ML20129F456
ML20129F456 | |
Person / Time | |
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Site: | FitzPatrick |
Issue date: | 10/23/1996 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20129F432 | List: |
References | |
50-333-96-06, 50-333-96-6, NUDOCS 9610290129 | |
Download: ML20129F456 (47) | |
See also: IR 05000333/1996006
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U.S. NUCLEAR REGULATORY COMMISSION
Region i
Docket No.: 50-333
License No.: DPR-59
Report No.: 50-333/96-06
Licensee: New York Power Authority
Facility: James A. FitzPatrick Nuclear Power Plant
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Location: Post Office Box 41 I
Scriba, New York 13093 l
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Dates: July 28,1996 through September 28,1996 l
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l Inspectors: G. Hunegs, Senior Resident inspector ;
R. Fernandes, Resident inspector !
R. Barkley, Project Engineer ,
P. Bonnett, Resident inspector !
l L. Eckert, Radiation Specialist
j J. Furia, Senior Radiation Specialist ,
i J. Jang, Senior Radiation Specialist l
W. Schmidt, Senior Resident inspector l
R. Skokowski, Resident inspector !
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Approved by: Curtis J. Cowgill, Chief, Projects Branch 2
l Division of Reactor Projects !
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9610290129 961023
PDR ADOCK 05000333
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EXECUTIVE SUMMARY
James A. FitzPatrick Nuclear Power Plant
NRC Inspection Report No. 50-333/96-06
This integrated inspection included aspects of licensee operations, engineering,
maintenance, and plant support. The report includes the results of routine health physics
and effluent control program inspections. In addition, the results of a special team
inspection conducted to review the September 16,1996 reactor scram event are included.
Operations
Overall, the inspectors noted good performance by the operation staff during the inspection
period.
e During the performance of 345 KV backfeed transformer ground fault protective
relay calibration, two terminals were inadvertently shorted, which tripped the
generator output breakers and resulted in a plant scram. Because of the particular
relays involved, a residual transfer vice a fast transfer of electrical loads occurred,
resulting in the loss of numerous balance of plant loads. The inspectors determined,
with the exception of the issues noted below, that the abnormal and emergency i
procedures used during the event were appropriate and gave the guidance and
information needed by the operators and that operators responded well.
e An inadequate procedure to restore the'uninterruptible power supply (UPS) bus and
a broad scoped protective tag-out impeded the prompt restoration of UPS. Loss of l
UPS power to some control room indications, the plant paging system and the !
security computer made communications and plant access difficult. Communication
difficulties were managed by utilization of radios. The de-energizing of the reactor
protection system (RPS) was an operator error and the misdiagnosis of the plant ,
conditions with regards to the RPS was a training weakness. Additionally, the l
training operators received for residual transfer events was unrepresentative of the
actual plant response. l
e The inspectors determined that overall, the PORC appropriately addressed nuclear
safety matters related to the September 16th plant scram. Action items required for ;
start-up were satisfactorily resolved, and overall, the startup was performed in a ,
safe and prudent manner. !
e The condenser response related to the September 16th event (i.e. the MSIV
isolation signal input on low condenser vacuum) remains an unresolved item (50- ;
333/96006-02).
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Executive Summary (cont'd)
Maintenance
- The LCO maintenance activity to replace the A LPCI battery was conducted very
well with significant efforts to reduce the duration in which the plant was in the
LCO. The quality of the maintenance performed and the level of effort devoted to
the planning of the job was very good. The inspector did note that the seismic
qualification process of the battery cells, via similarity, did not ensure that the
component was an exact one-for-one replacement of the previously qualified
battery. The inspectors will followup on this issue to determine whether any
unqualifiable equipment was installed in the plant (IFl 50-333/96006-03).
- The maintenance staff responded well to the failure of the B EDG to properly 1
sequence during surveillance testing by identifying the cause and taking appropriate i
corrective actions. Subsequent documentation in LER 96-009 was clear, concise i
and provided sufficient information on the. cause and corrective actions taken and
planned for the future.
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e The 24V instrument Battery Replacement maintenance was performed well and had
the appropriate engineering, quality assurance and operations involvement.
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- Post work testing for the replacement of a capacitor in the HPCI inverter power I
supply was good and the timeliness of the corrective actions to industry information
on inverter failures was adequate.
- The licensee's actions to determine the cause of the continued difficulty over the
last six months with manually loading the B and D EDGs during surveillance testing
and increasing the testing frequency were appropriate.
- The risk significance of the 345 kV relay maintenance was not recognized during
planning or conduct of the work. The technician recognized the plant impact and
risk significance of the maintenance, but did not relay this to supervisors or control l
room staff. The subsequent personnci error resulted in a significant challenge to )
plant operators and a substantial disruption in plant activities. Contributing causes l
were improper work request planning, failure to communicate plant risk, and failure l
to properly protect energized adjacent terminals (VIO 50-333/96006-01).
Enaineerina
e Troubleshooting associated with the September 16 and 18 failures of the RHR D
circuit breaker were adequate, and the corrective actions taken to modify the
applicable safety-related circuit breakers were appropriate. However, the inspector
considered troubleshooting associated with the May 8,1996, failure of the RHR D
circuit breaker to lack the expected rigor, in that troubleshooting assumed the
location of the problem without adequate confirmation. Furthermore, the root cause
of a previous failure on May 8,1996, lacked rigor, and more thorough
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Executive Summary (cont'd)
troubleshooting, such as confirmation of this root cause, may have located a
. problem with the 52SM/LS contact 5-6 and prevented the failure of RHR D pump
during the September 16,1996, plant transient.
- The inspector concluded that adequate controls were implemented, following the
failure of a TIPS power supply and opening of three containment isolation valves, to
ensure compliance with technical specifications (TS) for inoperable containment
I isolation valves. The licensee is continuing to investigate the failure of the power
supply and opening of the isolation valves and as such the issue will remain
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unresolved pending the results of their design review (URI 50-333/96006-004).
- * The inspectors reviewed and closed URI 95-21-02. The inspector concluded that
the engineering staff performed a thorough and detailed root cause investigation of
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the EQ fuse discrepancies identified to date and developed a comprehensive series
of corrective actions to prevent recurrence. However, the inspector determined that
since documentation of the environmental qualification of fuses were not in an
auditable form, as required by 10 CFR 50.49.j, a violation of NRC requirements
occurred. -This violation was not cited in accordance with Section Vll.B.1 of the
Plant Sucoort
- During the September 16,1996, event, the implementation of the emergency plan
was a sound decision. The event was appropriately classified, timely notifications
made, and the TSC and OSC were properly staffed and provided assistance to
operators in a timely manner. EP procedures, logs and status boards were in use
and no significant EP facility discrepancies were evident. EP radiological activities
were well coordinated. Based on surveys and environmental radiation monitoring
results, there was no indication of any increased radiation levels associated with the
event. Security force members responded in a timely manner to assist with plant
communications and vital area access.
- Tne licensee implemented and maintained excellent radioactive liquid and gaseous
effluent control programs, sufficient to protect the public health and safety and the
environment. The chemistry staff also demonstrated good knowledge and ability,
and effectively implemented effluent controls in accordance with regulatory
requirements. Maintenance and attention provided to the station ventilation
systems was superior.
- The licensee continues to address previous concerns regarding radiation worker
practices and the performance of the radiation protection staff. Training of radiation
workers has become a licensee strength. Audits, surveillancas and self-
assessments of the radiation protection program continue to improve.
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j TABLE OF CONTENTS
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EX EC UTIV E S U M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii :
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TAB LE O F CO NT E NTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v
Summary of Pla nt Statu s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1. O p e r a t i on s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .. . . . . . . . . . . . . . . . . . . . . . 1
01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
01.1 Generator Load Reject and Plant Trip Overview ............. 1
01.2 Startup O bservations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
O2 Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 3
O 2.1 Engineered Safety Feature (ESF) System Walkdowns (71707) . . . 3
03 Operations Procedures and Documentation ..................... 4
03.1 Procedure Adequacy ............................ ... 4
04 Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 5
04.1 Operator Performance ............................... 5
04.2 Uninterruptible Power Supply (UPS) MG Set Recovery ........ 6
04.3 De-energizing of the Reactor Protection System (RPS) Electrical
Buses ........................................... 7
05 Operator Training and Qualification . . . . . . . . . . . . . . . . . . . . . . . . . . . 8
06 Operations Organization and Administration . . . . . . . . . . . . . . . . . . . . . 9
06.1 Plant Operations Review Committee . . . . . . . . . . . . . . . . . . . . . 9
11. M a i n t e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
M1 Conduct of Maintenance ................................. 10
M 1.1 General Comments ................................ 10
M1.2 Surveillance Observations ........................... 10 .
