ML20137T046

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Insp Rept 50-302/97-01 on 970112-0222.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support
ML20137T046
Person / Time
Site: Crystal River Duke energy icon.png
Issue date: 03/24/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20137S969 List:
References
50-302-97-01, 50-302-97-1, NUDOCS 9704150302
Download: ML20137T046 (68)


See also: IR 05000302/1997001

Text

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'U.S. NUCLEAR REGULATORY COMMISSION

REGION 2

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. Docket No: 50-302

License No: ~0PR-72

Report No: 50-302/97-01

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~ Licensee: Florida Power Corporation

Facility: Crystal River 3 Nuclear Station

Location: 15760 West Power Line Street

Crystal River, FL 34428-6708

Dates: January 12 through February 22, 1997

' Inspectors: S. Cahill, Senior Resident Inspector

T. Cooper. Resident Inspector

B Crowley, Reactor Inspector, paragraphs E2.1, E8.1,

E8.4 E8.10

P. Fillion, Reactor Inspector, paragraph E8.5

L Mellen Project Engineer, . paragraphs E8.4. E8.7

L. Raghavan, Project Manager. paragra)h E1.4

R. Schin Reactor-Inspector, paragrapis E1.3, E8.2,

E8.3

H. Thomas. Reactor Inspector. paragraphs E8.6, E8.8.

E8.9

Approved by: K. Landis, Chief. Projects Branch 3

Division of Reactor Projects

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9704150302 970324 N

PDR ADOCK 05000302 '?

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EXECUTIVE SUMMARY

Crystal River 3 Nuclear Station

NRC Inspection Report 50-302/97-01 (

This integrated inspection included aspects of licensee performance in 5

operations, engineering.' maintenance, and plant support. The re) ort covers a. j

, 6-week period of resident inspection:-in addition, it includes tie results of  !

announced inspections by four reactor inspectors, the project engineer from

l- - Region II. and the NRR project manager. .;

I Ooerations

] Problems with inconsistent logging criteria and unclear and unenforced ,

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. procedural expectations were observed by the inspectors in operations logs -

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(paragraph 01.2).  !

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' A Violation (VIO 50-302/97-01-01) was' identified for clearance tagging .

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recuirements which were inadequate to preclude personnel and equipment hazards  !

. anc resulted in a valve being repositioned while under a red tag clearance 3

(paragraph 01.3). .

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Several attention to' detail and poor process problems indicated that

- deficiencies could exist in the licensee's expectations and process for .

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configuration and status control of plant equipment (paragraphs 01.3. 01.4. l

7- and 01.5).

A Violation (VIO 50-302/97-01-02) was identified for failure to follow

'- procedures, resulting in an inadvertent emergency diesel generator start. i

Contributors to this event, such as poor briefing and preparation of the

operator, assigning the operator to extraneous tasks during the performance of

! a time sensitive evolution, and the operator failing to perform vital steps of ,

. the procedure are indicative of performance problems which still exist in l

1 plant operations (paragraph 01.6).

The licensee staff exhibited an adequate level of conservative decision making

and questioning attitude. Several good examples were observed but some poor

t examples continue to be found. Licensee management continues to emphasize

development of a conservative safety culture (paragraph 04.1).

Licensee self-assessment activities were being actively restructured in an

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attempt to improve their effectiveness. Some change related problems were

observed due.to implementing new programs (paragraph 07.1).

E The inspectors concluded the new corrective action program was functioning

- adequately, but several deficiencies detracted from its effectiveness. The

licensee was actively working to improve the process and correct these

deficiencies (paragraph 07.2).

liaintenance

Several personnel errors and programmatic instrument calibration problems were I

identified as.a Violation (VIO 50-302/97-01-04) of Technical Specification

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Surveillance Requirement 3.7.13.1 for spent fuel pool level verifications 1

(paragraph M1.1). ,

The decision to assess the maintenance controls of the plant computer was a

proactive initiative on the part of licensee management. The assessment

resulted in more stringent controls being implemented _ (paragraph M1.2).

Problems were encountered throughout the performance of the Emergency Diesel

Generator 1A outage. Lack of coordination was identified as a key

contributor. A weakness was identified for the absence of a mechanism to

ensure that tasks scheduled for the weekend that were not completed were

rescheduled for the subsequent week (paragraph M1.3).

A Non-Cited Violation (NCV 50-302/97-01-05) was identified for an inadequate

surveillance procedure to test the operability of the toxic gas chlorine

detectors (paragraph M1.5). 1

Weaknesses were identified with licensee work planning. Work packages were

planned for inappropriate plant conditions, were provided to field operators l

unfamiliar with the impact of the task. and were not thoroughly evaluated for  ;

control impacts and updated to preclude future problems (paragraphs M1.6. i

M1.7).

Enaineerina

The inspectors observed good support from Technical Support system engineers

to Operations for emergent issues (paragraph E1.1).

A Non-Cited Violation (NCV 50-302/97-01-10) was identified for inadequate

design control. Non-Safety Related Components % Safety Related Applications -

Two Examples: Thyrite Surge Protection Device. Operator and Controller for

MUV-103. The licensee has taken the necessary immediate corrective actions

and has added final resolution of these issues to the restart restraint list

(paragraph E1.2).

An Unresolved Item (URI 50-302/97-01-06) was identified regarding concerns

with the design, licensing basis, and Technical Specifications for the high

pressure injection system. In addition, the inspector noted that the

licensee's recently completed extent of condition review (time line) for the i

makeup /HPI system design did not identify any of these concerns (paragraph

E1.3).

The inspectors noted improvement in the quality and thoroughness of 50.59 )

evaluations for recent engineering products over those generated one - two

years ago. However, the sample size reviewed was small and therefore, further

review will be required to verify improvements and acceptability of the

overall 50.59 program (paragraph E1.4). i

The licensee discovered problems with diesel generator test instrumentation l

inaccuracy that was not factored into surveillance testing requirements,

potentially rendering the diesel generators ino)erable. However, the

corrective action was timely and thorough rid t1e inspectors considered it an

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. example of a problem found as corrective action for a previous problem f

.(paragraph E1.6).  !

An error in' the FSAR was identified, where the FSAR stated-incorrectly that -

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for a design basis accident the peak cladding temperature would exceed 2300 l

degrees F (the regulatory limit is 2200 degrees F). In addition.-the  !

inspector noted that the licensee's current FSAR review project had not 1

identified this FSAR error (paragraph E1.1).

The inspectors noted that the licensee's definition of a design basis issue,

as defined in Procedures CP-111, CP-150, and CP-151 was not clearly broad

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enough to ensure that the requirements of 10 CFR 50, Appendix B, Criterion i

III: 10 CFR 50,72: and 10 CFR 50.73 would be met (paragraph E2.1). l

-The inspectors followed up on and closed a total of three violations and one l

Licensee Event Report (paragraphs E8.1. E8.2, E8.3).  !

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A violation (VIO 50-302/97-01-07) was identified for ' inadequate design control  ;

-in that. design assumptions for Auxiliary Building temperatures used in the i

Environmental and Seismic Qualification Program Manual (ESOPM) and instrument i

loop uncertainty setpoint calculations were not properly translated into l

procedures for calibration of instruments, the Enhanced Design Basis Document,

cr the Final Safety Analysis Report. Additionally, there were no procedures

for ensuring the Auxiliary Building temperatures would be maintained withir;

the ranges. assumed by the ESOPM and instrument setpoint calculations and the,c

were no records of daily temperatures in the Auxiliary Building (paragraph

E8.4).

A violation (VIO 50-302/97-01-09) was identified for inadequate corrective

actions for cable ampacity (paragraph E8.5).

An Unresolved Item (URI 50-302/97-01-08) was identified regarding the adequacy

of procedures to take the plant from hot standby to cold shutdown from outside i

the control room in the event of a fire (paragraph E8.6). i

The inspectors noted that the licensee performed detailed evaluations and is

developing solutions for the issues identified in GL 96-06. Overall. the

Modification Approval Record package, including the'10 CFR 50.59 evaluation.

design, procurement, and installation of the containment penetration process

31 ping expansion chambers was detailed and well documented, demonstrating good

Engineering performance. One weakness was identified concerning completion of

the ISI Requirements check-sheet (paragraph E8.10).

P1 ant Sucoort-

On January 30. 1997, a second example of violation No. A(4)(01043) which was  !

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' issued'in EA 97-012 was identified by the creation of a penetration path into

the protected area via a breach in a condenser waterbox (paragraph 51.1).

A Non-Cited Violation (NCV 50-302/97-01-03) was identified for an inadequate '

fire system recirculation procedure. System recirculation flow limits were

not included in system procedures or the Fire Protection Plan, resulting in i

all . fire pumps inadvertently being rendered inoperable (paragraph F3.1).  !

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The inspectors assessed the licensee *s performance concerning the five areas of continuing NRC concern in the following

3aragraphs: the assessment is limited to the specific issue addressed in the respective paragraph.

NRC AREA 0F CONCERN ASSESSMENT PARAGRAPH

E1.2 E1.5 E1.6 E2.1 E8.1 E8.2 E8.3 E8.4 E8.5 E8.6 E8.7 E8.8 E8.9 E8.10

Management oversight G G G A G A G I A A G A' A G'

Engineering Effectiveness G G G G A G I I G G G A- G

Knowledge of design basis G G G I A G A G

Compliance With Regulations G fi G A G A G I I I G- G G G

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operator Perfonnance G A i

5 - Superior G = Good A = Adequate / Acceptable I = Inadequate Elank = Not Evaluated /Insuf ficient Information

E1.2: 10 CFR 50.59 Safety Evaluations

E1.5: Decay Heat Valve (DHV) 21 Operability Evaluation

E1.6: Evaluation of Dranetz Test Instrument Inaccuracies on Emergency Diesel Generator Testing

E2.1: Corrective Action and Reportability Issues

E8.1: Corrective actions for Violation 50-302/96-05-05. Failure to Follow Procedures for Updating Design Basis Documents

E8.2: Corrective actions for violation 50-302/96-05-07 Inadequate Receiving Inspections for Battery Chargers; and  ;'

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Licensee Event Report 96-12-02. Operation Outside Design Basis Caused by Battery Chargers Having Inadequate Test

Results Accepted in Error

E8.3: Corrective actions for Violation 50-302/96-05-08. Failure to Follow Purchasing Procedures for Inverters

E8.4: EA 95-16. Use of Nonconservative Trip Setpoints for Safety-Related Equipment '

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E8.5: IFI 96-201-13. Cable Ampacity Exceeded for DHP-1A [DCP-1A] Feeder Cable and Others

E8.6: Unresolved Item (URI) 50-302/96-201-04 Nonsafety-Related Positioners on Safety-Related Valves

E8.7: Inspector Followup Item (IFI) 50-302/95-15-01. Design Requirements for Nitrogen Overpressure .i

E8.8: VIO 50-302/96-09-07 Inadequate Corrective Action for Implementation of EFIC Task Force Recommendations

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E8.9: VIO 50-302/95-21-03. Failure to Isolate the Class IE from the Non Class IE Electrical Circuitry for the Reactor

Building Purge and Mini-Purge Valves ,

E8.10: NRC Generic Letter 96-06. Assurance of Equipment Operability and Containment Integrity During Design-  ;

-Basis Accident Conditions

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Report Details

Summary of Plant Status J

The unit remained in Mode 5 throughout the inspection period, continuing in i

the outage that began on September 2, 1996. An outage on the "A" train of l

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emergency core cooling system (ECCS) equipment was conducted to perform

corrective maintenance and implement a design change on the 1A Emergency  !

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Diesel Generator (EDG) to u) grade the EDG turbocharger nozzle rings and

replace the intercooler wit 1 a more efficient versico. These changes were i

expected to result in 150 kilowatts (Kw) of increased diesel capacity. The IB i

EDG will be upgraded during a pending "B" train outage'. The development of I

other modification packages continues, although no major modification began l

implementation during this inspection period. ]

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I. Operatiom  !

01 Conduct of Operations i

01,1 General Comments (71707)  !

Using Inspection Procedure 71707 the inspectors conducted frequent

reviews of ongoing plant operations. Operators were professional in

that control room access was well controlled, communications were

normally thorough, and alarm response was good. The inspectors observed

several shift turnover meetings and observed that they were generally

formal and information was effectively communicated. Members of various

support groups such as the duty Technical Support system engineer

attended to support Operations needs.

As discussed in paragraphs M1.3 M1.6 and M1.7. the inspectors observed

several examples of inadequate communications and scheduling between

Operations and Maintenance personnel that resulted in challenges to the

operators and missed post-maintenance tests.

Housekeeping in the plant was routinely monitored and found to be

adequate although several examples of poor control of maintenance

equipment adjacent to 3rotected train components were identified by the

inspectors. None of t1e noted discrepancies comprised a significant

operational concern.

Overall, the inspectors observed some good examples of conservative

decision making and questioning attitude by plant operators as discussed

in paragraphs 01.4 and 04.1. However, several attention to detail and

poor process problems discussed in paragraphs 01.4. 5 and 6 below caused

the-inspectors to conclude that deficiencies existed in the licenses's

process for configuration and status control of plant equipment.

01.2 Operator Loas (71707)

The inspectors identified several significant items discussed elsewhere

in this report such as an inadvertent EDG start and a subsequent

-Operations investigation, a protected area security breach, and

mispositioned valves that were not logged in the Operations Shift ,

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Supervisor logs. The inspectors also identified equipment removed from

service such as Chill Water Pump 1A which was entered in narrative logs

but not in the Equipment Out of Service tracking log. The inspectors .

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also observed inconsistencies between Shift Supervisor and Shift Manager

logs and between individual Shift Supervisors logs. The inspectors

reviewed 0)erations Instruction 01-5. Log Keeping. Revision 2. and

observed tlat several requirements were not clear and those that were

clear were not consistently enforced by management. Requirements such

as logging the time of turnover were not being implemented by Shift l

Supervisors on Duty (SS00) nor expected by management. Additionally.

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practices such as recording log entry times versus event occurrence

times in the SSOD logs were not delineated in 01-5. The ins)ector

- observed that there was no guidance on the content of Shift ianager (SM) t

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logs nor guidance on the coordination between the SM and SS00 logs, both

of which often contain the same content. The inspector discussed these

observations with Operations management who issued a Night Order. on r

February 4 clarifying management expectations for log entry thresholds.

The licensee incorporated these deficiencies in their revision to OI-5

being developed as an action for their Management Corrective Action Plan

II (MCAP). The inspectors concluded licensee management had not made

their expectations clear and had not held SS0Ds accountable to the ,

expectations in 01-5.

01.3 Valve Stroked While Red Taaaed Under a Clearance _. ,

a. Insoection Scooe (71707)

On February 6. 1997, condenser water box air removal (AR) valve ARV-1

was o)ened while red tagged under an active clearance which supported '

water)ox work. The inspectors evaluated the licensee's response to the

problem.

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b. Observations and Findinas

Tagging Order 97-1-140 was issued to support mechanical work in the D [

waterbox of the main condenser. Tag R-008 was hung to require the main

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control board switch for valve ARV-1 to be in the closed )osition. This

was the only point of control and the only tag hung for ARV-1 which was

an air-operated valve. On February 6 the instrument technician assigned

to perform work on the solenoid valve in the air supply line to the

valve operator for ARV-1 was directed to verify the failure mode of the

valve. The technician reported that ARV-1 failed open on loss of air. '

was not tagged, and was within the red tagged boundary of the mechanical

work clearance. Neither the technician nor SS00 was aware that ARV-1

was red tagged closed on the main control board. Consequently, the

technician was authorized by the SS00 to work on the solenoid. Although  !

the control room operators recognized after the technician left that ,

ARV-1 was red tagged and they tried to page him, they were unable to ,

contact him and ARV-1 opened when he' started to work on the solenoid.  !

The potential consequences were minimized because the technician,

although not required by procedure, had alerted the mechanical workers '

to exit the waterbox prior to his solenoid work because he knew ARV-1

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- workers. Nevertheless the inspectors were very concerned that a valve 1

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was able to be opened when on an active clearance, was not tagged

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, locally, and was a fail-open air-operated valve that was not gagged -

shut. The' licensee's clearance Procedure CP-115. Nuclear Plant Tags and

Tagging Orders, Revision 73, did not require local tagging of components

J or gagging of air-operated valves unless they were designated as. system 1

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boundary valves Even then, CP-115 did not require tags on the J

componentsmanihulatedtogaganairvalveorisolateandventthe i
motive air. supply. The inspectors concluded these deficiencies l

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constituted an inadequate. procedure which directly contributed to the  !

ARV-1 event. Criterion V.of Appendix B to 10 CFR 50 . Instruction.

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- Procedures and Drawings, requires in part, that activities affecting

quality shall be prescribed by documented _ procedures of a type ,

appropriate to the circumstances. Therefore, the failure of CP-115 to i

require local tagging of components and specify appropriate controls for

gagging of air-operated valves for red-tag clearances is a violation.

VIO 50-302/97-01-01, Inadequate Clearance Tagging Requirements.

The licensee took thorough corrective actions the following day after

)lant management became aware of the event at their morning meeting.

iowever, the inspectors were concerned that the significance was not

recognized by shift management at the time of occurrence, and

a)propriate actions were not implemented until almost 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> later.

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T1e inspectors also noted that the SS00 did not make an entry in his log

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discussing the problems on the day of occurrence.. After managemelt  !

initiated an Operations Investigation per Operations Instruction 12,  !

Investigation of Abnormal Events Revision 1, a maintenance and tagging .

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standdown was conducted that lasted three days. The event was briefed

to all available maintenance personnel, and approximately 120 tagging

orders were verified for adequacy. The licensee found numerous examples

that did not comply with CP-115 requirements or management expectations- i

these were documented on corrective action system precursor card (PC)  !

. 97-0921. These included 27 examples of components that were system

boundaries but were not annotated as boundary valves on tagging orders, ,

ten examples of local control points not tagged, and two examples of air  :

valves not in their fail safe position. The licensee also found that

different operators had varying methods of implementing identical

clearance orders. This indicated to the inspectors that CP-115 guidance

was not clear and that licensee management was not adequately overseeing

the process to ensure expectations were met and clearance orders were

consistent. The inspectors also reviewed CP-115 and concluded the

format was primarily an unprioritized listing of requirements which

contributed to the inconsistent implementation.

Licensee management was already concerned about a perceived negative  !

' trend in tagging orders im)lemented per CP-115 and had initiated a root  ;

- cause investigation under )C 96-5487 on December 5, 1996. However, this  ;

i corrective action effort was assigned a due date of February 15, 1997, 4

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so it was not timely enough to preclude this event. The licensee

. incorporated their findings and corrective actions for the above

problems into the ongoing investigation. ,

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c. Ccnclusions  ;

Although the inspectors determined the resultant safety impact of this  :

event was minor, the potential exists for further violations of the l

integrity of the clearance program. The inspectors were very concerned  !

