-11 Single Failure Vulnerability Unncessary ML20202J0911997-12-0202 December 1997 Safety Evaluation Accepting Proposed Exemption,Which Meets Special Circumstance Given in 10CFR50.12(a)(2)(ii) ML20198S2411997-10-31031 October 1997 SE Accepting Licensee Request for Deviations from Recommendations in Reg Guide 1.97,Rev 2 for Temp & Flow Monitoring Instrumentation for Cooling Water to ESF Sys Components & Containment Isolation Valve Position ML20212G5991997-10-27027 October 1997 Safety Evaluation Supporting Amend 103 to License DPR-21 ML20217K8801997-10-27027 October 1997 Correction to Safety Evaluation Supporting Amend 103 to License DPR-21.Phrase or Rod Block Protection Has Been Deleted from Listed Sentence in Staff Associated SE ML20212F1381997-10-22022 October 1997 Safety Evaluation Supporting Amend 102 to License DPR-21 ML20217M9301997-08-19019 August 1997 Safety Evaluation Accepting Continued Operation W/O High Startup Rate Trip by Nene for Millstone,Unit 2 ML20149J2661997-07-23023 July 1997 Safety Evaluation Accepting Changes & Reanalyses in ECCS Evaluation Models & Application of Models for Plant,Unit 2 ML20141L8821997-05-28028 May 1997 Safety Evaluation Supporting Amend 101 to License DPR-21 ML20138A0111997-04-23023 April 1997 Safety Evaluation Accepting Licensee Proposal,Not to Perform Type C Leakage Rate Testing on 14 Subject CIVs ML20137V5931997-04-15015 April 1997 Safety Evaluation Supporting Amend 100 to License DPR-21 ML20137U3121997-04-10010 April 1997 Safety Evaluation Supporting Amends 99,206 & 135 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20134A0331997-01-23023 January 1997 Safety Evaluation Accepting Util Proposed Alternatives to ASME Code Requirements ML20133N3401997-01-14014 January 1997 Safety Evaluation Supporting Amend 98 to License DPR-21 ML20135C4221996-12-0202 December 1996 Safety Evaluation Accepting Proposed Alternative Described in Relief Request R-1 Re Valve Inservice Testing Program at Facility ML20128P4381996-10-0909 October 1996 Safety Evaluation Accepting Review of Cracked Weld Operability Calculations & Staff Response to NRC Task Interference Agreement ML20128L7541996-10-0404 October 1996 Safety Evaluation Supporting Amend 97 to License DPR-21 ML20248C5451995-05-0202 May 1995 SER on Millstone Unit 3 Individual Plant Exam of External Events to Identify plant-specific Vulnerabilities,If Any,To Severe Accidents & Rept Results Together W/Any licensee-determined Improvements & C/A to Commission ML20248C5731994-07-19019 July 1994 SER Step 1 Review of Individual Plant Exam of External Fire Events for Millstone Unit 3 ML20059H4991994-01-24024 January 1994 Safety Evaluation Accepting Revised Responses to IEB-80-04 Re MSLB Reanalysis 1999-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
Text
- , _ _ _ . . . . - - - .- - - - . . . - . . .-
N &
. a UNITED STATES j Ow) e S NUCLEAR REGULATORY COMMISSION
@/ ..,g f WASHINGTON, D.C. 00565-0001 SAFETY EyalHATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO.101 i TO FACILITY OPERATING LICENSE NO. DPR-21 NORTHEAST NUCLEAR ENERGY COMPANY MILLSTONE NUCLEAR POWER STATION. UNIT 1 4
DOCKET NO. 50-245 i
1.0 INTRODUCTION
l By letter dated March 6, 1997, the Northeast Nuclear Energy Company (the 4
licensee) submitted a request for changes to the Millstone Nuclear Power Station, Unit 1 Technical Specifications (TS). The requested changes would revise the TS for (1) allowable outage times (A0T) for specified protective
- instrumentation, and (2) reactor building access control.
