ML20141K786
ML20141K786 | |
Person / Time | |
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Site: | Pilgrim |
Issue date: | 05/22/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20141K783 | List: |
References | |
50-293-97-02, 50-293-97-2, NUDOCS 9705300012 | |
Download: ML20141K786 (50) | |
See also: IR 05000293/1997002
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ENCLOSURE 2 4
U.S. NUCLEAR REGULATORY COMMISSION
REGION l
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Docket No.60-293
Licensee No. DPR-35
Report No. 97-02
i Licensee: Boston Edison Company
800 Boylston Street
Boston, Massachusetts 02199
Facility: Pilgrim Nuclear Power Station i
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I Location: Plymouth, Massachusetts ,
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Dates: March 3 - April 28,1997
. Inspectors: Richard A. Laura, Senior Resident inspector
l .Beth E. Korona, Resident inspector-
Suresh Chaudhary, DRS Engineering Inspector ,
Ed Knutson,-Vermont Yankee Resident inspector .
Patrick Madden, NRR Senior Fire Protection Engineer
l James Noggle,' DRS Radiation Specialist i
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Approved by: Richard Conte, Projects Branch 8
l Division of Reactor Projects
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PDR ADOCK 05000293
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EXECUTIVE SUMMARY )
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Pilgrim Nuclear Power Station I
NRC Inspection Report 50-293/97-02
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This integrated inspection included aspects of licensee operations, engineering,
maintenance, and plant support. The report covers resident inspection for the period of
March 3 through April 28,1997. In addition, it includes the results of announced
inspections by regional radiation and inservice inspection specialists.
Ooerations:
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Operator performed RFO11 activities wellincluding the oversight of the vendor fuel
handlers during core reload activities. The management decision to confirm the integrity of
the used fuel bundles during in-pool gas sipping activities directly led to the identification !
of a second leaking fuel pin. Two of the three longstanding operator work arounds that '
came into effect during the shutdown into RF011 were corrected. Operations training
personnel performed a detailed and insightful review of operator performance during the
previous reactor scram due to malfunctioning feedwater system regulating valves. (Section
01.1) ;
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Two minor equipment deficiencies were identified during control room panel walkdowns
which were discussed with members of the operating crew. Also, an operations tagging i
problem was evident when a worker was observed to be conducting maintenance on a '
pressurized valve when an isolation valve was 1 to 2 turns open from the full closed
position. (Section 01.1) ]
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Operators responded well to the main transformer failure on March 7. Good command-
and-control resulted in restoration of augmented fuel pool cooling with a very small rise in
spent fuel pool temperature and careful transferral of plant loads to the startup '
transformer. (Section 01.2)
Operators responded well to the unusual event due to the complete loss of offsite power
on April 1. Effective command-and-control was demonstrated by appropriate declaration of
an Unusual Event, entrance into EOP-4, and presence of the emergency director in the
control room. The decision to remain in the Unusual Event (UE) after the 23 KV line was
restored, pending restoration of the 345 KV lines and stability in the lines, showed a ,
prepared approach. Operators closely followed appropriate procedures to restore l
temporary power to non-safety related equipment to exit EOP-4 and restore fuel pool I
cooling. (Section 01.3) i
Although operators were aware of the loss of auxiliary power to the SBO diesel after the
main transformer failure, actions were not timely enough to prevent loss of the SBO diesel
evailability. This resulted from an inadequate procedure and ineffective interface with the
system engineer. (Section 02.1)
The readiness for restart meeting effectively reviewed numerous issues prior to restart.
Operators performed start-up and power ascension activities in a professional and
controlled manner with due regard for nucloar safety. A few minor deficiencies were
identified by the NRC during the final drywell close-out inspection performed with reactor
pressure at 1000 psig. Two equipment / system degraded conditions (URI 97-02-01)
involving the degraded operation of control rods and feedwater system regulating valves
impacted operational activities during start-up and power ascension from RF011. Strong
operator command-and-control was evident during the turbine overspeed testing. Four
attempts were needed to re-synchronize the generator back onto the electrical grid due to
an operator training weakness. (Section 04.1)
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Maintenance:
Pre-evolutionary briefs for observed tests were thorough and stressed procedure
adherence, proper chain-of-command and self-checking. Operations management was '
often present to provide oversight and stress the importance of several of the tests
performed. The questioning attitude of an operator during an ECCS load sequencing with
loss of offsite power test prompted better preparation for the test and further review of the
procedure for improvement. Degraded reactor pressure vessel flange temperature elements
delayed the reactor pressure vessel leakage test and required a temporary modification to 1
be installed prior to startup. Portions of the test were reran when a recorder was not
turned on. (Section M1.1)
The BECo response to a fire in the "B" RFP motor was timely and effective. Short term +
corrective actions were thorough and addressed the apparent cause (degraded motor
heaters) for all three RFPs. Existing preventive maintenance on safety related pump motors
provides reasonable assurance that these motors are not susceptible to similar failure.
(Section M2.1)
Efforts to transport, install, modify and ultimately energize the new main transformer,
following the failure of the original transformer on March 7, reflected good overall control
by the maintenance and engineering staffs. Careful transportation, appropriate electrical
calculation revisions, and required modifications to associated equipment were verified
which led to successful energization on April 21. (Section M2.2)
A brief loss of shutdown cooling (LER 97-006) resulted from inadequate procedure 2.2.14.
BECo corrective actions were appropriate to the circumstances. (Section M3.1)
The new vessel stud tensioners worked smoothly with no problems during vessel
reassembly. This resulted in less manual effort required by the refuel crew workers and
a!so less radiation exposure due to the efficiency of the new tensioners. Damage to all
four main steam line plugs occurred with a resultant loose part falling into the vessel due to
an inadequate vessel reassembly procedure. The procedural inadequacy resulted from an
over-reliance on verbal vendor information based on experiences at other BWRs rather than
a detailed technical review of design drawings to confirm the proper clearances between
the steam separator and the plugs. However, a proper safety perspective was evident by
removing the separator and retrieving the loose part. An RFO11 lessons learned review
was planned to develop what worked well and areas for improvement. (Section M6.1)
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I Enaineerina:
The unexpected automatic isolation of the 480/120 V regulating transformers resulted from
brief and severe undervoltage transients during a winter storm. The reason the isolations
were unexpected was that the design documentation did not specify the isolation function
of the transformers on under/overvoltage. This failure to maintain adequate design control
is the first example of a violation of 10 CFR Part 50 Appendix B, Criterion Ill, Design
Control (VIO 97-02-02). (Section E2.1)
Inadequate electrical configuration involving MO-1301-53 resulted in an unnecessary
challenge to the RCIC system turbine and increased safety system unavailability time. The
overall RCIC unavailability time still remained very low. This failure to maintain adequate
design control is the second example of a violation of 10 CFR Part 50, Appendix B,
Criterion lil, Design Control (VIO 97-02-02). (Section E2.2)
Five REM of additional radiation exposure was used to rework several of the ECCS suction
l strainer slip joints that were misaligned. A preliminary review determined the likely cause
l involved a weakr ess in the templating and fabrication process. Although engineering ,
i personnel identified the misalignment by watching a videotape, the engineering design l
documents did not highlight the critical nature of the slip joint clearances. As a result, the
l project implementation staff assumed the clearances were for construction fit-up; and, o
also, vendor QA personnel did not have a specific hold point inspection requirement. The I
design engineer and BECo OA personnel did not review the vendor inspection plan.
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(Section E3.1) i
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Ultrasonic examinations performed during RFO11 as part of the core shroud inspection plan
revealed no reportable indications of V-17 and V-18 vertical welds. Engineering and
quality assurance personnel promptly evaluated industry experience on core shroud issues
that were documented in NRC information Notice 97-17. (Section E7.1)
Based on the above observation, review of documentation, and discussion with personnel
responsible for ISl program implementation, the inspector concluded that the licensee's ISI
program plan, with relief requests, is approved by the NRC, and is satisfactorily maintained
in an updated condition. The NDE personnel are properly qualified / certified, and
inspections / examinations are adequately performed and documented. Jet pump
nonconforming issues did not affect immediate operability but the final corrective actions
were not planned and remain as an inspector follow item IFl 97-02-03. (Section E8.1)
Plant Succort:
RP control points were well staffed and functioned very well in providing the radiological
l protection requirements of the workers. Some drywell posting and industrial safety
l concerns were noted and corrected by the licensee. (Section R1.1)
Effective air sampling was provided in the work areas, and proper procedures were
followed in determining internal exposures. The control of contamination and limiting
internal exposures through the use of respiratory protection during RFO11 was very
effective. (Section R1.2)
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Chemical decontamination of the recirculation piping system effectively mitigated the four-
fold increase in drywell dose rates experienced this outage, however, due to an unforeseen
interference and vendor equipment limitation, the decontamination effects were limited, l
- with drywell dose rates remaining generally higher than previous refueling outage values. I
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(Section R1.3)
l Facility modifications involving RCA access and RCA tool control were recently streamlined
l and greatly enlarged. These modifications effectively increased the worker's interface with
i RP personnel and provided an increased supply of RCA tools to meet the worker's needs.
l These were excellent improvements to the RCA access control program. (Section R2)
Effective RP personnel resource allocation was observed during RFO11. (Section R6)
The recording of radiological occurrences has experienced an approximate six-fold increase j
due to a recently implemented problem reporting threshold. It was too early to assess the l
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results of the newly revised problem report process on correcting and lowering the number ,
of radiological occurrences. (Section R7) I
The emergency plan was implemented as required during the Unusual Event on April 1,
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1997. After the event, an accurate event report was written that reviewed the
organization's response and identified any problems encountered. Appropriate corrective
actions were identified and tracked to resolve the minor _ difficulties encountered. (Section
P1.1)
The existing configuration of radiation monitors on the refuel floor does not satisfy the
requirements of 10 CFR 70.24, " Criticality accident requirements." In addition, BECo has
not conducted evacuation drills as required by this part. BECo committed to come into
compliance with the regulation or receive an exemption prior to receiving, handling, or
l storing any new fuel. The NRC is currently reviewing the problem in light of its
Enforcement Policy. Accordingly, this area is unresolved (URI 97 02-04) pending further -
NRC staff review. (Section P2.1)
Based on the on-site review of the existing plant conditions and fire protection features,
the inspector concluded that the fire protection enhancements should provide reasonable
assurance that if this event or a similar one were to occur, the transformer oil fire hazard
would be controlled and the potential fire effects on safe shutdown and safety related
electrical components would be minimized. The new fire protection enhancements will
provide an additional level of fire safety diversity. (Section F2.1)
The fire hazard analysis did not reflect potential fire loading in the turbine building and
radwaste area commensurate with the oil spill after the main transformer failure because
this was not an anticipated failure mode. The enhancements to install berms in the turbine
building and drain lines on the isophase duct lines will limit the fire loading effect on these
areas should a similar failure occur in the future. The fire hazard analysis report was
updated to reflect these changes before plant startup following RFO11. (Section F3.1)
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TABLE OF CONTENTS
EX EC UTIV E SU M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
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l Sum m a ry of Pla nt St a tu s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . , 1
1. OPERATIONS .................................................. 2
l 01 Cond uct o f O pe ratio ns . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2
l 01.1 General Comments ................................. 2
01.2 Main Transformer Failure While in Backfeed Alignment ....... 3 l
01.3 Unusual Event Due to Complete Loss of Offsite Power . . . . . . . . 5
O2 Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 7 4
O 2.1 Station Blackout Diesel Generator Failure During Loss of 345 I
KVPower........................................ 7 )
04 Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 9 l
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04.1 Plant Restart and Power Ascension . . . . . . . . . . . . . . . . . . . . . . 9 l
08 Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
08.1 (Closed) LER 95-003: Manual Scram Due To Main Gentwor
Stator Cooling Water Temperature Control Valve Feilure . . ... 12
11. MAINTENANCE ............................................... 13
M1 Conduct of Maintenance .......................... ...... 13
M 1.1 General Comments ................................ 13 I
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M2 Maintenance and Material Condition of Facilities and Equipment ..... 14
l M 2.1 Reactor Feedwater Pump Motor Heater Failure . . . . . . . . .... 14
M2.2 Main Transformer Replacement . . . . . . . . . . . . . . . . . . . . . . . . 15
M3 Maintenance Procedures and Documentation . . . . . . . . . . . . . . . . . . . 16
M3.1 (Closed) LER 97-006: Unexpected Shutdown Cooling Isolation
During Troubleshooting ............................. 16
M6 Maintenance Organization and Administration .................. 18
M 6.1 Refueling Floor Maintenance Activities .................. 18
111. E N G I N E E R I N G . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
l E2 Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . 20
E2.1 De-energization of 120 Volt Safeguards Control Power Panels
During Storm .............................. ..... 20
E2.2 RCIC Turbine Overspeed Trip ......................... 21
- E3 Engineering Procedures and Documentation . . . . . . . . . . . . . . . . . . . . 22
E3.1 ECCS Torus Suction Strainer ......................... 22
E7 Quality Assurance in Engineering Activities . . . . . . . . . . . . . . . . . . . . 24
E7.1 Core Shroud Vertical Weld inspection Results ............. 24
E8 Miscellaneous Engineering issues ........................... 24
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E8.1 Inservice inspection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
l E8.2 (Update) URI 94-26-01: Diesel Generator Turbo Assist
i Solenoid Valve Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
I V. PL A NT S U PPO RT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
R1 Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 27
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R1.1. External Exposure Control ........................... 27
l R1.2 Internal Exposure Control . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30
R1.3 As Low As is Reasonably Achievable (ALARA) . . . . . . . . . . . . . 30
R2 Status of RP&C Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . 32
R6 RP&C Organization and Administration ....................... 33 l
- R7 Quality Assurance in RP&C Activities ........................ 33 !
! P1 Condu ct of EP Activitie s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34 l
P1.1 Emergency Plan Implementation During Unusual Event . . . . . . . 34 l
P2 Status of EP Facilities, Equipment, and Resources ............... 35
P2.1 Criticality Accident Requirements . . . . . . . . . . . . . . . . . . . . . . 35
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F2 Status of Fire Protection Facilities and Equipment . . . . . . . . . . . . . . . . 36
L F2.1 Fire Protection Assessment of Main Transformer Failure . . . . . . 36
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F3- Fire Protection Procedures and Documentation . . . . . . . . . . . . . . . . . . 39
l F3.1 Fire Hazard Analysis Review . . . . . . . . . . . . . . . . . . . . . . . . . . 39
V. M AN AG EM ENT M EETI N G S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 40
X1 Exit Meeting Sum m ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 40
X4 Review of UFS AR Commitments . . . . . . . . . . . . . . . . . . . . . . . . . . . . 40
INSPECTION PRO CEDURES USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 41
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lTEMS OPENED, CLOSED, AND UPDATED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 42
LIST OF ACRONYMS USED ......................................... 43
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REPORT DETAILS
Summarv of Plant Status
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i Pilgrim Nuclear Power Station (PNPS) began the period shut down and in refueling outage j
- 11 (RFO11), which commenced on February 15,1997. During the outage, several ,
maintenance activities were completed including refueling of the reactor core, replacement !
of core plate plugs, installation of new, larger emergency core cooling system suction
strainers, and chemical decontamination of portions of recirculation system piping.