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that similar communications errors and program deficiencies could result

in a more significant hazardo'us situation. lhe inspectors considered. ,

these problems to be indicative of potential deficiencies in the l

licensee's overall process for configuration and status control-of plant  ;

equipment. l

01.4 Ventina of Decay Heat Removal System (71707)- i

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The inspectors observed that the Operations staff was concerned about  :

previous problems ex)erienced with restoration of an out of service j

L decay heat removal ()H) system train. Upon opening the system isolation  ;

valves between the DH system and the reactor coolant system (RCS). '

pressurizer liquid level had decreased several inches, indicating air

was introduced into the RCS. This occurred even though the DH system

had been properly vented per procedure. The Operations staff developed

new work instructions (WI) to augment the OH system venting process and

verify the amount and location in the RCS where the air collected. The  ;

inspector witnessed the Plant Review Committee (PRC) review and approval

of these WIs. Although the inspector noted the lack of independent

verification in the restoration steps of one of the two Wis, the

inspector observed that the licensee effectively addressed concerns with

air accumulating in the reactor vessel head and developed conservative

guidance to assist the operators. The licensee's efforts were not

totally successful because 3ressurizer level still decreased upon DH

system restoration, althougl less than before. The licensee concluded a

new high point vent was recuired to effectively vent from under the j

system isolation valves anc included that as a restart item on their i

restart commitment checklist. PC 97-1052 and 1059 were generated to j

track resolution. The inspectors concluded that the missed independent j

verification was another example of potential deficiencies in the i

licensee's overall process for configuration and status control of plant

equipment. However, plant operators exhibited a conservative concern

and a good effort was made by the licensee to resolve it.

01.5 Miscositioned Valve Events (71707)

The inspectors reviewed the licensee's response to four examples of

mispositioned valves that occurred over a three day period. A raw water

system vent valve was inadvertently left open by an operator placing a

-heat exchanger-in service and was discovered after a pump start resulted

in water flowing from the valve A nitrogen system valve was found in

the incorrect position following maintenance activities. A makeup

system valve and station air valve were a)parently closed to isolate air j

leaks without any procedur91 controls. T1e licensee ap3ropriately

. recognized the overall impb cations of the combined pro)lem and

initiated a common root cause investigation. During the review the

inspector questioned the method of control and verification fcr root

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isolation valves to instruments that are commonly operated by instrument

technicians. The licensee recognized that they did not have a procedure

to verify.the )osition of these valves to aneumatic valve controllers i

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and initiated )C 97-0733 to implement furtler corrective action. The .

licensee promptly issued an 0)erations Study Book entry to promulgate

the problems to operators. T1e licensee's investigation has revealed  ;

that equipment alteration logs were not required to be retained as-  ;

quality records for minor work packages. This made it impossible to i

, verify the last known position or. verification of several valves or l

components, hindering the licensee's investigation.- The licensee and

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inspector also recognized that management's expectations were to perform  !

concurrent and independent verifications. These expectations were l

developed for previous mispositioning problems and were not being l

consistently implemented. .The licensee's common root cause was being i

finalized at the close of this Inspection Report period so their final  ;

assessment and corrective actions will be reviewed in the next report  !

4 period. .The inspectors considered these problems to be indicative of i

potential deficiencies in the licensee's overall process for I

configuration and status control of plant equipment.

l 01.6 Inadvertent Start of EDG-1 A .

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a. Insoection Scooe (71707. 40500) j

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While performing the Modification Approval Record (MAR) functional test

restoration of EDG-1A at 9:18 p.m. on February 1.1997, during the

manual roll of the diesel to clear oil and moisture from the cylinders.  !

the diesel inadvertently started and accelerated to full speed. Control  !

room alarms were received for the automatic start of the diesel  !

generator room fans. AHF-22A and AHF-22B. The control room operator was  ;

called by the plant operator performing the restoration. who notified

him of the inadvertent start. A Senior Reactor Operator (SRO) and plant i

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operator were dispatched from the control room to secure the diesel i

generator.  ;

b. Observations and Findinas

The inspectors reviewed the licensee's investigation. which revealed i

l that the MAR functional test was originally scheduled to be performed to i

completion by a dedicated crew that had been extensively briefed and  !

rehearsed for the task. Delays in the performance of the functional  ;

test resulted in the dedicated crew being relieved by a crew that  !

received only a face to face turnover on the task. ,

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The procedure to restore the EDG after the MAR functional test. MAR 96-  ;

10-05-01 TP-1. Attachment A. stated that after the diesel engine had  !

been stopped for at least 15 minutes. but not more than 20 minutes. '

steps 4.6.30 through 4.6.34 should be performed. These steps are  !

intended to roll the diesel slowly to vent moisture and oil out of the

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cylinders. Step 4.6.30 trips the fuel racks. which should prevent an

inadvertent diesel start while rolling it with air. The licensee

reviewed the procedure for adequacy and concluded that the functional  ;

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test procedure'was adequate and in sufficient detail to perform the task

without failure.

After the diesel had been stopped,' but prior to com]leting the steps.to

roll the diesel, the control room operator called t1e plant operator and

directed him to perform a different task. The plant operator inquired

as to the im)ortance of the function, but did not inform the control ,

room as to t1e status of the MAR functional' test restoration procedure. !

When the plant o)erator returned to the MAR functional test procedure,

over 19 minutes lad elapsed since the diesel had been stopped. The  !

operator proceeded to roll the diesel over, but did not complete all  ;

required steps in the procedure, including 4.6.30, which would have l

prevented an inadvertent diesel start.

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Technical Specification (TS) 5;6.1.1 requires, in part, that procedures i

be implemented covering activities as recommended in Regulatory Guide l

1.33, Appendix A. Revision 2. dated February 1978. A)pendix A  !

recommends administrative procedures to cover the aut1orities and

responsibilities for safe operation and shutdown, procedure adherence

and temporary change method. The licensee implemented the above

Appendix A recommendations, in part, through Procedure Al-500, Conduct

of Operations and 01-09, Operations Procedures. 01-09 requires that

activities will be performed in accordance with approved instructions.

The operator's failure to' comply with the instructions in MAR 96-10-05-

01 TP-1. Attachment A is a violation. VIO 50-302/97-01-02. Failure to

Follow Procedures, Resulting in an Inadvertent Emergency Diesel

Generator Start.  !

c. Conclusions

The failure of a non-licensed operator to follow the MAR functional test

procedure resulted in an inadvertent emergency diesel generator start.

Contributors to this event, such as poor briefing and preparation of the

operator, assigning the operator to extraneous tasks during the

performance of a time sensitive evolution, and the operator failing to

perform vital steps of the procedure are indicative of performance

problems which still exist in plant operations.

04 Operator Knowledge and Performance i

04.1 00erator Awareness and Ouestionino Attitude

a. Insoection Scone (71707)

The inspectors continue to monitor operator performance in response to

previously documented deficiencies. .

1

b. Observations and Findinas

The inspectors have observed numerous examples of operator performance

that were indicative of the status of the licensee's safety culture. l

The licensee has made it a priority to improve this aspect by supporting !

!

!

7

and encouraging questioning attitudes and open decision making. Some

examples of questioning attitude and conservative decision making

included: the control room refusal to authorize inappropriate scheduled

Mode 5 work, questioning of the IB DH pump oil usage trend prior to a

train A outage that resulted in delaying the outage for a week to

resolve, questioning of DH system venting problems, drain valve work

that was conservatively stopped without the normal makeup path in

service, and engineered safeguards cabinet work that was sto] ped due to

a fuse concern. The fuse concern turned out to be not a pro)lem but

operators conservatively delayed work for a day to ensure their concern

was resolved. Another example of questioning attitude was the work of

engineering to troubleshoot and discover 3roblems with chlorine monitor l

testing. These items are discussed elsew1ere in this report.

Some examples of poor conservatism and questioning attitude were also

observed. They include the scheduling of the inappropriate Mode 5 work

caught by the operators, the initial change by the operations shift of i

fire protection system recirculation flow on verbal and incomplete l

guidance late reports required by 10 CFk 50.72 (addressed in IR 50- 1

302/97-04), a poor briefing and preparation of an EDG operator for an l

evolution, and assigning the EDG operator to extraneous tasks during the

performance of a time sensitive evolution which contributed to an

inadvertent EDG start due to a missed procedural step.  ;

c. Conclusions

The licensee staff exhibited an adequate level of conservative decision

making and questioning attitude. Several good examples were observed

but some poor examples continue to be found. Lict see management

continues to emphasize development of a conservat W safety culture.

06 Operations Organization and Administration

06.1 Effective February 18, 1997. Mr. J. Cowan assumed the duties of Vice

President. Nuclear Production, from Mr. P. Beard. Senior Vice President.

Nuclear Operations. The following Directors and their departments now

report to Mr. Cowan:

. Mr. B. Hickle. Director. Nuclear Plant Operations

. Mr. R. Widell. Director. Training

. Mr. W. Conklin. Director Materials and Controls

. Mr. D. Kunsemiller. Director, Site Support

The following executives now report to the Senior Vice President.

Nuclear Operations (Mr. R. Anderson, effective March 3. 1997):

. Mr. J. Holden. Director. Nuclear Engineering and Projects

. Mr. J. Baumstark. Director. Quality Programs

. Mr. J. Cowan. Vice President. Nuclea- Production

- - . - - - - . .- . . . - -

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8

07- . Quality Assurance in Operations

07.1 Licensee Self-Assessment Activities

a. Insoection Scooe (71707. 40500)

The inspectors' reviewed various self-assessment activities which

included:

. _ Routine reviews of Nuclear Quality Assessments (NOA) activities;

e Observation of an exit interview for a N0A monthly audit.

  • Observation of several Plant Review Committee (PRC) meetings and

review of PRC Meeting minutes:

e Observation of the licensee's internal Restart Readiness Review

Panel meetings:

  • Observations of subcommittee and full Nuclear General Review

Committee (NGRC) meetings on January 14 and 15.

b. Observations and Findinas

N0A reports appeared thorough and diverse. The inspectors noted several

examples of timely and responsive NOA surveillances in potential problem

areas. N0A Audit 97-01 had several good findings in the Engineering

area. but the inspector observed that an Engineering representative did

not attend the audit exit meeting The licensee recognized the negative

impact this had on resolution of the findings and took appropriate

corrective action to ensure it would not recur. The inspector reviewed

N0A staffing plans and observed that the licensee had established a two

year rotation plan for four N0A auditor positions, staggered at six

month intervals, and was attempting to target rotation candidates for

inclusion into N0A versus accepting other de)artments' excess personnel.

The inspector concluded this would enhance tie effectiveness of NOA.

The inspector also observed that all N0A findings are entered into the

licensee's corrective action program via generation of a Precursor Card

(PC) and that the NOA auditor determined the grading of the resultant

PC. Changes to the grade and consecuently to the -level of investigation

the PC received had to be concurrec on by NOA. The ins)ector concluded

this was a beneficial practice that enhanced N0A owners 11p of issues.

The PRC provided a thorough review of issues. A good, detailed

discussion and rejection of an issue was noted regarding the

implementation of modification on reactor building

chambers to address Generic Letter 96-06 concerrs. Although

penetration

theexpansion

inspector observed an omitted independent verification requirement, as

. discussed in )aragraph 01.4. PRC discussion of the DH system venting

concern was tlorough. conservative, and probing. The committee

carefully reviewed an associated 10 CFR 50.59 evaluation and challenged

several~ decision points taken by the author. The chain of custody

- - . - - - .- - - - . . . - - . _ _ - - . - - . - - -

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forms, implemented to address previous problems regarding implementation

of PRC ex)ectations that formed the basis for approving items- appeared

.

. to be worcing successfully. The inspector verified several examples .

Where the completion of an item was delayed until.the PRC custody form  !

was completed. At the end of the inspection period, the licensee was in  !

the process of evaluating several restrictions to the use of alternate i

PRC members and establishing a full time PRC director to increase

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1

. consistency and oversight. The inspector concluded the licensee's i

! planned changes would increase the effectiveness and value added of the  :

.

PRC. which has already exhibited improvement from previous PRC

!

performance in the areas of questioning attitude and willingness to set

.: a high standard and to reject items that do not meet that. standard. PRC

meeting minutes were noted to be thorough and accurate representations

of the items presented.  ;

i The NGRC conducted an extensive review of site activities. The l

inspector observed that numerous, new offsite and onsite members have i

been incorporated and that member ex3ectations were promulgated by the i

new chairman in an effort to raise t1e standard of expectations for NGRC l

l conduct and questioning attitude. One offsite member was absent for j

'

personal reasons but did ensure his input was considered by faxing in i

comments and questions. The absent member's subcommittee, the Quality I

and Regulatory Verification Subcommittee, had all new internal members

and was hampered by the absence of the chairman and the lack of guidance ,

and expectations as to the final desired product the subcommittee was to

produce. The inspector concluded all subcommittee members needed to  !

review their charter. The inspector also observed that several offsite i

members departed prior to the conclusion of the NGRC agenda due to it  !

being longer than in the past. The inspector discussed these '

observations with the NGRC Chairman who is taking corrective action.

The inspector concluded that the NGRC exhibited an atmosphere sup)orting

rigorous questioning and open discussion that was suoportive of t1eir

role as site management oversight.

c. Conclusions

The inspectors concluded the licensee was actively restructuring their

self-assessment activities in an attempt to improve their programs.

Although some problems were observed. they were primarily change related

and due to people gaining familiarity with a new process or a new

program.

07'.2 Imolementation of New Corrective Action Proaram i

a. Insoection Stone (71707. 40500)  !

The inspectors have continually monitored the new corrective action

process the licensee implemented in November of 1996 by the following: ,

  • -Reviews of most precursor cards entered in to the system:  ;
  • Observation of a management CAR 6 meeting:

--- -. . - . . . . -

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10

. Observations of corrective action Precursor Card Screening

Committee meetings.

b. Observations and Findinas

The inspectors observed that the licensee's program as defined by CP-

111. Processing of Precursor Cards for Corrective Action program.

Revision 55. still contained numerous deficiencies and poorly defined

expectations. However, the licensee's new corrective program manager,

who assumed his position in January 1997. has recognized several of the

same problems in parallel and was actively developing changes to the

process. Examples of the problems observed by the inspectors and the

licensee included:

e initial event corrective action not covered under the scope of the

precursor card:

  • no specific requirement to veri #y extent of condition for a

problem adverse to quality:

. the role of the CARB is not well defined:

e lack of specific standard formats:

i

e granting of extensions controlled by root cause leaders doing the

work; and

e poor management visibility and knowledge of timeliness and root

cause investigation status:

The inspectors also observed that the arogram was burdensome to

administer due to the large number of 3Cs. Approximately one thousand

Pcs were initiated in January 1997, which indicated the process had an

appropriately low threshold, although thoroughly dispositioning this

many problems remained a challenge to the licensee.

c. Conclusions

The inspectors concluded the corrective action program was functioning

adequately, but several deficiencies detracted from its effectiveness.

The licensee was actively working to improve the process and correct

these deficiencies.

07.3 Manaaement Assessment in Plant Doerations

a, inspection Scone (40500)

The inspectors reviewed the first month's results of the licensee's

initiative to monitor supervisory effectiveness in the area of

operations.

11

b. Observations and Findinas

The licensee has begun an initiative to evaluate management oversight

effectiveness in the area of operations. The performance indicators

chosen included the following:

o tracking the amount of time assessing operations by not only the

operations de)artment, but by maintenance, engineering, plant

management. slift managers, and senior managers;

e tracking the amount of crew observations by shift supervisory

personnel:

e a composite ranking of crew performance: (This was done by

assessing the results of all observations oy all departments); and

e assessing the operators in: knowledge, procedure use, questioning

attitude, communications, self-checking, briefings, teamwork, and

safety.

The inspectors reviewed the results of the first month of assessment.

It was noted that this program was new and disparities existed in

performance assessments for the same crews between the various groups.

The licensee has also identified this and was working to develop better l

criteria. It was also noted that some groups and shift supervisors were

not meeting expectations for performing observations.

c. Conclusions

The inspectors realized that since this was a new program and that with

just the single data point, no conclusions could be reached. The

inspectors will continue to follow the implementation of the program to

assess its effectiveness.

08 Miscellaneous Operations Issues (92901)

08.1 (Closed) VIO 50-302/96-05-01: Failure to Follow Procedures to Initiate

Corrective Action for Bent Main Steam Line Hanaers.

(Closed) URI 50-302/96-05-02: Desian Concerns with the Main Steam Lime

Hanaers Used in Seismic and Other Dynamic Load ADDlications

Details of these problems were previously documented in Inspection

Report (IR) 50-302/96-05. The technical adequacy of the licensee's

response to these problems was reviewed and accepted by the NRC staff as

documented in a letter to Florida Power Corporation (FPC) dated

January 22, 1997. The inspectors verified that the licensee had

appro)riately initiated corrective actions for subsequent suspected

opera)ility problems. Consequently, this item is closed.

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JL Maintenance l

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M1 Conduct of Maintenance

M1.1 Soent Fuel Pool Level Transmitters

!

a. -!

Insoection Scoce (61726._ G707)

.

~ Evaluate that maintenance and surveillances of the Spent Fuel Pool Level  !

Transmitters are conducted in accordance with TS 3.7.13  !

!

.

b. Observations and Findinas

On October 31, 1996, it was recognized by the licensee that the i

instruments normally used to perform Technical Specification (TS) i

surveillance requirement (SR) 3.7.13.1 were out of calibration. Work l

Request (WR) NU 0338665 was written on that day to fabricate a measuring +

stick, which could be used to measure spent fuel pool level.  ;

TS 3,7.13 requires that during irradiated fuel movement. at least once  :

per seven days, the spent fuel pool level be verified to be greater than ,

156 feet above plant datum. Level Transmitters SF-1-LT1 and SF-1-LT2 -

feed indicators in the main control room which are normally used for the -

TS surveillance.

Instrumentation and Control (I&C) shop technicians attempted to

calibrate SF-1-LT1, but were unable to calibrate the instrument within ,

the required .5% tolerance. The licensee issued Precursor Card (PC) 96- t

5697 on December 16. 1996, to document that both instruments were out of '

calibration and that SF-1-LT1 could not be calibrated within tolerance.  !

The licensee' completed an apparent cause determination on January 15, ,

1997. As part of the apparent cause determination, the licensee  !

evaluated the issue and concluded that no TS violations had occurred.

This was based on the premise that since the surveillance procedure

acceptance criteria were conservative compared to the TS requirements.  :

any drift of the instrument would be accounted for. TM s position was

challenged by the inspectors. Surveillances must be congleted with -

calibrated instrumentation to be valid.  !

l

As part of the apparent cause determination the licensee reviewed the  ;

calibration history of these instruments. It was identified that the

last time SF-1-LT2 was calibrated was February 28, 1992, and the last ,

time SF-1-LT1 was calibrated was in November 10, 1987. The licensee's  :

calibration program required these instruments to be calibrated once I

every two years.

The inspector reviewed the last com)leted data sheets for both  !

instruments. While a complete cali) ration was com)leted on SF-1-LT2,  ;

only a single point calibration was completed on S -1-LT1 which simply  :

compared the transmitter to the level indicatcr reading. This was j

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performed on November 10, 1987.'but the review and approval was not

completed until February 1, 1988.

The inspector's review located'a completed Problem Re) ort (PR) 90-8002.

which was written on November 21, 1990, to identify tlat SF '.-LT1 and

SF-1-LT2 were out of calibration. At that time, operations was notified

that the instruments were inoperable and could not be used for the

surveillance. The PR also had a corrective action to periodically

notify the operations department that the instruments were inoperable

until the problem was corrected. Under the corrective actions for this

PR. WR 271688 was completed for SF-1-LT2 on December 14. 1990. However,

a note was attached to the PR which stated that WR 27.1687 written for

SF-1-LP . rould not be completed as the instrument would not calibrate

within t d Dances. As a result of the inability to calibrate the

instrurr,ent. Re

on February 4.1991.questThefor

PREngineering

was closed onAssistance

February 11.(REA)

1991,91-114

with a was written

statement that all corrective actions were completed. SF-1-LT1 was not

in calibration at that time, but an engineering-hold was placed on the

calibration of the instruments pending the completion of the REA

actions.