I
2.0 BACKGROUND
A licensee self-assessment determined that performance of certain 4
surveillances would result in short periods when protective instrumentation is inoperable and the TS require tripping of the initiation logic associated with
! the instrumentation to be tested. To correct this TS wording weakness, the licensee proposed changes to its TS using the NRC guidance provided in Standard TS, NUREG-0123, " Standard Technical Specifications for General Electric Boiling Water Reactors (BWR/5)," Revision 3 (NUREG-0123) and improved Standard TS, NUREG-1433, " Standard Technical Specifications General Electric Plants BWR/4," Revision 1 (NUREG-1433).
i Additionally, other testing and maintenance may result in the secondary d
containment not being in compliance with the TS. The Containment Systems
, Limiting Condition for Operation (LCO) does not specify an A0T for restoration i of secondary containment. Also, no surveillance requirement exists to
, periodically confirm that at least one door in each of the double-doored
- accesses to the secondary containment is closed.
The licensee's proposed amendment is designed to eliminate the above 4
identified weaknesses by adopting appropriate guidelines pertaining to protective instrumentation from NUREG-0123 and NUREG-1433, and reactor i
building access control from NUREG-1433.
3.0 EVALUATION 3.1 Instrumentation Allowable Outage Times i The licensee is proposing to insert "A channel may be placed in an inoperable
, status for up to two hours during periods of required surveillance without placing the Trip System in the tripped condition provided the associated Trip 9706030092 970528 l PDR ADOCK 05000245 P PDR .
i Function [or function) maintains trip capability. Otherwise, ..." in Note 1 of Table 3.1.1, " Reactor Protection System (SCRAM) Instrumentation Requirements;" Table 3.2.1, " Instrumentation that Initiates Primary Containment Isolation Functions;" Table 3.2.2, " Instrumentation that Initiates and Controls the Emergency Core Cooling Systems;" and Table 3.2.3,
" Instrumentation that Initiates Rod Block." This TS change will allow the licensee to perform surveillance tests without placing the applicable trip system in the trtpped condition.
The licensee's current TS are nonstandard and contain weaknesses that were addressed by the staff in the standardized TS (e.g., NUREG-0123 and NUREG-1433). The licensee plans to more completely address these weaknesses in the future by fully converting to the TS recommended in NUREG-1433.
However, the licensee does not plan on submitting this request until 1998. In this case, literal corpliance with the current TS wording would cause the licensee to place protective instrumentation undergoing a surveillance in the tripped condition. However, an instrument in a tripped condition cannot be fully tested. Also, placing the instrument in a tripped condition during a surveillance increases the chance of spurious plant transients (since a false trip signal on the remaining channel will cause a safety system initiation).
The staff determined that the licensee's proposed TS wording is consistent with the applicable portions of NUREG-0123 and is therefore acceptable. The staff also notes that its subsequent guidance (i.e., NUREG-1433) allows a 6-hour time period for conducting these types of surveillances.
Additionally, the licensee is proposing to insert "One air ejector off-gas system radiation monitor may be placed in an inoperable status for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> during periods of required surveillance without placing the Trip System in the tripped condition. Otherwise, from..." in TS 3.2.D.2. The basis for this change is the same as that for the change discussed above.
However, for the instrumentation discussed above, NUREG-0123 recommends a 2-hour A0T for conducting the surveillances and the licensee is requesting a 2-hour A0T. In this case, as noted by the licensee, NUREG-0123 recommends a 1-hour A0T. The licensee provided the following justification for a 2-hour A0T for this instrument:
These radiation monitors are arranged in a two-out-of-two logic; therefore, both must trip to initiate the required action (closure of the off-gas isolation valve to the main stack). This action, however, is automatically delayed by 15 minutes. A high radiation condition sensed by the monitor in service would provide sufficient time to take corrective actions. Since a two-hour A0T is deemed acceptable for instrumentation in systems such as the Reactor Protection System and Emergency Core Cooling System, it is appropriate to apply a two-hour A0T to these radiation monitors.
The licensee also stated that:
Additionally, the NUREG-0123 A0T of one hour does not allow sufficient time to perform required surveillance testing without placing undue stress on the test performer.
l '
l' The staff reviewed the licensee's proposal and agrees that due to the >
15-minute actuation delay, the plant operators will have adequate time to take j
the appropriate action if a real actuation signal occurs. Also, testing the 15-minute actuation delay would by itself take up a significant portion of the 1-hour test period recommended in NUREG-0123. Additionally, the 2-hour period is consistent with the testing period allowed for the other instrumentation A0Ts in the licensee's request. Therefore, the licensee's proposal to deviate from the recommendation in NUREG-0123 and instead allow a 2-hour period to l conduct the surveillance test is acceptable. '
The licensee also proposed to substitute "shall" for "may" in existing Note 1
- of TS Table 3.2.2. Currently, the note reads "If the first column cannot be 1 met for one of the trip systems, that system may be tripped." The use of the
, word "shall" instead of "may" makes it clear _to the operators that this action t
is a requirement and not an option. Therefore, the licensee's proposed wording revision for Note 1 of TS Table 3.2.2 is an acceptable TS clarification.