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At 14:49 on March 7,1997, while in a backfeed lineup, the main transformer failed.
(Sections 1.01.2 and 1.02.1) At the time, the other source of 345 KV power, the startup
- transformer, was out of service for maintenance. The loss of 345 KV power constituted a
j partial loss of offsite power, causing the automatic start of the "B" emergency diesel
j- generator and reactor building and partial primary containment isolation system Group II
l isolations. An emergency notification (EN 31912) was made to the NRC pursuant to 10
i CFR 50.72(b)(2)(ii). The resident inspector responded to the control room and observed l
- recovery efforts and transfer of the emergency buses to the startup transformer. The !
restoration was completed during early morning hours on March 8. Following this event,
BECo transported a spare transformer from the Millstone Nuclear Generating Station,
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modified and installed it for use at PNPS (Section ll.M1.1).
On March 21, at 13:36, shutdown cooling was lost to the reactor vessel for 24 minutes.
j The loss resulted from troubleshooting activities on a ground in the 125 VDC system
(Section ll.M3.1). Operators reported the loss to the NRC as required by 10 CFR
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j 50.72(b)(2)(ii). (EN 31992)
At 02:57, on April 1, operators declared an UE due to the total loss of offsite power
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(LOOP) (EN 32059) The LOOP occurred during a strong northeastern storm with high
winds and heavy snow accumulations in eastern Massachusetts (Section 1.01.3). A total
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loss of offsite power is defined as the loss of both 345 KV and the 23 KV offsite power
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lines. As a result of the loss of offsite power, a primary containment isolation system
(PCIS) partial Group lil isolation signal resulted in the isolation of shutdown cooling.
. Shutdown cooling was lost for approximately 13 minutes. (EN 32060) The resident
- inspector responded to the site and observed recovery actions. Operators terminated the
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UE at 23:47 that night, after all three offsite power lines were restored. The UE and PCIS
! isolation were reported to the NRC as required by 10 CFR 50.72(a)(1)(i) and 50.72(b)(2)(ii),
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respectively. Both NRC headquarters and Region I emergency response centers entered
the monitoring mode during the UE. NRC emergency response personnel were periodically
briefed on plant status and weather conditions in the Plymouth area by the resident
inspector and BECo personnel, as required.
Operators brought the reactor critical at 19:53 on April 14. Operators placed the unit on-
line through the newly-installed main transformer at 0445 on April 21. Operators
continued to increase power and performed required testing at the appropriate power
levels. On April 28, at 17:00, operators took the reactor to approximately 100 percent
power.
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l On April 17, at 13:15, operators declared the reactor core isciation cooling system (RCIC)
inoperable after it failed to perform as expected during a quarterly surveillance test
(Section Ill.E2.2). Operators entered the required 14 day limiting condition for operation.
Following troubleshooting activities, the RCIC system was declarr,d operable later that day.
The reactor remained at approximately 18 percent power througnout the time RCIC was
inoperable,
l. OPERATIONS
01 Conduct of Operations'
01.1 General Comments (71707)
Using Inspection Procedure 71707, the inspector conducted frequent reviews of ongoing
plant operations. In general, the conduct of operations was professional and safety
conscious. During tours of the control room, the inspectors discussed any observed
alarms with the operators and verified that they were aware of any lit alarms and the
reasons for them. Anomalies noted during tours were discussed with the 905 reactor
operator or the nuclear watch engineer (NWE). The loss of position indication for one
safety relief valve (SRV) and a malfunctioning, reading 400 gallons / minute with no
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operating RHR pump, "A" 1. cop RHR total flow digital indicator were identified by the
! inspector and discussed with members of the crew. The loss of SRV position indication
resulted from a burned-out light bulb and a problem report was initiated to resolve the "A"
RHR total flow indicator deficiency. These two items were isolated in nature but
represented opportunities for more effective operator and management control room panel l
walkdowns. The inspector also witnessed a tagging problem when a condenser bay i
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worker disassembled the #1 valve to LV-3150 (nonsafety related) which was unknowingly
pressurized with air. Discussions with the worker revealed the isolation valve was tagged i
shut but was actually 1 to 2 turns open from the full close position. Problem report l
l 97.1031 was written to document and evaluate this problem. Operations department l
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management later determined that the apparent / direct cause was unknown. Other tagouts
were checked with no other similar problems identified.
in-pool gas sipping during refueling operations identified a second leaking fuel bundle which I
was subsequently reconstituted. The inspector notes that the decision to verify the I
integrity of all reloaded fuel bundles reflected a proper emphasis on nuclear safety.
Reload of the reactor core was completed in a professional manner with effective oversight
of the contracted fuel handlers by BECo senior reactor operators. Major loop swaps of
safety related systems were well controlled. Since the individual operating procedure line-
ups contained both trains, operators had to split out the loops and initiate a problem report
as specified by the conduct of operations procedure. This delayed operators from
completing all reviews prior to restoring systems back to an operable status. All
valve / component line-ups were appropriately completed prior to plant restart.
' Topical headings such as O1, M8, etc., are used in accordance with the NRC standardized
reactor inspection report outline. Individual reports are not expected to address all outline topics.
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l The operator training department completed a detailed review of operator performance
l during the reactor scram that occurred during the shutdown to begin RF011. Progress
l was made prior to restart from RF011 to eliminate 2 of the 3 significant work arounds that
j came into effect during the February 15,1997 post reactor scram period. MO-220-3 was
l replaced with a new and more conventional style valve and CV-1239 (RWCU letdown
- control valve) was repaired by replacing the valve trim and implementing a design change
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to the low and high pressure interlock setpoints to eliminate the need to use the
mechanical blocking device. Corrective actions were planned to resolve the temporary loss
l of the control rod full-in light indication in the near term.
The inspector attended the offsite review committee (NSRAC) meeting held on April 9,
l 1997. At the meeting, various BECo managers made presentations to the NSRAC
l members. The NSRAC members effectively recognized and reminded BECo managers of
! the significance of the loss of the use of the station blackout (SBO) diesel during the
transformer failure event on March 7,1997. The radiation protection department manager
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provided an excellent briefing on the radiological aspects of RFO11 and overall
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performance in this department.
01.2 Main Transformer Failure While in Backfeed Alignment
a. Insoection Scope (71707)
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On March 7 at 14:49, an internal fault caused the isolation of the main transformer. The
inspector observed operator and plant personnel actions in the control room and other site >
locations. The inspector reviewed the report issued by the lessons learned team
established after the transformer failure and periodically discussed aspects of the team's
review with the team leader.
b. Observations and Findinas
On March 7, PNPS was in a refueling outage and the main transformer was supplying 345
KV offsite power to the plant, including the safety related 4160 V buses, through a
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backscuttle arrangement through the auxiliary transformer. The other transformer which
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may be used to supply 345 KV power, the startup transformer, was tagged out of service
for planned maintenance as was the "A" emergency diesel generator (EDG). The
shutdown transformer was powered from the 23 KV offsite power line and also the station
blackout (SBO) diesel generator (DG) remained available as an alternate source of power.
All nuclear fuel had been offloaded and was stored in the spent fuel pool. The spent fuel
pool was cooled by the "A" loop of augmented fuel pool cooling (AFPC) which ties the
l residual heat removal system into the fuel pool cooling system to handle the decay heat
, generated by the offloaded fuel.
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At 14:49 an internal fault caused the isolation of the main transformer. Because the
startup transformer was unavailable to supply power to safety related buses A5 and A6,
the "B" EDG automatically started and loaded onto bus A6, as designed. Because the "A"
EDG was out of service, the shutdown transformer automatically closed onto bus A5 as
expected. A reactor building isolation system (RBIS) and partial primary containment
isolation system Group 2 isolation also occurred, as expected, when power was lost to
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PCIS. As a result of the dead bus when the main transformer was lost, AFPC isolated.
L Operators followed procedure 2.2.85.2, Augmented Fuel Pool Cooling (Without Shutdown I
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Cooling) Mode 2, and retumed the system to service approximately 50 minutes later, with .
an_ insignificant increase in fuel pool temperature of 2 degrees Fahrenheit. The inspector l
l observed effective nuclear operations sur Jsor (NOS) command and control which l
resulted in the retum of AFPC to servD ' p , rocedure and entrance into procedure i
2.4.16, Distribution Alignment Electrico, uystem Malfunctions. Operators followed the l
- steps of Attachment 13, Loss of Power Flow Chart, to maintain / supply power to safety I
L related equipment. BECo personnel quickly identified the need to restore the startup )
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transformer to operation, reviewed the . status of the maintenance which had been )
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performed and worked to clear the associated tagouts in a timely manner.
The intemal fault failed a bushing which allowed approximately 1000 gallons of
transformer oil to gravity drain into the main transformer's rock trap, located outside.
Approximately 4300 gallons of oil also gravity drained through the isophase bus ducting .'
into the turbine building. The inspector observed portions of the cleanup effort and noted )
effective containment actions by personnel immediately after the failure which prevented )
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oil from flowing from the turbine trucklock area outside. Within an hour of the transformer
l failure, the fire brigade was dispatched to the turbine building and remained mobilized in2
l standby until 345 KV power was restored via the startup transformer. Also, an
announcement was made to ban all smoking on site. Sections IV.F2.1 and F3.1 discuss
the transformer oil spill and fire hazard analysis.
, Approximately six hours into the event, operators attempted to start the SBO DG which
l subsequently tripped due to low oil pressure. This topic is discussed in Section 1.02.1. l
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This diesel was not required to supply power during this event since the 23 KV line was
not lost and no adverse weather conditions existed.
Maintenance and operations personnel returned the startup transformer to service at 01:13
on March 8. The inspector observed operators carefully transfer site loads to the
transformer in accordance with procedure, The inspector noted that operators restored the
l non-safety related loads first in order to verify that there were no problems with the
i transformer which could have caused cycling of the emergency buses had they been
j: placed on the transformer first and it tripped. Buses A5 and A6 were transferred to the
i startup transformer at 01:56 and 02:53, respectively. Operators secured the RHR pump in
AFPC prior to the transfer of A6 and restarted it after power was restored. This action
prevented AFPC from automatically isolating on the dead bus as it had when the main
transformer was lost. AFPC was isolated for approximately 25 minutes with no significant a
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spent fuel pool temperature increase. At 03:21 operators secured the "B" EDG, which ran
satisfactorily throughout the event.
A lessons learned team was established after the event. The team discussed the event
with applicable parties; reviewed and identified improvements to procedures, analyses,
interfaces, etc; and entered corrective actions into the plant database to be tracked. The
- team identified several areas for improvement including a review of design modifications
! and compensatory measures for the SBO diesel, enhanced transformer monitoring,
l review / revision of the fire hazards analysis, and installation of emergency lockers at various
v
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.- _. - . _ _ _. ._ .. _ _ _ _ _ _ . . _ __ _ ____ _
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locations. The inspector verified that each action item was assigned a due date, owner,
and a number which will be tracked via existing programs including the problem report
system.
c. Conclusions
Operators responded well to the main transformer failure on March 7. Good command and
control resulted in restoration of augmented fuel pool cooling with a very small rise in
spent fuel pool temperature and careful transferral of plant loads to the startup
transformer,
01.3 Unusual Event Due to Complete Loss of Offsite Power
a. Insoection Scope (93702)
At 03:49 on April 1, the operators declared an UE at PNPS due to the inability to provide I
offsite electrical power to the safety related electrical buses. The inspector responded to
the site to observe operator and plant personnel actions during the unusual event. The
-
inspector also attended the subsequent event critique and reviewed the critique report and
corrective actions initiated. Detail on the emergency response is documented in Section-
IV.P 1.1.
b. Observations and Findinos
The UE occurred ouring a severe Northeastern storm which resulted in the loss of the two l
preferred 345 KV offsite power lines (i.e. the number 342 Canal and 355 Bridgewater),
that had been supplying the station's switchyard and startup transformer, as well as the
23 KV offsite line that had been supplying the shutdown transformer. 345 KV is the
preferred source of offsite power, while the 23 KV line is the secondary source of offsite
power. Prior to the event, the plant was in RFO 11 with the reactor fuel loaded into the
core and the vessel reassembled. Power to plant loads was supplied by the 345 KV
switchyard through the startup transformer. The main transformer, through which 345 KV
power may also be supplied, remained out of service since the March 7 failuce of the old
transformer. The new transformer was onsite but installation was not complete. Core
cooling was supplied by the residual heat removal system in the shutdown cooling mode.
The spent fuel pool cooling system was in service maintaining fuel pool temperature
approximately 82 degrees Fahrenheit.
The 342 line began to receive intermittent isolations at approximately 22:21 on March 31.
At 02:25 operators isolated the 355 line from the switchyard. Operators then started both
EDGs and placed them on their associated emergency buses in anticipation of the potential
loss of the 355 line. At 02:57 the 342 line was lost. Upon the loss of both 345 KV
l sources, and the resultant loss of the startup transformer, the non-safety related buses de-
l
energized which caused the de-energization of the reactor protection system motor-
'
-generator sets and the resultant isolation of shutdown cooling. Operators quickly restored
shutdown cooling within 13 minutes with no discernable increase in temperature.
Operators started the station blackout diesel generator at 03:25 and ran it unloaded in
( accordance with procedure 2.2.146 because power was lost to its auxiliaries when the
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non-safety related buses de-energized. The last offsite power line, 23 KV, was lost at
l
03:39. At 03:49 operators appropriately declared the unusual event in accordance with
emergency action level (EAL) 6.3.2.1, Electrical System Failures, of the PNPS Emergency
Plan due to the inability to immediately provide a source of offsite AC power to buses A5
and A6.
Although the 23 KV line was restored at approximately 06:43, plant management
conservatively decided not to declassify the event until stability could be assured and at
least one 345 KV line was restored. The 355 line was restored and closed into the PNPS
switchyard at 21:44. Both 345 KV lines were returned to service and the safety related
emergency buses were transferred to the startup transformer at 23:39. Operators
subsequently terminated the UE at 23:47.