The REA stated that the instrument could not be calibrated and that

parts were becoming hard to obtain. Original plans under the REA were

to replace the existing displacer system with ultrasonic level 3

indicators. However, when problems were encountered with ultrasonic  :

level indicators installed on a different system the proposed )

modification was cancelled. No other corrective actions were taken. j

5 1

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During the period while SF-1-LT1 was out of calibration, there were ten I

Jeriods during which irradiated fuel was moved. During the period while

,'

)oth of the instruments were out of calibration, there were five periods

when irradiated fuel was moved. Technical Specification Surveillance

'

Requirement 3.7.13.1 requires that the licensee verify the fuel storage

pool water level is 2156 foot above plant datum once per 7 days during

movement of irradiated fuel assemblies in the fuel storage pool. The

s failure to perform a valid surveillance is a violation. VIO 50-302/97-

01-04. Failure to Perform Technical Specification Surveillance for Spent

Fuel Pool Level.

Following identification of weaknesses by the licensee and ths 1

inspectors in the original apparent cause determination. the licensee

upgraded the PC to a level B. which requires a formal root cause

evaluation.

4

While 3erforming the root cause evaluation, one of the causes identified

was a areak down in the preventative maintenance (PM) process which

calibrated in-field instruments. It was identified that if the PM had

been deferred. it often was not rescheduled. The licensee identified

approximately 150 instruments that were out of calibration and an

additional 720 instruments that were past the nominal calibration date,

but still within the allowed 25 percent grace period.

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The licensee evaluated the out of calibration instruments and identified

several instances where the instruments were used in safety related

applications for operating data or surveillances. Four Pcs were issued

to address these issues. EDG-1B was declared ccnditionally operable and

potentially inoperable based on out of calibration jacket coolant water

temperature instruments. The licensee veri fied that redundant

calibrated instruments were available on the aiesel generator. The

licensee is taking corrective actions to address these identified

deficiencies. Programmatic weaknesses which contributed to the

violation are being assessed by the licensee.

c. Conclusions

Several personnel errors and programmatic instrument calibration

problems were identified as a Violation (VIO 50-302/97-01-04) of

technical specification surveillance requirement 3.7.13.1 for Spent Fuel

Pool Level verifications.

M1.2 Work Controls on the Plant ComDuter

a. Insoection Scone (62707)

The inspectors reviewed an initiative by the licensee to evaluate and

improve work controls on the plant computers.

b. Observation and Findinas

In response to concerns identified by the Director. Nuclear Plant

Operations (DNP0), a surveillance was performed by the Quality Programs

department.on work controls on the plant computers. These computers are

used in the main control room for various parameter monitoring and alarm

functions.

The surveillance. OPS-97-0003 was completed on January 10, 1997, and

presented to the DNPO in the daily staff meeting. The surveillance

identified several areas where weaknesses were evident and improvements

were recommended. These identified weaknesses were as follows.

e A PM/ surveillance program had not been established to ensure

reliabilit, of the plant computer. Maintenance had only been

performed on the computer when the system failed,

o The entry conditions for licensee procedure AP-430. Loss of

Control Room Alarms were nonconservative. Partial plant computer

loss may be sustained, rendering critical plant parameters

unavailable, but a partial loss was not explicitly addressed in

the procedare.

  • Work activities being performed to troubleshoot and repair the

plant computer taking place under WR NU 339899, were outside the

scope of the WR 15

e Poor work practices were evident as a result of an inspection of

the Plant Computer cabinets and component terminations.

The licensee maintenance and system engineering management agreed that

any work performed on the plant computer, other than rebooting, and be

done under a WR, with I&C sup) ort. This agreement was documented by an

internal memorandum from the ianager. Nuclear Plant Technical Support to

the DNP0.

To date corrective actions to address the other identified weaknesses

have not been performed. An initial assessment of AP-430 by operations

was that no weakness existed, but this was rejected by the Quality

Programs department and returned to operations for further review.

c. ponclusions

The decision to assess the maintenance controls of the plant computer

was a proactive initiative on the part of the licensee management. The

assessment resulted in more stringent controls being implemented.

M1.3 Maintenance Observations

a. Insoection Scope (62707. 92902. 62703)

The inspectors observed maintenance activities during the EDG-1A system

outage. Adherence to work instructions, resolution. of identified

problems, proper maintenance practices and documentation were assessed.

b. Observations and Findinas

WR NU 0339596 was written by the licensee to perform an upgrade to EDG-

1A to allow a larger continuous run rating. New turbochargers and dual- )

'

pass combustion air intercoolers were installed in accordance with MAR

96-10-05-01. During the various period.s that the inspectors witnessed

the work, good Foreign Material Exclusion (FME) controls and work

control practices were observed. Continual presence by engineering,

both systems and design, and maintenance management was observed. The

work practices observed in the field revealed no problems.

Problems were encountered with other aspects of the task, however. The

original scope of the diesel outage was scheduled for approximately one

week. Delays and other problems resulted in the outage taking

approximately two weeks to complete. '

On January 22. 1997, the mechanical maintenance technicians working on

the diesel witnessed electrical arcing which was reported to management.

WR NU 340315 was issued to trouble shoot and repair the observed

problems. The inspectors reviewed the electrical maintenance and I&C

logs and found that on three occasions technicians were dispatched who

were unable to locate the arcing. These delays resulted in delays to

restart of the diesel following completion of maintenance and

modi fications. The I&C technician did not consult with the mechanical

.

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16

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maintenance technician, concerning the exact location of the arcing,

until the outage schedule had been impacted. Quality Programs, as part

of Audit 97-01, issued PC 97-806 on January 30, 1997, stating that the

functional test of MAR 96-10-05-01 was delayed as a result of

management's failure to recognize the impact that performing the WR

would have on the test.

The trouble shooting finally identified, on January 30, 1997, that

insulation on a wire feeding speed switch EG-19-SS had been broken,

causing an intermittent short. While identifying this problem, a

-

different wire was identified that had been pinched that had to be

replaced. According to drawings the wire was # 12 AWG, but the

'

technicians identified the wire in the field to be # 14 AWG. Delays

were caused while engineering researched and found that the correct wire

was # 14 AWG. Revisions to the drawing were submitted.

.

Other problems were encountered during the performance of the

maintenance and modifications. Jacket coolant was refilled using one

section of the operations procedure before it was realized that a new

section existed for filling the system with corrosion and biological

inhibitors.

A leaking instrument tube line was identified on February 1.1997,

during post installation testing of the MAR. The leak appeared to be

colored water, which indicated that it was jacket coolant water. The

leak was not isolable and necessitated repairs prior to restoring the

diesel to functional status.

,

On February 1,1997, after repairs were completed to the leaking

instrument tubing. the EDG was run for the MAR functional test and post

maintenance testing. The following day, on February 2,1997 it was

identified that several post maintenance test (PMT) packages on EDG-1A

had been omitted during the diesel run of the previous day. Pcs97-723,

97-757, and '97-755 were written to document several missed PMTs on the

EDG-1A.

On February 3. 1997. PC 97-895 was written to document missed PMTs on

maintenance on RWP-2A and RWV-38. The licensee's apparent cause

evaluation on all of these missed PMTs revealed that they had all been

scheduled to be completed on January 31. 1997. When work delays

prevented the completion of the PMTs on that day. no mechanism existed

to maintain the tasks on the schedule or to place the tasks on the

following week's schedule. All of the PMTs were rescheduled and were

successfully completed. The lack of a mechanism to recognize

uncompleted tasks and maintain them on the schedule was identified as a

weakness.

On February 5. 1997., the inspectors attended a post job critique for the

EDG-1A maintenance and modifications. It was identified at this meeting

that there was no assigned person responsible to coordinate all of the

various tasks. Factors contributing to the problems encountered

included the weakness discussed above in the scheduling process, too few

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17

people prepared and briefed for the tasks to relieve personnel dedicated

to aerforming the tasks, and a lack of a coordinated review of work

paccages prior to issuance. The lack of a responsible individual to

coordinate the task has been o recurring issue at the site.

,

c. Conclusions

Problems were encountered throughout the performance of the EDG-1A

outage. Lack of coordination was identified as a key contributor. A >

weakness was identified for the absence of a mechanism to ensure that

tasks scheduled for the weekend that were not completed were rescheduled

for the subsequent week.

M1.4 Imoroner Documentation of Test Instrument Connections

a. Insoection Scoce (62707)

As part of the installation of MAR 96-10-05-01 on EDG-1A. a Dranetz data

accuisition system was installed to perform post modification testing

4

anc future testing. During review of the post installation work

package, the licensee discovered that the documentation for the

installation had not been completed by the relay technician.  !

b. Observations and Findinas

PC 97-738 was written on February 3,19?;7. to identify this failure to

document the completion of the work. The apparent cause determination J

that the licensee made determined that poor communications between the )

project manager and the relay technician had not clearly identified the -

need to complete the documentation.

The inspectors interviewed the project manager and reviewed the

installed system data from the previous diesel test runs. The data were

within the expected range. Discussions with the licensee revealed that,

if the system had been connected incorrectly, no data would have been

received. The relay technicians routinely installed this equi) ment at

both the nuclear site and at the fossil units. According to t1e

licensee, this was normally considered within the skill-of-the-craft for

relay technicians. The instructions were developed for electrical l

maintenance and I&C technicians, who do not normally install these

instruments, by the technician who performed the installation.

1

c. Conclusions l

As a result of the incomplete documentation for a MAR package .

completion, the need for better communications has been identified by

the licensee. The test instrument has been verified to have been "

properly installed. No further actions are required.

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M1.5 Testina of Toxic Gas Chlorine Monitors

a. Insoection Scope (61726. 37551)

The licensee has proactively been performing testing on a station

constructed to re)roduce the installed toxic gas chlorine monitor. This

initiative was tacen in an effort to increase reliability of the

installed system. The inspectors have been monitoring these tests,

witnessing the efforts of the engineering staff conducting the tests.

b. Qbg_r.y_qt

b r Ions and Findinas

Testing revealed a lack of repeatability for time response testing of

the system. The acceptance criteria was 15 seconds from receipt of the

chlorine at the remote sensor until completion of the control room

emergency ventilation system switching to recirculation mode. Normally,

per PT-366. Toxic Gas Detection System Calibration (Train A) and PT-367.

Toxic Gas Detection System Calibration (Train B). time response testing

is performed immediately following span testing, which supplies chlorine

test gas to the sensor. On February 10. 1997, the licensee performed

the span test but elected to wait until the next day to perform the

response time test and to evaluate the effect of not having put chlorine

gas previously on the sensor. This was the condition that would exist

on a valid chlorine gas actuation. Without the span test being

performed immediately prior to performing the response time test. the

response time test failed.

Further tests revealed that when the sensor was exposed to chlorine

prior to the response time test, the response times were reduced. PC

97-978 was written on February 12, 1997, to document that the toxic gas

chlorine monitors may need to be exposed to chlorine for an unknown

period of time before they can respond fast enough to pass the 15 second

acceptance criteria. By performing the span test 3rior to the response

time test. the system was preconditioned to pass t1e response time test.

As a result, the licensee declared both trains of chlorine monitors

inoperable and placed the control room emergency ventilation system in

the recirculation mode. The licensee was evaluating installed designs

at other licensee's facilities in an attempt to identify a reliable

design. The licensee indicated a plan to install a reliable system

prior to restart from the current outage.

Te-Snical Specification 5.6.1.1 requires, in part, that procedures be

developed and implemented covering activities as recommended in

Regulatory Guide 1.33 Appendix A. Revision 2 of February 1978. Among

these are surveillance procedures for each surveillance test listed in

the technical specifications. The design basis, as defined in the Final

Safety Analysis Report (FSAR), Section 9.7.3.1. for the Control Room

Emergency Ventilation System (CREVS). included two trains of toxic gas

chlorine monitors which were to be operable at all times. This was to

allow the system to maintain control room habitability during a toxic

gas release. Technical Specification Surveillance Requirement 3.7.12.3

_. . _

19

required that the licensee verify each CREVS train actuates to the .

emergency recirculation mode on an actual or simulated actuation signal,

at least once per 24 months.

c. Conclusions l

The inadequate procedure, which allowed the preconditioning of the

chlorine sensor, prevented an accurate response time test from being

performed. The licensee took prompt corrective actions by declaring the

toxic gas monitors inoperable and placing the CREVS in the recirculation

mode. The licensee was actively pursuing long term corrective actions <

by working with the sensor manufacturer and consulting engineers. This ,

licensee identified violation meets the requirements outlined in Section

VII of the Enforcement Policy and will not be cited. This issue is

'.

identified as Non-Cited Violation NCV 50-302/97-01-05. Inadequate i

Surveillance Procedure to Test Operability of the Toxic Gas Chlorine  !

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Detectors.

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M1.6 Schedulino of Work on Non-Nuclear Instrumentation  ;

a. .[0.s.pgqtion Scooe (62707)

On February 4.1997, the licensee identified that the weekly work

schedule had clearances being placed on the pressure transmitter

isolation valves for Instruments RC-132-PT and RC-131-PT1.

'

b. Observations and Findinas

Work packages were taken to the main control room for approval to begin

4

work. The operations SSOD identified that neither the work packages (WR

, NU 0337967 for RC-131-PT1 and WR NU 0337968 for RC-132-PT) nor the

schedule provided any indication or recognition that the transmitters ,

provide in)ut signals to the Power Operated Relief Valves (PORVs) and l

'

the Decay deat drop line auto closure initiation. The PORV is required

to be operable in modes 1. 2 and 3. The Auto Close Initiation system is

recuired to be operable in modes 1. 2. 3 and 4. In the present plant

moce. neither system was required to be operable. However, this was not

'

clear on the work request packages, and no evaluation had been completed

for the impact of removing these instruments from service. The SSOD

refused to authorize the work packages until a full evaluation of the

impact of the isolation of the instruments had been completed.

!

c. Conclusions

Scheduling of work packages which do not identify the impact on plant

conditions and provided work packages to the field operators who do not '

recognize the impact of the task is a recurring problem. This is

identified as a weakness in the implementation of the work planning

program.

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20

M1.7 Unolanned Alarm Durina Instrumentation and Controls Work

a. Insoection Scope (62707)

On February 3, 1997, an annunciator alarm was received in the main

control room for feedwater control valve air failure. At the time of

the incident, the unit was in mode 5, and feedwater was not in

operation. The alarm was not expected as the result of any work in

progress. At the time the alarm was received, the inspector was in the

control room and witnessed the licensee's response.

b. Observations and Findinas

Investigation revealed that I&C technicians were performing work on FWV- -

39, which caused the alarms. It was confirmed that the operations work

controls supervisor was aware of the work in progress, but he was not

aware of any ex)ected alarms. The inspector questioned the I&C

technicians. T1ey were not aware that the alarm would result from the

task they were performing and the WR did not indicate that an alarm

would be received.

c. Conclusions

Several events contributed to the operators not being aware that an

alarm might be received. Although the work controls supervisor was

aware of the work in progress, the operations shift was not. The lack

of indication on the work package contributed to the confusion. The

inspectors identified that even though the mechanisms exist to include

warnings about these observed problems in the work packages, the lessons

learned are rarely considered when planning a work package. Instead,

the process relies on the technicians and operations review to identify 1

problems. This lack of thorough evaluation is another example of the  !

weakness in the implementation of the work planning program identified i

in paragraph M1.6. 1

M8 Hiscellaneous Maintenance Issues

M8.1 (Ocen) URI 50-302/96-17-03. Failure to Conduct Reauired Technical

Soecification Surveillance Testina on Safety Related Circuitry I

a. Insoection Scoce (37551. 92902)

On January 31. 1997, the licensee identified that test deficiencies

existed in licensee Procedures SP-907A Monthly Functional Test of 4160V

ES Bus "A" Undervoltage and Degraded Grid Relaying and SP-907B, j

Monthly Functional Test of 4160V ES Bus "B" Undervoltage and Degraded

'

Grid Relaying.

,

b. Observations and Findinas

The test deficiency identified that contacts in all three channels of

the first level undervoltage relays (FLUR) and second level undervoltage i

21

relays-(SLUR) were not being tested in accordance with the TS  :

requirements. The FLUR and SLUR relay contacts were subsecuently tested .;

satisfactorily in accordance with the TS. This issue is-icentified as. i

an additional example of URI 50-302/96-17-03. Failure to Conduct

Required Technical Specification Surveillance Testing on Safety Related  !

Circuitry, pending completion of the licensee's review under Generic  !

Letter (GL) 96-01.  !

.

c. Conclusions

No further actions are required at this time. URI 50-302/96-17-03'

remains open pending completion of the licensee's GL 96-01 review and l

.the inspectors' assessment of the findings. l

JJL. Enaineering 5

El Conduct of Engineering I

El.1 General Comments (37551) j

The inspectors reviewed various Engineering and support activities which I

included presentations to licensee management on January 31 1997 'and i

February 11. 1997, by the Emergency Diesel Generator (EDG) and Emergency

Feedwater (EFW) Interim Fix Option Team. The team was chartered to

assess the feasibility of starting the plant up with the interim 150 Kw 1

load upgrade but prior to the )lanned long term larger upgrade of the . 1

EDG capacity. The inspector o) served that this was a multi-disciplined

team, which took a conservative and questioning approach to the design

basis challenges that must be resolved before those systems would be

acceptable for restart. The inspector concluded the team was being very

realistic and appropriately involved Framatome vendor support to address

design issues.

The inspectors also reviewed activities associated with resolution of

corroded primary valve seats and difficulties in obtaining an effective

vent of decay heat system piping. Engineering personnel provided good ,

} support for the remainder of the reviewed or witnessed activities.

Activities were found to be adequate, well controlled, and documentation

usually provided sufficient detail and appeared technically adequate.

Additional details regarding notable issues are described below.

E1.2 Non-Safety Related Comoonents in Safety Related Acolications j

I

'

a. Insoection Scone (37551. 92903)

The inspectors reviewed the licensee's investigation and corrective

actions for an issue identified where non-safety related components were

used.in a safety related application.

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22

b. Observations and Findinas

During a review of the licensee's 10 CFR 50 Appendix R program, the

licensee identified a need for voltage protection on current

'

transformers (cts) installed on several systems. The decision was made

to review MAR 77-07-01-14, which was installed in 1985 as a part of the

Ap)endix R upgrade. The secondary protection installed as part of this

' MAR 3rotected the Cts which provided remote indication of amps. vars.

'

and (ilowatts for the EDGs in the main control room. During the review.

. the engineer identified that these protectica devices were neither

seismically qualified nor procured as safety related.

PC 97-0050 was issued on January 9.1997, to document this finding. At

that time, the EDGs were evaluated to be conditionally operable /

potentially inoperable, pending the final review of the impact of the

non-safety related devices being installed. This was based on the

assumption that in mode 5. loading would be greatly reduced and load

management (which requires the kilowatt indication) would not be

necessary.