M1.3 Conclusions on Conduct of Maintenance . . . . . . . . . . . . . . . . . 11 l
M 1.4 On-Line Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
lil. Engineering .................................................. 17
E8 Miscellaneous Engineering Issues (37551) . . . . . . . . . . . . . . . . . . . . . 17
E8.1 Review of the Residual Bus Transfer during the September 16
Plant Transient ................................... 17 j
E8.2 Failure of the D Residual Heat Removal Pump Circuit Breaker j
During Torus Water Cooling .......................... 18 l
E8.3 Traversing In-Core Probe (TIP) System Ball Valve Control I
Failure ......................................... 21 l
E8.4 (Closed) (URI) 50-333/95021-02: Environmentally Qualified i
(EO) Electrical Fuses ............................... 21 l
E8.5 Review of UFSAR Commitments . . . . . . . . . . . . . . . . . . . . . . . 22
I V. Pl a nt S u p po rt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23 i
R1 Radiological Protection and Chemistry (RP&C) Controls (84750) ..... 23
R1.1 Management Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
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Table of Contents (cont'd)
R1.2 Review of the Offsite Dose Calculation Manual (ODCM) ...... 24
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R1.3 Implementation of Radioactive Liquid and Gaseous Effluent
Control Programs . . . . . . . . . . . . . . . . . . . . ............. 25
R1.4 Calibration of Effluent / Process Radiation Monitoring Systems
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(RMS).......................................... 26
R1.5 Air Cleaning Systems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
R5 Staff Training and Qualifications in RP&C ..................... 27
R6 RP&C Organization and Administration ....................... 28
R7 Quality Assurance in RP&C Activities ........................ 30
R8 Miscellaneous issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30
R8.1 Evaluation of Unmonitored Release After September 16,1996
Scram ......................................... 30
P1 Conduct of Emergency Preparedness (EP) Activities . . . . . . . . . . . . . . 31
P3 EP Procedures and Documentation .......................... 32
F8 Miscellaneous Fire Protection issues . . . . . . . . . . . . . . . . . . . . . . . . . 32
F8.1 Performance of the Fire Suppression System during the
] September 16 Plant Transient . . . . . . . . . . . . . . . . . . . . . . . . . 32
S1 Conduct of Security and Safeguards Activities . . . . . . . . . . . . . . . . . . 33
V. M a n ag e m e nt M e eting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33
X1 Exit Me eting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33
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ATTACHMENTS
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Attachment 1 - EP Implementing Procedures Reviewed
i Attachment 2 - Procedures Reviewed Related to September 16,1996 Event
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Report Details l
Summary of Plant Status
The unit operated at 100% power until the September 16,1996, reactor scram.
Following the short forced outage and completion of corrective actions for
the event, the plant was critical on September 21 and returned to power on
September 23. The plant was operating at 70% power at the end of the inspection
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1. Operations
01 Conduct of Operations
01.1 Generator Load Reject and Plant Trio Overview
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On September 16,1996, the plant was operating at 100% power. The
uninterruptible power supply (UPS) motor-generator set was out of service for
maintenance and the UPS bus was being supplied from the alternate feed. All '
emergency core cooling system (ECCS) equipment was operable. Instrument and
control (l&C) technicians were replacing a 345 kilo-volt (KV) reverse power relay
when at 1:04 p.m., the screwdriver being used by one of the I&C technicians
slipped and touched two terminals of a generator ground protection relay. The
outgoing power circuit breakers tripped and initiated a generator load reject.
Turbine control valves received a fast close signal and turbine bypass valves opened
to dump excess steam to the condenser. A reactor scram signal was initiated by
the turbine control valves fast closure signal.
By design, the inadvertent operation of the reverse power relay operated additional
relays which blocked the fast transfer of plant buses to reserve power. A slower
residual transfer occurred and the plant buses saw an interruption of power. The
4KV buses were re-energized from reserve power after bus voltages fell to less than
25% of rated voltage. As a result of the residual transfer, many 4KV loads,
including condensate and condensate booster pumps, circulating water pumps,
service air compressors and most plant equipment power supplies (600V or lower
loads) were automatically tripped off due to the undervoltage condition and had to
be manually restored later by operator actions.
The alternate feed breaker to the UPS panel tripped on undervoltage during the
residual transfer resulting in a loss of all UPS loads including the page/ party
(Gaitronics), sound power phones, control room radio base r,tation and some plant
telephones, feedwater control and electro-hydraulic control (EHC) control power
circuits and some indications on the full core display.
When the voltage on the two emergency 4KV buses fell below 62% for 2.4
seconds, the four emergency diesel generators (EDGs) started as required. By the
time the EDGs reached rated speed and voltage, the residual transfer had restored
power to the two emergency buses; thus the EDG output breakers did not close.
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The generator trip caused the control valves to close rapidly and the bypass valves
to open. Reactor pressure increased to 1082 psig at 4 seconds after the trip,
during which the "G" safety relief valve (SRV) cycled open for a few seconds.
Reactor water level decreased as a result of the scram and turbine feed pump trip
resulting in both the high pressure coolant injection (HPCI) and reactor core isolation
cooling (RCIC) automatically initiating. Reactor water level reached its lowest
recorded level of 126 inches versus a normal operating level of 201.5 inches.
, Reactor pressure vessel (RPV) level was restored and maintained using HPCI and
RCIC pumps. For the duration of the transient, pressure was controlled using HPCI,
RCIC and manual operation of the SRVs.
With the initialloss of the electrical busses, the main circulating water pumps were
de-energized. This resulted in the loss of condenser heat removal capability and
condenser inlet water temperatures reached 225 degrees F because of continued
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heat addition from cascading steam and feedwater from the feedwater heating
system. Condenser back pressure increased until pressure increased above a point
at which one of the low pressure turbine rupture discs and reactor feed pump
rupture discs ruptured. The discs ruptured approximately 9 minutes after the I
reactor scram (about 1:13 p.m.). Electrical power was restored to the electrical
buses and loads were restored beginning appioximately 1:19 p.m.. At 1:40 p.m. a
notification of unusual event was declared and the technical support center (TSC)
and operational support center (OSC) were activated.
After the rupture discs were repaired and condenser integrity was restored, main
condenser heat removal capability was verified, and NYPA exited the emergency
plan. Normal shutdown cooling was established at 5:44 a.m. on September 20.
a. insoection Scoce
! The inspector reviewed the overall event to determine if the plant response was
bounded by the Final Safety Analysis Report (FSAR). The inspector reviewed the
transient analysis and discussed the event with plant management personnel. j
b. Observations and Findinas
The transient is described in FSAR Section 14.5.2.1, Control Valve Fast Closure -
Generator Load Rejection. The analysis described the plant response with bypass
valves available. Because of the residual bus transfer, the electro-hydraulic control
(EHC) pumps were de-energized and bypass valve (BPV) operation could not be
sustained long-term. This, however, did not impair the ability to reduce reactor
pressure through the BPV and the safety relief valve (SRV) operation; the reactor
operators maintained reactor pressure vessel (RPV) pressure and level control using
the high pressure emergency core cooling syrwms. The inspector determined that
the temporary loss of off-site power did not imnact the ability for emergency core
cooling systems to operate and fulfill their safety function.
The condenser response was evaluated against the FSAR descriptions. FSAR
section 7.11.2 states that "the condenser protection rupture disc is set at 5 psig...
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Because of the closure of the main steam isolation valves (MSIVs) on low 1
condenser vacuum, there will be no actuation of the rupture disc." The section l
continues with "However, in the unlikely event the rupture disc should rupture, the
resultant doses would not exceed those resulting from the steam line break inside ,
the turbine building as discussed in FSAR chapter 14." The licensee stated that '
Section 7.11.2 of the FSAR does not consider all conditions. The low condenser i
vacuum closure of the MSIVs is bypassed when the reactor mode switch is not in I
Run and the turbine stop valves are closed. By procedure, operators place the
mode switch in the Shutdown position after a reactor scram which bypasses the
low condenser vacuum MSIV closure signal. The licensee is continuing to evaluate i
the condenser response related to this event in conjunction with General Electric.
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The NRC plans to review the results of their evaluation.
c. Conclusions
The condenser response related to this event (i.e. the MSIV isolation signal input on
low condenser vacuum) is unresolved item (50-333/96006-02).