When the second 345 KV line was lost, a startup transformer lockout alarm was received
in the control room. However, when the relays which actuate the lockout relay were
checked, no flags were observed. Maintenance personnel were contacted and investigated
the cause for the lockout. Until the cause for the lockout was identified, the startup l
'
transformer could not be returned to service, since plant procedures required the cause of
the lockout to be known before the relay was reset. in order to facilitate thorough
troubleshooting of the transformer, it was tagged out of service. An oil sample was taken
to determine whether an internal fault had occurred and a megger was also performed.
Both the megger and oil sample results were satisfactory and showed that the transformer
was not damaged. Following these careful troubleshooting activities, the transfo mer was
returned to service and energized at 23:39. The non-safety related buses were restored
first to ensure that no problems were identified during the restoration which cc,uld damage
the safety related buses. The inspector reviewed the associated alarm response procedure
and discussed the lockout with the emergency director (operations manager) and
determined that the lockout relay is actuated when a differential phase condition, ground
differential condition, or phase overcurrent condition occurs. Through discussion of the -
cause of the lockout with engineering personnel, the inspector learned the cause of the
lockout was believed to be actuation of one or more of the differential trip relays during the
storm.
At 06:02 the control room received RHR and RCIC quadrant leakage alarms. At 06:55 the
inspector observed operators appropriately enter EOP-4, Secondary Containment Control,
because approximately 3 inches of water was found on the floor of the "B" quadrant,
which contains the "B" core spray pump, "B" and "D" RHR pumps, and associated piping
l and components. The entry condition for EOP-4 is one inch or greater of water in any
quadrant. The water was believed to be accumulating from normal building leakage into
the reactor building drain system. Upon the loss of non-safety related buses, the reactor
building sump pumps were also lost therefore the water could not be pumped out of the
building. The de-energization of the non-safety related buses also took fuel pool cooling
(FPC) out of service since they are the power supply for the FPC pumps. BECo had
developed procedures to supply temporary power to the buses associated with these
systems and these procedures were entered in a timely manner. The inspector observed
periodic reports to the control room on quadrant water level and fuel pool temperature.
Power was restored to the fuel pool cooling pumps at approximately 09:30 with a total
heatup of six degrees. Tha rise in temperature was not significant and did not affect the
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safety of the fuel in the fuel pool. At 12:17 power was also restored to the reactor
building sump pumps which were then energized and started, allowing operators to exit
EOP-4 at approximately 14:11. The water level in the "B" quadrant room did not rise
above 4 inches, well below the 21 inches evaluated in PNPS pipe break and flooding
analyses. There was no damage to the emergency pumps as a result of the water on the
floor.
The inspector attended the event critique conducted on April 2 which was attended by
appropriate operations, emergency preparedness, maintenance, engineering and licensing
personnel. The critique was led by the deputy plant manager and thoroughly discussed the
sequence of events, current plant status, and immediate corrective actions. The various
departments communicated well to understand how the plant equipment operated and
,
identify potential problems. The critique report was detailed and covered the information
presented at the critique. The report also listed several areas or events that required
further action. The inspector verified that all corrective actions listed were assigned a due
date and owner. The inspector noted that items were tracked via a PR or other method,
c. Conclusions
Operators responded well to the unusual event due to the complete loss of offsite power
on April 1. Effective command-and-control was demonstrated by appropriate declaration of
an Unusual Event, entrance into EOP-4, and presence of the emergency director in the
control room. The decision to remain in the UE after the 23 KV line was restored, pending
restoration of the 345 KV lines and stability in the lines, showed a prepared approach.
Operators closely followed appropriate procedures to restore temporary power to non-
safety related equipment to exit EOP-4 and restore fuel pool cooling.
O2 Operational Status of Facilities and Equipment
02.1 Station Blackout Diescl Generator Failure During Loss of 345 KV Power
a. Inspection Scoce (71707)
Approximately six hours after the main transformer failure on March 7, the station blackout
diesel failed to run when operators attempted to start it. The inspector discussed the
condition with operators that night, subsequently reviewed applicable procedures and
corrective actions, and discussed the event with the system engineer and operations
personnel,
b. Observations and Findinas
Approximately six hours after the main transformer was lost on March 7, operators
attempted to run the SBO diesel which subsequently tripped due to low oil pressure. The
SBO diesel auxiliaries were powered by non-safety related sources which were lost when
the main transformer failed. The auxiliary systems serve to keep the diesel ready to start
and include the lubricating oil pump and jacket water immersion heaters. Operators
attempted to start the diesel to ensure the auxiliary systems would keep the diesel warm
enough for the diesel to be available if required during the event. Precaution number 7 in
._
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Procedure 2.2.146, Station Blackout Diesel Generator, Revision 13, dated 10/24/95,
,
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stated, "On a loss of off-site power the SBO DG maintenance MCC B40 will not be
powered. During cold weather this could affect the availability... Consideration should be
given to running the SBO DG to power MCC B40." Through subsequent discussion with
the system engineer and NWE, the inspector determined that early in the event the NWE
realized the auxiliaries were lost and contacted the system engineer for guidance on when
to run the diesel to ensure availability. The system engineer recommended running the
diesel when the jacket cooling water temperature decreased to 60 degrees Fahrenheit.
l
Through review of the SBO DG daily surveillance and discussion with engineering
personnel, the inspector determined SBO jacket water temperature is maintained at 80 to
130 degrees.
At 21:04, operators received a low jacket water temperature alarm at which time the
temperature was approximately 76 degrees. At 21:25 operators' attempt to start the
diesel failed when the diesel tripped on low oil pressure. PR 97.9182 was issued for the
diesel failure and the appropriate limiting condition for operation was entered. The SBO
diesel, upon a loss of the 23 KV line, may be used to supply power to the shutdown
transformer and one of the two safety-related buses. The loss of the SBO diesel reduced
the redundancy of power available to the A5 and A6 buses. Although the weather
conditions were not an obvious threat to the offsite line (i.e., winds were calm and no
storm was expected), the potential existed for a loss of all power to the A5 bus. The
inspector determined that procedure 2.2.146 was inadequate in that it did not provide
sufficient guidance on how to maintain the SBO available upon the loss of its auxiliary bus.
BECo took timely corrective actions to revise the procedure via an SRO change such that
the diesel was available throughout the complete loss of offsite power experienced on April
1 as discussed in Section 1.01.3. The SRO change, completed on March 31, added
Section 7.4, Starting and Running the SBO DG at idle, to provide instruction to operators.
Precaution statement 7 was further revised to provide additional guidance on when the
diesel should be run. The revision used the values for starting air pressure and jacket
water temperature which are verified during the daily operator tour. The additional SRO
change added flexibility for the operators to secure the diesel after these values are met to
preclude running the diesel for unnecessary extended periods of time. Procedure 2.4.16
was also revised to direct operation of the SBO when a sequential or partialloss of offsite
power occurs. in addition, the Vice President of Nuclear Operations and Station Director
has committed to modify the plant to supply independent power to the SBO diesel
auxiliaries by the end of March 1998. This licensee identified and corrected violation is
being treated as a Non Cited Vblation, consistent with Section Vll.B.1 of the NRC
l On April 18, the NRC issued Information Notice (IN) 97-21, Availability of Alternate AC
l Power Source Designed for Station Blackout Event to inform licensees of the potential
j unavailability of alternate power supplies during SBO events including the March 7 event at
i PNPS.
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c. Conclusions
Although operators were aware of the loss of auxiliary power to the SBO diesel after the
main transformer failure, actions were not timely enough to prevent loss of the SBO diesel
availability. This resulted due to an inadequate procedure and ineffective interface with the
system engineer.
04 Operator Knowledge and Performance
04.1 Plant Restart and Power Ascension
a. inspection Scoce (71707)
Portions of plant restart and power ascension activities were monitored, including deep
back shift inspection, to observe operations department and overall equipment performance 4
following RF011.
b. Observations and Findinas
On April 10, the inspector attended a day long, readiness for restart meeting conducted in
accordance with Mission Organization & Policy (MOP) procedure D.3.6, Committee
Charters. Prior to the start of the meeting, no written material was specifically available to
the NMC members in preparation for the meeting. The inspector also noted that MOP
D 3.6 provided sparse general guidance including the timeliness of conducting the meeting
relative to restart.
At the meeting, various manager.s made presentations to the nuclear managers committee l
(NMC) on the status of each departments major work completed, work outstanding and-
work deferred from RFO11. The department briefings were detailed and insightful. One
discussion involved the status of scaffolds left erected adjacent to safety related
equipment. The inspector did note small progress in the reduction of longstanding
scaffolds adjacent to safety related equipment. For example, a longstanding scaffold
erected around a sensitive instrument rack located on the 51 foot elevation of the reactor
building was removed. This scaffold was removed because BECo erected a permanent
work platform in the same location. However, significant scaffolds remained erected in the
"A" RHR quadrant room which were intended to be addressed as part of the continuing
plant upgrade process.
Special emphasis was placed on resolution of safety related issues. The engineering staff
briefed the NMC on degradation of the seawater side of the "B" reactor building closed
cooling water (RBCCW) heat exchanger. After a significant storm on April 1,1997, the
l resistance of the seawater side of the "B" heat exchanger significantly increased.
l Operations personnel performed several backwashes but were unable to substantially clear
I
the potential macrofouling. Problem report 97.9261 was generated to document the
problem, evaluate and obtain corrective actions. Engineering personnel generated a new
flowrate versus DP curve that provided more operational flexibility. After the readiness for
restart meeting, the inspector reviewed the performance data for the "B" RBCCW heat
exchanger. The inspector was concerned that the increase in system resistance of the
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seawater side of the "B" RBCCW heat exchanger experienced during the storm was not
initially alleviated by the backwashes. At this point, the inspector considered this a restart
issue even though engineering personnel analyzed that the degradation was acceptable
based on the new operability curve. After further backwashes, the "B" RBCCW heat
exchanger performance improved significantly returning more margin to operability.
Operators brought the reactor critical at 7:53 pm on April 14,1997. The inspector
observed the approach to criticality and plant heat-up. Nuclear instrumentation (i.e., SRMs
& IRMs) performed reliability during the start-up including the overlap period between SRM
and IRMs. The inspector noted that the reliable performance of the SRMs and IRMs
reflected positively on the l&C and engineering staffs. Proper use of procedures was
observed and evidence of operations department management oversight. Operations
support personnel interfaced effectively with members of the operating crew on reactivity
control management. Portions of the reactor core isolation cooling (RCIC) and high
pressure coolant injection (HPCI) testing were observed with no problems identified. One
inadvertent trip of the RCIC turbine resulted from a design control issue further discussed
in the engineering section of this report.
Two significant equipment / system issues emerged during the start-up which adversely .
affected operational activities. Operators experienced great difficulty in the initial
movements (i.e., positions 00-04,04-08) of several control rods, increased drive water
pressure was routinely needed to free the control rods from the full-in position of 00. After
initial rod movement, the control rods generally moved satisfactorily. Two control rods
under a withdrawal signal actually inserted. Also, another control rod moved too rapidly
when withdrawn. The inspector observed proper operator response to each control rod
anomaly. Needle valve adjustments at the hydraulic control unit manifold corrected the
adverse conditions and start-up proceeded.
The inspector interviewed operators and the control rod drive (CRD) system engineer to
determine the cause of the sluggish performance of the initial control rod movement and
the three aforementioned individual control rod problems. The inspector learned that
control rod stroke time testing, not to be confused with control rod scram time testing,
was initially in the outage schedule but was removed from the schedule during the outage.
Stroke time testing per procedure 2.2.87, Control Rod Drive System, Section 7.11, Drive
Speed Adjustment was not performed during RFO10 or RFO11. The stroke time testing
ensures proper needle valve settings and allows for removal of air from the system.
Problem report 97.9279 was initiated to address the sluggish performance of the initial
control rod movement which was assigned as a significant condition requiring a formal root
cause.
A second equipment issue which became an operational impact during start-up and power
ascension involved the feed water system regulating valves (FRVs). At lower power level
with one feed pump in service, large swings of approximately 1.3 million pounds
mass / hour in feed water flow were observed. Actual changes in reactor vessel water level
were minimal. The swings in feed water flow lessened as power was increased to 100%.
Operators responded effectively to the oscillations by immediately informing engineering
personnel and initiating a problem report to obtain corrective action. The inspector
expressed concern that the feed flow oscillations could adversely affect the next significant
11
downpower or shutdown. During the shutdown to enter RFO11, a feed water system
regulating valve malfunction resulted in a manual reactor scram. Plant management again
initiated an interdisciplinary team to solve the feed water control system problems. The I
degraded conditions associated with the FRVs and sluggish control rod movement
constitute an unresolved item (URI 97-02-01) pending further BECo engineering and NRC
review.
The inspector entered the drywell with operations and maintenance personnel for the final
close-out inspection at 1000 psig reactor pressure. A detailed briefing was conducted by
radiological protection (RP) technicians and the use of neutron dosimetry was required.
Four of the drywell-to-torus downcomers were visually examined to confirm no foreign
material existed that could impede water / steam flow during a postulated accident. No
loose fibrous material was observed in the drywell. The inspector identified several minor
deficiencies during the close-out inspection with the most significant involving water
leakage from control rod drive (CRD) 34-03 at a rate of one drop /3 seconds. Closer ;
examination of the source of the leakage by the maintenance department manager
determined the leakage originated from top side of the lower CRD bolted flange and not
from the core vessel stub tube region. Some smallitems such as discarded weld rods,
nuts, bolts, and washers were observed laying loose on the different elevations in the ,
drywell. The inspector determined during the drywell close-out inspection that the
downcomers were free of foreign material, no loose fibrous material existed and some
minor deficiencies were identified. RP personnel provided a thorough briefing prior to the
entry and accompanied the inspection team into the drywell.
Operators synchronized the generator onto the electrical grid for a four hour warm-up
period prior to the start of turbine overspeed testing accomplished by procedure 8.2.1,
Turbine Overspeed Testing. The inspector observed the entire portion of overspeed testing
and re-synchronization of the generator back onto the electrical grid. Two tests of the
back-up overspeed trip and three tests of the emergency governor overspeed were
successfully completed as required. The test results during redundant test were almost
identical and within band. Strengths noticed during the test included strong command-and-
control by the nuclear operating supervisor (NOS) who was qualified and very experienced
as a nuclear watch engineer (NWE). Also contributing to the effective communications
was the effectiveness of the new portable cellular phones which was a significant
improvement. Reactor operators cerformed switch manipulations using effective self
checking techniques throughout the evolutica. There was clear evidence of operations
department, plant and senior management presence in the control room. Operations
personnel interfaced smoothly with the General Electric turbine specialist. Operators
closely monitored turbine vibrations especially on the no. 6 bearing which reached a
maximum reading of 9 mils. The test procedure properly contained clear abort criteria for
high turbine vibrations. Excellent operator performance was observed during the turbine
overspeed testing.