On January 21, 1997, it was identified that although the load demands in

mode 5 would be low, the controlling procedure for a load management  ;

during a loss of offsite power (LOOP) event would be AP-770. Emergency i

<

Diesel Generator Actuation. This procedure did not address the reduced i

load demands and could lead to overloading the diesel generators, if no

kilowatt indication was available. The shift supervisor declared both

diesel generators inoperable and entered TS action statement 3.8.3.

EDG-1A was already inoperable for preplanned maintenance and

modifications.

4

The licensee continued evaluating the devices while the Operability

Concerns Resolution (OCR) was completed. A spare protector was

disassembled and inspected. The device is a thyrite type of device

which prevents voltage surges which could damage circuitry. The device

was also supplied to an independent contractor for evaluation.

The contractor concluded that the device would perform its intended

function both during and following a seismic event. The licensee issued

the completed OCR on January 26, 1997, and concluded that the diesels

were operable, but degraded. EDG-1B was declared operable. but EDG-1A

remained inoperable pending completion of the ongoing diesel outage.

r

The licensee is currently evaluating replacement protectors and the

necessary requirements to upgrade the existing protectors to safety

related.

In a second example during preparation to replace MUV-103, the

Engineered Safeguards (ES) isolation valve between the makeup system and

the Reactor Coolant Bleed Tanks (RCBT). the boric acid storage tanks

(BAST). and the demineralized water supply, the licensee discovered that

the installed operator and controller for this safety related valve were

non-safety related. In the licensee's accident analysis, this valve was

.

23

assumed to isolate for a moderator dilution event. With the non-safety

related components installed, this valve cannot be assured to operate

when required. The licensee plans to replace this valve prior to

restoring the makeup system and has added it to their restart restraint

list.

c. Conclusions

The inspectors concluded that these problems were further examples of

inadequate design control. The licensee has taken the necessary

immediate corrective actions and has added final resolution of these

issues to the restart restraint list. This licensee identified

violation meets the requirements outlined in Section VII.B. of the

Enforcement Policy and will not be cited. This issue is identified as i

Non-Cited Violation NCV 50-302/97-01-10. Inadequate Design Control. Non-

Safety Related Components in Safety Related Applications - Two Examples: .

Thyrite Surge Protection Device. Operator and Controller for MUV-103.

El.3 HPI System Modifications to Imorove SBLOCA Marains

a. Insoection Scoce (37550)

In a letter to the NRC dated October 28, 1996, the licensee described

eight design issues that would be addressed prior to restarting the

plant. Design Issue 2. high pressure injection (HPI) system

modifications to improve small break loss of coolant accident (SBLOCA) I

margins, described improving design margins in the HPI system by adding l

flow limiting venturies and crossover piping. However, the licensee

stated that these modifications would not be made prior to restart

because the HPI system currently met its design and licensing basis.

During this inspection the inspector reviewed some aspects of the HPI l

'

system to verify that it did currently meet its design and licensing

basis.

b. Observations and Findinas

l

(1) Peak Claddina Temoerature Exceedina 2300 Dearees F

The inspector reviewed the Final Safety Analysis Report (FSAR).

)aragraph 6.1.1. Emergency Core Cooling System (ECCS) Design

3ases, and noted the following statements:

" Assuming the loss of one core flood tank (CFT) and using

the ground rules specified in Part 4 of Appendix A of the

Interim Acceptance Criteria (where the CFT water is assumed

to be lost after the end of blowdown), the 8.55 square foot

cold leg split results in a cladding temperature rise

exceeding 2300 degrees F because of the long adiabatic

heatup period. The above case assumes the loss of one CFT

coincident with the failure of a diesel. This amounts to a

simultaneous active and passive failure. If only the

passive failure was considered, that is, credit was taken  ;

. . _ _ _ . . . _ . _ _ _ _ _ ._ _ _ _ _ . _ _ _ _ _ _ .

!

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-for both' low pressure injection (LPI) and high pressure [

injection (HPI) pumps, the cladding temperature could be~  !

held below 2140 degrees F if expected rather than design i

peaks are employed." --;

,

The inspector's concern with these statements was that they were [

'

not-consistent with the current design requirements. 10 CFR [

.

50.46. Acce)tance Criteria for Emergency Core Cooling Systems l

-(ECCS) for _ight Water Nuclear Power Reactors, requires that the 1

peak. cladding temperature (PCT) shall not exceed 2200 degrees F >

'

for all design basis events. Also. 10 CFR 50, Appendix A. General i

Design Criteria for Nuclear Power Plants, requires that plants be

!s designed against an initiating event (i.e., a break in a core i

flood tank line) concurrent with a single failure (i.e., failure  :

of a diesel generator). However, the aoove FSAR statements

indicated that, for.such a design basis event, the PCT could l

l

exceed 2300 degrees F. -l .

'

The inspector informed the licensee of this concern, and i

'

subsequent licensee and ins)ector review of design and licensing i

.information revealed that t1e FSAR statements were incorrect.

4

Supplement No. 4 to the Safety Evaluation Report by the Office of i

Nuclear Reactor Regulation, dated January 28, 1977, stated that  !

Babcock and Wilcox had provided revised ECCS 3erformance  :

calculations for the worct case break using tie revised evaluation

model which demonstrated that the PCT and the percent of local and

,

core-wide metal-water reaction remained below the limits specified

. in 10 CFR 50 46.~ Supplement 4 further concluded that the analysis i

of the ECCS performance conformed to the acceptance criteria in 10 l

CFR 50.46. The inspector verified that the Babcock and Wilcox

'

i revised ECCS performance calculations (BAW-10103. Rev. 3. Topical

'

Report of 1977) did conclude that the worst case LOCA was an 8.55

square foot cold leg split, which resulted in a PCT of less that

c 2200 degrees F. Further. BAW-10103 calculations did include

,

failure of a diesel generator concurrent with the LOCA.

i Based on the results of this review, the licensee initiated a

, change to correct the FSAR. The inspector verified that the

incorrect statements had been in the FSAR since 1973, prior to

plant licensing. The inspector also verified that the licensee

initiated PC 97-0784 on January 30, 1997, to address the error in

the FSAR. Since the error was an old design issue in the original

, FSAR that was reviewed by the NRC prior to licensing of the plant.

< and the licensee promatly initiated corrective actions. the

,

inspector concluded tlat enforcement action for this FSAR error

i

was not warranted.

,

4

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_ _ - _

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25

':

(2) Reauired 00erator Actions for SBLOCA Mitiaation

(a) FSAR Revision 23 Increased the Number of Reauired Operator  !

Actions i

The inspector reviewed FSAR paragraph 6.1.3.1.1,. Design

Evaluation of the HPI System for RCS Cold Leg Small Break '

LOCA: FSAR paragraph 6.1.3.1.2. HPI Line Break Small Break

LOCA: and FSAR paragraph 14.2.2.5.7 Small Break LOCA: and

noted that changes recently made. in Rev. 23. included:

Rev. 23 added two required operator actions to mitigate a

SBLOCA event concurrent with the failure of an EDG. It

described the following required operator actions:

(1) Within 10 minutes after event initiation. the operator

must' select an alternate power supply and open two >

injection valves. This operator action was in the i

previous FSAR revision.

3

(ii) Within 20 minutes after event initiation. the operator l

must isolate normal makeup flow and also isolate RCP  ;

seal injection flow. These two operator actions were I

not in the previous FSAR revision, j

l

Rev. 23 added a required operator action to isolate an HPI l

injection line that was broken (with flow substantially l

higher than the other injection lines). The previous FSAR l

revision included a required operator action to balance i

flows in the HPI injection lines - that operator action was

replaced by the new required action of isolating an

injection line that was broken.

Also, Rev. 23 added a required o)erator action in the event

of a LOCA in the letdown line, w1en the operator would be  !

required to isolate letdown flow. This operator action was

not in the previous FSAR revision.

FSAR Rev. 23 also stated that HPI flow to the core during

the first 10 minutes after event initiation (with concurrent

failure of an EDG) would be only 36% of the total HPI flow. .

After the operator opened the two remaining injection l

valves. HPI flow to the core would increase to a greater j'

percentage of total HPI flow. The previous FSAR revision

stated that HPI flow to the reactor must be the ecuivalent

of 70% of the flow of one HPI pump, and that woulc be

achieved by four injection lines with one HPI pump.

The inspector concluded that FSAR Rev. 23 increased the

number of required operator actions for SBLOCA mitigation

(from two to five). Also, Rev. 23 described a reduced

__ __ __ _ . ._____ __ . . _ _ _ .- _ _ .. _

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26 .,

amount of HPI flow.to the reactor, higher peak clad  ;

-temperatures, and. higher offsite doses. .

(b) HPI Licensino Basis in 1979 Included One Ooerator Action )

The inspector reviewed licensing information, which included'

various letters between the licensee and the NRC leading to  ;

an NRC Safety Evaluation. dated May 29, 1979. The Safety  !

Evaluation concluded that the licensee's small break LOCA

analysis and ECCS design were in conformance with the l

requirements of 10 CFR 50.46 and noted that the design  ;

included an operator action to initiate HPI to two injection  :

lines within 10 minutes. In addition, the Safety Evaluation i

stated that the operator action will provide a minimum of j

four injection lines and one HPI pump, which will provide at  :

least the 70% of the flow of one pump to the reactor that  ;

the licensee determined was needed. The Safety Evaluation i

'

also stated that all three HPI pumps are automatically-

started when the ES signal is actuated. (The licensee's ,

current design included starting only two HPI pumps on an ES

'

signal.) In a )revious licensee letter on ECCS Small Breaks i

Analysis dated rebruary 28, 1979, the licensee stated that  !

operator actions to isolate normal makeup or RCP seal i

injection were not needed, because the normal makeup is

isolated automatically on an ES signal and without isolating

RCP seal injection more than 70% of the flow from one HPI l

pump is available as injection into the RCS. In a letter

dated October 9, 1978, the licensee stated that analyses  ;

were being performed to determine if operator action was  ;

needed to balance the HPI flow in the injection lines and  ;

that if balancing was required, then the licensee would  !

install flow limiters to preclude the need for such operator l

action. In another letter dated November 7,1978, the

-

licensee stated that the analyses showed that no operator i

action was needed for flow balancing in the HPI injection l

'

lines. In summary, the NRC had licensed the licensee's ECCS

system design with provision for one operator action within  !

10 minutes which would ensure at least 70% of the flow of I

one HPI pump to the reactor. l

The inspector concluded that the licensing basis from 1979 ,

included only one required operator action for SBLOCA

mitigation. ,

(c) 'SBLOCA Calculation in 1996 Included Seven 00erator Actions

The inspector reviewed the licensee's current calculation '

for Small Break LOCAs. M96-0032. Reevaluation of HPI

Requirements During Small Break LOCAs, dated May 2,1996.

This calculation was also identified as Framatome i

Technologies Incorporated (FTI) calculation 51-1245866-00.  !

The calculation stated that seven operator actions were {

f

!

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. - . .- --

- -

27

required to mitigate the spectrum of small break LOCAs: 1)

trip all running RCPs within two minutes. 2) initiate HPI

flow through all four injection lines within 10 minutes, 3)

isolate letdown within 10 minutes. 4) isolate RCP seal

injection within 20 minutes, 5) isolate normal makeup within

20 minutes, 6) ensure adecuate HPI flow within 20 minutes,

and 7) ensure adequate EFk flow within 20 minutes. The

calculation also stated that during the performance of the

hydraulic analyses. FTI discovered that the HPI flows

provided by the licensee's system were less than the HPI

flows used in the FTI analysis of record for cold leg pump

discharge breaks. This flow deficit was primarily due to ,

the generic B&W plant modeling assumptions in the FTI

'

analysis of record (i.e., normal makeup and RCP seal

injection automatically isolated on ESAS) and not accounting

for the time delay involved in the licensee's operator

actions to manually isolate normal makeup and RCP seal

injection.

'

The inspector concluded that the SBLOCA calculation of 1996

included seven required operator actions for SBLOCA

mitigation. l

The seven required operator actions in the 1996 calculation were 1

more than the one required operator action in the 1979 licensing  !

basis. The seven were also more than the five required operator

actions in the recent FSAR Rev. 23 and more than the two required

operator actions in the previous FSAR revision. The inspector

noted that the increase in required operator actions may represent

a potential increase in the probability of occurrence of a

malfunction of equipment important to safety and therefore, per 10

CFR 50.59, prior NRC review and approval would be requireo.

However, the inspector considered that further review of ti.is

issue was needed to determine if any of the added operator actions

had been reviewed and approved by the NRC between 1979 and 1996.

In addition. inspector review was needed of any procedure, plant

design, or FSAR changes (and related 50.59 safety evaluations)

that added required operator actions or deleted automatic actions.

This issue is identified as the first example of URI 50-302/97-01-

06, HPI System Design, Licensing Basis, and TS Concerns.

1

(3) HPI Desian Not Consistent With Licensino Basis

The inspector noted that Calculation M96-0032 identified a design l

control error with the HPI system. It stated that the licensee's I

licensing submittals on HPI system design and SBLOCA in 1978 and

1979 (and the NRC SER in 1979) incorrectly assumed that normal

makeup and RCP seal injection were automatically isolated at

Crystal River 3. (The 1979 B&W SBLOCA calculation, on which CR3

relied, assumed that normal makeup and RCP seal injection were l

automatically isolated based on a generic B&W plant.) However, l

the CR3 design did not include automatic isolation of normal

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28

makeup and RCP seal injection. Consequently, the CR3 design would

su) ply less HPI flow to the reactor than assumed in the 1979 B&W

SB_0CA calculation. Calculation M96-0032 stated that isolation of

normal makeup and seal injection was necessary to keep peak clad >

temperatures for a design basis SBLOCA telow 2200 degrees F. The

inspector concluded that the CR3 HPI system was apparently outside

its licensing basis from 1979 through 1997. The inspector also

considered that further review was needed of the consequent impact

on HPI system operability during the period of 1979 throagh 1997

(including what operator actions were included in E0Ps). This

issue is identified as the second example of URI 50-302/97-01-06.

HPI System Design Licensing Basis, and TS Concerns.

(4) HPI Desian Not Consistent With TS

The inspector noted that the CR3 TS included LC0 allowable outage

times for one train of HPI but included no allowable outage time

for both trains of HPI. However, the CR3 HPI system design

included several motor operated valves that were in both trains of

HPI (i.e.: MUV-3 and MUV-9. HPI pump discharge crosstie valves:

MUV-23. MUV-24. MUV-25. and MUV-26. HPI injection valves: and MUV-

27. normal makeup valve). All of these valves had required

surveillances (i.e. , quarterly stroke time tests) and maintenance

(i.e., gearbox & grease inspection). Initial inspector review

indicated that the licensee may have performed some of these j

surveillance or maintenance activities while the HPI system was i

required to be operable. The inspector considered that further (

review was needed to determine when these valves were out of  !

service for surveillance testing cr maintenance with the plant in j

Mode 4 or above during the last three years, and in each case how '

TS compliance was affected. This issue is identified as the third i

'

example of URI 50-302/97-01-06. HPI System Design. Licensing

Basis, and TS Concerns.

(5) Licensee Desian Bases and FSAR Reviews Did Not Identify These

.1ssies

As 3 art of the licensee's extent of condition review for design

pro)lems, the licensee was constructing time lines for selected

safety systems. The time lines would, for example, review changes

'

to the systems from the initial licensing basis (i.e.,

modifications, operating procedure changes, licensing basis

changes. FSAR changes. TS changes) to assure that the licensing

and design bases had been maintained.

The inspector reviewed the licensee's time line for the makeup /HPI

system that had been completed on February 10. 1997, and noted

that the time line identified a number of good questions and

potential issues. However, the time line did not identify any of

the issues raised by the inspector in URI 50-302/97-01-06. HPI

System Design. Licensing Basis and TS Concerns.

-. - . _ - -

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29  ;

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The inspector also noted that the licensee's current FSAR review '

project had not identified the above FSAR error (regarding peak  !

cladding temperature exceeding 2300 degrees F). The licensee's l

FSAR reviewer stated that the review was focused on verifying that  !

FSAR information was implemented in operating, surveillance, and I

maintenance procedures: system DBDs: and TS. However, the review

basically assumed that information in the FSAR was correct. The l

reviewer stated that, therefore, the FSAR review would not have i

been expected to identify such errors in the FSAR. j

i

c. Conclusions i

,

i

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l An unresolved item was identified regarding the design of the HPI

i system: URI 50-302/97-01-06. HPI System Design, Licensing Basis, and TS j

Concerns. Inspector concerns included the following.

1

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Since 19'9 6, seven operator actions were identified for SBLOCA

i mitigation: however, the licensing basis since 1979 contained only

one operator action.

- Prior to 1996 the licensee's SBLOCA analysis incorrectly assumed

that RCP seal injection and normal makeup were automatically

isolated.

- The effect on system operability was not assessed with both HPI

trains sharing several active components.

In addition, the inspector noted that the licensee's recently completed j

extent of condition review (time line) for the makeup /HPI system design '

did not identify any of the inspector's concerns.

An error in the FSAR was identified, where the FSAR stated incorrectly )

that for a design basis accident the peak cladding temperature would j

exceed 2300 degrees F (the regulatory limit is 2200 degrees F). In  :

addition, the inspector noted that the licensee's current FSAR review l

project had not identified this FSAR error. ,

!

Since this issue was left as an unresolved item with more inspection

needed to reach conclusions. the inspector did not at this time assess  ;

the licensee's performance with respect to this issue in the five NRC l

continuing areas of concern. l

1

El.4 10 CFR 50.59 Safety Evaluations

a. Insoection Scone (37550) l

The inspectors reviewed 10 CFR 50.59 safety evaluations for recent

engineering products to assess their adequacy.

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b. Observations and Findinos

.

i The inspectors reviewed 10 CFR 50.59 evaluations for one modification. l

!

MAR 96-10-04-01. Installation of Overpressure Protection for Isolated  !

Piping Sections'(GL 96-06). dated January 3. 1997: and for one design

basis document change. EDBD TC No. 536. HPI Flows and BWST Circulation.

' dated January.16'. 1997: and assessed both as adequate, thorough, and  :

detailed. The inspectors also reviewed the.10' CFR 50.59 evaluation for  !

'

an FSAR change. FSAR Table 6-1 Correction dated January 24, 1997, which

involved core flood tank level and 3ressure; and-noted that it lacked ,

l < sufficient clarity and detail to mace a determination on acce)tability.  :

Overall the inspectors noted improvement in the quality of t1e recent i

50.59 safety evaluations reviewed over those of one - two years ago. ,

The inspectors reviewed a 10 CFR 50.59 screening for MAR 94-09-02-01. DC  ;

I

Cooling Instrument Enhancements, dated June 27. 1996, which involved

non-safety instrument air to DCV-7. 18, 177, and 178. The inspectors

assessed this 10 CFR 50.59 screening as having a lack of sufficient

detail to support the conclusion that a full 10 CFR 50.59 safety

evaluation was not required.

c. Conclusions

The inspectors reviewed a small sample of 10 CFR 50.59 safety

evaluations for engineering products and noted improvement in the

cuality and thoroughness over those generated one - two years ago.

towever, the sample size was small and therefore, further review will be

needed to verify adequacy of the overall 10 CFR 50.59 program.