01.2 Startuo Observations
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a. Insoection Scope (71707)
The inspectors observed portions of the reactor startup conducted from September
21 to 23.
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b. Observations and Findinas
The startup was characterized by clear operator communications and procedure use,
attentive management oversight, and effective control by shift supervision. Shift -
turnovers were performed in a controlled manner and crew briefings were good.
c. Conclusions
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The overall startup was performed in a safe and prudent manner. I
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O2 Operational Status of Facilities and Equipment
O2.1 Enaineered Safetv Feature (ESF) System Walkdowns (71707)
The inspectors used Inspection Procedure 71707 to walk down accessible portions
of the following ESF systems:
- RHR Service Water System i
e LPCI Battery
- Emergency Service Water System
Equipment operability, material condition, and housekeeping were acceptable in all !
Cases.
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03 Operations Procedures and Documentation
03.1 Procedure Adeauacy
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a. Insoection Scoce l
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The inspector reviewed the abnormal and emergency operating procedures (AOP i
and EOP) listed in Attachment 2 to determine the adequacy of the guidance given to
the control room staff,
b. Observations and Findinas
The inspector determined that the abnormal and emergency operating procedures
gave appropriate guidance overall to the operators throughout the event.
Specifically, AOP-21, Loss of UPS, directed operators to verify the reactor
shutdown using back-panel indication because the front panel indications were de-
energized. The AOP also listed equipment and indications that were affected by the
UPS loss. AOP-1, Reactor Scram, and EOP-2, Reactor Pressure Vessel Control, (
sufficiently directed operator actions for stabilizing the plant and maintaining RPV
pressure and level control.
The inspector identified that the AOPs and EOPs did not direct operators to shut the
main steam isolation valves (MSIVs) in the event of a complete loss of vacuum.
The MSIVs automatically shut when main condenser vacuum reaches 8 inches (hg),
but the trip is bypassed when the reactor mode switch is not in RUN and the turbine
stop valves are shut. Operations management addressed this issue by initiating a
revision to the AOP-1, Reactor Scram and AOP-31, Loss of Condenser Vacuum,
procedures.
The senior licensed operator performing the Post Transient Evaluation identified that
AOP-57, Recovery from Residual Bus Transfer, stated that an MSIV Group 1
isolation was an automatic action. This action, however, was not the case and the
procedere was corrected. The inspector noted that these procedure deficiencies did
not negatively impact the operators performance during the event.
c. Conclusions
The inspector determined that the abnormal and emergency procedures used during
the event were adequate and gave the appropriate guidance and information needed
by the operators.
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04 Operator Knowledge and Performance
04.1 Operator Performance
a. Insoection Scope
The inspector reviewed overall operator performance during the event, including
scram verification, RPV pressure and level control, actions taken to cooldown the
RPV and restore the main condenser. The inspector reviewed operating logs,
procedures, and discussed the operator's actions with licensee management and
personnel,
b. Observations and Findinas
The control room operators responded well to the event performing the appropriate
actions as directed in the abnormal and emergency operating procedures to mitigate
the transient. The operators used alternate methods of verifying the reactor was
shutdown since the normal control panel indications were de-energized by the loss
of the UPS. Operators manually verified that all scram valves were open locally at
the hydraulic control units, to assure all control rods were fully inserted and later
confirmed that all control rods were fully inserted when power was restored to the
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UPS.
A reactor operator effectively maintained level and pressure control of the RPV
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using the high pressure coolant injection (HPCI) and reactor core injection cooling
(RCIC) systems and the safety relief valves (SRVs) to stabilize and cooldown the
reactor. The operators maintained an 80 degree cooldown rate using the above
mentioned systems until the condenser was returned to service and the cooldown
was completed using bypass valves. Pressure and temperature limits were not
exceeded throughout this evolution.
The operators responded, appropriately to the complete loss of condenser vacuum.
Due to the temporary loss of off-site power, all major plant systems were de-
energized. The operators did not immediately restart the circulating water pumps to
restore condenser vacuum because of the need to restart service water,
compressed air, and other systems necessary to support the circulating water
system and plant cooldown in accordance with the AOPs.
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The control room operators restarted the circulating water pumps about seven hours
into the event after the rupture disks were repaired and established a condenser
vacuum after 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />. The operators then completed the RPV cooldown using
bypass valves to the main condenser. The inspector determined that these actions
were appropriate and within the guidance of plant operating procedures.
c. Conclusions
In generally, the control room operators responded well to the event. Operators
immediately verified the reactor shutdown, stabilized pressure and level, and cooled
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down the RPV in a controlled manner. Control room supervision methodically
restored plant systems to enable repair of the main condenser rupture disc and re-
establish condenser vacuum to complete the plant cooldown. An exception to the
otherwise good performance was the operator actions taken to de-energize the
reactor protection system (RPS) bus (see section 04.3). However, a performance
issue related to securing the reactor protection system is discussed in Section 4.3
of the report.
04.2 Uninurruotible Power Sucolv (UPS) MG Set Recovery
a. Inspection Scoce (93702)
During the residual transfer of the plant electrical buses, the alternate feed breaker
to the UPS panel tripped on under voltage and by design did not reclose following
the transfer. This resulted in a loss of all UPS loads, including plant internal
communications (Gaitronics), feedwater control, high range effluent radiation
monitors, security computer, and various control room indications. The breaker was
manually closed by the operators 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and thirteen minutes following the plant
trip. The inspector conducted interviews, reviewed plant drawings and procedures
to determine if the power supply was restored in a timely manner and the impact on
the restoration of the plant.
b. Observations and Findinos
The UPS provides power to vital low voltage loads and utilizes a double motor
generator set (AC & DC motor) as the power source. The AC motor is powered
from the vital bus and the DC motor is powered from the battery. Under normal
circumstances the UPS transfers from the AC power source to the DC power source
upon loss of voltage to the vital bus. However, on September 12, the UPS MG set
had been removed for corrective maintenance to repair a bad motor bearing and
was not available during the transient. The UPS loads at that time were placed on
the alternate feeder breaker which provides power via the 12500 emergency bus.
The alternate feeder breaker is a unique low voltage molded case circuit breaker in
that it has an electric motor operating mechanism on the front of the breaker.
When the operators responded to the tripped UPS panel in the electric bay, they
noted that the alternate feeder breaker was " flagged" in the on position. Walk
down of the power supply to the UPS distribution panel by the operators determined
that the circuit had power. After getting permission from the control room, the
electrical supervisor opened the breaker operating mechanism door to observe the
position of the handle on the actual alternate power breaker. He discovered that
the breaker was indeed tripped open. The original diagnosis that the breaker was
closed was the result of the operating mechanism flag not repositioning when the
breaker trips on under voltage. Using appropriate electrical safety precautions the
electricians attempted to reset and manually close the breaker. When the attempt
was unsuccessful, the electricians stopped and reviewed the circuitry for any
problems. Subsequently a senior reactor operator returned to the panel, and was
able to reset the breaker manually, thereby resetting the UPS bus.
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The inspector reviewed the plant drawings and determined that control power was
available to the alternate feeder breaker following the residual transfer. However,
because of the paralleling switch on the UPS panel being protective tagged in the
off position for maintenance, the operators could not have closed the breaker
electrically without first clearing the protective tag. This tagout represented a
conservative personnel and equipment protection boundary; the delay posed by this
tagout had no significant effect on the overall outcome of this plant event.
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Additionally the inspector determined that the abnormal operating procedure
AOP-21, Loss Of UPS, would not have properly directed the restoration of the
alternate feeder breaker. The electrical operation of the breaker is such that the
under voltage coil opens the breaker and the motor operator functions to reset the
breaker so that it is ready to close automatically or when the operating switch at
the UPS panel is taken to the close position. The AOP did not have procedural
guidance for resetting the alternate feeder breaker and therefore would not have
'
allowed electrical closure of the breaker. The AOP did give subsequent guidance on j
manually closing the breaker; however, it did not give guidance on removing the
operating mechanism and operation of the molded case circuit breaker. As a result,
the licensee elected to revise the procedure and conduct training with operations
personnel on the UPS alternate feed breaker. Additionally, the work control center
is taking steps to ensure the ability to operate the UPS paralleling switch is not
significantly impeded during future protective tag-outs.
c. Conclusions
The inspector concluded that the absence of clear direction on the manual operation
of the UPS feeder breaker in the AOP and a tagout delayed the licensee in restoring
the UPS. This delay had no measurable impact on the outcome of this plant event.