Four attempts by the reactor operator were necessary to synchronize the generator back
onto the electrical grid. After a few attempts, the operator increased the speed of the
synchroscope needle based on advice from the NWE. The inspector interviewed the
operator who explained that he had performed the evolution once before in two attempts.
Operations management and training personnel informed the inspector that the personnel
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l had received specific training on the simulator including synchronization of the generator
onto the grid. The inspector determined that the multiple attempts needed to
resynchronize onto the electrical grid reflected an operator weakness. However, operator
training personnel later informed the inspector of the need for increased training when
synchronizing onto the grid including a detailed review of the out-of-phase block function.
Operators completed power ascension returning the unit back to 100% power without
l incident.
l
c. Conclusions
!
- The readiness for restart meeting effectively reviewed numerous issues prior to restart.
Operators performed start-up and power ascension activities in a professional and
controlled manner with due regard for nuclear safety. A few minor deficiencies were
identified by the NRC during the final drywell close-out inspection performed with reactor
pressure at 1000 psig. Two equipment / system degraded conditions (URI 97-02-01)
i
involving the degraded operation of control rods and feedwater system regulating valves
! impacted operational activities during start-up and power ascension from RFO11. Strong
operator command-and-control was evident during the turbine overspeed testing. Four
attempts were needed to re-synchronize the generator back onto the electrical grid due to
an operator training weakness.
08 Miscellaneous Operations issues (92700, 92901)
l 08.1 (Closed) LER 95-003: Manual Scram Due To Main Generator Stator Cooling Water
Temperature Control Valve Failure
l On March 24,1995, failure of the main generator stator cooling water (SCW) system
temperature control valve resulted in rising temperature on the main generator. Coincident
with immediate SCW system troubleshooting actions, operators reduced reactor power to
l mitigate the condition in preparation for a possible reactor scram. Despite prompt operator
i action to correct the condition, a manual reactor scram was inserted at 60 percent reactor
power, when temperature continued to rise to the point of causing an automatic generator
runback. Details of this event are discussed in inspection report 95-07.
BECo determined that the root cause of this event was failure of a mechanical linkage in
the SCW temperature control valve controller. Specifically, two components of the linkage
(a threaded rod and a nylon connector) separated, which resulted in the controller failing to
the full bypass position. As corrective action, the controller was replaced.
The inspector concluded that the licensee's corrective action was appropriate and that the
failure of the controller could not reasonably have been anticipated because the unit had
only been in service for two years. Based on this review, along with the assessment of
operator response to the event as presented in inspection report 95-07, this LER is closed.
.
i 13
II. MAINTENANCE
M1 Conduct of Maintenance
M1.1 General Comments
a. insoection Scope (61726,62707)
Using inspection procedures 61726 and 62707, the inspector observed portions of
selected maintenance and surveillance activities to verify proper calibration of test
instrumentation, use of approved procedures, performance of the work by qualified
personnel, conformance to limiting conditions for operation, and correct system restoration
following maintenance and/or testing. The following activities were observed:
1
e TP 9730 ECCS Suction Strainer Postwork Testing
e 2.1.8.5 Reactor Vessel Pressurization and Temperature Control for Class 1 System
Leakage Test
- 8.M.3-1 Special Test for Automatic Load Sequencing of Diesels and Shutdown l
Transformer With Simulated Loss of Off-site Power
- 8.2.7 Special Test for Shutdown Transformer Load Test
e 8.5.6.2 Special Test for ADS System Manual Opening of Relief Ja'ves
b. Observations and Findinas
All pre-evolution briefs (PEBs) were thorough and clearly communicated the purpose and
sequencing of testing. Proper self-checking and effective communication were stressed.
The inspector observed knowledgeable operators and maintenance and instrumentation and
controls (l&C) technicians perform activities in accordance with approved procedures.
Prior to performing procedure 8.5.6.2, a communications check and dry run of the
procedure was performed to ensure each participant understood their function and
responsibility. As a result, the test was completed satisfactorily and the safety relief
valves were opened for the shortest amount of time possible.
Per the PNPS inservice inspection program, a complete hydrostatic test of the reactor
pressure vessel was not required this refueling outage, therefore, a Class 1 system leakage
pressure test of the reactor vessel was conducted at approximately 1050 psig. The
inspector observed a PEB for procedure 2.1.8.5 on March 26. The briefing was attended
by appropriate operations, engineering, and quality control personnel as well as the
operations manager. The brief thoroughly discussed chain-of-command and progression
through the procedure. The inspector discussed the visual inspection with the VT-2
certified quality assurance inspectors who performed the inspection. The QA inspectors
were knowledgeable of the test and their responsibilities The inspector specifically
confirmed that the inspectors were aware of their responsibility to check the connection
points of the chemical decontamination equipment in the drywell, used during RFO 11.
! The inspector determined that the required inspection points were well understood by
l BECo personnel. Due to inadequate readings of the vessel flange thermocouples, the
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pressurization test was delayed a few days. PR 97.1487 was issued to document the low
- reading on all flange temperature elements. A temporary modification was installed to
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allow operators to read the actual vessel temperature at the drywell entrance. Prior to
restart, the temporary modification was configured to provide flange temperature in the ;
control room. This modification will remain in place until RFO 12, when new, permanent I
l
temperature elements are planned to be installed. The inspector reviewed the results of
the leak inspection performed on March 29 and determined that the inspections were
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thorough and identified various leaks which were evaluated and corrected as necessary
)
prior to restart.
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Procedures 8.2.7 and 8.M.3-1 were performad together on the evening of April 8. The l
PEB was attended by the operations manager who stressed clear communication and
- taking the time to perform it correctly, asking questions if necessary. The test director
reviewed the reason for the two tests and their sequencing. Operators exhibited a
questioning attitude during the briefing which prompted operations to prepare a tagout to
,
- open main steamline drains when the reactor pressure vessel head vents closed during the
procedure. PR 97.1608 was written to document the need for a review of the procedures q
for completeness. Also, since these two tests are typically performed together, the PR will i
d
- address combining the two into one to reduce the sequencing effort required. The tests
i were generally well performed and effective test control was maintained. Personnel
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stopped the test when discrepancies were noted and systems were returned to their .
normal lineups after test completion.
.
During a review of chart recorder data after the tests were performed, the test director
discovered and the inspector observed that data was missing from the recorder in the
j control room. Temporary chart recorders were installed for the test to provide data on
j diesel loading, breaker closure times, etc. The failure to gather this data required portions
of 8.M.3-1 to be re-performed. PR 97.1802 was written to document this arror.
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c. Conclusions
Pre-evolutionary briefs for observed tests were thorough and stressed procedure
adherence, proper chain-of-command and self checking. Operations management was
often present to provide oversight and stress the importance of several of the tests
performed. The questioning attitude of an operator during an ECCS load sequencing with
loss of offsite power test prompted better preparation for the test and further review of the
procedure for improvement. Degraded reactor pressure vessel flange temperature elements
delayed the reactor pressure vessel leakage test and required a temporary modification to
be installed prior to startup. Portions of the test were reran when a recorder was not
turned on.
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 Reactor Feedwater Pump Motor Heater Failure
a. Insoection Scoce (62703)
The inspector reviewed the circumstances surrounding a small electrical fire that occurred
in the "B" reactor feedwater pump (RFP) motor, including BECo's cause determination and
correctiva actions.
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b. Observations and Findinos
On March 23,1997, an operator observed smoke coming from the "E>" RFP motor. At the '
time, the motor breaker was removed and the main line conductors were grounded for
maintenance protection, so 4160 VAC power was not present at the motor; however, the
240 VAC motor heaters had been energized for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Plant personnel
responded by de-energizing the motor heaters, which eliminated all electrical power from
the motor. The small electrical fire was extinguished using portable chemical and carbon
dioxide fire extinguishers. BECo estimated that the fire lasted two minutes. Subsequent
! ' inspection revealed that the motor heaters had short circuited. Arcing had apparently
ignited residual oil inside the motor casing, and fire then spread to insulation on the motor
main power cables and the sealant used in the floor cable penetration. No emergency
classification (i.e., unusual event) was required. The event was not reportable.
The licensee initiated problem report (PR) 97.9226 to determine the root cause of the
event. Prior to completion of this evaluation, the licensee determined that all RFP motor .)s
I
, heaters should be replaced; this action was completed prior to plant startup. Electrical
( testing of the "B" RFP motor indicated that the motor had not been damaged during the
~m event. - However, given the age of the motor, along with its being contaminated by soot#
and chemical fire extinguishing agent, the licensee concluded that it should be cleaned
The portions of the three main power cables that had been damaged by fire were also
replaced. Sealant in the floor cable penetrations for all three RFPs was replaced with a
flame retardant material. The restored "B" RFP motor was re-installed on April 27.
The inspector questioned whether motors in safety related applications had been examined
as part of the preventive maintenance program for susceptibility to motor heater failure.
Motors for pumps in the emergency core cooling systems (ECCS) had been examined
during 1996 with no similar problems identified, and testing of the motor heaters was a
. part of this examination,
c. Conclusions
The BECo response to a fire in the "B" RFP motor was timely and effective. Short term
corrective actions were thorough and addressed the apparent cause (degraded motor
heaters) for all three RFPs. Existing preventive maintenance on safety related pump motors
provides reasonable assurance that these motors are not susceptible to similar failure.
M2.2 Main Transformer Replacement
a. Insoection Scope (62707) I
Following the main transformer failure on March 7, BECo determined that the old
'
transformer would not be practical to rebuild. Therefore, through a prearranged agreement
with Northeast Utilities, BECo transported a spare transformer from the Millstone Nuclear
Generating Station and installed it at PNPS. The inspectors observed portions of the main
- ransformer transfer, installation, and operation.
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b. Observations and Findinas
.
The transfer and replacement involved extensive time and coordination between the two i
'
sites and between the PNPS engineering and maintenance departments. The inspectors
observed careful transfer of the new transformer from Millstone to Pilgrim. Extensive hold-
down equipment was used to ensure that the transformer would not be separated from the
barge which carried it into the boat launch area at Pilgrim. In addition, modifications were
, made to the boat launch area including temporary improvement of the road to the ramp
4
and construction of a ramp from the barge to the road. The inspector also noted that open
ports of the new transformer were sufficiently covered to protect the internals from
4
weather and foreign materialintrusion.
-
Engineering developed and maintenance implemented design changes to the transformer I
and existing isophase ductwork to allow the new transformer to be installed on the same
pad the old transformer had occupied. The new transformer is larger than the old, rated at j
880 MVA and 784 MVA, respectively. Thereforc, modificaticns were required. The i
inspector discussed the related calculations pe> formed with engineering personnel and l
confirmed that the voltage rating for the two transformers were the same (i.e. high voltage !
- -
- winding rated at 345 KV and low voltage winding rated at 23 KV) and appropriate ..
'
electrical calculations were reviewed and revised as necessary with the specific attributes
of the new transformer.
4
i The isophase ducting was modified to include drains to prevent oil from gravity draining
i into the turbine building upon a transformer failure as it did on March 7. The inspector
l walked down the transformer and verified these modifications were made. No leaks or
other problems were identified during the walkdown. The transformer was post work
a
tested and subsequently succrssfully energized on April 21.
!
C. Conclusions
Efforts to transprat, install, modify and ultimately energize the new main transformer,
'
following the failure of the original transformer on March 7, reflected good overall control
by the maintenance and engineering staffs. Careful transportation, appropriate electrical
- calculation revisions, and required modifications to associated equipment were verified
j which facilitated successful energization on April 21.
d
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,
M3 Maintenance Procedures and Documentation
M3.1 (Closed) LER 97-006: Unexpected Shutdown Cooling isolation During
.
Troubleshooting
i
a. Inspection Scope (62707)
,
During troubleshooting activities on March 21,1997, an unexpected isolation of the
4
shutdown cooling mode of residual heat removal occurred. The inspector discussed the
event with station personnel and reviewed the associated procedure and Licensee Event
Report (LER)97-006, Inadvertent Group 3 Isolation While Troubleshooting a 125 VDC
Ground on the "A" Battery.
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b. Observations and Findinns
On March 21,1997, maintenance personnel used procedure 3.M.1-34, Generic
Troubleshootiag & Maintenance Procedure, to troubleshoot a 125 VDC "A" battery alarm
which had been received in the control room earlier that day. The 3.M.1-34 directed
personnel to cycle breakers on panel D4. Prior to the troubleshooting, the "B" RHR pump
was operating in the shutdown cooling mode. Circuit breaker D4-8 was opened and then
closed per 3.M.1-34. Upon re-closure, motor-operated valve MO-1001-50, shutdown
cooling inboard isolation valve, automatically isolated and the "B" RHR pump tripped as a
result. Operators entered procedure 2.4.25, Loss of Shutdown Cooling, and re-established
shutdown cooling in approximately 24 minutes. No increase in the moderator temperature
of 85 degrees Fahrenheit was observed as a result of the isolation.
LER 97-006 stated the isolation resulted from a " relay race" when the breaker was cycled.
Prior to granting approval for the troubleshooting to commence, the nuclear operating
supervisor (NOS) reviewed the troubleshooting plan and procedure 2.2.14,125 ADC
Battery Systems, for the effects to the plant when opening the proposed breakers. The
inspector verified that the procedure did not mention the potential for the closure of the
1001-50 valve upon closure of the breaker; it only stated that the Group 3 RHR isolation
relays would not function for the 1001-50 valve, to isolate the system when the breaker
was opened. The unanticipated condition was when the breaker was closed, two relays
timed out in a sequence resulting in the closure of valve 1001-50.
The LER stated, and the inspector confirmed, that the isolation occurred because of a
procedure deficiency in which BECo personnel failed to recognize the potential for the
shutdown cooling isolation during this evolution. The purpose of procedure 2.4.45, which
the NOS reviewed prior t; approving the troubleshooting activity, is to provide, "..a
detailed instruction for Operations personnel for operating the 125 VDC Battery System..."
However, this procedure did not state the effect of re-closing this breaker.
Operators responded appropriately to the unexpected isolation and restored the system
within 24 minutes with no adverse effect on moderator temperature. In addition, BECo
stopped the troubleshooting activity and reviewed the troubleshooting plan prior to
recommencing the maintenance to preclude this isolation or a similar occurrence. The
inspector verified at that time that the shutdown cooling isolation outboard valve, which
was susceptible to the same isolation, was not part of the troubleshooting plan and the
D4-8 breaker would not be cycled again. Procedure 2.2.14 was also revised prior to the
resumption of work and incorporated notes for both the inboard and outboard isolation
valves. PR 97.9220 was issued to document the event. A formal root cause evaluation
was assigned to the maintenance department but was not yet completed prior to the end
of this report period. This licensee identified and corrected violation is being treated as a
Non Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy.
c. Conclusions
A brief loss of shutdown cooling (LER 97-006) resulted from inadequate procedure 2.2.14.