The inspector assessed the licensee's performance, with respect to this

issue, in the five NRC continuing areas of concern:

  • Management Oversight - Good

. Engineering Effectisteness - Good

. Knowledge of the Design Basis Good

. Compliance with Regulations - Good

. Operator Performance - N/A

E1.5 Decay Heat Valve (DHV) 21 00erability Evaluation

a. Insoection Scone (37551)

The inspectors reviewed the licensee's investigation and disposition of

internal corrosion found on DHV-21. the pump inlet manual isolation

valve for decay heat pump (DHP) 1A.

b. Observations and Findinos

The licensee discovered significant seat leakage while draining DHP-1A

for maintenance on January 20. 1997. Upon disassembly the licensee

observed severe localized corrosion of the seat rings that were

determined to be made of carbon steel. Vendor drawings for the valve

_ _ - _ - - _ _ , _ _

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indicated that the seat rings should be constructed of 316 stainless .

steel, the correct material for this primary system application. The  :

licensee appropriately generated precursor card (PC) 97-0472 to

implement corrective action and identified 3 other identical valves that ,

were used in the plant. DHV-32.' the inlet isolation valve to DHP-18.  !

was used in January. 1997, as a boundary valve for pump work and had not

exhibited any seat leakage. The other two valves. DHV-39 and 40. which 1

are the pump suction valves on the lines from the reactor coolant j

system, were also verified to be seating properly during recent. ,

maintenance evolutions. The licensee was confident that the seats in

these valves were stainless steel based on this performance, but they

still plan to inspect DHV-32 as a precautionary measure during the B

train emergency systems outage scheduled for the week of March 10, 1997.

The licensee was unable to procure a replacement valve for DHV-21 from  !

the vendor quickly, and the corrosion damage coupled with high local

radiation dose rates made repair unfeasible. Consequently, the licensee ,

initiated an Operability Concerns Resolution document to investigate i

. whether the DH system could be considered operable with the valve

reassembled and the seating surface _ removed. The licensee removed all

loose seat material and corrosion 3roducts to ensure they were not

entrained into the RCS and reassem) led the valve. The investigation '

revealed the valve was not required to close for any safety function, so

its inability to close was acceptable until a permanent repair or

replacement option could be determined. The ins)ector observed that the

licensee's. primary consideration was restoring tie out of service decay  ;

heat removal train in order to reestablish two redundant methods of  :

decay heat removal. The inspector reviewed the licensee's 10 CFR 50.59  ;

assessment and safety evaluation and did not identify any deficiencies.

Identification of a permanent fix was still pending at the end of the '

report period.

c. Conclusion .

!

The inspector concluded the licensee displayed an appropriate priority  !'

to restore a second decay heat removal system to service and performed a

thorough and conservative analysis to justify the decision to leave an

inoperable manual valve in the system and evaluate extent of condition.

The inspector assessed the licensee's performance, with respect to this l

issue in the five NRC continuing areas of concern. ,

e Management Oversight - Good i

e Engineering Effectiveness - Good  ;

e Knowledge of the Design Basis - Good

. Compliance with Regulations - Good -

. Operator Performance -

N/A l

t

i

i

.

6

m.. a .n ., - .- ,,.

__

,

i

32

E1.6 $ valuation of Dranetz Test Instrument Inaccuracies on Emeraency Diesel i

'

Generator Testina

a. Insoection Scoce (37551)

The inspectors reviewed the licensee's investigation and disposition of

EDG test instrument inaccuracies contained in Operability Concerns

Resolution (OCR) Report EG-97-EDG-1A/1B and interviewed licensee

Technical Support Engineering managers and engineers,

b. Observations and Findinas

The OCR was primarily concerned with whether the EDGs exceeding maximum

load limits during full load testing and if they satisfied the

surveillance requirements (SR). ' 1.8.1.11 requires a maximum load

test at a load between 3100 and 3200 kw be 3erformed every 24 months.

This test was last done in April, 1996, on ]oth EDGs using the Dranetz

test instrumentation. However, instrument error from the Dranetz was

not factored in to the testing, and consequently the testing bands were

identical to the SR band of 3100 to 3250 kw. This oversight was

discovered by a licensee engineer in January.1997, while preparing a

post-modification test tc support corrective actions to upgrade EDG

capacity. The engineer questioned why the normal load test in

Surveillance Procedure (SP) 354A/B had a narrower test band to account

for instrument error while the maximum load test did not. Based on this

concern, the licensee initiated the OCR and performed a calculation and I

testing to determine the reliable accuracy of the Dranetz  ;

instrumentation. The OCR investigation was com]lete on February. 19, i

and revealed that a calculated error of +/- 54 (w was necessary to be

a) plied to the April, 1996, testing. After review of the testing data.  !

tie licensee determined that the worst case low (logged reading minus 54  ;

Kw) results for both EDG A and B were intermittently below the lower  !

testing limit of 3100 Kw. The licensee conservatively determined the )

'

EDGs were previously inoperable because they had not fulfilled the

requirements of SR 3.8.1.11 and that a Licensee Event Report (LER) per i

10 CFR 50.73 was required. The A EDG had been tested satisfactorily in

January,1997, with revised Dranetz limits so it remained operable. The i

"B" EDG was scheduled to be tested the weekend of February 22. to j

restore its operability. The OCR and calculation developed an im) roved '

1

Dranetz inaccuracy of +/- 38 Kw based on a different test probe tlat was

used for this subsequent testing.

The OCR also determined that the worst case high (logged reading plus 54

Kw) results for both EDG A and B were intermittently above the upper

testing limit of 3250 Kw which also corresponds to the EDG 30 minute

rating. They determined EDG A had ootentially exceeded the limit for 6

minutes and EDG B had for 15 minutes during the April,1996, testing.

The OCR contained a detailed justification for continued o)eration in

Mode 5 that assessed the potential degradation this would lave on the

ability of the EDG to accomplish its function. The inspector reviewed

this justification, found it very detailed, and did not identify any  :

-

problems with the licensee's conclusions that the EDGs were operable for

-

)

_ . . - .

,

,

.

k

l

l I

.;

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33  !

t

Mode 5 loading with the given portion of the 30 minute rating used. The l

l licensee plans to perform outage inspections of both EDGs during their i

! current outage which will reset the 30 minute ratings to a full 30 i

minutes.

c. Conclusions l

l

'

The ins)ectors were concerned that the EDGs were potentially inoperable

since tle last refueling outage in 1996. However, the >roblem was found j

l

by the licensee while developing a functional test whici was corrective  !

l action for a previously cited problem with EDG loading capacity. I

i Corrective action since discovery has been timely and EDG A has already l

, been retested. The inspector concluded the OCR involved large amount of 1

l -detailed and thorough engineering work and provided a well defined plan  ;

that had operations staff involvement. Therefore, this issues an is .

considered example of a problem found as corrective action for a i

previous problem. l

The. inspector assessed the licensee's performance, with respect to this

issue, in the five NRC continuing areas of concern.

l

  • Management Oversight - Good i

. Engineering Effectiveness - Good

. Knowledge of the Design Basis - Good

e Compliance with Regulations - Good .

'

  • Operator Performance - Good

E2 Engineering Support of Facilities and Equipment

E2.1' Corrective Action and Reportability Issues

a. Insoection Scooe (92903)

The NRC had identified a number of concerns with corrective action and

reportability as noted in apparent violations EEI 50-302/96-12-03 and

EEI 50-302/96-19-02. As part of the followup for these issues, the

inspectors reviewed the licensee's recently issued corrective action

Procedure CP-111. Processina of Precursor Cards for Corrective Action

Program. Revision 55 relative to the definition of a DBI as defined in

the procedure.

b. Observations and Findinas

The definition of a DBI was detailed in paragraphs 3.1.3 and 3.1.4 of

Procedure CP-111. The definition given was the same as that in

Procedure CP-150. Identifying and Processing Operability Concerns and

Procedure CP-151. External Reporting Requirements.

The definition. as written in the above procedures, equated a DBI with

o>erating outside the design _ basis as referenced in 10 CFR 50.72 and 10

C:R 50.73.and indicated that a DBI exists only if a system, structure,

or component (SSCF is unable to perform its safety function in

l

__. . . .- .

_ . __. __ _ _

-

i

'!

'

- 34

2  ;

preventing or mitigating design basis events. The inspectors. pointed t

i

out that this definition appeared to be narrow, considering the  ;

i definition of design basis given in 10 CFR 50.2 and the requirements of.  ;

10 CFR 50. Appendix B. Criterion III. relative to design control. When  ;

questioned by the . inspectors the Manager. Nuclear Licensing stated that - ,

- the definition was not meant to be that narrow, but he could see how it

could be interpreted that way. He stated that the definition would be i

revised to state more clearly what was intended.

c. Conclusions fi

! - The definition of a DBI. as defined in Procedures CP-111. CP-150. and

i

'

CP-151 was not broad enough to ensure that the requirements of 10 CFR ,

50. Appendix B. Criterion III.'10 CFR 50.72 and 10 CFR 50.73 would be i

met. The licensee agreed the definition did not clearly state their

intent and stated that procedures would be revised to clarify their

.

intent.  ;

The inspector assessed the licensee's performance, with respect to this

3

issue, in the five NRC continuing areas of concern- i

I

,

e Management Oversight -

Adequate  :

.

.- Engineering Effectiveness - N/A .

Knowledge of the Design Basis

'

. -

N/A  !

e Compliance with Regulations -

Adequate

Operator Performance

'

e -

N/A

E8.1 (Closed) VIO 50-302/96-05-05. Failure to Follow Procedures for Vodatina

QBian Basis Documents (DBDs)

a. Insoection Scoce (92903)

.

This issue involved failure to issue a Temporary Change (TC) to the

Enhanced Design Basis Document (EDBD) and failure to ensure that TCs to i

the EDBD were incorporated into the EDBD as required by procedures. The  !

'

licensee's letter of response dated August 12. 1996. was reviewed and

found acceptable. The inspectors reviewed the licensee's corrective

i actions as detailed in paragraph b. below.

,

b. Observations and Findinas

This violation was issued for two examples of failure to follow

'

procedures for updating the EDBD. In one example, a TC to the Makeup

..

System EDBD was not issued when a plant modification changed the

t Hydrogen Addition Pressure Regulator setting from 10 psig to 19.5 psig.  ;

In the other example, the 12 month review of the EDBDs had not been

performed and documented, resulting in DBD Tcs not being incorporated

within the required two year time.

1

!

4

h

.

i

em,-n.---s e e- -m e ~+,e e - =,-,. m- ,

-

,,n, -m e.-_ r , , . -

, , , , ,7._. - , ,

. . _ - . .. . ._ . . . - . . . - _ . _ . . -- - . . . _ . -.

'

l

'

!

L

l

35 ,

e

Licensee corrective actions 'were documented in Problem Report (PR) 96-

0230. The inspectors verified licensee corrective actions by reviewing. i

'

the following documents:

'

'

-

. Completed PR 96-0230.  ;

I

-

Temporary Change 487 to the EDBD - which properly documented the l

Hydrogen Addition Pressure Regulator setting.  !

I .

Revision 7 of NEP Procedure 216, Plant Design Basis Documents - i

!

which enhanced requirements for revising DBDs. -

i

l

- Revision 9 of NEP Procedure 213. Design Analysis / Calculations - .

'

which required identification of plant documents affected by a  !

change and tracking by the Nuclear Operations Tracking and  :

Expediting System until incorporation into applicable plant

documents. j

-

On the Job Training (0JT) Session Attendance Records - which l

documented review of the problem with applicable Design Engineers,  ;

Verification Engineers Supervisors, and Configuration Management  :

personnel. 1

-

Documentation that incorporation of Tcs into the EDBD was up-to-

date and that a system had been established to ensure that future

TCs are incorporated on schedule.

c. Conclusions

The inspector determined that the licensee had identified the root

causes and implemented adequate corrective actions. Based on the above

review, Violation 50-302/96-05-05 is closed.

The inspector assessed the licensee's perfcrmance with respect to this

issue, in the five areas of continuing NRC concern:

. Management Oversight - Good

. Engineering Effectiveness - Good .

  • Knowledge of the Design Basis - N/A l

. Compliance with Regulations - Good i

. Operator Performance - N/A

E8.2 -(Closed) VIO 50-302/96-05-07. Inadeauate Receivino Insoections for

Battec / Charcers

(Closed) LER 96-12-02. Doeration Outside Desian Basis Caused by Battery

Charaers Havino Inadeauate Test Results AcceDted in Error

1

i

. ..1 .. .m.r _ _ . . _ _ . _ . . , _

. _ ._, . I

36

a. Insoection Scooe (92700. 92903)

The inspector followed up on the licensee's corrective actions for this

violation and LER.

b. Observations and Findinas

The inspector verified that the licensee had completed all of the

corrective actions stated in this LER and most of the corrective actions

stated in the response to this Notice of Violation, including:

-

Replacing the backup " swing" battery chargers DPBC-1E and DPBC-1F

with new chargers.

-

Incorporating additional guidance into the Nuclear Procurement and

Storage Manual (NP&SM) for receipt inspectors' review of

engineering software acceptability letters provided by

engineerir.g.

-

Adding a requirement into the NP&SM for verifying that nameplate i

data complied with Purchase Requisition requirements. l

-

Distributing a copy of the related event report (LER 96-12-02). l

along with management's expectations, to design engineers.  !

procurement engineers, and receipt inspectors.

-

Updating the Preventive Maintenance Program to ensure that printed

circuit cards and capacitors are replaced in the battery chargers

on a five year frequency.

One corrective action, convening a Management Review Panel to further

review the issue, had not been completed. The inspector found that this  !

item and the third item above (verifying nameplate data) were not

tracked by the licensee to assure they were accomplished. They were not

in the licensee's corrective action system or the Nuclear Operations

Tracking and Expediting System (NOTES). However, the licensee had

recently made plans to have a review panel review the corrective actions l

for essentially all of the violations from 1996, including this one. l

This violation and LER are closed.

c. Conclusions

Violation 50-302/96-05-07. Inadequate Receiving Inspections for Battery

Chargers: and LER 96-12-02. Operation Outside Design Basis Caused by

Battery Chargers Having Inadequate Test Results Accepted in Error, are

closed. The inspector noted, and commented to the licensee, that their

tracking of corrective actions for violations was incomplete. i

37

The inspector assessed the licensee's performance, with respect to this

issue in the five areas of continuing NRC concern:

. Management Oversight - Adequate

. Engineering Effectiveness - Adequate

. Knowledge of the Design Basis - N/A

. Compliance with Regulations - Adequate

. Operator Performance - N/A

E8.3 (Closed) VIO 50-302/96-05-08. Failure to Follow Purchasino Procedures

for Inverters

a. Insoection Scoce (92903)

The inspector followed up on the licensee's corrective actions for this

violation.

b. Observations and Findinas

The inspector verified that the licensee had completed the corrective

actions for this violation, as stated in their response to the Notice of

Violation, including:

-

Requiring Nuclear Engineering Design personnel to read the related

Problem Report and Nuclear Engineering Procedure 220.

-

Requiring Buyers Associates to read the Nuclear Procurement and

Storage Manual. Section 3.3.

-

Processing a Procurement Requisition Amendment.

-

Revising the associated mini-specification.

The inspector noted that the completion of all of these corrective

actions was tracked and documented in the file for Problem Report 96-

0187. This item is closed.

c. Conclusions

Violation 50-302/96-05-08. Failure to Follow Purchasing Procedures for

Inverters, is closed. The ins)ector assessed the licensee's

)erformance, with respect to t11s issue, in the five areas of continuing

4RC concern:

. Management Oversight - Good

. Engineering Effectiveness - Good

. Knowledge of the Design Basis - N/A

. Compliance with Regulations - Good

. Operator Performance - N/A

._ _ __ _ ._ _ --_ ___ _ _ _ _ . _ __. . _ . _ _ _ ___ _ _ __

,

~

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38 l

.5

E8.4 (Ocen) EA 95-16. Use of Nonconservative Trio Setooints for Safety-  !

i

Related Eauioment

i

a. Insoection ScoDe (92903. 37500)  ;

!

As part of the continuing review of corrective actions for EA 95-16. j

the. inspectors reviewed several new instrument loop uncertainty setpoint

i

calculations. In IR 95-06 the inspectors found that the only safety--  !

l related trip setpoint calculation completed did not follow the ,

I methodology specified in Instrument Society of America (ISA) 67.04, part

l II. as referenced by instrumentation and controls Design Criteria .

Instrument-String Error /Setpoint Determination Methodology. To assess l

.the progress the licensee had made in this area, the inspector reviewed l

a sample of the most recent instrument string error /setpoints.  ;

! b. Observations and Findinas

Four recent instrument loop uncertainty (instrument string error) i

setpoint calculations were reviewed. These included: j

!

I-89-0013. Containment Air Temperature. Revision 6.  !

I-95-0002. SW Pump Discharge Header Pressure Calculation.  ;

Revision 2 -

I-95-0001. SW Heat Exchanger Outlet Temperature Error i

Calculation. Revision 2

I-91-0004. Nuclear Service Closed Cycle Cooling Surge Tank .

Instrumentation Accuracies. Revision 3

These calculations were well documented, with well founded assumptions. l

and followed the methodology specified in ISA 67.04. Part II. as

referenced by instrumentation and controls Design Criteria Instrument

String Error /Setpoint Determination Methodology. These calculations

were a significant improvement over calculations reviewed in IR 95-06.

The inspectors selected several instrument loop uncertainty setpoint

calculations that included instrumentation in the Auxiliary Building to

ensure the temperature assumptions used in design calculations for

Instrument string error or loop uncertainty determinations were

appropriately maintained. The instruments selected were: ,

Instrument Calculation ESOPM Zone Reauired Temoerature i

SW-3-PI M95-002 Zone 11 55 - 97 F

SW-123-TI M95-001 Zone 12 65 - 97 F -

SW-124-TI M95-001 Zone 12 65 - 97 F

SW-125-TI M95-001 Zone 12 65 - 97 F

SW-126-TI M95-001 Zone 12 65 - 97 F

SW-139-LT 191-004 Zone 11 55 - 97 F

SW-228-LT 191-004 . Zone 11 55 - 97 F

,

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. , . . , , . , . . . - . , , , _.,m.,#

.- - -- _ -. .. - . . _ - _ - - . . - -. -.-

!

!

t

39

The inspector verified that the Environmental and Seismic Qualification -

Program Manual (ESOPM) environmental assumptions were used in the-

instrument loop uncertainty setpoint calculations.

The inspector then reviewed the procedures used in the calibration of  ;

these instruments to ensure that these environmental assumptions -

contained in the' instrument loop uncertainty calculations were addressed  ;

in the procedure. The procedures reviewed were:  ;

SP-161C Remote Shutdown Instrument Calibration. Revision 13

PT-170 Nuclear Service Closed Cooling Surge Tank (SWT-1) i

'

Instrumentation Calibration. Revision 0

The inspector found that the calibration temperatures were not specified i

and that the procedures for calibration of instruments located in the c

'

Auxiliary Building did not assure that the Auxiliary Building .

temperatures were maintained within the temperature ranges assumed in

the instrument loop uncertainty setpoint calculations. There were no ,

procedural restrictions placed to prevent calibrating or operating the

instruments at temperatures outside the temperatures assumed in the *

ESOPM or the instrument loop uncertainty setpoint calculations.  ;

Additionally, there were no 3rocedures for ensuring the Auxiliary l

Building temperatures would ]e maintained within the ranges specified by i

the ESOPM or the instrument loop uncertainty setpoint calculations.  ;

Therefore, the inspectors examined how ambient temperatures were ,

controlled in the Control Building and the Auxiliary Building.