The loss of the plant page and security computer made communications and plant
access difficult, but were managed by utilization of radios and posting security
guards.
04.3 De-eneraizina of the Reactor Protection Svstem (RPS) Electrical Buses
a. Insoection Scone (93702) i
l
The inspector conducted interviews and reviewed plant drawings and procedures to
determine the issues concerning the RPS power supply restoration during the
September 16 event. The impact on the restoration of the plant was also assessed.
b. Observations and Findinas i
l
Following the generator load reject and subsequent scram, the shift manager (SM)
ordered a shift of the RPS to the alternate power supply. This was done by the SM i
because he interpreted the dark full core display and the radiation monitor
annunciators alarming to be indicative of a loss of power to the RPS. RPS was
shifted to a deenergized bus which resulted in the MSIVs closing. j
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{ The operator tasked with transferring the power supplies failed to question the f act
i
that the white "MG-SET" light above the RPS power selector switch and the
darkened "TRANS" light meant that the system was energized and that the
alternate power supply was not. The inspector determined through walkdowns and
review of operating procedure OP-18, Reactor Protection System, that the
'
, procedure had sufficient guidance to properly shift RPS. However, because of the
'
number of activities and distractions present, the operator improperly transferred
RPS.
'
Through interviews, the inspector learned that the operators were of the impression i
that if the full core display was dark, that the RPS was de-energized in addition the l
) operators felt that the numerous radiation monitor annunciators were also indicative I
'
of a loss of RPS. The full core display is only partially powered from the RPS bus,
- with additional power coming from the UPS and non vital buses. The inspector
determined, through review of plant drawings and procedures, that the loss of the
- UPS bus would cause a similar alarming annunciator board, with respect to radiation I
,
monitors, as a loss of RPS.
c. Conclusions
l
The inspector concluded that the de-energizing of the RPS was an operator error '
- and that the misdiagnosis of the plant conditions with regards to the RPS was a
training weakness.
j 05 Operator Training and Qualification
,
a. inspection Scope
,
The inspector reviewed simulator training regarding residual bus transfers and
discussed this issue with the training staff and operations personnel,
b. Observations and Findinos
i
Control room operators informed the inspector that they had believed that the
reactor protection system (RPS) bus was de-energized during the event. This was
partially due to their training experience at the plant specific simulator and due to
confusion regarding the power supplies for the full core display. )
The simulator ca.1 not replicate a residual bus transfer because the computer is not
modeled for this type of transient. To accomplish the effects of the scenario, ,
training instructors insert manual overrides to create the transient affecting I
simulator fidelity with the plant. The RPS was always de-energized during the
training scenario. l
The control rod Full-in and Full-out as well as other light indications on the full core
display are powered from the UPS power supply. During the event, the operators )
became confused as to the power supply that fed the full core display, and
1
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4
operators believed that the RPS power supply was de-energized. Operation
management determined that the operator's training was deficient in this area.
.
The Plant Operations Review Committee (PORC) discussed this issue during their
i final review of the post transient evaluation. The PORC tasked the training staff to
- identify other scenarios that had simulator fidelity issues which could result in
negative training prior to start-up. Four training scenarios were ultimately identified;
these scenarios will not be used until modified and revalidated. Further, Operations
"
management conducted training sessions for the operators regarding the power
,
supplies for the full core display and other control room indications prior to startup.
c. Conclusions
i The inspector concluded that the training operators received for residual transfer
events was unrepresentative of the actual plant response. The PORC initiated a
- corrective action item for the simulator staff to identify other faulty training
d
scenarios. Operations management reviewed these negative indications with the
operations staff prior to re-starting the reactor.
06 Operations Organization and Administration
06.1 Plant Ooerations Review Committee
a. Inspection Scoce
The inspector observed the Plant Operations Review Committee's (PORC) final
review of the Post Transient Evaluation and of I&C's root cause assessment into the
cause of the event,
b. Observations and Findinos
The PORC concluded that there were no unresolved safety questions associated
with this event. PORC discussed the event, station personnel performance,
equipment performance, corrective actions required and lessons learned. These
discussions were open and candid. The PORC chairman emphasized the importance
of managers to communicate expectations to the plant staff, the importance of
possessing a questioning attitude when unexpected results occur and of self-
checking to preclude mistakes caused by over-confidence. The chairman identified
several other follow-up issues required to be completed prior to startup that were
subsequently resolved by the PORC.
c. Conclusions
The inspector determined that overall, the PORC adequately addressed matters
related to nuclear safety. Action items required for start-up were resolved to the
satisfaction of the PORC. The most significant items were independently reviewed
by the resident inspectors, including the conduct of training for operators and
administrative control of the TIP system.
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11. Maintenance
1
1
j M1 Conduct of Maintenance
M 1.1 General Comments
a. Insoection Scooe (62703)
The inspectors observed all or portions of the following work activities:
- WR 95-07873 replacement of 24VDC instrument battery
- WR 96-02875 calibrate 71-59N-1UPRN05 transformer ground fault
protective relay
- WR 96-01045 installation of alternate decay heat removal system per
modification F1-95-121
- WR 96-04877 turbine exhaust rupture disk
b. Observations and Findinas
The inspectors found the work performed under these activities to be technically
sound and thorough. All work observed was performed with the work package
present and in active use. Technicians were experienced and knowledgeable of
their assigned task. The inspectors frequently observed supervisors and system
engineers monitoring job progress, and quality control personnel were present
whenever required by procedure. When applicable, appropriate radiation control-
measures were in place.
M1.2 Surveillance Observations
The inspectors observed and reviewed portions of ongoing and completed
surveillance tests to assess performance in accordance with approved procedures
and Limiting Conditions for Operation, removal and restoration of equipment, and j
deficiency review and resolution. The following tests were reviewed: l
l
- ST-2X RHR service water flow rate, strainer and inservice test
- ST-35 A Containment spray / cooling system logic system functional test
b. Observations and Findinas J
The licensee conducted the above surveillance appropriately and in accordance with !
procedural and administrative requirements. Good coordination and communication I
were observed during performance of the surveillance. ;
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i
M1.3 C_q._plusions
n on Conduct of Maintenance
Overall, maintenance and surveillance activities were well conducted, with good
adherence to both administrative and maintenance procedures.
M1.4 On-Line Maintenance
M 1.4.1 24V instrument Batterv Reofacement
a. Insoection Scooe (62703)
During this inspection period, the licensee changed out the two sets of instrument
batteries as the result of a seismic qualification user's group recommendation for
other batteries at the plant. The inspector observed the maintenance activities and
reviewed the acceptance testing documentation to verify that the work had been
done in accordance with station procedures and industry practices. j
!
b. Observations and Findinas !
The two instrument batteries are made up of two sets of twelve individual cells.
The replacement cells for each battery was a C&D Power Systems model KCR-7
battery, classified as QA category I and having seismic design and installation
requirements. Each redundant batter', pair provides backup power during loss of off
site power or loss of power to its associated battery charger for two SRM/lRM trip
units, and several process radiation monitors in the plant. The replacement was
performed with the plant operating and the work was performed in a manner that
maintained the battery available for service and fully operable. The battery was
maintained operable by bringing fully charged spare cells on a portable cart into the
battery room and connecting the spare cells in parallel with the cells being replaced.
After the new cells were in place and connected to the bus, the parallel connections
to the spare cells were broke and the sequence was repeated for the other sets of
cells.
The battery work was performed in accordance with maintenance procedure MP-
57.06, Battery Maintenance, Revision 16. The evolution was controlled by a
temporary operating procedure TOP-234,24 VDC Instrument Battery Replacement
With Reactor in Run Mode, which sequenced the replacement of the batteries.
The inspectors observed the proper procedures and work control documents in use.
Maintenance personnel had established and implemented appropriate ignition, fire
prevention and personnel safety controls. The maintenance was performed well,
with the mechanics being very thorough with moving, assembling and testing the
cells.
The inspector noted that the acceptance criteria for the post installation resistance
readings in the maintenance procedure was not in accordance with IEEE Standard
484-1987, Recommended Practice for Installation Design and Installation of Large
Lead Storage Batteries for Generating Stations and Substations. The maintenance
. _ . - _ . - - . _ . -. . - - ---
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procedure had an acceptance criteria of less than 60 microhms. The IEEE standard
,
includes direction to remake and remeasure any connection that has a resistance
measurement more than 10% or 5 micro ohms, whichever is greater., over the
average of each type of connector. Subsequent to this, the licensee reviewed the
data and determined that three connections did not meet this IEEE criterion. Their
evaluation determine that although the resistance values did not meet this criterion, j
the resistance readings were lower than the previous readings and thus acceptable. ,
This was also the case for one connection on the initialinstallation of the A station i
battery in 1995. The licensee subsequently changed the procedure to reflect the
connection resistance readings requirements for new battery installations in the
procedure.