BECo corrective actions were appropriate to the circumstances.
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M6 Maintenance Organization and Administration
M6.1 Refueling Floor Maintenance Activities
a. insoection Scooe (36800,62707)
Af ter the completion of in-vessel work during RF011, portions of the reactor reassembly )
process were observed including evaluation of significant problems experienced. During I
l the reactor disassembly process the newer vintage vessel stud nut tensioners failed to
work as documented in NRC inspection report No. 97-01, Section M6.1.
l
b. Observations and Findinas
Reactor vessel reassembly activities progressed well. Some difficulty was experienced )
l
when lowering the moisture separator back into the vessel using procedure 3.M.4-48.3, '
Vessel Reassembly. Members of the refueling crew observed that a main steam line (MSL)
!
plug seal piston actuator shaft broke off and fell down into the vessel. This created an
l adverse foreign material exclusion (FME) condition with a loose part in the vessel. Problem
i report 97.9203 was generated to document, evaluate and correct the condition. BECo
! management directed that the steam separator be removed from the vessel and the loose
part retrieved. Upon closer inspection, all main steam line plugs were physically damaged
- through contact with the moisture separator. The loose part was retrieved from the vessel
and reassembly activities continued. The action to retrieve the loose part rather than
'
perform a loose part evaluatico accepting the adverse condition reflected a proper focus on
safety principles.
The inspector reviewed procedure 3.M.4-48, Section 8.6, installation of Steam Separator,
and interviewed various members of the refueling management team and outage
management to determine the potential cause for the physical contact between the steam l
separator and main steam line plugs. Procedure 3.M.4-48 did not specifically address the '
configuration of the MSL plugs during installation of the steam separator. The event
revealed that the MSL may be installed during steam separator installation but not
pressurized since the actuator shaft sticks out an additional 9 inches for each plug.
Pressurizing the plugs placed the actuator shaft in the travel path of the steam separator
which lowers down into the vessel on guides. The inspector concluded that refueling
procedure 3.M.4-48 was inadequate by not addressing steam separator installation with
MSL plugs installed and pressurized. This licensee identified (through the event) and .
i corrected violation is being treated as a Non-Cited Violation, consistent with Section
'
Vll.B.1 of the NRC Enforcement Policy.
!
At the time of the event, all four MSL plugs were installed and pressurized with air. The
l decision was made prior to the event by outage management and the refueling
management group to leave the MSL plugs installed and pressurized based primarily on j
l input from the MSL plug vendor and also the GE refueling manager. The rationale for
- leaving the MSL plugs installed was to allow continued work on the downstream main
l steam isolation valves (MSIV) in parallel with installation of the vessel internals. The
'
design of the MSL plugs was to provide a watertight seal to allow maintenance on the
MSIVs without pressurization which was only required during the localleak rate test )
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(LLRT). Hence, the decision to leave the plugs pressurized after the LLRT when installing
the vessel internals was intended to avoid any possible plug leakage into the maintenance
area. The actual dimensions and clearances of the MSL plugs verses the vesselinternals
were never technically verified but rather based on vendor input form experiences at other
BWRs. The inspector determined that the over-reliance on verbal vendor information and
the lack of a detailed technical review of PNPS design drawings caused this event and the
aforementioned procedure inadequacy.
After the internals were installed and the reactor vessel head lowered into place, the
reactor vessel head stud nuts were tensioned using the new style tensioners. These
tensioners failed during RFO10 and during disassembly in RFO11. The new tensioners -
l
worked smoothly with no problems experienced. An advantage of the new tensioners was ;
less worker effort to operate the tensioners and less worker radiation exposure due to !
faster tensioner operation. BECo determined that the previous problems experienced with
the new tensioners resulted from the tensioners becoming slightly cocked due to
interference with the curvature of the reactor vessel head. Apparently, when the new i
tensioners were procured for RF010, the dimensions of the reactor vessel head were '
based on drawings and not actual conditions. The slight taper of the head was offset by
the use of a spacer which allowed the tensioners to load properly.
The refueling outage manager informed the inspector of a deteiled lessons learned review
scheduled to be performed. A written report will document the review results including
positive attributes and opportunities to improve. A log book was maintained by the
refueling floor manager with a listing of items for improvement.
c. Conclusions
The new vessel stud tensioners worked smooth 4 with no problems during vessel
reassembly. This resulted in less manual effort required by the refuel crew workers and
also less radiation exposure due to the efficiency of the new tensioners. Damage to all
four main steam line plugs occurred with a resultant loose part fa! ling into the vessel due to
an inadequate vessel reassembly procedure. The procedural inadequacy resulted from an
over-reliance on verbal vendor information based on experiences at other BWRs rather than
a detailed technical review of design drawings to confirm the proper clearances between
the steam separator and the plugs. However, a proper safety focus was evident by
removing the separator and retrieving the loose part. An RFO11 lessons learned review
was planned to develop what worked well and areas for improvement.
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lit. ENGINEERING
E2 Engineering Support of Facilities and Equipment
E2.1 De-energization of 120 Volt Safeguards Control Power Pansis During Storm
a. Insoection Scope (37551,92903)
Prior to the unusual event discussed in Section 1.01.3, the safety-related 120 Volt
safeguards control power buses Y3 and Y4 de-energized while the safety related 4160 V
buses AS and A6 remained energized. The inspector reviewed operator logs and LER 97-
07 and discussed the event with the electrical engineering manager.
i
b. Observations and Findinas
On April 1 at 01:35 safeguards control power buses Y3 and Y4 were de-energized when
regulating voltage transformers X55 and X56 de-energized. Y3 and Y4 supply power to
the normally-energized control logic relays in PCIS and RBIS and pressure switches that .
monitor the header pressure of the salt service water (SSW) system and reactor building l
closed cooling water system (RBCCW). The de-energization resulted in a PCIS Group VI l
isolation (RWCU) and an RBIS isolation signal and resultant automatic start of the standby
gas treatment trains. The SSW pump and RBCCW pumps that were in service at the time
stopped. The Y3 and Y4 panels again de-energized at 0209. Operators took appropriate
corrective actions after both losses and restarted the SSW and RBCCW pumps within 1
minute and reset the Y3 and Y4 buses, RBIS and PCIS, as appropriate.
The loss of povver to panels Y3/Y4 was detectable, operator response actions were l
proceduralized, immediate safety functions were not adversely affected and the panels
were powered in sufficient time to support longer term safety functions. Also, the manual
start function for the affected SSW and RBCCW pumps was not affected.
BECo determined the panels de-energized because their voltage regulating transformers
automatically shut down during short but severe storm-related undervoltage conditions, as
low as 350 V at the regulating transformer. Two other voltage regulating transformers,
X57 and X58, had the same design. X58 supplies part of the power for the "B" train of
the post accident sampling system (PASS) and also shut down during the storm. X59
supplied power to the "A" train of PASS but was tagged out of service for maintenance
when the storm occurred.
All four voltage regulating transformers were installed in 1992 per a design modification
(PDC 91-59A) BECo had not been aware of the isolation feature because the design
specification, E15A, did not require or prohibit an automatic shutdown on voltage
'
transients less than 384 V and greater than 576 V. Further, the design documentation
provided from the manufacturer did not identify the automatic shutdown feature at less
than 384 V. The transformers were designed and tested to regulate input voltages from
384-576 with a specified output. The testing performed on the transformers did not
envelope the low voltages experienced during the storm and therefore did not detect the
. _ _ _ . _ . _. _ . _ _ _ _ . _ _ _ . _ . _ _ _ . _ . _ . _ . _ _ _ _ _ _ . . _ . - _ . . _ . _ . ,
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,
trip setpoints. The human performance aspects of the cause of the deficiency in
j engineering specification EISA is being evaluated per PR 97.9245. Safety evaluation (SE)
I 2664 which accompanied the 1992 design modification did not evaluate the consequences
of an undervoltage transient shutdown of the regulating transformers. PR 97.1658 was ,
generated to document this problem and track associated corrective action. This failure to
maintain adequate design control is the first example of a violation _of 10 CFR Part 50
Appendix B, Criterion Ill, Design Control (VIO 97 02-02).
! In addition, PR 97.1778 was written to document the SSW and RBCCW pump shutdowns.
As stated above, the voltages at the 480 V load centers were estimated at 322 and that at l
the MCCs powered by these load centers would have been less. The SSW and RBCCW - i
pumps are fed from those MCCs and are set to trip at an MCC voltage of approximately I
l 322 V.
l Prior to restart, BECo modified the voltage regulating transformers and disabled the j
l undervoltage and overvoltage shutdown functions, by replacing the microprocessor control
units. When incoming voltage falls outside the design range these transformers will
operate in the unregulated mode.
c. Conclusions
The unexpected automatic isolation of the 480/120 V regulating transformers resulted from
brief and severe undervoltage transients during a winter storm. The reason the isolations
- were unexpected was that the design documentation did not specify the isolation function
of the transformers on under/overvoltage. This failure to maintain adequate design control
is the first example of a violation of 10 CFR Part 50 Appendix B, Criterion ill, Design
Control (VIO 97-02-02).
E2.2 RCIC Turbine Overspeed Trip
1
a. Insoection Scoce (37551.93702)
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During start-up from RFO11, the RCIC system turbine tripped on overspeed during full flow
surveillance testing. The inspector monitored the troubleshooting effort and reviewed the
cause. Problem report 97.9290 was generated to review the event, determine cause and
corrective actions. The requisite 10 CFR 50.72 NRC formal notification was made and a
10 CFR 50.73 report was initiated,
b. Observations and Findinas
Evaluation of RCIC system EPIC computer traces revealed that MO 1301-53, Full Flow
l- Test Valve, went full shut after being jogged briefly in the shut direction from the full open
position. As a result, the RCIC turbine speed control system continuously increased, in an
attempt to establish 400 gallons / minute, that led to the overspeed trip. Prior to RFO11
MO-1301-53 functioned as jog open/ jog close. Electrical maintenance personnel inspected
MO-1301-53 which was wired in the field to function as a jog open/ seal-in close valve.
r. Electrical design drawing MIG 27 depicted MO-1301-53 as jog open/ seal-in close; however,
j' the valve had been previously modified at an indeterminate date to function as jog open/ jog
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l close and design drawing mig 27 was never updated. As part of the corrective actions
2
taken after the turbine trip, FRN 93-38 21 was issued and implemented to reconfigure the
4
breaker assembly so MO 1301-53 functioned as jog open/ jog close. The RCIC system
l turbine subsequently passed full flow testing and was declared operable. Additionally,
i design drawing MIG 27 was modified to reflect the change which included the removal of
j an electrical jumper from terminal board (TB) 4 to TB 14 in the new breaker cubicle D781.
j. The modification made during RFO11 was to address potential degradation of electrical
4
contacts as discussed in NRC Generic Letter 89-10. Problem report 97.9290 was initiated
l which included a review to determine the underlying cause.
!
- ' BECo initiated a review to d' etermine when the potential undocumented modification was
made. Engineering personnel verified the undocumented modification by examining the old
.
4
breaker assembly which was replaced during RF011. The inspector determined that the
,
undocumented modification to the breaker assembly was not reflected in drawing MIG 27 ~
- - and was the second example of a design control violation (VIO 97-02-02) of 10 CFR 50,
l Appendix B, Criterion 111, Design Control. Criterion lli requires that measure shall be
, established to ensure that the function of a component are correctly translated into
- drawings. The inspector noted that this error resulted in an unnecessary challenge to the
l RCIC turbine and also increased RCIC unavailability time. The electrical engineering -
l department manager acknowledged these concerns. A preliminary problem bounding
l review determined that the problem only had the potential to exist in the HPCI system full
j flow test valve; however, a field verification of the same valve in the HPCI system
- identified no problem.
j
c. Conclusions
'
.
'
Inadequate electrical configuration involving the breaker for MO 1301-53 resulted in an
. unnecessary challenge to the RCIC system turbine and increased safety system
l unavailability time. The overall RCIC unavailability timo still remained very :nw.
,
This failure to maintain adequate design control is the second example of a violation of 10
CFR Part 50, Appendix 8, Criterion lil, Design Control (VIO 97-02-02).
E3 Engineering Procedures and Documentation
!..
l E3.1 ECCS Torus Suction Strainer
i
. a. Insoection Scoce (37551)
i
- After successful full flow post modification testing and return to service of the new larger
- ECCS suction strainers, rework of three slip joints was required to restore critical
'
. clearances. The inspector reviewed the issues associated with the slip joint rework which
. resulted in an additional 5 REM of radiation exposure. Installation of the new strainers was
a_ challenge due to the emerging nature of the issue, the need for substantial underwater
4.
work in the torus and general lack of industry experience in completing the task.
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b. Observations and Findinas
Each of the two ECCS suction strainer assemblies installed in the torus underwater had
three suction lines connected for two RHR pumps and 1 CS system pump. Each of the six
total suction lines connected to the strainers incorporated a slip joint design to
accommodate for movement to ensure loads were not adversely transferred to the torus
shell. After completion of physical work and with the strainers turned over to operations
for service, engineering personnel requested an underwater videotape of the slip joint
areas. Three of the six slip joints were found misaligned. The spool pieces had to be
slightly twisted, marked, removed from the water, new bolt flange holes drilled and
reinstalled. A fourth slip joint was also reworked to provide increased clearance margins.
The inspector considered the identification and restoration of the proper slip joint clearance
margins reflected a proper BECo safety perspective.
The inspector interviewed key BECo personnel and paperwork associated with the ECCS
strainer project to determine the cause for the slip joint rawork. A vendor (WSI) was
contracted to fabricate and install the strainer. BECo had not determined the final root
cause but preliminarily determined that the cause involved the templating method used to
fabricate the spool pieces between each strainer assembly and the pump suction lines. A
special tool was used underwater which generally consisted of two angled mating surfaces
connected by two long rods that could be pressurized between the strainer assembly and
pump suction line flange to form a template. BECo believed that the template must have
moved or cocked when pressurized therefore affecting the measurements for the spool
piece fabrication. Alignment pins at each end of the template tool were used in lieu of
bolts. The alignment pins potentially allowed movement of the mating surfaces when
pressurized adversely affecting dimensions for fabrication. At the end of this inspection
period, BECo was interfacing with WSI to substantiate this potential cause.