4 Additionally, the licensee made changes to the TS Bases to reflect the above
- TS changes.
3.2 Secondary Containment Integrity
- The licensee is proposing to change the required corrective action if the TS's containment integrity requirements cannot be met. Specifically, paragraph j 3.7.C.2. will be changed as follows:
Current wording:
If the above [i.e., the 3.7.C.1 operability requirements] cannot j be met, immediately suspend the activities listed in 3.7.C.I.a and 3.7.C.1.b and establish, within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, conditions where secondary containment integrity is not required [e.g., cold l shutdown].
Proposed wording:
} If the above [again, the 3.7.C.1 operability requirements] cannot l be met:
4
, a. immediately suspend the activities listed in 3.7.C.I.a and 3.7.C l.b; and 1
l b. when in RUN, STARTUP/H0T STANDBY, or H0T SHUTDOWN, restore i secondary containment to OPERABLE status within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> or establish, within the succeeding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, conditions where secondary containment integrity is not required (e.g., cold shutdown].
i The licensee's proposed wording clarification is consistent with the intent of the current wording with the exception that the licensee's proposal would add a 4-hour time period to allow plant operators to restore secondary containment to operable status if it is found inoperable while the plant is in run, 4
4
s startup/ hot standby, or hot shutdown. Although the licensee's proposed i 4
wording differs from the current TS, the licensee's proposal is consistent ,
with the staff's applicable TS wording in NUREG-1433. The NUREG-1433 l justification for this 4-hour time period is- !
~
The 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> Completion Time provides for a period of time to correct the problem that is commensurate with the importance of maintaining secondary containment during [run, startup/ hot standby, or hot shutdown). This time period also ensures that the probability of an accident (requiring secondary containment operability) occurring during periods where secondary containment is inoperable is minimal.
Since the licensee's proposed wording is consistent with the NUREG-1433 guidance, it is acceptable.
The licensee also proposed to add a new secondary containment . surveillance
- requirement, that would read:
- b. At least once a month, verify at least one door in each j secondary containment access opening is closed.
4 i
This proposed surveillance requirement is a new requirement that would help ensure that infiltration of outside air of such a magnitude as to prevent
- maintaining the desired negative pressure does not occur. The licensee's I j proposed surveillance requirement wording is less restrictive than the staff's recommending wording in NUREG-1433 which requires, in part, that "all" i secondary containment equipment hatches and access doors be verified closed.
However, the licensee's proposal is acceptable because: (1) it is consistent with the current plant design basis as noted in the TS definition of secondary
- containment integrity (which states, in part, "At least one door in each access opening is closed."), and (2) it is a conservative improvement over the
- current TS surveillance requirement which only requires a test once per operating cycle and prior to fuel movement (the licensee's proposed monthly testing frequency is consistent with the 31-day testing frequency recommended in NUREG-1433).
Additionally, the licensee made changes to the TS Bases to reflect the above TS changes.
4.0 STATE CONSULTATION
. In accordance with the Commission's regulations, the Connecticut State official was notified of the proposed issuance of the amendment. The State official had no comments.
t
5.0 ENVIRONMENTAL CONSIDERATION
The amendment changes a requirement with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20 and changes surveillance requirements. The NRC staff has determined
- i. that the amendment involves no significant increase in the amounts, and no l significant change in the types, of any effluents that may be released
? $
- l offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a i
proposed finding that the amendment involves no significant hazards i consideration, and there has been no public comment on such finding (62 FR 14462 dated March 26,1997). Accordingly, the amendment meets the l eligibility criteria for categorical exclusion set forth in 10 CFR '
51.22(c)(9). Pursuant to 10 CFR 51.22(b) no environmental impact statement or
- environmental assessment need be prepared in connection with the issuance of i the amendment.
6.0 CONCLUSION
The Commission has concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amendment will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributor: S. Dembek Date: May 28, 1997
,