1
c. Conclusions
The inspector concluded that the maintenance was performed well and had the l
appropriate engineering, quality assurance and operations involvement. The j
licensee did not incorporate the complete acceptance standard for battery resistance
readings in the maintenance procedure. This reflected a lack of tieroughness in the !
preparation of the procedure. Subsequently, this error in the procedure was
adequately addressed.
M 1.4.2 LPCI MOV Batterv Power Sucolv Reolacement
a. Insoection Scone (62703)
!
'
The inspector reviewed the preparation for and conduct of the replacement of the A
low pressure coolant injection (LPCI) motor operated valve (MOV) independent
power supply battery during a limiting condition for operation (LCO) maintenance -
evolution. The inspector reviewed the physical condition of the installed
replacement battery, commercial grade dedication documentation for the battery, ;
the LCO preparation checklist, portions of maintenance procedures (MP)-057.06,
Revision 17, " Battery Maintenance", which was performed as part of the post-
maintenance testing on the battery, and MST-71.11, Revision 8, governing
quarterly surveillance testing on the battery.
i
b. Observations and Findinas i
This LCO maintenance activity was thoroughly evaluated prior to its conduct and
was approved based on its minimal potential safety implications to the plant. The ,
LCO maintenance evolution was well planned, supported and controlled as i
evidenced by the successful completion of the evolution in just under two days,
versus nearly 3.5 days as originally planned. The job was worked on a 24-hour
basis and considerable efforts were made by the assigned LCO coordinator and
other key individuals involved to minimize the duration the battery was out of
service as well as resolve emergent concerns. The quality of the installation work
was very good.
l
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.
13
The inspector identified that the battery was dedicated for seismic application via
similarity to a previously quahfied battery (i.e. the battery cell size and model
number were the same as hattery cells previously procured under a 10 CFR 50
Appendix B program and seismically qualified by the manufacturer). However,
discussions with the battery manufacturer confirmed that there was recent changes
to the battery design (i.e. material changes to the battery cap to improve impact
resistance, terminal post seal changes) which raised the question whether the new
battery cells were an exact one-for-one replacement. Subsequent engineering
analysis of the design modifications confirmed that the design changes to the
battery enhanced vice detracted from the seismic qualification of the battery. DER
96-971 was written to characterize and remedy the procurement process deficiency
identified in this matter.
c. Conclusions
The LCO maintenance activity to replace the A LPCI battery was conducted very
well with significant efforts to reduce the duration in which the plant was in the
LCO. The quality of the maintenance performed and the level of effort devoted to
the planning of the job was very good. The inspector did note that the seismic
qualification process of commercial grade equipment, such as the battery cells, via
similarity, did not ensure that the component was an exact one-for-one replacement
of a previously qualified component. The inspectors will followup on the findings of
DER 96-971 to determine the extent of this issue and whether any equipment that
is not seismica;ly qualifiable was installed in the plant (IFl 50-333/96006-03).
M 1.4.3 Failure of B EDG to Start Durina Surveillance Testina
a. Inspection Scoce (62703)
The inspector reviewed the reasons and corrective actions taken for a failure of the
B ernergency diesel generator start sequence during surveillance testing on July 22.
Including a detailed review of wiring schematics, plant procedures, EDG operating
manual, and subsequently the licensee event report (LER 96-009) submitted on
August 22.
b. Observations and Findinas
Operations personnel made proper log and TS action statement entries,
documenting the situation after the B EDG was declared inoperable. Following the
test failure, operations and instrument and control (l&C) personnel took good
actions to review the possible causes, including discussions with personnel in the
switchgear room. This led to the determination that the reverse power relay had
energized, and that it happened before the assumed 3.5 second time delay.
Troubleshooting effectively determined that an incorrectly installed time delay relay
and a failed motor on the D EDG governor booster pump, resulted in the tripping of
the EDG. The observation that the reverse power relay had energize too early led
the licensee, through electrical prints, to determine that the voltage sensing time
.,
.
14
delay relay which energizes the reverse power relay had not been installed in the
correct location. In effect this led to a time delay being set at 0.8 sec from the
designed 3.5 sec. However, the licensee was prennted with a problem since this
relay had been installed in this configuration in 1990 and the EDG had started
successfully during monthly surveillance testing, except for one instance in 1992
when the D EDG governor booster pump was found failed. Subsequent
troubleshooting found that the D EDG governor booster pump had failed in this
instance as well.
NYPA identified that two other relays had been incorrectly installed during 1990.
The inspector found that the two additional incorrectly installed relays would not
have affected any other safety related functions of the EDG control circuits,
c. Conclusions
Surveillance testing properly identified equipment conditions which led to the B EDG i
not properly sequencing during a surveillance test start. The failure of the B EDG to l
properly sequence resulted from an incorrectly installed time delay relay in the
reverse power sensing circuit and the failure of the D EDG governor booster pump.
NYPA did not identify the incorrect instailation of the time delay relay in 1992 when
a similar failure occurred. However, the surveillance tests conducted since then
proved that the EDG would have performed its design function. NYPA responded
well to the failure, identified tita causes and took appropriate corrective actions.
Subsequent documantation in LER 96-009 was clear, concise and provided
sufficient information on the cause and corrective actions taken and planned for the
future.
M 1.4.4 HPCI Inverter Failure
a. Insoection Scoce (62703)
On September 6, the HPCI inverter failed. The licensee performed trouble shooting
and determined the cause to be the failure of a capacitor inside the inverter. The
inspector reviewed the post work testing documentation for the replacement
capacitor and discussed the activities with the maintenance staff.
b. Observations and Findinos
The inspector reviewed the equipment vendor manual and compared the
manufacturers information with the post work test data and found it to be
satisfactory. The inspector also reviewed the licensee's response to NRC and
industry information on failed inverters as documented in the licensee's SOER 83-
03. The inspector determined that the licensee had originally evaluated the industry
information in 1984. The issue was reviewed again by the licensee in 1992 and in
1993 additional corrective actions were incorporated into the licensee's tracking
program. The past corrective actions by the licensee included incorporation of
electrolytic capacitor testing and/or replacement in a preventative maintenance
program for the inverters. As this recent failure was an oil filled capacitor, it was
.
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15 l
!
not included in the preventive maintenance program. The licensee plans on
replacing the oil filled capacitors in the HPCI and RCIC power supply inverters in the I
next refueling outage.
c. Conclusions
The inspector concluded that the corrective actions were appropriate and that the
inverter failure rates was low. The inspector determined that the post work testing
and the timeliness of the corrective actions to be adequate. i
M1.4.5 Failure of EDGs to Load Prooerlv
i
a. insoection Scooe (62703) l
On March 15, when attempting to performing ST-98, EDG Full Load Test and ESW
Pump Operability Test, the D EDG load started to increase more than the operator j
expected. Trouble shooting by the license at that time failed to identify any )
problems, however the droop circuit was suspect. On August 23, and September i
9, the problem reappeared on the D and B EDGs respectively. The inspectors
- reviewed the events to assess the maintenance troubleshooting activities and
operability of the EDGs.
b. Observations and Findinas
During both recent events after several manipulations of the governor speed control
switch, the operator determined the performance of the EDG was improper and
opened the output breaker. The B and D EDGs were declared inoperable and the ;
applicable LCO was entered. Trouble shooting was performed with strip chart '
recorders and instrumentation installed. The licensee was not able to identify the j
problem, but changed out the droop switches on both the B and D EDGs. The '
licensee had similar problems back in the 1977 time frame with the A EDG and I
problems with the B EDG in the 1980 time frame. The droop switches were l
replaced at that time and the problems did not reappear until this year.
In discussion with the licensee engineering staff, the inspector learned that the ;
droop switch is utilized only during surveillance testing when the operators are 1
manually connecting the EDG to a live bus. With the switch in the normal position,
the EDG load circuit is such that it senses load and automatically increases speed to l
pick up the electricalload as the safety related equipment starts. This feature is
undesirable during surveillance testing because the bus is already loaded and
connected to the main grid at 60 hertz. With the switch in normal, following
synchronization, the EDG would try to take all the load and would overload. The
droop circuit does the opposite. In the droop mode, when the EDG senses load, it
slows down the EDG and therefore does not assume any load. At this point, the i
operator uses the speed adjust control switch to load the EDG to the required ST l
value.