Several other ancillary issues became evident that may have led to earlier identification of
the slip joint clearance issues. First, the design drawing (C1 A360) for the strainer slip joint
showed centerline-to-centerline fit-up with no notation of the critical nature of the
clearances. As a result, the inspector learned that the BECo project implementation staff
and torus divers assumed that the slip joint clearances was a device to allow construction
fit-up of the spool pieces. Second, the vendor quality assurance (QA) personnel did not
detect the slip joint misalignment primarily because no specific hold point was required and
only remote video camera monitoring was available of the underwater work. Third, the
design engineer and BECo QA did not review the inspection plan prepared by the vendor
QA personnel. BECo QA personnel were more actively involved during the procurement
phase of the strainer parts and the torus drywell close-out process. The inspector
determined that these ancillary weaknesses contributed to the late identification of the
problem. The BECo design engineer, project manager and engineer, and BECo quality
assurance personnel agreed with these lessons learned.
l c. Conclusions
l
Five REM of additional radiation exposure was used to rework several of the ECCS suction
strainer slip joints that were misaligned. A preliminary review determined the likely cause
involved a weakness in the templating and fabrication process. Although engineering
_ __ __ ._ _ _ . _ ._ ._ _._ _ __ _ _.._ ._ _ ._ . . _ _ . _
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personnel identified the misalignment by watching a videotape, the engineering design l
l documents did not highlight the critical nature of the slip joint clearances. As a result, the
!
project implementation staff assumed the clearances were for construction fit-up; and,
also, vendor QA personnel did not have a specific hold point inspection requirement. The
! design engineer and BECo OA personnel did not review the vendor inspection plan.
E7 Quality Assurance in Engineering Activities
E7.1 Core Shroud Vertical Weld Inspection Results
a. Inspection Scoce (37551,92903)
A review of the results of the PNPS core shroud inspection was performed to determine
any obvious applicability of the issues described in NRC Information Notice 97-17,
Cracking of Vertical Core Shroud Welds and Degraded Repair. BECo's core shroud 1
inspection plan was submitted to the NRC along with the ISI Plan submittal for RFO11, i
dated October 30,1996. The plan specified, in part, ultrasonic inspection of accessible
portions of 25% of the equivalent length of all vertical welds (approx.134 inches) from the
vessel internal diameter. Also, a VT-3 examination of one complete tie rod and a VT-1 -
inspection of welds at one gusset plate.
b. Observations and Findinas
During this inspection period in RFO11, BECo inspected, in part, vertical core shroud welds
V-17 and V-18 which were comparable to the same weld locations at NMP1 in the core
beltline region. An equivalent weld length of 138.75 inches was examined. No reportable
indications were recorded during the ultrasonic examinations of the V-17 and V-18 core
shroud vertical welds. Further, inspection of one complete tie rod and gusset plate welds
revealed no notable problems. The inspector interviewed several engineering and quality
assurance personnel and determined that BECo personnel knew of the NMP1 issues and
were closely fo!!owing the developments as well as any potential generic implications.
c. Conclusions
Ultrasonic examinations performed during RFO11 as part of the core shroud inspection plan
revealed no reportable indications of V-17 and V-18 vertical welds. Engineering and
quality assurance personnel promptly evaluated industry experience on core shroud issues
that were identified at NMP1 as documented in NRC Information Notice 97-17, dated April
4,1997.
E8 Miscellaneous Engineering issues
i E8.1 Inservice inspection
a. Inspection Scope (73753. 92903)
,
The objective of this inspection was to determine that the inservice (ISI), repair, and
i replacement of Class 1,2, and 3 pressere retaining components are performed in
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accordance with the Technical Specification (TS), the applicable ASME Code, NRC l
requirements, and industry initiatives, including any relief requests granted by the NRC. ]
l
The scope of the inspection included the review of the licensee's ISI program plan for .l
Pilgrim Station, procedures, qualificatic.n of inspection / examination personnel, schedule of I
planned Isis for the refueling outage 11, and observation of ISI work. I
b. Observations and Findinas
l 1. The Third Ten-Year Interval for the Pilgrim Nuclear Station Inservice inspection
l began on July 1,1995. The licensee developed the ISI plan in accordance with the j
requirements of 10 CFR 50.55(a) and the 1989 Edition of the American Society of l
,
Mechanical Engineers (ASME) Boiler and Pressure Vessel Code, Section XI,
l Subsections IWA, IWB, lWC, LWD, and IWF, for inspection Program B.
I
Accordingly, the inspection plan provided the necessary details of planned ISI for ;
l Code Class 1,2, and 3 pressure retaining components and supports. The j
!
inspection interval is divided into three periods. This is the first period of the third
,
inspection interval.
l l
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The ten-year interval ISI plan was accepted by the NRC by a letter dated March 20, 'l
- 1997, from P. D. Milano of the NRC to E. T. Boulette of the licensee. The relief ;
requests, as appropriate, were properly documented and approved. The relief l
!- requests, PRR-7 and PRR-18, were not required, and PRRs 1,2, and 13 were
withdrawn. The inspector verified that the approvals of PRR by the NRC, and the
withdrawals of PRRs ny the licensee were properly documented in the ISI plan. At
the time of Pilgrim Station's construction, ASME Code only covered nuclear vessel
and piping up to and including the first isolation or check valve. Therefore, piping
and valves at Pilgrim were designed and built to the requirements of USAS B31.1.0-
1967; thus, there are no ASME Section Ill, Class 1,2, or 3 systems at the plant.
The components subject to ISI are depicted on the ISI boundary drawings, and
included in the plan; and the augmented examinations are documented in the
Quality Control Instruction No. 20-48, " Control of Augmented Examination." The
inspector did not have any questions regarding the Pilgrim ISI program plan.
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2. The review of the qualification / certification of the personnel engaged in the NDE of
the ISI program indicated that the inspectors were properly qualified by formal and !
l practical training, and were certified to proper levels of inspection / examination
l responsibility in different examination methods; e.g., Visual examination (VT), Liquid
l Penetrant (PT), Magnetic Particle (MT), or Ultrasonic Examination (UT). The
l licensee has engaged General Electric (GE) for providing all the remote vessel
i internal examination, and GE is also providing almost all working level NDE l
inspectors for the outage ISI work.
L 3. The inspector observed the mockup of the automatic UT machine in the GE lab.
l This machine was used in the UT examination of the safe-end welds in the reactor.
l The inspector also reviewed the video record of the steam dryer leveling screw
} .(Remote VT). This examination was performed by a miniature, remotely operated
<
TV camera. The inspector noted that the video images were of very high quality
i
!
!
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. -. , - ._, . _- . _ _ -
26
with sufficient definition to disclose any defect discernible by VT examination. The
core spray piping weld inside the reactor vessel was also examined by remote
submerged UT equipment, GE CSI-2000, used by GE at the site. The inspector
reviewed the EPRI-BWR VesselInternals Project memorandum evaluating the use of
this equipment.
The inspector also witnessed manual MT examinations of the weld, Nos.1303 and
1304, on the main steam line inside the drywell performed by a Level 11 MT
inspector. The examination was satisfactory, and the NDE inspector was
knowledgeable in MT techniques. The inspector determined that remote VT of
leveling screws, remote UT of core spray piping, and manual MT of weld were
acceptable.
The inspector reviewed the licensee's snubber testing program. The requirements
are set forth in the TS, Section 3.6.1/4.6.1 of the plant TS. The licensee's
procedures provide instructions for snubber examination and testing. Procedure No.
3.M.4-63, " Functional Testing of Mechanical Snubbers," provides instructions for
functional testing of PSA-mechanical snubbers; Procedure No. 3.M.4-37, for
hydraulic snubbers; and Procedure No. 3.M.4-28, for the visual examination and -
service life verification of safety-related snubbers. The inspector reviewed the -
procedures and some completed examinations. The inspector had no concerns in I
this area.
4. Inspection of jet pump swing gates during RFO11 revealed that several swing gates ;
latch pins were not fully engaged and some restrainer bracket set screws were not l
in contact with the jet pump mixer. General Electric performed major jet pump work l
at PNPS approximately 10 years ago. The swing gates provide mid support to the l
jet pump assembly. Two swing gates were replaced but additional lead time was
l
needed to procure additional material. BECo safety evaluation (SE) 3084, based on l
extensive analyses, concluded that the jet pumps remained operable with the non- l
conforming conditions. The inspector noted that SE 3084 did not provide the final
corrective actions planned for the identified nonconforming conditions. No specific i
vendor or NRC generic guidance existed that provided guidance on this in-vessel I
issue. NRC Region I initiated a task interf ace agreement to NRC headquarters to
review the longer term aspects of this issue and potential generic applicability. The
BECo long term corrective action remain as an inspector follow item (IFl 97-02-03).
c. Conclusions
Based on the above observation, review of documentation, and discussion with personnel
responsible for ISI program implementation, the inspector concluded that the licensee's ISI
program plan, with relief requests, is approved by the NRC, and is satisfactorily maintained
in an updated condition. The NDE personnel are properly qualified / certified, and
,
inspections / examinations are adequately performed and documented. Jet pump
l nonconforming issues did not affect immediate operability but the final corrective actions
were not planned and remain as IFl 97-02-03.
l
,
- _ _ - - - -- - - .
l 27
1
E8.2 (Update) URI 94 26-01: Diesel Generator Turbo Assist Solenoid Valve Testing ,
l
a. Insoection Scope (92903)
The inspector reviewed the status of BECo's actions to address the high failure rate of the
diesel generator turbo assist solenoid valves.
l b. Observations, Findinas, and Conclusions
!
On January 24,1994, the "B" emergency diesel generator (EDG) failed to start within the j
maximum allowable time due to simultaneous failure of the two turbo assist solenoid 1
valves. Corrective action consisted of a system modification to allow on-line testing and
l . replacement of these valves, along with an increased test frequency. However, the l
l inspector questioned the adequacy of these actions after additional single-valve failures l
continued to be identified. As a result, the licensee initiated a problem report, PR 96.9413, l
l to examine the issue further. Since the cause of failure was previously identified to be ]
moisture in the air start system, the corrective action strategy shifted to replacing the '
valves with a design that is compatible with this environment. Systems engineering has
recommended use of a valve that is similar in design to the air start solenoid valves, which
have proven to be reliable. Pending review of this modification package, or other final .
j
corrective action, this item remains open. '
IV. PLANT SUPPORT
R1 Radiological Protection and Chemistry (RP&C) Controls
R1.1 External Exposure Control
a. Insoection Scoce (83750)
The inspector made tours of the major radiological work areas during the 1997 refueling
outage and observed work in progress, observed postings and control over work areas, and
made independent radiation surveys in areas for comparison with licensee surveys and for
the evaluation of shielding. In addition, the inspector reviewed licensee surveys and
exposure documentation records and conducted interviews with licensee personnel.
b. Observations and Findinas
The licensee established satellite RP control points to provide focused control over station
areas.
The refueling floor RP control point was established in a clean area located on the refueling
floor. During previous outages, this control point was established one elevation below the
refueling floor due to dose rate considerations. For this refueling outage, a cylindrical
concrete shield was installed around the reactor vessel head while stationed on the
l refueling floor, which provided a 0.5 mR/hr background area for the RP control point. Also
new this outage, the licensee had built and manned a refueling floor observation room
located high above the refueling floor. This observation room was manned by operations
__
28
and outage management personnel and served to coordinate the refueling floor outage
activities. Although this room exhibited a 1.5 mR/hr dose rate and was manned for
extended periods of time resulting in additional refueling exposure, the coordination of
work crews and additional work supervision oversight resulted in improved refueling floor
critical path performance and reduced overall exposures for this area.
The Torus was the focus of considerable work activity during this outage. In order to
address the NRC issue of ECCS strainer plugging, the licensee had designed, fabricated
and was installing new ECCS strainers in the Torus. To reduce dose rates, the licensee
conducted an underwater desludging operation utilizing divers. The inspector reviewed
licensee's surveys of the underwater Torus work areas to determine if adequate survey
detail of the diver's work area had been performed. Initial surveys were performed at the
base of the Torus external shell and licensee calculations determined approximately 1 R/hr
sludge deposits would be encountered by the divers. In addition, inside Torus surveys
were conducted covering approximately one-half of the underwater area at regular
intervals. During diving operations, the diver carried a radiation orobe that provided
continuous readout at the Torus RP control point. The licensec provided extremity
dosimetry and whole body dosimetry for each dive. The licensee indicated that the
dosimetry readings corroborated the survey information. The inspector.also reviewed the.
safety aspects of underwater diving and determined that appropriate designated dive
tenders and dressed-out backup divers were included for each dive. The inspector
observed that a backup air supply was available in the event of loss of station air
compressor supply. Due to radioactive piping systems external to the Torus, the dose
rates to the Torus remained relatively high (10-20 mR/hr). The licensee indicated that the
external radiation sources were too extensive to shield. Due to the high man hours
involved in the Torus modifications, the project was estimated to cost over 100 person-
rem.
The drywell was a focus of considerable attention during this outage. During a September
1996 maintenance outage, the drywell dose rates were found to be approximately four
times normal expected levels. in order to mitigate the effects of the high dose rates on the
Spring 1997 refueling outage, the licensee decided to implement depleted zinc-oxide
injection in December 1996 and perform a recirculation system chemical decontamination
at the beginning of the refueling outage. In addition, a significant amount of drywell work
was deferred until the following refueling outage (e.g., ISI). The inspector made a
comparison of general area dose rates for the two principal work elevations in the drywell.
Sent 1996 Outaae Sorina 1997 Outaae Sprina 1995 Outaae
Drywell entry 200 mR/hr 50 mR/hr 25 mR/hr
1st level up 300 mR/hr 35,65/400 (Recirc suction) 40 mR/hr
As indicated by the comparisons, the work area dose rates were effectively reduced in
most drywell work areas, however, due to the limited success of the chemical
The drywell was not shielded during the September 1996 outage. Both the 1995 and 1997
refueling outage drywell dose rate values include benefits due to shielding.
l
l
29
decontamination, dose rates were elevated compared to the previous Pilgrim refueling l
outage. j
The drywell was posted and controlled as a locked high radiation area, with time keeping l
performed by control point RP personnel. A drywell " rover" RP technician was available
inside the drywell at all times to oversee work activities. During this outage, increased use I
of closed-circuit television surveillance was provided of various work areas at the drywell i
'
control point. The inspector observed good use of the remote surveillance by control point
personnel to assist the rover in conducting effective work coverage. The inspector
observed generally effective radiological briefings to workers, however, due to the
background noise levels and lack of space, the briefings were not always heard by all
members of a work crew greater than two. The inspector observed very limited
radiological postings in the drywell in spite of large dose rate gradients of 30-800 mR/hr.