Paragraph 9.7.2.7 of the Final Safety Analysis Report (FSAR) provided

4 the Operational Requirements for the Heating Ventilation and Air

4

Condition (HVAC) systems. FortheAuxiliaryBuilding, paragraph

9.7.2.7.f stated. " Minimum temperature in these areas is 60 F." For  ;

"

the Control Complex. paragraph 9.7.2.7.h. stated. ". ambient is

,

maintained at 75 F".

,

. For the Control Complex, the Enhanced Design Basis Document (EDBD)

specified 75 F for winter and 70 F for summer (general design

conditions used in sizing of equipment) as operational parameters. For ,

the Auxiliary Building, the EDBD specified 60 F minimum (for freeze l

protection and personnel comfort) and 122 F maximum (for environmental l

, control for electrical equipment) as operational parameters. ,

For the Control Complex the licensee 3rovided the inspectors a graph of

recorded tem)eratures for a year, whic1 showed that the temperature in j

the Control Room had been maintained within a range of 70 F - 80 F.  ;

However, based on interviews with licensee personnel and review of l

procedures, there was no program for moriitoring temperatures in the

[ Auxiliary Building.

.- 4

As noted in Section 8/7 of the EDBD. the purpose of the Auxiliary  ;

Building Heating Coils (AHHE-2A AHHE-28. and AHHE-12) was to maintain  ;

the Auxiliary and Fuel Handling Building at 60 F minimum. Review of  !

I

i;

. - _ . _ , ._. - - . _ _

_ . . . - __

_ . _ _ _ _ __ . - _ _ . __ _ _ ._ _

,

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40

the maintenance his' tory for the Auxiliary Building heaters and  ;

'

'

discussions with Engineering personnel revealed the following:

-

The heaters were not included in the Preventive Maintenance (PM)

Program. The instrument strings controlling the heaters are in

i the PM program and were being calibrated. The PMs for the -

1. instrument strings were im]lemented by Work Requests (WRs) NU

i

0266933. NU 0280142. and NJ 0305381.

-

In late 1995, as part of the boron reduction project, the. i

Auxiliary Building heaters were inspected to determine their

status and found to be not fully functional because of a number of i

blown fuses and other discrepancies. This was documented in Wrs

NU 0329662 and NU 0332052. At that time, the heaters were  :

-

repaired and made fully functional.  !

4  :

!

4 - In early January 1996. WR NU 0332052 was issued because heaters

.

were not maintaining Auxiliary Building temperatures at 60 F. A  :

blown control fuse was replaced and the heaters made operable.

Temperatures were found to be 55' F on the second floor of the

Auxiliary Building and 52 F on the spent fuel floor. The

temperature transmitter set)oint for the heaters was 50 F. in  ;

accordance with drawings. Request for Engineering Assistance -

'

(REA) 960031 was issued to change the heater setpoint to 60 F. I

since a 50 F setting was not consistent with the EDBD requirement

,

for maintaining the building at 60 F.

'

Based on the above rev'.ew, the inspectors could not determine if the

temperature in the Auxiliary Building in the past was always above the

minimum indicated in the FSAR and the EDBD. since temperatures have not

been periodically monitored. The heaters were not fully functional in

4

late 1995. However, it could not be determined how long the heaters

were not fully functional since the heaters were not included in the PM

program and temperatures were not monitored. Also, the temperature

transmitter that starts the heaters was set at 50 F. The input to the l

transmitter used the duct temperature just downstream of the air

handling unit, which was essentially the temperature of the incoming

outside air. Therefore, even if the heaters were fully functional, it

was doubtful to the inspectors that using the duct temperature as the 3

input to operate the heaters would result in the ambient temperature in l

'

the building being always maintained at 60 F minimum specified by the '

EDBD. Further, the 60 F minimum was not consistent with the ESOPM Zone

12 environmental assumptions of a 65 F minimum temperature.

, _c. Conclusions

The inspectors concluded that the licensee has made progress in

4 resolving the ITS setpoint program deficiencies. Four recent

calculations were well documented, with well founded assumptions, and

'followed the methodology specified in ISA 6'7. 04, part II. as referenced

by instrumentation and controls Design Criteria Instrument String

~

Error /Setpoint Determination Methodology. These calculations were a l

_. _ _

-

. _ _ _ ___ _

41

significant improvement over calculations reviewed in IR 95-06.

However, there were several loo) uncertainty calculations that were not

complete and were scheduled to )e completed by March 1.1997. The final

loop uncertainty determinations and instrument string error calculations

need to be reviewed by the NRC after they are issued, to complete the

followup inspection of EA 95-16.

The ins)ectors concluded that the Auxiliary Building temperature ranges

which t1e ESOPM environmental assumptions used for the instrument loop

uncertainty setpoint calculations were not maintained. Instrument

setpoint calculations assumed certain temperatures in the Auxiliary

Building for instrument calibration and operation. However, instrument

calibration procedures did not address these temaeratures: there were no

procedural restrictions in place to prevent cali) rating or operating the

instruments at temperatures outside the temperatures assumed in the

ESOPM or the instrument loop uncertainty setpoint calculations; and

there were no procedures for ensuring the Auxiliary Building

temperatures would be maintained within the ranges specified by the

ESOPM or the instrument loop uncertainty setpoint calculations. This is

a violation of design control requirements. VIO 50-302/97-01-07.

Instrument Loop Uncertainty Setpoint Calculation Assvaptions Not

Translated Into Procedures. l

The inspectors assessed the licensee's performance relative to lack of l

design control for Auxiliary Building temperatures assumed in instrument '

setpoint calculations, in the five areas of continuing NRC concern:

. Management Oversight - Inadequate

. Engineering Effectiveness - Inadequate

. Knowledge of the Design Basis - Inadequate l

  • Compliance with Regulations - Inadequate

. Operator Performance - N/A

E8.5 (Closed) IFI 96-201-13. Cable Amoacity Exceeded for DHP-1A fDCP-1Al

Feeder Cable and Others

a. Insoection Scone (92903) ,

l

'

During NRC inspection 96-201. inspectors reviewed Calculation E91-0020.

Rev 0, which sized safety-related AC power cables from the ampacity and

short-circuit considerations and noted that the calculation concluded

that the cable for DCP-1A and several other cables required further

evaluation. The licensee stated at that time that evaluation of the

problem cables had been completed. However, the licensee could not find ;

the evaluation for the inspector's review, and therefore. IFI 96-201-13

was established.

UFSAR Section 8.2.2.11.a states:

In general, motor and transformer feeder cables are rated at 125

percent of full load current. In some cases, the 125 percent of

full load current rating is not met. However. as a minimum, the 4

l

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42 i

1

.

'

cable will have a rating of 115 percent of full load current. l

This provides for motor and equipment operation at service factor

'

ratings. The reference used for cable selection is the CR-3

Electrical Design Criteria - Cable Ampacity Sizing.

.

The scope of the inspection was to determine whether the above stated

UFSAR recuirement had been met: whether ampacity calculations were done

in accorcance with published standards: and whether NRC requirements in

10 CFR 50. Appendix B. Criterion XVI. Corrective Action, were met.

b. Observations and Findinas

The licensee had three calculations which dealt with sizing cables for

ampacity. Calculation E91-0020 mentioned above covered the majority of

safety-related AC power cables. A second calculation covered sirigle

phase vital AC cables. A third calculation covered safety-related DC

cables.

The calculations were performed as part of the Electrical Calculation ,

Enhancement Program, and, for the most part. " sized" cables which were  !

already installed. The ampacity tables and derating factors upon which j

the calculations were based were taken from ICEA P-46-426. Power Cable

'

Ampacities.

With regard to Calculation E91-0020. the inspector determined the

following sequence of events through discussions with licensee engineers

and document review. In 1992, the calculation was being developed, and

engineers identified that several cables did not have the required

ampacity when the generic derating factors were apalied. This did not

necessarily mean that the cables were overloaded. Jut it did mean that

further analysis was necessary. Before the calculation was issued.

Problem Report 92-0124 was initiated (in September 1992) to cover the

potential problem cables. Forty-five cables were listed as potentially

not meeting the requirements described in the scope section above [22 .

had ampacity less that full load amperes (FLA). and 23 had ampacity i

greater than FLA but less than 125 percent of FLA]. PR 92-0124 also

mentioned that there was a generic problem with any cables covered with ,

fire barrier material. The problem was that the fire barrier ampacity j

derating factors being used throughout the industry were significantly l

non-conservative. The fire barrier problem was described in NRC  !

Information Notice 92-46.  !

The corrective action )lan for PR 92-0124 addressed the 22 circuits

having ampacity less tlan FLA. It did not have any corrective actions

for the other 23 cables or the fire barrier problem. The fact that the

corrective action plan did not include the fire barrier problem was of

minor significance, because PR 92-0057 had already been generated for

this problem in June 1992 PR 92-0124 was closed in June 1993. The

calculation was issued during December 1993. The conclusions section of

the calculation listed 18 cables that did not meet all of the design 3

criteria and 3 cables that would meet the criteria if certain specified l

tray fill blocks were put in place within the computerized cable and 1

)

. . . . - _- ..- . . .- - - - - . - . . ...

!

_t

43  !

raceway 3rogram. There was no problem report generated for these

cables: lowever. Electrical Calculation Enhancement Program Open Item i

No. 93-ECEP-070 was established. This item was still open at the time

of this inspection. Twelve of these cables were the'same as noted in PR

92-0124. and 9 cables were different than previously noted. After NRC

Ins)ection Report 50-302/96-201 identified a concern with how the -

pro)lems were handled, the licensee initiated Precursor Card 96-3705.  ;

The inspector reviewed the ampacity calculation sheets for 10 tooles 4

listed in PR 92-0124 as having ampacity less than full. load amperes.

The inspector observed that the calculation had been revised since

initiation of the PR, and these cables met all the criteria. These

cables were routed exclusively in conduit, and the originally applied ,

conduit grouping derate factor was found overly conservative upon  ;

exmination of the as-built configuration. The inspector confirmed. .

thrm gh review of records, that cable CHL-1 had been replaced with cable

CHL-t. which increased the ampacity to meet the criteria. Therefore.  ;

cables listed in PR 92-0124 as being problem cables but not included in  :

the list of problem cables in the calculation had been properly

resolved.

From the set of 23 cables listed in the problem report that had ampacity )

between 100 and 125 percent of full load amperes, the inspector reviewed  ;

the ampacity calculation sheets for three selected at random. The 1

inspector observed that these cables had been properly resolved.

Cable MTL-117 a 480-volt motor control center feeder cable, was listed

in Calculation E91-0020 ds a aotential problem and was also addressed in

Problem Report 92-124, which 1ad been closed out. The calculation

'

enhancement program open item indicated that this cable had been further

analyzed and found to meet all the criteria. The inspector walked down

. this cable route in the plant, reviewed the ampacity calculation sheet

(which had not been revised) and confirmed the load current. Based on

,

the as-built configuration and a) plication of the standard derate

factors the inspector believed tais cable had an ampacity problem. The

licensee retrieved the informal work notes upon which the conclusion

that cable MTL-117 was not a problem had been based. The licensee

reviewed the work notes during the inspection, and re)orted to the

, inspector that the calculation methodology in the worc notes was

questionable.

In Calculation E91-0020. Cable AHC-656, a 480-volt supply to control

room emergency ventilation return fan AHF-19B. was indicated to meet the

criteria for ampacity but cautioned that certain tray sections must be

limiced to less than 43 power conductors. This issue was not addressed

in a Problem Report. _The licensee's method to limit tray fill for a 4

particular tray section was to make the allowable fill equal the actual I

fill in the computer' based cable and raceway program. This technique

effectively placed a com) uter program block on adding any new cables to

the tray in question. T1e inspector identified that the com) uter

program block had not been implemented for the applicable ca)le tray

sections (tray 107, sections 7 and 8).

1

i j

J- _ . . - . - __. . - . _ - - - - _ _. - ._i

__ _ . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

44

Cable MTL-67, a 480-volt supply to motor control center MCC 3AB had

sufficient ampacity for the load, but Calculation E91-0020 indicated

that the overcurrent protective device was set too high to protect the

cable. This issue was not addressed in a Problem Report. The inspector

examined the solid state trip device settings in the plant, and

concluded that the set point (320 A) was too high to protect the cable

(ampacity 237 A). The inspector also noted that a new breaker setting

sheet had been issued in January 1995 which perpetuated the old

incorrect setpoint.

c. Conclusions

Inspector Followup Item 96-201-13 raised concerns about the resolution

for potential ampacity problems identified in 1992 and 1993. This

inspector concluded that a violation of NRC requirements in the area of

corrective action (10 CFR 50. Appendix B. Criterion XVI) had occurred.

This conclusion was based primarily on the fact that Calculation E91-

0020 had identified potential problems and indicated the need for

corrective action in 1993 but the corrective action had not been

implemented and/or the same aroblems still existed in 1997. l

Specifically Cable MTL-117 lad a questionable methodology applied I

within the problem report process, the tray fill block related to Cable i

AHC-656 had not been implemented. and the protective device setpoint for l

Cable MTL-67 had not been revised to protect the cable. These cables

were randomly selected for review by the inspector, and problems were

not necessarily limited to threa cables. This is a violation of

corrective action requirements 10 50-302/97-01-09. Inadequate

Corrective Actions for Cable Ampacity.

i

The ampacity calculation performed under the Electrical Calculation i

Enhancement Program was performed according to widely accepted industry

standards. A relatively small number of cables (order of magnitude one

percent), were identified as potential problems. Therefore, the

t

original design work for sizing cables performed in 1968 to 1977 time

frame, when subjected to rigorous up-to-date analysis, was shown to be

generally sound.

Ins)ector Followup Item 96-201-13. Cable Ampacity Exceeded for DHP-1A

[DC)-1A] Feeder Cable and Others, was closed. The issues are

encompassed by, and will be tracked under, the violation described

above.

The fact that the Electrical Calculation Enhancement Program was

completed represents management's willingness to ex)end resources to

identify actively discreaancies between the design Jasis and the as-

built plant However. t1e circumstances described above indicate that

once discrepancies were identified. sufficient care was not taken to

ensure resolution. The licensee planned to resolve all ampacity

concerns before restart of the unit, as evidenced by the fact that this

was an item on the licensee's plant restart list.

- _ _ _ _ _ _ _ _ _ _ - _ _ _ .

45

With regard to the issue of cable ampacities, the inspector assessed the

licensee's performance in the five NRC continuing areas of concecn as

follows:

  • Management Oversight - Adequate

. Engineering Effectiveness - Inadec uate '

. Knowledge of the Design Basis - Ac equate

. Compliance with Regulations -

Inadequate

. Operator Performance - N/A

E8.6 (00en) URI 50-302/96-201-04 Nonsafety-Related Positioners on Safetv-

Related Valves .

I

'

a. Insoect_Lon Scope (37550. 92903)

This UM involved a concern identified by the NRC during the Integrated  !

Performance Assessment Process (IPAP) inspection, where safety-related

air operated valves (DCV-17. DCV-18. DCV-177. and DCV-178) used to

control cooling water flow to the decay heat removal heat exchangers l

were connected to nonsafety-related positioners. The inspector followed i

up on the licensee's corrective actions for this item,

b. Observations and Findinas

1

Licensee corrective actions were documented in PR 96-0041 and PR 96- l

0220. The inspector reviewed the corrective actions that had been (

implemented or planned to address this item. The inspector reviewed l

these corrective actions for compliance with the FSAR. Technical l

Specifications, licensee Topical Design Basis Document. design control i

procedures, operating procedures, and 10 CFR 50 Appendix R.

The licensee had prepared MAR 94-09-02-01. DC Cooling Instrument

Enhancement, to address this issue. The modification was evaluated by ,

the licensee and determined to be a restart item. However. the '

inspector reviewed the licensee's scheduling of work during the current

shutdown and noted that, based on recommendations by operations. MAR 94-

09-02-01 was being scheduled for implementation during mode 1 operation

after CR-3 restarted. The inspector noted that this implementation

schedule was not consistent with the licensee's restart evaluation.

Licensee personnel indicated that the MAR would be re-reviewed to

determine the a]propriate implementation schedule. During further

review of this %R. the inspector noted that the 10 CFR 50.59 screening

determined that a 10 CFR 50.59 safety evaluation was not required. The

inspector reviewed the 50.59 screening and determined that the screening

was weak in that it lacked adequate detail to support the conclusion

that a 10 CFR 50.59 safety evaluation was not required.

As discussed in the NRC IPAP inspection report 50-302/96-201 (Appendix

C. paragraph 3.1.5), the NRC noted that implementation of MAR 94-09-02-

01 would address the NRC's concern regarding the nonsafety-related

positioners on Valves DCV-17. DCV-18. DCV-177. and DCV-178. However,

the NRC had noted that a licensee interpretation during development of ,

- .. -- - . - . - - - - _ - . . . . -- -- - _ . .

~

~.

b

46  ;

'

the above MAR mistakenly concluded that the nonsafety-related

positioners on the safety-related valves did not violate any design . .

criteria and that failures of nonsafety-related equipment postulated to

be less than 10E-6 need not be considered. The inspector discussed with

licensee personnel the IPAP team's observation regarding interpretation ,

of the design criteria. Licensee personnel indicated that the. design  !

'

criteria-in question was the Crystal River Unit 3 Topical Design Basis

Document (TDBD) for the Single Failure Criteria. Revision 1. dated ,

April 25.1994. The inspector reviewed the TDBD and noted that the IPAP

team questioned the applicability of the 10E-6 criteria included in the- '

TDBD for single failure of nonsafety-related components. This item.

remains open, and the NRC will continue to review this item to determine.

the licensee *s schedule for implementation of MAR 94-09-02-01 and

further review of the licensee s design criteria for single failure of, ,

nonsafety-related components to verify that it is consistent with NRC

requirements.

During further review of MAR 94-09-02-01, the inspector noted that the i

'

MAR identified certain operating procedures that needed to be revised as

a result this MAR. In addition to the operating procedures. identified

in the MAR. the inspector also reviewed licensee abnormal procedures

(AP) to determine if any were impacted by the MAR. One of the abnormal  ;

procedures reviewed by the inspector was AP-990. Shutdown From Outside l

Control Room. Revision 8. The inspector noted that this AP provided

procedural steps for taking the plant to hot standby and then directed

operations personnel to maintain the plant in hot standby until a

specific cooldown plan was formulated. The AP did not contain steps for ,

taking the plant from hot standby to cold shutdown, and the AP did not i

provide a reference or transition to any other procedure that would be

used by the operators to take the plant to cold shutdown. The inspector

discussed this issue with licensee personnel who stated that credit was i

being taken for Operating Procedure OP-209. Plant Cooldown Revision 87, j

which was the procedure that provided guidance to the operators for i

taking the plant from hot standby to cold shutdown. The inspector I

reviewed OP-209 and noted that Enclosure 1 to the procedure provided

information concerning cooldown following a fire in the main control l

room or cable spreading room. This enclosure provided general guidance ,

for certain fire scenarios and stated that this information was intended I

to assist plant personnel in designing a s)ecific cooldown procedure l

following main control room evacuation. T1e ins)ector determined that  !

the procedures (AP-990 and OP-209 being used eitler separately or in

'

conjunction with each other) did not provide adequate instructions for

taking the plant from hot standby to cold shutdown from outside the main

control room. The inspector reviewed FSAR Section 7.4.6. Auxiliary

Control Stations (Remote Shutdown System) and FSAR Section 9.8. Plant

Fire Protection Program. FSAR Section 7.4.6.5 states in part that the

design basis for the remote shutdown system is 10 CFR 50. Appendix R.