!
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16
The licensee plans on continuing the monitoring of the EDGs with additional
instrumentation during the increased surveillance testing and to change out the
droop switches on the A and C EDGs. The licensee also plans on performing an
equipment failure evaluation on the removed switch to attempt to determine if
contact oxidation was a factor in the problem.
c. Conclusions
The inspector concluded the licensee's actions to determine the cause of the
continued difficulty with loading the EDGs during surveillance testing were
appropriate.
M 1.4.6 345 KV Relav Calibration
a. Inspection Scone (62703)
!
During the performance of a 345 kV relay calibration, two terminals were
inadvertently shorted, which tripped the main generator output breakers. This
resulted in a main turbine trip and reactor scram as a result of the electricalload
loss (see section 01.1). The inspector reviewed the maintenance task chronology,
work package, maintenance and administrative procedures, department written
critique, and discussed the event with the maintenance supervisor.
b. Observations and Findinas
The scope of the work request was to remove the relay from service, remove the
external capacitor from the panel, calibrate the relay, reinstall the capacitor and
return the relay to service. A pre-job brief was conducted in accordance with ICSO-
20, instrument and Controls Pre-job Briefing. During the performance of the relay
and capacitor removal, the technician identified that the capacitor leads would have
to be disconnected from the terminal board area on the relay case instead of the
capacitor. This was not expected and is significant because the original work scope
encompassed a work area that was electrically separate from the operating plant.
As discussed in section E8.1 of this report, the relay is utilized when the plant is
shutdown and is electrically separate during normal plant operation. Working near
the terminal board area had the potential to, and in this case did, actuate the
protective feature of the relay causing the plant trip. Additionally, the technician
failed to electrically insulate the adjacent terminals prior to commencing the work.
As identified in the licensee's critique, the work package planning process,
conducted on June 6, for the relay calibration did not include a review of the
physical location and arrangement of the capacitor. Administrative Procedure (AP)
10.03, Work Package Planning, step 8.1.5 states, in part, to perform a walkdown
of the work site to obtain an understanding of the specific needs and location of the
work environment. Failure to adequately walkdown the work associated with WR
96-02875-00, to perform calibration of 71-59N-1UPRNOS, was not performed with
adequate detail to identify the high risk involved with performing the maintenance
with the plant at power.
_ . _ . _ __ _
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, The job scope required the removal of a capacitor from the back of the relay case. )
When faced with disconnecting the capacitor at the terminals, the technician did not '
stop the task. The technician recognized the plant impact if terminals 1 and 2 were
contacted but did not relay this to his supervisors or control room operators,
- Administrative Procedure AP-10.01, Problem identification and Work Control, step
j 8.5.7 states, in part, that personnel encountering unanticipated problems while
performing activities should stop work and notify department supervision. However .
, during the calibration of 71-59N-1UPRN05, when the technician discovered the
capacitor had soldered leads instead of mechanical fasteners, as expected, he failed
to notify his department supervision. In addition, Instrument Maintenance 1
Procedure IMP-G20, Generic Troubleshooting and Maintenance Procedure, I
referenced in the work request, states, in part, that prior to disconnecting wires,
ensure any adverse affects on plant equipment operation or operational status has i
been discussed with applicable control room operator (s) and shift manager.
, However, during the calibration of the relay, when the technician determined that l
1
the work had the potential to adversely affect the operation of the plant, he failed to l
notify control room operators, the shift manager, or his department supervision.
c. Conclusions
.
The risk significance of this maintenance was not recognized by the licensee during
'
. the work planning. When the risk was recognized, it was not communicated to the
'
control room operators or maintenance supervisor. The inspectors concluded that
the event was the result of improper work request planning, failure to communicate
- plant risk, and failure to properly protect energized adjacent terminals. Inadequate
walkdown during the planning process and the failure to communicate the risk on
the plant to control room operators constituted a procedure violation (VIO 50-
, 333/96006-01).
i
111. Enaineerina
E8 Miscellaneous Engineering issues (37551)
E8.1 Review of the Residual Bus Transfer durina the Seotember 16 Plant Transient
a. Insoection Scoce
! The inspector reviewed the electrical distribution bus transfer that resulted from the
- technician's error on September 16,1996. Additionally, the inspector reviewed the
1
design basis of the residual bus transfer as described in the Final Safety Analysis
to verify that the system operated as designed.
b. Observations and Findinas
'
As described in the FSAR, the automatic residual transfer takes place either after an
unsuccessful fast transfer, or when the nature of the disturbance will not allow a
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j- fast transfer. Residual transfer is delayed until the voltage on the affected bus has
- decayed to approximately 25% of the normal, allowing re-energizing of the buses
j without equipment damage.
I- 4
l The relay that the technician was calibrating, 59N-lUPRNOS, provides ground fault !
protection for the 24 kilo-volt (kV) isolated phase bus duct during the 345 kV
- . backfeed operation. During at power operation this relay is not connected to the
j system since ground protection is provided by other relays on the output of the
4
generator. The inspector independently verified that reported technician's error
l would have simulated actuation of Relay 59N-lUPR05, and that the relay actuation i
j would result in a residual bus transfer. Additionally, the inspector verified that the
{ residual transfer operated as design.
i
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During a review of the FitzPatrick design basis document (DBD) for the electrice' ,
distribution system, the inspector identified that the actuation of Relay N59- ;
IUPRN05 was not included in Section 4.0, " System Interfaces / Boundaries,
'
j
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j interlocks, and Actuations," for the affected circuit breakers, even though the relay
j was installed at the time the DBD was developed. However, the installation of the
relay was described in Section 8.38 of the Electrical Distribution System DBD, as
. ;
part of the system history of modifications. Although the DBD is not a required
document, it is used by the licensee for informational purposes. The licensee
intends to revise the electrical distribution system DBD Section 4.0 to included
Relay N59-luPRN05 as tracked by ACTS ltem 22509. *
c. Conclusions j
The inspectors determined that the reported technician error would have simulated
the actuation of the Relay 59N-lUPR05, which resulted in the residual bus transfer.
Additionally, the inspector verified that the residual transfer operated as designed.
E8.2 Failure of the D Residual Heat Removal Pumo Circuit Breaker Durina Torus Water
Coolina ;
a. Insoection Scope
Following the scram on September 16,1996, Residual Heat Removal (RHR) D
circuit breaker failed to close during an attempt to manually start the pump for torus
cooling. Torus water cooling was required to compensate for the heat added from
Safety Relief Valves (SRVs), High Pressure Coolant injection (HPCI) and Reactor
Core Isolation Cooling (RCIC), which were used to control reactor pressure during
the transient. The licensee initiated troubleshooting efforts to determined the
reason for the RHR D breaker failure. Throughout the transient, A,C and B RHR
pumps provided sufficient torus water cooling. The inspector reviewed the ,
licensee's troubleshooting activities associated with the failed start attempt, and the l
subsequent corrective actions. Additionally, the inspector reviewed the
maintenance history for the RHR D and other 4160 volt circuit breakers.
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b. Observations and Findinas
The initial troubleshooting on September 16, of the RHR D circuit breaker (4160 volt
General Electric (GE) Magne Blast, Model AMH-4.76-250-1D) indicated an "open" in
the closing circuit. After racking out the breaker for further troubleshooting, checks
of the circuit breaker internals indicated continuity. Additionally, no abnormal
indications were identified during a visual inspection of the breaker. The breaker
was racked in and operators successfully closed the breaker from the control room.
Based on a previous failure of the same circuit breaker, the licensee suspected that
the breaker was not racked in tight enough. This would cause the contacts
associated with the positive interlock to remain open and prevent the breaker from
closing. The positive interlock provides personnel safety during breaker racking
operations, which prevents the racking in of a closed circuit breaker.
On September 17, following the event, the licensee performed additional l
troubleshooting and noted that racking the breaker out slightly (less then a half of I
turn on the rackout tool) caused the same indication of an open in the closing !
circuitry as was observed during the troubleshooting the day before. As a result,
the licensee replaced the 52lS switch associated with the positive interlock, and
cleaned and lubricawd the racking mechanisms as preventive measures. The
breaker was cycled satisfactorily as a post maintenance test (PMT).
Based on the indications that the RHR D circuit breaker was not fully racked in, the
licensee wrote WRs 96-04852-00 through 33 to verify that all safety-related circuit
breakers that have an automatic close function were racked in fully. The PMT for
these WRs was the satisfactory remote start of the connected equipment. On
September 18, during the PMT for RHR D, the circuit breaker again failed to close.