The inspector observed many areas of the drywell with missing floor grating and in all
cases, they were marked with safety tape warning boundaries. In one large area of the
41-foot elevation on the B-loop side, grating was missing and the area was posted with !
safety tape, however, it was the only passageway through the area and workers were !
observed passing through this area. After this unacceptable personnel safety situation was
reported to the licensee, prompt action was taken by installing planking over the area. Itv
should be noted that missing drywell grating conditions were also reported by the NRC
during the previous refueling outage. I
c. .C_gnclusions
The refueling floor activities were provided with increased oversight from previous outages
through relocating the RP control point onto the refueling floor and with the installation of
an operations supervision observation office that was manned during the outage.
The Torus diving operations were conducted with appropriate safety precautions with
appropriate dosimetry monitoring and adequate surveys conducted. Due to the high dose
rate gradient in water, detailed surveying techniques were warranted and improved
approaches were discussed with licensee personnel. l
The drywell was an area of significant radiological challenge during this outage. A
chemical decontamination of the recirculation piping system was successful, but resulted in
limited success. RP controls were effective in providing a roving RP technician at all times
and through the use of closed-circuit television surveillance of principal work areas.
Radiological briefings were well presented, however, the drywell control point environment
was not conducive for briefings to work crews greater than two individuals. The inspector
observed very few radiological informational postings in the drywell and, due to large dose
rate variations, and limited effectiveness of radiological briefings, the inspector determined
that drywell postings were weak. Removed floor grating continued to be a personnel
safety issue in the drywell and required correction during this outage as it was during the
previous refueling outage.
In general, the RP control points were well staffed and functioned very wellin providing
the radiological protection requirements of the workers. Some drywell posting and
industrial safety concerns were noted and corrected by the licensee.
. . _ _ ~ _ . _ . _ . . _ _ _ _ . _ _ _ . . _ - _ . - _ . _ _ _ _ _ . _ _ . _ .
30
R1.2 Internal Exposure Control
a. Insoection Scoce (83750)
The inspector reviewed all air sample results for the first 26 days of the outage, applicable
air sample-based internal exposure tracking results, bioassay measurement results, and
finalinternal exposure assessment reports. The inspector also interviewed cognizant
licensee personnel.
b. - Observations and Findinas
The inspector determined that approximately 37 air samples were taken per day during the
outage. Generally, air samples indicated less than 20 DAC (derived air concentration).
The exceptions involved machining of a valve and turbine grit blasting activities.' The air
.
sample results'were properly screened for high activity, and all air samples indicating 2.4
DAC were investigated with assigned DAC hour tracking provided for the applicable
- workers. Most of the high air sample activity represented work where respiratory
protection was assigned. There were two cases where workers were calculated to have
w ~. - received 2,4 DAC-hours; once during initial cutting of the LPCI loop selection logic sensing
lines for chemical decontamination injection, and once during the rewelding of the same -
lines following chemical decontamination activities. Initial internal exposure tracking
indicated 3 workers had received 4.3 DAC-hours and two workers had received 5,9 DAC-
hours. The licensee conducted followup whole body counting bioassay measurements that
indicated 4 of these workers had not received any measurable internal exposure. The
other worker was counted on March 5,1997 with an initial positive measurement, and i
was subsequently surveyed when a hot particle was found on the individual, however, a
final bioassay measurement was not performed. According to calculations, there was a
potential of 61 mrem internal exposure to be resolved that had not been appropriately
dispositioned at the time of this inspection.
l
c. Conclusions
The inspector determined that effective air sampling was provided in the work areas, and
that proper procedures were followed in determining internal exposures. The licensee was
-very effective in controlling contamination and limiting internal exposures through the use
of respiratory protection. During the first 26 days of the refueling outage, only five
individuals had initial DAC-hour tracking. Appropriate followup bioassay measurements -
had been performed with the exception of one worker that had not been completely -
dispositioned at the time of this inspection.
R1.3 As Low As is Reasonably Achievable (ALARA)
a. Insoection Scope (83750)
.
j The inspector reviewed the licensee's collective radiation exposure status ard dose
j reduction results for the February-March 1997 refueling outage. This review included
j independent radiation surveys, review of licensee documents, and interviews with the RP
i staff.
-. . - ._ . . . . - . - . . - - - . - - . - . . . - . - _ - - - -.
31 ;
b. Observations and Findinos
l
i
As mentioned in Section R1.1 above, the licensee conducted a chemical decontamination
of the recirculation piping system during the initial period of the refueling outage in order to l
reduce the high radiation fields ir. the drywell. This effort was partially successful. I
Interference precluded the installation of the "A" loop recirculation suction nozzle plug and
prevented decontamination of the "A" recirculation suction piping. In addition, due to a
lack of flow throttling capability on the vendor's decontamination equipment (a single loop
decontamination was not anticipated), the "B" recirculation nozzle plugs (discharge and
suction) became unseated resulting in excessive reactor water inleakage and termination of
the chemical decontamination after only one cycle of nitric permanganate and oxalic acid
washes had been completed (four cycles had been planned). Results were mixed. Very
effective decontamination factors were achieved in some areas with reduction factors
ranging from 10-55. The recirculation discharge risers achieved very good dose rate
reductions for both recirculation loops. The B-loop recirculation discharge ringheader dose
rates increased by 40% and both A & B loop recirculation suction piping increased by more
than double from the pre-chemical decontamination dose rates. The effective chemical
decontamination in some areas combined with doubling of dose rates in other areas,
, resulted in large variations in drywell dose rates. The licensee also provided a good v v.
shielding effort to further reduce some of the higher drywell dose rate areas.
A comparison of refueling outage dose estimates versus actual doses with 2/3 of the
outage completed is provided below.
Original Outage Dose Estimate (1/23/97) Actual Doses Obtained 26 days of 39 days i
Outside Drywell 225.5 person-rem 238.9 person-rem (15.7 emergent work)
3.0 chem decon cost 2.7 chem decon cost
Drywell 117.2 (with scope reduction) 79.4 (with 19.2 emergent work)
17.0 chem decon cost 40.0 chem decon cost
Drywell Total 134.2 119.4
, Planned Work 362.7 326.1
l (contingency 76.2) 34.9 emergent
l OUTAGE TOTAL 439 person-rem 361.0 person-rem
With the outage approximately 2/3 complete, the drywell work scope appears to be on
track, with significant additional dose costs for chemical decon 40 person-rem versus 18.5
person-rem. The licensee's original estimate of 20 person-rem for chemical
decontamination increased to over 40 person-rem. This was due to oversight in the need
for scaffolding to reach the LPCIloop selection logic sensing lines and increased dose rates
after the recirculation system was drained. The refueling activity doses also appear to be
tracking as estimated. Outside drywell work projects to be approximately 50% over the
estimate, with a projected outage exposure of approximately 520 person-rem, which is
- comparable to the licensee's revised outage goal of 510 person-rem. The licensee initially
estimated the high pressure turbine overhaul to cost 35.6 person-rem with much lower
dose rates than expected, this work has cost approximately 1.7 person-rem. Original
j licensee estimates for the torus desludging and ECCS suction strainer modification was 17
4
32
person-rem. More detailed man-hour estimating redefined the estimate to approximately
100 person-rem.
c. Conclusions
Chemical decontamination of the recirculation piping system effectively mitigated the fcur-
fold increase in drywell dose rates experienced this outage, however, due to an unforessen
interference and vendor equipment limitation, the decontamination effects were limited,
with drywell dose rates remaining generally higher than previous refueling outage values.
R2 Status of RP&C Facilities and Equipment
a. Insoection Scope (83750)
The inspector toured the station and discussed several facility modifications with licensee
personnel.
b. Observations and Findinas
During this inspection, the inspector conducted numerous tours of the plant during outage
conditions and noted that all required radiological postings and locked areas met regulatory
requirements. No deficiencies were noted in this area.
In preparation for the outage several notable facility changes have occurred that affect the
RP program. Previously, the control room annex was a non-RCA area located inside the
RCA. Currently, the requirement for work control signoffs has been moved out of the
control room and is now performed on the second floor of the new administration building.
A new passageway was constructed that connects the control room annex with the
second floor of the new wiministration building, which allows personnel access to the
control room annex without entering and exiting through the RCA. In January 1997, the
principal access point for the RCA, the " red line," had been completely reconfigured and
greatly enlarged in order to enhance the flow of personnel through the principal RCA
boundary. An area several times larger has been added with new personnel contamination
monitors and easier access to RP staff behind a large counter area. Also in January 1997,
the contaminated tool depot was enlarged to several times its original size, with a
commensurate increase in tool inventory. Contaminated tools may be returned to the same
facility, which now incorporates a tool decontamination and monitoring area.
During this outage, the inspector observed the above enhanced facilities working very well,
with excellent throughput of workers. Also the new " red line" added a satellite dosimetry
' office to allow resolving dosimetry concerns without leaving the RCA access control point.
Very good accessibility to RP staff was observed and the RCA tool depot appeared to be
well stocked and serviced the workers needs effectively.
!
.
_ _ - .. m - . - . . _ _ _ -. . _ __ _ _ _.~ . __ _ _. _ _- _. __ __ _ _ _ _
__ ,
1
33
c. Conclusions
Facility modifications involving RCA access and RCA tool control were recently streamlined
and greatly enlarged. These modifications effectively increased the worker's interface with
RP personnel provided an increased supply of RCA tools to meet the worker's needs.
These were excellent improvements to the RCA access control program.
R6 RP&C Organization and Administration
l
l a. Inspection Scooe (83750)
The radiation protection organization was reviewed for outage staffing levels based on
documentation review and on observations in the principal work areas during the
performance of outage work activities,
b. Observations and Findinas
The licensee expanded the RP organization to include 80 contractor RP technicians and 7
- RP personnel on loan from other nuclear power plants. including the 25 permanent station
l ,
- RP technicians, there were approximately 120 RP technicians servicing the refueling outage
l needs. Eight permanent station RP supervisors provided responsibility for major plant areas
! with 12 lead technicians tasked with lead responsibilities at specific RP control points. The
j
'
satellite control points included: RCA access point (the red line), condenser bay, turbine
deck, reactor building, drywell, torus, and the refueling floor. The inspector reviewed
ongoing work activities through most of these locations and observed no shortages of RP
coverage during the inspection period.
I c. Conclusions
!
j The licensee applied effective RP personnel resources for the refueling outage.
R7 Quality Assurance in RP&C Activities
a. insoection Scope (83750)
The inspector reviewed the licensee's Radiological Problem Reports for two months of
l' 1997 since major process changes were made to the Problem Report program in January
l 1997. This was based on a review of licensee documentation and interviews with
l cognizant licensee personnel.
b. Observations and Findinas
The inspector observed that the number of Problem Reports written has increased since
January. During 1996 approximately 1300 reports were documented and for the first two
months of 1997 approximately 1300 reports have already been written. The inspector's
- screening of these latest reports indicates that there are not more problems occurring, but
that the threshold for recording discrepancies or recommendations has been lowered. The
inspector noted only three radiological problem reports that appeared to be of safety
4
,
..
l
l
i 34
consequence during the January through early March 1997 time frame. Each of the three
l problem reports was being reviewed be a team of individuals tasked with recommending
corrective actions addressing each of the identified causes. The approach appeared to be
thorough, however, all three problem reports were still open and in various states of review
at the time of this inspection and an assessment of results could not be made at the
.
present time.
l
c. Conclusions
The licensee's corrective action program was revised in January 1997 and since that time
the recording of radiological occurrences has resulted in an approximate six-fold increase.
The threshold for reporting has been lowered with very few radiological events of safety
consequence having been reported. It is currently too early to assess the results of the
newly revised Problem Report process on correcting radiological occurrences.
P1 Conduct of EP Activities
P1.1 Emergency Plan implementation During Unusual Event
a. Insoection Scoce (71750)
BECo declared an UE on April 1 due to the complete loss of offsite power. The details of
this event are discussed in Section 1.01.3 of this report. The inspector observed
emergency plan actions performed in the control room during the event and reviewed
BECo's " Review of events pertaining to UE #97-01, Loss of Offsite Power" report issued
April 7,1997.
b. Observations and Findinas
During the UE, the inspector observed transmission and clear communication of followup
notifications of the event and related information to the state and local officials from
NWE's office in the control room. The inspector observed the notifications did not detract
from operator communication during the event. The emergency director remained in the
control room and fully aware of plant and equipment status throughout the event.
The assessment of the emergency organization's performance during the UE was v
performed in accordance with Emergency Preparedness Implementing Procedure EP-IP-520,
Recovery. The report described the event, identified strengths, difficulties encountered,
and recommended corrective actions. The report was accurate and identified appropriate
areas for improvement with associated action items. No significant problems were
identified,
c. Conclusions
The emergency plan was implemented as required during the Unusual Event on April 1,
1997. After the event, an accurate event report was written that reviewed the
organization's response and identified any problems encountered. Appropriate corrective
actions were identified and tracked to resolve the minor difficulties encountered.
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35
P2 Status of EP Facilitle?, Equipment, and Resources
i
P2.1 Criticality Accident Requirements
1
a. insoection Scoce (71750) i
The inspector reviewed BECo's compliance with 10 CFR 70.24, " Criticality accident
requirements." The inspection included interviews with licensing and engineering
, personnel; and review of the Updated Final Safety Analysis Report (UFSAR), station
!
procedures, related docketed correspondence between BECo and the NRC, and Regulatory
l-
Guide (RG) 8.12, " Criticality Accident Alarm Systems," Revisions 1 and 2.
!
b. Observations and Findinos l
l' In the summer of 1996, the office of Nuclear Reactor Regulation (NRR) requested j
information from licensees regarding their compliance with 10 CFR 70.24. Since PNPS j
was licensed prior to December 6,1974, BECo was subject to sections a(2) and a(3) of the l
rule. Section a(2) specifies preset alarm setpoint limits for the monitoring devices in I
addition to maximum distance from the special nuclear material subject to a criticality .
- accident. Specifically, a(2) requires, "The monitoring devices shall have a preset alarm
'
point of not less than 5 millirem per hour ...nor more than 20 millirem per hour." Section
a(3) specifies, in part, "The licensee shall maintain emergency procedures for each area in
which this licensed special nuclear material is handled, used, or stored ... These procedures
must include the conduct of drills..."
Prior to operation, BECo was exempted from 10 CFR 70.24 under its Materials License
SNM-1193. On December 6,1974, BECo requested the exemption be transferred to their
Operating License DPR-35. By letter dated January 8,1975, the NRC denied the request.
Following this denial, on April 1,1975, BECo requested an exemption from Section al3).