Section.L. FSAR Section 9.8.6 states that plant procedures developed in

accordance with 10 CFR 50. Appendix R. Sections III.G and III.L

establish means~to bring the plant from operating to cold shutdown. The-

-

inspector further concluded, that licensee Procedures AP-990 and OP-209 I

did not meet the requirements of 10 CFR 50. Appendix R. The guidance in

-

_ _ _ _ _

l

,

47

Procedure OP-209, which directs operations persennel to develop a

specific cooldown 3rocedure to tace the plant to cold shutdown based on

an assessment of t1e fire scenario and equipment availabil:ty, does not

meet the criteria in Section III.L of 10 CFR 50, Appendix . Section

III.L states that procedures shall be in effect to impleme,4 the

capability of being able to take the plant to cold shutdowa within 72

hours following main control room evacuation due to a fire. Licensee

personnel stated that AP-990 and OP-209 meet the intent of Section  !

III.L. The inspector informed the licensee that, this issue was I

unresolved pending further NRC review of applicable SERs which discuss l

the licensee's Appendix R program. This issue will be identified as URI

50-302/97-01-08. Adecuacy of Procedures to Take the Plant from Hot

Standby to Cold Shutcown from Outside the Control Room.

c. Conclusions  !

I

The inspector concluded that the schedule for implementation of MAR 94-

09-02-01 to address the issue of nonsafety-related positioners on l

safety-related valves was inconsistent with the licensee's restart aanel

recommendation. The inspector concluded that licensee Procedures A)-990

and OP-209. used either separately or in conjunction with each other,

did not provide adequate instructions for taking the plant to cold

shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> following main control room evacuation due to a

fire. These procedures did not meet the requirements of Section III.L

of 10 CFR 50, Appendix R. A URI was identified pending further NRC

review of applicable SERs which discuss the licensee's Appendix R

program. ,

i

The inspector assessed the licensee's performance, with respect to this

issue, in the five areas of continuing NRC concern:

  • Management Oversight - Adequate

. Engineering Effectiveness - Good

. Knowledge of the Design Basis - Good

. Compliance with Regulations -

Inadequate

  • Operator Performance - N/A

E8.7 (Closed) Inspector Followup Item (IFI) 50-302/95-15-01. Desian

Reauirements for Nitrocen Overoressure

a. Insoection Scope (92903)

This IFI dealt with a unique feature of the Crystal River nuclear

service water system, a surge tank that was pressurized with nitrogen

and not located at the highest point in the system. The function of the

tank appeared to be for ensuring the system pressure remained at 60 psi.

Following Inspection 50-302/95-15 the licensee reviewed the system

design basis and determined that the setpoints associated with the surge

tank should be verified. This IFI was reinspected in inspection report

50-302/96-21: however, the IFI was left open pending the review of the

calculations and validation that the alarms were changed.

l

- -. .... - . .. .-. ..-.-. . - ._. -. - . - - - . _ - . . . - ..

!

!

1

48 j

b. Observations and Findinas l

The inspector reviewed the applicable calculations:  !

!

, M95-0035, SW System Inventory Transient Analysis Revision 1.  !

! ~

M93-0018. Nuclear Service Closed Cycle Surge tank (SWT-1) l

Volume. Revision 1.  ;

.

M92-0019. SW Surge Tank Tie-in Pressure Drop Analysis, Revision  ;

, 3. 191-0004, Nuclear Service Closed Cycle Surge Tank l

Instrumentation Accuracies. Revision 3.  !

1 . i

Calculation M95-0035 demonstrated that the as-found setpaints for SW-

'

,

134-PSI and S'4-137-LS were not appropriate. The setpoints for these l

'

l instruments were changed in 191-0004. These setpoint changes were

included in Surveillance Test PT-170, Nuclear Service Closed Cycle Surge l

Tank (SWT-1) Instrument Calibration. l

'

There was' one area of confusion regarding the units of the exact

location _of the SW Surge Tank High Level alarm. The calibration

Procedure PT-170 described the set Joint as 109'6". The annunciator

'

.

alarm Procedure ESAB-A-01-08 descri)ed the location as 10'0". The

2

calculation 191-004 described the location as 109'6" plant elevation.  !

'

! 11*6" tank elevation, or 10' transmitter elevation. Calculation M95-

0035 Assumption 5.6. tank drawing on page 22 of 23. tank drawing on page
10 of.10 describes the Hi-alarm setpoint as 111'-0". The November 22,

1995, letter IOC NED95-0691 described the setpoint changing from 110'6"

to 109'6". Finally, the vendor Drawing 5-315-D1. listed the normal

water level at 109'6" (Normal operating level - Tank bottom elevation +

tank height - distance from top of tank to normal water level) = (109'6"

- 98' + 16'- 4'6"). This level was at the high alarm setpoint. The

inspector was informed that although this drawing was available through

'

document control, it was an original tank drawing and was not used for

L any specific purpose.

c. Conclusions

The inspector found that there were four separate level measurement

<

systems used to refer to this setpoint. These were:

a

(1) Distance from an arbitrary plant datum point

. (2) Distance from the floor of the room in which the tank is located

(3) Distance from the inside edge of the bottom of the tank

,

(4) Distance from an arbitrary zero in the tank

The inspector concluded that, while the four different elevation systems

used to refer to the same point, other than presenting the possibility

for future errors there were no consequences for this particular

calculation or its resulting setpoint. The inspector concluded that the

licensee had ccmpleted the loop uncertainty calculation and

l

. -- - .- -- - .,

49

appropriately calibrated the affected instrumentation, and that these

actions adequately addressed the portions of IFI 95-15-01. Design

Requirements for Nitrogen Overpressure, that were not reviewed or closed

in IR 50-302/96-21.

The inspector assessed the licensee's performance, with respect to this

issue, in the five areas of continuing NRC concern:

Management Oversight - Management oversight was judged to be good, in

that, there was management involvement throughout the project, and when

small procedural concerns were identified they were dealt with in an

expeditious manner.

Engineering Effectiveness - The engineering was judged as good. The

conclusions were acceptable and the new setpoints were technically sound

and were appropriately translated into procedures.

Knowledge of Design Bases - The licensee's design basis knowledge was

judged as adequate. The reason that this IFI was opened was because

there was not a com]lete understanding of the systems design basis. At

the conclusion of t11s calculation the licensee had reconstructed the

design basis for the SW surge tank. One aspect of calculation. 191-

0004. Nuclear Service Closed Cycle Surge Tank Instrumentation

Accuracies. Revision 3 that was not appropriately addressed was the

translation of the associated nuclear service closed cycle surge tank

Auxiliary Building instrumentation accuracies into appro]riate

calibration procedures. This is addressed in paragraph E8.4.

Compliance With Regulations - The utility demonstrated the appropriate

amount of regulatory sensitivity for this issue. There was reasonably

timely work, the calculations were accurate, and the results were

available for review. The inspector judged this area as good.

Operator Performance - There was limited operations involvement in this

3roject. However, as noted above there were inconsistencies in units

)etween the annunciator response procedure and the calibration

procedure. There were apparently discrepancies between the actual level

and the level reported in an original vendor drawing. However, in spite

of this potential confusion, the appropriate levels appear to be on the

installed equipment and in the alarm response procedure, the area of

operations was judged as adequate.

. Management Oversight - Good

. Engineering Effectiveness - Good

. Knowledge of the Design Basis - Adequate

. Compliance with Regulations - Good

. Operator Performance - Adequate

--. - . - . -

,

50

E8.8 i0oen) VIO 50-302/96-09-07. Inadeauate Corrective Action for

Lmolementation of EFIC Task Force Recommendations

a. Inspection Scoce (37550. 92903)

This violation involved failure of the licensee to take adequate and ,

timely corrective actions to implement recommendations from the l

Emergency Feedwater Initiation and Control (EFIC) task force. The

inspector followed up on the licensee's corrective actions for this j

violation.

b. Observations and Findinas ,

The inspector reviewed the corrective actions specified in the .

licensee's response to this violation. The inspector reviewed these )

corrective actions for compliance with the FSAR. TS, and applicable  ;

licensee procedures. The inspector noted that some of the corrective l

actions specified in the response had been implemented. Corrective l

actions implemented included all Requests for Engineering Assistance

(REA), which recuested a plant modification, being reviewed and approved  ;

by the Plant Mocification Review Group (PMRG): a list of high priority l

'

modifications was being maintained by the PMRG: high priority EFIC/EFW

issues were being addressed during the present shutdown: and additional

resources (permanent and contract personnel) were added to the  ;

engineering organization to ensure that high priority tasks were being

worked. The inspector noted that the modifications to address the high

priority EFIC/EFW issues had not been implemented.

During review of the corrective actions, the inspector noted that many

of the EFIC Task Force recommendations were not included on the .

licensee's restart list. The inspector questioned licensee personnel as l

to whether the EFIC Task Force recommendations had been or would be l

evaluated against their restart criteria. This question was further 1

amplified when the inspector noted that precursor card (PC) No. 97-0595

was initiated on January 28, 1997, which questioned whether one of the

EFIC Task Force recommendations should be evaluated as a restart

restraint during the current shutdown rather than the scheduled

implementation during Refuel 11. Licensee personnel indicated that PC

97-0595 would be evaluated against their restart criteria by the restart

panel. This item remains open )ending further review of the licensee's

evaluation of PC 97-0595 and otler EFIC Task Force recommendations by

the restart panel. l

c. Conclusion

The inspector concluded that the licensee had implemented a number of

corrective actions to address this violation. However, not all EFIC

Task Force recommendations had been reviewed by the licensee using their

restart criteria.

l

I

1

_ ___ __ __ ._ _ . _ _ _ _ . - _ _

.

51

The inspector assessed the licensee's performance, with respect to this

issue. in the five areas of_ continuing NRC concern:

  • Management Oversight - Adequate
  • Engineering Effectiveness - Good
  • Knowledge of the Design Basis - N/A

e Compliance with Regulations - Good

. Operator Performance - N/A

E8.9 (Ocen) VIO 50-302/95-21-03. Failure to Isolate the Class IE from the Non

Class IE Electrical Circuitry for the Reactor Buildina Purae and Mini-

?urae Valves

a. Insoection Scoce (37550. 92903)

This violation involved failure of the licensee to isolate Class IE from

Non Class IE electrical' circuitry for the reactor building purge and

mini-purge valves. The inspector followed up on the licensee s

corrective actions for this violation.

b. Observations and Findinas

The inspector reviewed the corrective actions specified in the

licensee's response to this violation. The corrective actions were

reviewed for compliance with the FSAR. TS, and applicable licensee

procedures. The inspector noted that some of the corrective action

. specified in the response had been completed. Other corrective actions

involved implementation of modifications to address the issue. Some of

the modifications had been implemented. During review of the corrective

actions, the inspector noted that the licensee's evaluation of

alternatives to the present non-isolated design of the control circuits

for reactor building purge valves AHV-1A and AHV-1D had not been

completed by the scheduled date of December 20, 1996. The new schedule

date for completion of the evaluation was changed to May 1998. The

inspector discussed this change with licensee personnel who indicated

that the schedule change was due to an increase of other higher priority

issues such as EFIC/EFW and EDG loading. The inspector also questioned

whether this issue had been evaluated as a potential restart issue and

licensee personnel indicated that the issue had not been evaluated by

their restart panel. This item remains open.

c. Conclusion

The inspector concluded that the licensee has completed some of the

specified corrective actions to address this issue. However, due to

workload and higher priority issues related to the EFIC/EFW and EDG

loading, the scheduled completion date for other-corrective actions was

not met and the completion date was extended.

._

52

The inspector assessed the licensee's performance, with respect to this

issue, in the five areas of continuing NRC concern:

. Management Oversight - Adequate

. Engineering Effectiveness - Adequate

+ Knowledge of the Design Basis - N/A

+ Compliance with Regulations - Good

. Operator Performance - N/A

E8.10 (Ocen) NRC Generic letter 96-06. Assurance of Eauioment Doerability and

Containment Intearity Durina Desian-Basis Accident Conditions

a. Insoection Scooe (92903)

GL 96-06. issued September 30, 1996, requested certain actions from all

operating nuclear power reactors relative to the following safety-

significant issues:

-

During a loss of coolant accident (LOCA) or a main steamline break

(MSLB). cooling water systems serving the containment air coolers

may be exposed to waterhammer for which they were not designed.

-

During LOCA and MSLB scenarios, cooling water systems serving the

containment air coolers may experience two-phase flow conditions

that were not considered in heat removal assumptions resulting in

system design and operability questions.

- Thermally induced overpressurization of isolated water-filled

piping sections in containment could jeo]ardize the ability of

accident-mitigating systems to perform t1eir safety functions and

cold lead to breach of containment integrity via bypass leakage.

In this inspection, the inspectors examined the licensee's actions to

date for evaluation and corrective actions relative to thermally induced

overpressurization of isolated piping sections.

b. Observations and Findinas

GL 96-06 requested that licensees determine if aiping systems that

penetrate the containment were susceptible to tiermal expansion so that

overpressurization of piping could occur. If systems were found to be

susceptiole, licensees were expected to assess the operability of

affected systems and take rcrrective action as appropriate. Licensees

were requested to submit a written summary report within 120 days of the

date of the GL letter stating the actions taken in response to the

requested actions, including conclusions reached relative to

susceptibility for overpressurization of piping that penetrates the

containment. the basis for continued operability of affected systems,

and corrective actions that were implemented or planned.

The licensee's 120 day response was submitted on January 27, 1997. The

response detailed the review performed to determine containment

.- . .- - . . - . - . - - ..

f

i

'

53  !

penetration piping susceptible to overpressurization. For the .

containment penetration process piping susceptible to ,

overpressurization, the licensee has designed and is installing rupture -i

discs and expansion chambers to allow for expansion of the process  ;

fluid. For all susceptible penetrations, except SW system penetrations i

314 and 318 rupture discs will be enclosed in expansion chambers j

located outside the containment. For-SW 2enetrations 314 and 318, t

rupture discs will be installed inside tie containment without expansion' '

'

chambers. The rupture discs will be connected to the process piping

with 3/8" diameter tubing. In addition-to installation of expansion >

chambers for containment penetration piping, the licensee was still  !

evaluating the need for additional relief valves in other piping. -

'

Although, based on the size of piping (tubing) between process piping

and the expansion chambers, the expansion chamber would be exempt from

ASME Section XI requirements. the licensee applied ASME Section XI

requirements to the design, fabrication and installation of the  ;

expansion chambers. This resulted in the use of USAS B31.1. 1967 l

Edition and B31.7. 1969 Edition as the applicable Codes. ]

The inspectors observed the following relative to design, procurement ,

and installation of the expansion chambers: I

-

Engineering - The inspectors reviewed the approved MAR 96-10-04-

01, including the 10 CFR 50.59 Evaluation and the Installation

Instructions.

During review of the MAR package the ins)ector noted that the

Inservice Inspection (ISI) Requirements cleck sheet had not been

properly completed. The ISI check sheet is used during the MAR

development and review arocess to have ISM personnel review the

MAR package to ensure tlat ISM requirements are adecuately

addressed. For MAR 96-10-04-01, the check sheet hac been signed

by the Nuclear ISM Specialist indicating his review, but he failed

to check-mark the ISI Requirements as " Acceptable" or -

" Unacceptable". For this case the failure to complete the ISI

Requirements form 3roperly was not that significant since no ISI

was required and t1ere was a later required review for ISI

requirements at the time of issue of the installation work

packages. However, issue of the MAR package without the ISI check

sheet being properly completed indicates a weakness in the MAR

review and approval process. The licensee issued a Precursor Card '

to document and take appropriate corrective actions for this

weakness. Also, prior to this inspection, the licensee had

identified the need to strengthen-their procedures in the area of

ISI review of MAR packages. Procedure revisions were in process.

For containment penetrations 314 and 318, which will have rupture

discs installed inside the containment without expansion chambers,

the inspectors questioned the licensee relative to the need to

provide an exclusion zone around the rupture discs to ensure that

future modifications do not install equipment where it might be

. . -.

54

damaged in the event of a rupture disc rupture. Engineering

personnel stated that the need for an exclusion area would be

evaluated and added if considered necessary.

-

Procurement - Sample records from Purchase Ceder F810203D

3rocurement package were reviewed. Records raviewed included: FPC

Receiving Inspection Report and Inspection Plan: Welding Services.

Inc. (WSI) Certificate of Conformance: Fabrication Traveler

36077001 for chambers MURS-1 and MURS-2: Weld Data Sheets for

Welds SW-1. 2. 3. 4. 5. and 6: radiographic film reader sheets for

chambers CARS-1. MURS-1. CFPS-1. SFRS-1 and DHRS-1: certification

for NDE materials: and FPC letters of approval for Welding

Specifications. NDE Procedures, and welder qualifications.

-

Installation Activities -

The inspectors observed portions of the welding and liquid

penetrant (PT) examination for weld CA-85-86 on WR NU 0339386,

welds CA-85-85 and CA-85-127 on WR NU 0339390, and weld CA-85-149 l

on WR NU 0339392. In addition, for the welds observed, welder

qualification records, weld material test reports. NDE examiner

certification records, and penetrant material test reports were

reviewed. I

!

c. Conclusions I

The inspector concluded that the licensee was performing detailed  ;

evaluations and developing solutions for the issues identified in GL 96-

06. Overall, the MAR package, including the 10 CFR 50.59 evaluation,

for design, procurement, and installation of the containment penetration

process piping expansion chambers was detailed and well documented,

demonstrating good Engineering performance. Procurement activities were

detailed and well documented. Welding and inspection work activities

associated with installation of the expansion chambers were good with

detailed, neat, and well-maintained documentation.

One weakness was identified relative to completion of the ISI

Requirements check-sheet.

The inspector assessed the licensee's performance, with respect to this

issue, in the five NRC continuing areas c' concern:

. Management Oversight - Good

. Engineering Effectiveness - Good

. Knowledge of the Design Basis - Good

. Compliance with Regulations - Good

. Operator Performance - N/A

55

IV. Plant Support

F3 Fire Protection Procedures and Documentation

F3.1 Fire Protection System Recirculation Limits

a. Insoection Scooe (71707)

The inspectors reviewed the licensee *s response to improper control of

fire pump recirculation flow that resulted in a condition where all

three fire pumps were rendered inoperable.

b. Observations and Findinas

On January 17, 1997, the licensee placed motor-driven fire service pump

(FSP) 1 in service per Operating Procedure (0P) 880. Fire Service

System. Revision 9. to recirculate both fire service tanks. This

implemented Operation Instruction (01) 13. Adverse Weather Conditions.

Revision 1. for potentially freezing temperatures. The two other fire

pumps. diesel-driven FSP-2A and FSP-2B, were both rendered ino)erable on

January 17 because both fire pump building fans had to be disa) led and

placed in pull-to-lock as required by 01-13. This removed the

combustion air supply for the diesel FSPs so they had to be declared

inoperable. On January 18 a concern was raised about the continued

lifting of the FSP-1 discharge relief valve due to the low recirculation

flow of 600 gpm and corresponding high discharge pressure. This was a

concern because the relief valve water was directed to the turbine i

building sump and required processing prior to being released offsite. l

The recirculation flow was raised to 2000 gpm after consulting with a

fire protection engineer to lower the pressure and reseat the valve.