1
WR 96-0482-32 was written as a detailed troubleshooting plan to further !
investigate the RHR D circuit breaker failures. Continuity checks of the closing
circuitry indicated the same "open" as identified on September 16. Detail
troubleshooting indicated that the "open" was at contacts 5-6 of switch 52SM/LS,
and not at the 52lS switch as earlier suspected. Additionally, the licensee verified
certain breaker measurements were within the manufacturer's allowed tolerances,
and found no indication of breaker misalignment. Failure analysis by the licensee
determined the cause to be a loose fixed contact within the switch resulting in
intermittent failure of the contacts to always make at the same point. This resulted
in the contacts intermittently closing on the high resistance tiim coating and
preventing the continuity within the closing circuit. The inspector observed portions
of the troubleshooting performed under WR 96-04852-32 and considered it to be
appropriate. The inspector also examined the internals of the failed switch and
contacts, and reviewed Memo JMD 96-425 and determined the failure mode to be
reasonable.
Contacts 5-6 of switch 52SM/LS provide the function for an automatic close
permissive or for a white light indication. Neither of these functions are used at
FitzPatrick. The licensee identified that switch 52SM/LS contacts 5-6 were not
required as a result of a February 1996 failure of the switch in both RHR service
.
.
20
water (SW) pump circuit breakers. These failures were described in NRC Inspection
Reports 50-333/96-01 & 96-03. Additionally, the RHR SW pump circuit breaker
failures were described in Licensee Event Report (LER) 50-333/96-002. The license
determined that these failures were age-related and replaced the 52SM/LS contacts
5-6 in all safety-related circuit breakers having more than 1,500 close cycles, which I
included the RHR D pump breaker. The license also developed Modification D1-96-
052 to jumper out the switch 52SM/LS contacts 5-6 on all safety-related 4160 ;
circuit breakers that require automatic or manual closure to perform the intended
accident mitigation function. This modification was scheduled to be installed during
the upcoming refueling outage scheduled for October 1996. However, as a result
of the problems identified with the RHR D breaker, the licensee completed the
modification on all applicable breakers prior to plant startup. The inspectors i
determine the modification to be technically sound, containing the required reviews '
and approvals. The inspector also reviewed the WR to install the modification on
the RHR D circuit breaker and determined it to be adequate, containing an
appropriate post modification test.
The inspector reviewed the maintenance history of the RHR D circuit breaker with i
the maintenance engineer. After the 52SM/LS switch was repaired in February
'
1996, the breaker had successfully passed all required surveillances until May 8,
1996, when it failed to close during the performance of Procedure ST-2HB, LPCI i
Initiation Logic System 8 Functional Test." WR 96-02944-00 was used to complete l
the troubleshooting of this failure, and cause of the failure was documenteri in j
Memo JMD-96-277, dated June 3,1996. The memo provided several possible j
causes for this failure, all associated with the positive interlock portion of the
,
closing circuitry. The licensee determined that no corrective actions were required I
since the safety-related breakers that have a close function, are regularly operated I
and surveillance tested, which would detect positive interlock related failures. I
Between May 8 and September 12,1996, the breaker had been successfully cycled I
six times without a failure.
The inspector reviewed the surveillance completed on May 8, and the related work
documentation. The inspector noted that, although the licensee had identified the
apparent root cause to be associated with the positive interlock portion of the
closing circuitry, they were unable to confirm the failure location.
c. Conclusions
The inspectors determined that the troubleshooting associated with the September
16 and 18 failures of the RHR D circuit breakers was adequate and the corrective
actions taken to modify the applicable safety-related circuit breakers was
appropriate. However, the inspector considered troubleshooting associated with the
May 8,1996, failure of the RHR D circuit breaker to lack rigor, in that it did not i
adequately review the recent past problems with the 52SM/LS, and it assumed the
location of the problem without positive confirmation.
!
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21
E8.3 Traversina In-Core Probe (TIP) Svstem Ball Valve Control Failure
a. Inspection Scope (73051)
During restoration of power, following the September 16 turbine trip, a power
supply failure in the TIP torque control unit caused the three TIP ball valves to open
with a Group 2 containment isolation signal present. The inspector reviewed the
licensee's actions to comply with TS and corrective actions for failure of the
containment isolation valve.
b. Observations and Findinas
The licensee declared the TIP system inoperable and removed power from the motor
control units. The power to the motor control units was subsequently
administratively controlled utilizing a protective tagout request (PTR) and reactor ,
analyst procedure RAP-7.3.14, Traversing incore Probe System. The procedure j
directs clearing of the PTR prior to commencing TIP runs and the re-establishment
^
of the PTR when the work is completed. In addition, the isolation valves are being
tracked daily by performance of ST-1H, Primary Containment Isolation Valve l
Inoperable Test and in the control room LCO log. l
The TIP system was upgraded in February 1991 (modification F1-88-253) to improve l
system reliability, availability, and accuracy. This Siemens design replaced an older
General Electric design and, as reported by NYPA, is the only Siemens unit ;
operating in this application in the United States. Preliminary review by the licensee
determined that a power supply failure in the torque control unit caused an errant'
signal to be sent from the position encoders to the valve control unit for the three
ball valves. The errant signal indicated that the TIP probes were in the vessel and
the valve logic is such that this signal results in the ball valves opening.
c. Conclusion:
The inspector concluded that adequate controls were in place to ensure compliance
with technical specifications (TS) for an inoperable containment isolation valve. The j
licensee is continuing to investigate the failure of the power supply and opening of
the isolation valves therefore this issue will remain unresolved (URI 50-333/96006-
04).
E8.4 (Closed) (URI) 50-333/95021-02: Environmentally Qualified (EO) Electrical Fuses -
a. Insoection Scope
The inspector reviewed the licensee's action plan, JSED-APL-95-019, Revision 4,
governing the discrepant fuses in EQ applications noted in NRC Inspection Report
50-333/95-21, as well as root cause evaluation report JAF-RPT-ELEC-02316 on this
issue. The inspector also reviewed the licensee's EQ justifications for continued
operation [[::JAF-EQ-JC|JAF-EQ-JC]].O-96-01, Revision 1, and 96-02, Revision 0, as well as AP- ]
5.12, Revision 4, Replacement of Electrical Fuses.
.
.
22
b. Observations and Findinas
After inspection of the fuses in all 138 EQ motor control centers and electrical
panels, a total of 18 fuse discrepancies were identified and were subsequently
resolved by fuse replacement or development of EQ supporting documentation.
Identification of EQ fuse concerns and subsequent change out of the fuses in
question was completed on all equipment within the applicable LCO action time.
The root cause evaluation determined that the majority of the discrepancies were
caused by breakdowns in the fuse selection process as well as weaknesses in the
modification / work process interface. Specifically, operators and maintenance
personnel confused fuses that are environmentally qualified with fuses that were
procured for safety-related, non EQ applications as they were identical in
appearance. Furthermore, adequate documentation verifying the environmental
qualification of certain fuses qualified by similarity was not provided or errors were
made in the Bill of Materials for the fuses in specific components. However, in six
of the 18 cases, the breakdown in the process governing the installation of EQ
fuses could not be determined.
A broad range of corrective actions were implemented to prevent a recurrence of
this problem to address each of the root causes identified. Substantial progress has
been made in the implementation of these corrective actions which included a
revision to AP-5.12, Employee Training, quality assurance (QA) follow-up audits and
creation of a procedure on generating a proper Bill of Materials.
The inspector noted that the licensee has an ongoing fuse control action plan to
address additional non-EQ fuse discrepancies identified recently, most in response
to an operations department effort to validate the accuracy of operator aids in the
plant. This action plan, JSED-APL-95-008, is in the process of being implemented.
c. Conclusions
The licensee performed a thorough and detailed root cause investigation of the EQ
fuse discrepancies identified and developed a comprehensive series of corrective
actions to prevent recurrence. The majority of these corrective actions have been
completed. The success of these corrective actions is, in part, reflected by the
absence of EQ related fuse discrepancies in the last six months in spite of an
extensive ongoing fuse control program verification and improvement program.
However, since documentation of the environmental qualification of the fuses in
question was not in an auditable form as required by 10 CFR 50.49.j, a violation of
NRC requirements occurred. This violation will not be cited in accordance with
Section Vll.B.1 of the NRC Enforcement Manual as the violation was licensee
identified, non-recurring, promptly and thoroughly corrected and of low safety
significance (50-333/9606-05).