The NRC denied this request by letter dated June 30,1975. Therefore, BECo was subject
to the requirements of 70.24 since the expiration of Materials License SNM-1193,
l
i Through many discussions with BECo personnel and review of related documentation, the
inspector discovered that BECo has gamma radiation-detecting area radiation monitors
(ARMS) located on the refuel floor and in the new fuel storage vault, as required by the
rule. These monitors are listed in UFSAR Section 7.13, Area Radiation Monitoring System.
l -- -The ARMS which are potentially relevant to this rule are 1) new fuel storage area,2) new
l fuel vault,3) refuel floor shield plug area,4) spent fuel pool area. All but the new fuel
vault ARM are located on the refuel floor. The new fuel vault ARM is located inside the
vault and can be accessed by removal of floor plugs on the refuel floor. All ARMS are
calibrated using procedure 6.5-160, Calibration of the Area Radiation Monitoring System.
The inspector verified that the new fuel storage area, shield plug area, and spent fuel pool
area ARMS were calibrated semiannually. However, reviev. of the calibration procedure
and copies of the as-left settings on these monitors revealed that the alarm setpoints are
40 mR/hr and 100 mR/hr, contrary to the requirements of the rule.
4
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!
I l
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36 l
l The new fuel vault monitor has not been calibrated at least since 1990 due to the fact that
l the new fuel vault was not used to store new fuel. The inspector verified that procedure
l 4.2, inspection and Channeling of Nuclear Fuel, contains a prerequisite which requires the
l new fuel vault area radiation monitor calibration to be performed prior to storing new fuel l
l in the vault. Since then, as observed by the inspector this outage, new fuel has been
stored in the spent fuel pool after it is removed from its shipping container on the refuel
floor and inspected. In other recent outages new fuel has been stored in the spent fuel
pool after inspection and the new fuel vault has not been used. During the review of
procedure 6.5-160, the inspector determined that although the intent was to calibrate this
i detector only when needed, both a note in Section 8.0 of the procedure and a note on
Attachment 1, ARM Summary, either allude to special requirements or state that the new
l
fuel storage area detector must be calibrated if the vault is to be used. Both notes were
intended to focus on the fuel vault detector. After the inspector questioned these notes,
BECo initiated a nomenclature change to clarify the procedure and nameplate on the
detectors to correct these oversights. The inspector verified that the detectors were
l calibrated as intended. The inspector determined that the ARM alarm setpoints do not
meet the requirements of 10 CFR 70.24(a)(2).
GECo reviewad the history of criticality accident drills and determined that although >
procedures 5.1.3.5 and later 5.8.1 existed, no such drills have been conducted since
1979, in 1980, Cuality Assurance Audit 80-16 issued deficiency report (DR) 646 for the
failure to conduct refueling floor drills. This DR was inappropriately closed in June 1981,
l based on the fact that procedure 5.1.3.5, which had referenced 70.24, was retired and
superseded by procedure 5.8.1, which did not specifically require a refuel floor drill. BECo
currently has no procedure for criticality evacuation drills, which is also a violation of the
rule,
c. Conclusions
l
The existing configuration of radiation monitors on the refuel floor does not satisfy the
requirements of 10 CFR 70.24, " Criticality accident requirements." In addition, BECo has
not conducted evacuation drills as required by this part. BECo committed to come into
compliance with the regulation or receive an exemption prior to receiving, handling, or
storing any new fuel. This problem has minimal safety consequences. The NRC is
currently reviewing the problem in light of its Enforcement Policy. Accordingly, this area is
unresolved (97-02-04) pending further NRC staff review.
F2 Status of Fire Protection Facilities and Equipment
F2.1 Fire Protection Assessment of Main Transformer Failure
j a. Insoection Scoce (7175_0_1
i
!
On March 71997, PNPS was shut down and in a refueling outage when it experienced a
main transformer fault as described in Section 1.01.2. This fault caused one of the phase
bushings / insulators to fail. Upon its failure, approximately 5,400 gallons of mineral oil
contained in the upper transformer housing leaked out of the bushings and into the bus
duct. The inspector discussed the event with BECo personnel, toured the plant areas
i
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affected by the transformer failure and resulting oil spill, and assessed the adequacy of the
existing plant fire protection features and fire enhancements proposed by BECo against a l
postulated fire using the event conditions. I
b. Observations & Findinas
l
Of the 5,400 gallons of oil which leaked from the transformer bushing, 4,300 gallons )
flowed through the bus duct and into the turbine building via the bus duct air cooler. The
'
oilleaked out of the air cooler through the air intake opening and onto the turbine building
floor. The oil covered the turbine building floor (Elevation 23'- 0") bounded by column-
lines A-15 to A-20 and C.2-15 to C.2-20. Since PNPS is a BWR, the turbine building is
divided by a concrete biological shield wall. This wall separates the low and high pressure
turbine and its condenser from the generator end of the turbine / generator assembly. This
wall also formed the oil spill boundary along the A-15 to C.2-15 column line. The oil in the j
turbine building collected around the hydrogen seal oil unit, under the generator and
exciter, under the generator hydrogen addition control station', the stator winding liquid
cooling unit, the fire protection deluge valves for the transformer fire protection systems,
r the low pressure carbon dioxide (CO2 ) storage unit (used for fire protection and generator
l . purge) and in the equipment / truck bay. The concrete block walls (3-hour fire barrier) along i
j column lines 8-18 to C.2-18, B 18 to B-19, B-19 to C.2-19, and C.2-19 to C.2-20 separate
]
~ the "B" train essential switchgear room from the turbine building. These walls acted as an '
oil spill boundary. Oil did however flow under the double leaf fire door in the fire barrier
walllocated along column line B-18 to B-19 and collected around and inside Motor Control
Centers (MCCs), the exciter control panel, and the neutral ground cubicle. In addition the j
oil flowed down the stairs located near column line A-15. On elevation 6'-0" oil collected ;
in the area of the radwaste monitoring tanks, the treated hold-up tanks, tha corridor
adjacent to these tanks and the room which contains the instrument air compressors.
During power operations, transformer faults such as that experienced at PNPS frequently
result in transformer oil fires. Therefore, if this event had occurred during power
operations there is a high likelihood that the oil would have ignited, resulting in a serious
fire that could have presented significant challenges to the plant and certain essential
functions.
POSTULATED FIRE
l -
' ' Based on the event conditions and the overall combustibility of the oil (mineral oil has a >
flash point 275 F), a postulated fire would develop in a moderate manner with dense
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smoke. The sprinkler protection in the turbine building would actuate to control the upper
hot gas layer in the area of the generator and the hydrogen seal oil unit and the hydrogen
addition station. It is possible that the fire could propagate down the stairs via burning oil
l and involve the radwaste holding tank area and its adjacent corridor on elevation 6'-0".
Under these conditions smoke and hot gases could be transported via the open
,
i
l 'According to the licensee, the hydrogen line is equipped with an excess flow check valve.
l This valve is designed to isolate the gas flow in the line in the event it senses excessive gas flow
conditions such as those created by a piping integrity failure.
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equipment / truck bay to the elevations above the fire affected floor. Due to the plant
configuration, smoke could fill the turbine operating floor and the turbine building roof line.
Power-operated roof ventilators located near the turbine building roof's center line could be
l used to vent some smoke out of the building. In addition, smoke propagation into the "A"
! essential switchgear room is probable. Smoke can enter this room through the ventilation
opening which interfaces with the equipment / truck bay on elevation 37'-O". With respect
l to the "B" switchgear room, it is possible foi a fire to propagate under the door. This fire
c'ould develop a hot gas layer in the upper half of this room sufficient to transfer heat to
'
the cables in the cable trays near the ceiling. The increasing temperature of the hot gas
layer could result in ignition of the cables and fire propagation along these cables in the
cable trays located near the ceiling. Under such conditions, it is probable that the
switchgear room could burnout.
The rolling equipment / truck fire door is normally closed. If it were opened by either fire
brigade or operations personnel, burning oil could flow out of the turbine building and down
the roadway leading to the equipment / truck bay.
EXISTING PLANT FIRE PROTECTION FEATURES
An automatic pre-action sprinkler system actuated by thermal fire detection devices is
provided at the ceiling over the turbine building floor area which was affected by the oil
spill. There was no automatic sprinkler protection provided for the adjacent
equipment / truck bay. The turbine building area is separated from the "B" train essential
switchgear room by a 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> fire-rated concrete block wall. All penetrat;ons through these
walls are provided with fire protection features such as penetration seals, doors and
dampers, that have an equivalent fire resistive rating to that of the fire barrier. The
structural steelinside the switchgear room is protected with fire-proofing material and area-
wide smoke detection capability is provided. A CO, manual fire fighting hose line is
located in this room and water fire fighting hose lines are located in plant areas adjacent to
this room and the turbine building area of concern.
PLANT FIRE PROTECTION ENHANCEMENTS
BECo is taking an engineering approach to minimize the fire hazard impact that a future
event of this type could have on the plant. In addition to the existing plant fire protection
features, BECo made the following fire protection design enhancements during the outage:
1. Installed containment curbs at the fire doors leading to the "B" essential switchgear
room and the stairway leading down to the liquid radwaste holding tanks. This
curbing will preclude oil flow under these doors and confine the oil hazard to the
Turbine building; and
2. Modified the bottom face of the three transformer iso-phase bushing boxes by
installing an 8-inch diameter down-comer drain line for each box. These drain lines
l were routed and drained to the transformer oil leak retention pit (rock trap). Each
! drain line was equipped with a rupture disk designed to open under 2 pounds per
! square inch of static oil pressure in the drain line down-comer. The end of the drain
i
line down-comer was capped with a screen to prevent small animal intrusion,
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l c. Conclusions
l Based on the on-site review of the existing plant conditions and fire protection features,
the inspector concluded that the fire protection enhancements should provide reasonable
l assurance that if this event or a similar one were to occur, the transformer oil fire hazard
l would be controlled and the potential fire effects on safe shutdown and safety related
l electrical components would be minimized. The new fire protection enhancements should
l provide an additional level of fire safety diversity.
l F3 Fire Protection Procedures and Documentation
F3.1 Fire Hazard Analysis Review
l
a. Inspection Scope (71750) I
l
After the transformer failure on March 7, the inspector reviewed BECo's Fire Hazard l
Analysis to determine whether an oil spill of such a magnitude had been considered in the I
analysis of the affected fire zones.
b. Observations and Findinas
The inspector reviewed the fire hazard analysis fire zone data sheets for turbine building
l elevation 23' up to 51" and radwaste and control building elevation -1' up to 23'. The
i
inspector discussed these sheets with a fire protection engineer and determined that fire
loading in this area comparable to the oil spill which occurred following the transformer
failure had not been considered in the fire hazard analysis.
As described in Section F2.1, BECo installed berms on the 23' elevation of the turbine I
building to prevent oil in this area from spreading into the "B" switchgear room and
radwaste corridor area. A berm was also installed by the door leading to the cable
spreading room area. In addition, drain lines were installed on the isophase bus ducts,
located outside of the turbine building, to direct any future oil coming through those ducts
l to the rock trap surrounding the transformer. The inspector verified that the fire hazard
analysis was revised to document these changes on April 11, prior to plant startup.
c. Conclusions
l The fire hazard analysis did not reflect potential fire loading in the turbine building and
radwaste area commensurate with the oil spill after the main transformer failure because
this was not an anticipated failure mode. The enhancements to install berms in the turbine
building and drain lines on the isophase duct lines willlimit the fire loading effect on these
l
areas should a similar failure occur in the future. The fire hazard analysis report was
j- updated to reflect these changes before plant startup following RF011.
l
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V. MANAGEMENT MEETINGS
X1 Exit Meeting Summary
l The inspectors presented the inspection results to members of licensee management at the
! conclusion of the inspection on May 16,1997. The licensee acknowledged the findings
j presented.
X4 Review of UFSAR Comm'tments
A recent discovery of a licensee operating their facility in a manner contrary to the UFSAR
description highlighted the need for additional verification that licensees were complying
with Updated Final Safety Analysis Report (UFSAR) commitments. For an indeterminate
time period, all reactor inspections will provide additional attention to UFSAR commitments
and their incorporation into plant practices and procedures. While performing inspections '
discussed in this report, inspectors reviewed the applicable portions of the UFSAR. No
inconsistencies were noted.
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INSPECTION PROCEDURES USED
IP 37551: Onsite Engineering
IP 40500: Effectiveness o' Licensee Controls in Identifying, Resolving, and Preventing
Problems
IP 61726: Surveillance Observation
IP 62707: Maintenance Observation
IP 71707: Plant Operations ;
IP 71750: Plant Support Activities
IP 82301: Evaluation of Exercises for Power Reactors
IP 83750: Occupational Radiation Exposur.
IP 92700: Onsite Followup of Written Repats of Non-routine Events at Power Reactor
Facilities
IP 92901: Followup - Operations
IP 92902: Followup - Maintenance !
IP 92903: Followup - Engineering 5
lP 92904: Followup - Plant Support
iP 93702: Prompt Onsite Response to Events at Operating Powec Reactors .
.
b
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ITEMS OPENED, CLOSED, AND UPDATED
OPENED
URI 97-02-01 Feed water system regulating valve and control rod initial movement
problems impacted operational activities during start-up from RFO11. j
VIO 97-02-02 Inadequate electrical design control for voltage regulating I
transformers and MO-1301-53 which adversely impacted safety
related equipment. l
IFl 97-02-03 Jet pump nonconforming conditions. l
URI 97-02-04 Compliance with 70.24
CLOSED
LER 95-003 Manual Scram.
LER 97-006 Inadequate procedure caused brief loss of shutdown cooling.
UPDATED
URI 94-26-01 EDG turbo assist valve reliability.
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LIST OF ACRONYMS USED
-
- AFPC Augrnented fuel pool cooling
ALARA As Low As is Reasonably Achievable
APRMs Average Power Range Monitors
j BECo Boston Edison Company
,
CFR Code of Federal Regulations
j ESF Engineered Safety Feature
'
HPCI High pressure coolant injection
l&C Instrumentation and Controls !
l IFl Inspection Follow-Up item
IR inspection Report
)
I
ISI Inservice inspection
i LER Licensee Event Report
- LOOP Loss of Offsite Power
LPCI Low pressure coolant injection l
MSIV Main rteam isolation valve
MSL Main Steal Line
NCV Non-Cited Violation
NOV Notice of Violation
NRC Nuclear Regulatory Commission l
NRR Office of Nuclear Reactor Regulation !
PASS Post accident sampling system
PNPS Pilgrim Nuclear Power Station i
PR Problem Report )
QA Quality Assurance j
RBIS Reactor building isolation system '
RCA Radiological controlled area
RCIC Reactor core isolation cooling
RFO Refueling outage
'
RP Radiological Protection l
SBGT Standby Gas Treatment
SBO Station Blackout
SRO Senior Reactor Operatof
TS Technical Specification
UE Unusual Event