Approximately five hours later, oncoming shift operators questioned the

impact of the higher recirculation flow rates on operability of FSP-1. i

Although OP-880 only contained a note to ensure recirculation flow does

not exceed 2000 gpm. further consultations with fire protection  :

engineers revealed that any flow above 600 gpm rendered the pump

'

inoperable due to the lower discharge pressure and flow diverted from

the header for recirculation. Consequently, all 3 FSPs were inoperable

for over five hours.

Shift supervision immediately recognized the seriousness of this

situation and restored the two diesel FSPs to operable, initiated an 01-

12 investigation, and developed a Short Term Instruction to provide

interim recirculation flow rate guidance. PC 97-357 was initiated to

perform a root cause investigation, and the Director of Nuclear Plant

Operations prioritized this issue by placing it on his "short fuse"

list. The root cause evaluation and corrective actions were developed

,

by January 31. Although subsecuent revisions delayed issuance of it

until February 5 and the licensee's Corrective Action Review Board

(CARB) did not review the event until February 18. the inspector noted

the licensee's root cause determination and corrective action plans were

adequate. The licensee determined that the 600 gpm recirculation limit

was not contained in procedures and was not reflected in the Fire

56

Protection Plan. Their investigation revealed several other

-

communication and procedural problems which they adequately addressed.

Consequently, this licensee identified violation meets the requirements

outlined in Section VII of the Enforcement Policy and will not be cited; f

This issue is identified as Non-Cited Violation NCV 50-302/97-01-03.  !

Inadequate Fire System Recirculation Procedure. i

t

c. Conclusion'  ;

.

The inspectors concluded that the subsequent operations shift exhibited '

l

a questioning attitude that resulted in the discovery of this condition. .

Corrective action was implemented in a timely manner although the delay  ;

'

for the CARB to review the corrective action plan left room for

improvement. The inspectors had concerns about the lack of guidance in  ;

the procedures for the operators to make operability determinations but i

were satisfied.that the licensee's corrective actions would address j

them.

R1 Radiological Protection and Chemistry (RP&C) Controls  ;

R1.1 General Comments (71750) i

The inspectors conducted routine tours of the licensee's radiologically  ;

controlled areas (RCA) and verified radiological controls such as

control of locked areas. surveys and postings, and access controls. The

inspectors routinely observed status of the radiation monitoring and

meteorological systems. Chemistry results were typically reviewed daily

during normal work days. Generally good performance was noted in these

areas. Highradiationareaswereciearlymarkedandlocked.

The inspectors observed daily priority is placed on tracking of

radiological exposure against outage goals. Although the goal and

exposure amount occasionally did not agree, the licensee was actively

refining their 3redictions and results were improving. The inspectors

also observed tlat the licensee accomplished a notable achievement. in

that the reactor building was decontaminated sufficiently to relax some

protective clothing requirements for tours and walkthroughs. The

inspectors did not identify any deficiencies in the areas of

radiological controls or chemistry.

51 Conduct of Security and Safeguards Activities

S1.1 Protected Area Security Breach

a. Insoection Scooe (71750)

On January 30. 1997, at 6:45 p.m. the licensee discovered a penetration

path into the protected area via a breach in a condenser waterbox. The

inspector reviewed the licensee's investigation documentation in PC 97-

0053 and Security Information Report 10815 and interviewed licensee

personnel, j

i

5

!

. - , , _ _ . ,, ,_

. _ _ , . .- . . - . ..-.- - - . ._ -

_

57

b. Observations and Findinas

The breach was discovered by an alert security officer who questioned

maintenance work that had removed components he did not recognize. The  !

breach was immediately posted as a compensatory measure and security

force members initiated efforts to determine the scope of the problem.

They determined that the breach had existed for aaproximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />

and was in excess of the allowable security plan areach size, so it did

constitute a protected area breach. The inspector noted that the i

maintenance work was stopped and the security guards performed an

inspection of the vital and protected areas to ensure they were not 3

compromised. The licensee reported the event as discussed in paragraph

01.2 and was developing a written Licensee Event Report. The inspector

determined that security 3ersonnel had been properly notified of the

maintenance work, and it lad been evaluated for the potential to cause a

breach. However following the removal of the com>onents the security 1

officer expressed a concern that a penetration pati was opened that was

not recognized by the licensee. Consequently, appropriate compensatory

measures were not implemented. The licensee had a similar penetration j

3athway via a waterbox breach on November 1.1996. which was identified

)y the NRC as Escalated Enforcement Item 50-302/96-18-04. The

corrective actions for that item and the January 30 occurrence were

discussed at an Enforcement Conference held at the NRC Region II Office

on February 14. 1997. The resulting enforcement action EA 97-012 was

issued on February 28. 1997. The above violation is an additional

example of violation No. A(4)(01043) which was issued in EA 97-012. The

inspectors determined that those corrective actions, which were not yet

fully implemented, would be adequate to address the problems. The

inspector also observed that licensee management assembled an effective

investigation team the next day to assess the potential for any other

penetration pathways although their expectation was that this effort

would be initiated by shift management at the time of occurrence.

c. Conclusions l

The inspectors identified the January 30 waterbox breach as a second

example of violation No. A(4)(01043) which was issued in EA 97-012. The

inspector concluded the licensee security staff displayed a questioning

attitude to discover the breach, but the licensee's initial

investigation was not prioritized properly as discussed above and in 1

paragraph 01.2. The inspectors concluded the licensee's planned j

corrective actions were appropriate to prevent recurrence.  !

S1.2 Security Event Loa Audit (71750)

The inspector audited the Security Event Log (SEL). required by Appendix

G of 10 CFR 73. for the first. second, and fourth quarters of calendar

year 1996. The inspector verified selected problems were adequately

logged and that log items were routinely reviewed by security

management. The ins)ector reviewed the Security Information Reports

(SIR) associated wit 1 several of the logged problems in detail and did

not identify any problems. These events included problems such as vital  !

i

l

_.

. - . - -- - - - .- . = . . -. - .. - -

h

!

!

58

l

area doors left unsecured, security badges inadvertently removed from  :

l the site, and human error events. The inspector also observed that a PC  :

document was generated on initiation of each SIR to include the problem ,

in the plant wide corrective action program. The inspector concluded  :

this was a good practice for both management visibility and trending ,

I purposes. The inspector did not identify any problems with the number  :

i

of events and observed that the trends in some areas such as unsecured i

vital doors were notably improved. The inspector concluded the licensee  :

was appropriately maintaining the Security Event Log. {

V.Manaaement Meetinas  !

X1 Exit Meeting Summary l

The inspection scope and findings were summarized on January 31. February 14  :

'

and February 27, 1997. Proprietary information is not contained in this

report. Dissenting comments were not received from the licensee.  ;

X2 Pre Decisional Enforcement Conference Summary

l

X2.1 An Enforcement Conference was held on January 24, 1997, in Region II to i

discuss apparent violations associated with the Emergency Diesel

tienerators, the Emergency Feedwater System and containment penetratioris.

Results of this meeting were issued as an escalated enforcement action

on March 12. 1997.

X2.2 An Enforcement Conference was held on February 14, 1997, in Region II to

discuss apparent violations associated with Security. These apparent

violations are discussed in Inspection Report 50-302/96-18. and

results of this meeting were issued as an escalated enforcement

action on February 28, 1997.

X3 Management Meeting Summary

X3.1 A public meeting was held on site at Crystal River February 12. 1997.

The purpose of the meeting was to discuss items related to restart. A

separate meeting summary was issued on February 19. 1997.

PARTIAL LIST OF PERSONS CONTACTED

Licensees

K. Baker. Manager. Nuclear Configuration Management

D. Bates. Manager. Quality Systems

J. Baumstark. Director. Quality Programs

-P. Beard. Senior Vice President. Nuclear Operations

.G. Becker. Manager. Nuclear 0)erations

.J. Cam) bell. Assistant Plant )irector, Maintenance

-W. Con (lin. Jr.. Director. Nuclear Operations Materials and Controls

J. Cowan. Vice President. Nuclear Production

D. Daniels. Manager. Nuclear Safety Assessment Team

R. Davis. Assistant Plant Director. Operations

._ .

59

D. DeMontfort. Manager. Nuclear Operations ,

M. Donovan. Supervisor. Rapid Engineering Response Team ,

B. Gutherman Manager. Nuclear Licensing l

G. Halnon. Assistant Director. Nuclear Operations Site Support

B. Hickle, Director, Nuclear Plant Operations ,

J. Holden. Director. Nuclear Engineering and Projects j

R. Knoll. Supervisor. Nuclear Engineering

H. Koon. Manager. Nuclear Production and Nuclear Outage

D. Kunsemiller. Director. Nuclear Operations Site Support

J. Maseda. Manager. Engineering Programs

R. McLaughlin. Nuclear Regulatory Specialist

D. Poole. NGRC Member

D. Roderick.-Manager.-Outage and Work Controls

W. Rossfeld. Manager. Site Nuclear Services

J. Stephenson. Manager Radiological Emergency Planning

F. Sullivan. Manager Nuclear Engineering Design

J. Terry. Manager. Nuclear Plant. Technical Support

J. Tunstill. Senior Nuclear Licensing Engineer

D. Watson. Manager. Nuclear Security

R. Widell. Director. Nuclear 0)erations Training

D. Wilder. Manager. Radiation protection and Chemistry

R. Yost. Manager. Nuclear Quality Assessment

NRC

B. Crowley. Reactor Inspector. Region II (January 27 through 31. 1997.

February 10 through 14, 1997)

P. Fillion. Reactor Inspector. Region II (January 27 through 31. 1997.

February 10 through 14, 1997)  !

F. Hebdon. Director. Directorate 11-3 NRR (February 12, 1997) l

J. Jaudon. Director. Division of Reactor Safety. Region II (February 11

through 12. 1997)

K, Landis. Branch Chief, Region II (January 27 through 29, 1997)

L. Mellen. Project Engineer. Region II (January 27 through 31, 1997. February

10 through 14. 1997)

L. Raghavan. Project Manager NRR (February 10 through 13, 1997)

R. Schin. Reactor Inspector. Region II (January 27 through 31. 1997. February

10 through 14. 1997)

M. Thomas. Reactor Inspector. Region II (January 27 through 31, 1997. February

10 through 14, 1997)

INSPECTION PROCEDURES USED

IP 37550: Engineering i

IP 37551: Onsite Engineering j

'

IP 40500: Effectiveness of Licensee Controls in Identifying. Resolving and

Preventing Problems  ;

IP,61726: Surveillance Observations 1

, IP 62703: Maintenance Observations i

IP 62707: Conduct of Maintenance i

"

IP 71707: Plant Operations

IP 71750: Plant Support Activities

_ _.. - .__ _ __ _ . - _ _ . . _ . _ _ _ --. - __ _

- - - - . - . - - - - - . . - . - . . - - - . - . - . - - .

,

!

r

i

i

60  !

\

-IP 9h'00: Onsite LER Review I

IP 92901: Followup - Operations  !

IP 92902: Followup - Maintenance  !

IP 92903: Followup - Engineering - i

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened i

i

lypf Item Number Status Descriotion and Reference  !

i

VIO 50-302/97-01-01 Open Inadequate Clearance Tagging Requirements.  ;

.(paragraph 01.3) l

VIO 50-302/97-01-02 Open -Failure to Follow Procedures, Resulting in  !'

an lnadv& tent Emergency Diesel Generator

Start. (paragraph 01.6)

VIO 50-302/97-01-04 Open Failure to Perform TecHeal Specification I

Surveillance for Spent M Pool Level. i

(paragraph M1.1) ,

URI 50-302/97-01-06 Open HPI System Design, Licensing Basis, and TS

Concerns. (paragraph E1.3)  ;

'

VIO 50-302/97-01-07 Open Instrument Loop Uncertainty Setpoint

Calculation Assumptions Not Translated

Into Procedures. (paragraph E8.4)

URI 50-302/97-01-08 Open Adequacy of Procedures to Take the Plant

from Hot Standby to Cold Shutdown from

Outside the Control Room. (paragraph E8.6)

VIO 50-302/97-01-09 Open Inadequate Corrective Actions for Cable

Ampacity. (para 0raph E8.5)

Closed

lysg Item Number Status Descriotion and Reference

NCV 50-302/97-01-03 Closed Inadecuate Fire System Recirculation

Procecure. (paragraph F3.1)

NCV 50-302/97-01-05 Closed Inadequate Surveillance Procedure to Test

Operability of Toxic Gas Chlorine

Detectors. (paragraph M1.5)

VIO ~ 50-302/96-05-01 Closed Failure to Follow Procedures to Initiate

Corrective Action for Bent Main Steam Line

Hangers. (paragraph 08.1)

VIO 50-302/96-05-05 Closed failure to Follow Procedures for Updating

\

.- . . _- - . .- - ,

. . _ ._ _ _ . - - . _ _ _ _ _ _ . ._ _ _ _ __ _ . _ . _ _ _ . . _ _ . _ . . . . _ ._._

!

!

!

!

61

f

DBDs. (paragraph E8.1) j

,

t VIO 50-302/96-05-07 Closed Inadequate Receiving Inspections for l

Battery Chargers. (paragraph E8.2) }

.

, VIO 50-302/96-05-08 Closed Failure to Follow Purchasing Procedures j

for Inverters. (paragraph E8.3) -

LER 50-302/96-12-02 Closed Operation Outside Design Basis Caused by

Battery Chargers Having Inadequate Test  ;

Results Accepted in Error. (paragraph i

'

E8.2)  !

.

IFI. 50-302/95-15-01 Closed Design Requirements for Nitrogen

Overpressure. (paragraph E8.7)

l ,

IFI '50-302/96-201-13 Closed Cable Ampacity Exceeded for DHP-1A [DCP- l

1A] Feeder Cable and Others. (paragraph  !

E8.5) l

1

i

'

URI 50-302/96-05-02 Closed Design Concerns with the Main Steam Lime i

Hangers Used in Seismic and Other Dynamic ,

Load Applications. (paragra)h 08.1)

. NCV 50-302/97-01-10 Closed Inadequate Design Control ion-Safety

Related Components in Safety Related

)'

Applications - Two Examples: Thyrite Surge

Protection Device. Operator and Controller

,

for MUV-103. (paragraph E1.2)

l D.lic_Ultd

1

l- Iyng Item Number Status Descriotion and Reference

,

4

URI 50-302/96-17-03 Open Failure to conduct required technical

.

specification surveillance testing on

safety related circuitry. (paragraph M8.1)

! URI 50-302/96-201-04 Open Non Safety-Related Positioners on Safety-

i Related Valves. (paragraph E8.6)

VIO 50-302/96-09-07 Open Inadequate Corrective Actions for

f Implementation of EFIC Task Force

Recommendations (paragraph E8.8)

- VIO 50-302/95-21-03 Open Failure to Isolate the Class IE from the

Non Class IE Electrical Circuitry for the

< Reactor Building Purge and Mini-Purge

,

Valves. (paragraph E8.9)

1

'

EA 50-302/96-016 Open Use of Nonconservative Trip Setpoints for

Safety-Related Equipment. (paragraph E8.4)

,

c .--~ - , _

_m_. , ___ , . . , _ , 4 ., ,_., , _ , _ _ _ . ,,__y _ _ -,m. ... . , . _ iw -

_ __ _ . . _. __

i

,

62

EA 50-302/97-012 Open Failure to Maintain Protected Area  !

Barriers. Second Example of EA 97-017.

Violation A(4)(01043). (paragraph S1.1)

LIST OF ACRONYMS USED

AI - Administrative Instruction '

AP - Abnormal Procedures

AR - Air Removal i

BAST - Boric Acid Storage Tank c

CARB - Corrective Action Review Board  :

CCHE - Control Complex Habitability Envelope

CFR - Code of Federal Regulations

CFT - Core Flood Tank

CREVS - Control Room Emergency Ventilation System i

CR3 - Crystal River Unit 3

CT - Current Transformers

DBD - Design Basis Document i

DBI - Design Basis Issue l

DH - Decay Heat

DHP - Decay Heat Pump i

DHV - Decay Heat Valve i

DNPD - Director Nuclear Plant Operations '

EA - Enforcement Action

ECCS - Emergency Core Cooling System

EDBD - Enhanced Design Basis Document

EDG - Emergency Diesel Generator

EEI - Escalation Enforcement Item

EFIC - Emergency Feedwater Initiation and Control

EFW - Emergency Feedwater

ES - Engineered Safeguards

ESOPM - Environmental and Seismic Qualification Program Manual

FLA - Full Load Am)eres

FLUR - First Level Jndervoltage Relays

FME - Foreign Material Exclusion

FPC - Florida Power Corporation

FSAR - Final Safety Analysis Report

FSP - Fire Service Pump

FTI - Framatome Technologies, Inc.

GL - Generic Letter

HPI - High Pressure Injection

HVAC - Heating Ventilation and Air Condition

I&C - Instrumentation and Control

IFI - Inspection Followup Item

IPAP - Integrated Performance Assessment Process

ISA - Instrument Society of America

ISI - Inservice Inspection

KW - Kilowatts

LER - Licensee Event Report

LOCA - Loss of Coolant Accident

LOOP - Loss of Offsite Power

LPI - Low Pressure Injection

63

MAR - Modification Approval-Record

MCAP - Management Corrective Action Plan

MSLB - Main Steamline Break i

MUV - Make-up Valve

NCV - Non-cited Violation

/ NEP - Nuclear Engineering Procedure  :

NGRC - Nuclear General Review Committee

NOTES - Nuclear Operations Tracking and Expediting System

NOV - Notice of Violation

NPSH - Net Positive Suction Head

NP&SM - Nuclear Procurement and Storage Manual

N0A - Nuclear Quality Assessments

NRC - Nuclear Regulatory Commission

NRR - Office of Nuclear Reactor Regulation

OCR - Operability Concerns Resolution

OI - Operating Instruction ,

OJT - On The Job Training

OP - Operating Procedure

PC' - Precursor Card

PM - Preventive Maintenance

PMRG - Plant Modification Review Group

PMT - Post Maintenance Test

PORV - Power Operated Relief Valve

PR - Problem Report

PRC - Plant Review Committee

PT - Licuid Penetrant Test

RCA - Raciologically Controlled Area

RCBT - Reactor Coolant Bleed Tanks

RCP - Reactor Coolant Pump

RCS - Reactor Coolant System

REA - Request for Engineering Assistance -

RG - Regulatory Guide >

RP&C - Radiological Protection and Chemistry

SBLOCA - Small Break Loss of Coolant Accident

SEL - Security Event Log i

SIR - Security Information Reports

SLUR - Second Level Undervoltage Relays

SM - Shift Manager

SP - Surveillance Procedure

SR - Surveillance Requirement

SRO - Senior Reactor Operator

SSC - System. Structure or Component

SSOD - Shift Supervisor on Duty

TC - Temporary Change

TDBD - Topical Design Basis Document

TS - Technical Specification

URI - Unresolved Item

VIO - Violation

WI - Work Instructions

WR - Work Request

. WSI - Welding Services. Inc.

,