E8.5 Review of UFSAR Commitments
A recent discovery of a licensee operating their facility in a manner contrary to the
updated final safety analysis report (UFSAR) description highlighted the need for a
_ _ _ __ _ - _ _ . . . _ . _ _ . ..__ - . __ _ _ _ _ ~
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23
special-focused review that compares plant practices, procedures, and/or
parameters to the UFSAR description. While performing the inspections discussed i
in this report, the inspectors reviewed the applica%s portions of the UFSAR that
related to the areas inspected. The inspectors verified that the UFSAR wording was l
l consistent with the observed plant practices, procedures and/or parameters.
. ,
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, IV. Plant Suonert I
'
R1 Radiological Protection and Chemistry (RP&C) Controls (84750)
>
l
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R1.1 Manaaement Controls
a. Inspection Scoce
The inspectors reviewed the management controls implemented by observation of
management-staff interactions; interviews; and review of program / organization
changes, quality assurance (QA) audits, and review of the semi-annual radioactive
effluent report.
b. Observations and Findinos
The inspectors reviewed changes to the organization and administration of the
radioactive liquid and gaseous effluent control programs and determined that I
responsibility for the programs had moved from the Operations General Manager to i
the Support Services General Manager. The Chemistry staff had primary
responsibility for conducting the radioactive liquid and gaseous effluent control !
programs. The Operations, Engineering, Radwaste, and Instrumentation and
Controls departments supported the radiological effluent control programs relative tc
air cleaning systems, radioactive liquid discharges, and radiation monitoring nystem
calibrations. ,
1
The inspectors reviewed QA Audit Report No.96-01J (completed
February 27,1996). The audit was conducted by Nuclear Quality Assurance (NOA) l
personnel and covered the radioactive liquid and gaseous effluent control programs.
The audit findings were administrative in nature and were not of regulatory
significance. The inspectors noted that the audit team was composed of members
with appropriate technical expertise to assess the radioactive liquid and gaseous
effluent control programs. The inspectors also reviewed QA Surveillance Report
(SR) No.1878 which assessed operations performance for o simulated liquid
effluent release. The inspectors considered this to be a good initiative on the part
of the licensee because there were no opportunities to observe an actual planned
release of liquid effluents during 1995.
The inspectors reviewed the 1995 Semi-annual Radioactive Effluent Release
Reports. These reports provided data indicating total released radioactivity for liquid
and gaseous effluents. These reports also summarized the assessment of the
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24
projected maximum individual and population doses resulting from routine
radioactive airborne and liquid effluents. Projected doses to the public were well
below the Technical Specification (TS) limits. The 1995 Semi-annual Reports ;
properly assessed unplanned releases, as required by TS. The inspectors l
determined that there were no anomalous measurements, omissions or adverse
trends in the reports.
c. Conclusions
The licensee implemented good management control and oversight of the quality of j
the radioactive liquid and gaseous effluent control programs. I
R1.2 Heview of the Offsite Dose Calculation Manual (ODCM)
i
a. Insoection Scone '
l
The inspectors reviewed the ODCM implemented at the FitzPatrick Nuclear Power I
Plant, including: (1) dose factors, (2) setpoint calculation methodology, (3)
bioaccumulation factors for aquatic sample media, (4) LER 96-001 which pertained I
to the ODCM, and (5) the impact of hydrogen water chemistry and the ability to
comply with 40 CFR 190.
b. Observations and Findinas
The ODCM provided descriptions of the sampling and analysis programs, which
were established for quantifying radioactive liquid and gaseous effluent
concentrations, and for calculating projected doses to the public. All necessary
parameters, such as effluent radiation monitor setpoint calculation methodologies,
site-specific dilution factors, and dose factors, were listed in the ODCM. The
licensee adopted other necessary parameters from Regulatory Guide 1.109. The
inspectors noted that the most recent submittal contained improved detail as
compared to previous submittals.
The inspectors reviewed the licensee's actions relative to LER 96-001, Failure to
implement Radiation Monitor instrumentation Setpoint Changes Following Revision
to the ODCM. The inspectors assessed that the LER dispositioned an ODCM-related
discrepancy that was not of regulatory significance. The inspectors had no further
questions regarding LER 96-001 and considered it closed.
The inspectors reviewed severallicensee studies concerning hydrogen water
chemistry and considered these studies to be comprehensive. Based upon the
licensee survey data, the licensee appeared to be in compliance with the
requirements of 40 CFR 190 relative dose to members of the public at the current
hydrogen injection rate of 18.5 scfm. The inspectors noted to the licensee that
there could be a potential for a compliance problem with 40 CFR 190 relative to
Niagara Mohawk Power (NMP) Corporation personnel occupying the adjacent NMP
owner controlled areas at higher hydrogen injection rates if no compensatory
measures were to be taken. The licensee was aware of this potential problem and
1
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25
was analyzing methods of managing this situation in anticipation of the need to
increase the hydrogen injection rates for increased protection against inter-granular
stress corrosion cracking.
c. Conclusions
The inspectors determined that the licensee's ODCM contained sufficient
specification, information, and instruction to acceptably implement and maintain the
radioactive liquid and gaseous effluent control programs. Licensee analyses of the
dose impact to members of the public as the result of hydrogen water chemistry
were good.
R1.3 Implementation of Radioactive Liauid and Gaseous Effluent Control Proarams
a. Inspection Scooe
inspection of this area consisted of: (1) physical walkdown of facilities and
equipment, including the control room; (2) review of selected licensee's procedures;
and (3) review of selected radioactive liquid and gaseous discharge permits with
respect to TS/ODCM requirements.
b. Observations and Findinas
During a plant tour, the inspectors noted that all effluent Radiation Monitoring ,
Systems (RMS) were operable at the time of this inspection. .The inspectors noted !
that the effluent control procedures were detailed, easy to follow, and ODCM '
requirements were incorporated into the appropriate procedures. The inspectors
also determined that the gaseous discharge permits were complete, and met the i
TS/ODCM requirements for sampling and analyses at the frequencies and lower I
limits of detection established in the TS.- I
During a discussion with Chemistry staff, the inspectors noted that the responsible H
individuals had maintained and cananced their knowledge in the areas of: (1) i
I
radioactive liquid and gaseous effluent controls; (2) effluent and process RMS; (3)
the application of procedures designed to protect the public health and safety, and
the environment; and (4) the TS and ODCM requirements.
c. Conclusion
Based on the above observations, reviews and discussions, the inspectors
determined that the licensee established, implemented, and maintained effective
radioactive liquid and gaseous effluent control programs.
- . - . - . . - - _ . - . - . - _ . - - - . - - . - . - - - . . - . . . . - - - . --
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i
- R1.4 Calibration of Effluent / Process Radiation Monitorino Systems (RMS)
! '
- a. Inspection Scone
l t
i
The inspectors reviewed the most recent calibration results for the following
! effluent and process RMS to determine the implementation of the TS requirements
j and Updated Final Safety Analysis Report (UFSAR) commitments:
$
e Liquid Radwaste Discharge Monitor,
l e Service Water Discharge Monitor,
l e Main Steam Line Radiation Monitors,
j e Reactor Building Closed Loop Cooling Radiation Manitor,
- e Main Stack - Normal and High Range Noble Gas Monitors,
- e Refuel Floor Exhaust Radiation Monitor,
j e Reactor Building Exhaust Radiation Monitor,
- * Turbine Building Exhaust - Normal and High Range Monitors,
i e Radwaste Building Exhaust - Normal and High Range Monitors, and 'i
e Offgas Radiation Monitor
b. Observations and Findinas
The l&C Department and Radiological and Environmental Services Department
(Chemistry) had the responsibility of performing electronic and radiological
calibrations, respectively, for the above effluent / process radiation monitors. A
system engineer had the responsibility to maintain the above RMS operable and
upgrade the system, as necessary. All radiological calibration results reviewed were
within the licensee's acceptance criteria.
/ During the review of the above RMS radiological calibration results, the inspectors
independently verified several calibration results, including linearity tests and
conversion factors. The inspectors used a linear regression for the comparisons and
the comparisons were in good agreement. The licensee stated that a statistical
method, such as a linear regression, would be reviewed and applied as necessary.
The inspectors discussed effluent RMS operability / reliability with Chemistry staff.
From this interview, the inspectors determined that the Chemistry staff had good
knowledge of the effluent RMS relative to operability requirements and performance
history. The inspectors also noted that Chemistry trended the operability of the
effluent RMS.
The licensee maintained a system for monitoring the reliability of the effluent RMS.
The licensee tracked the comparison between effluent monitor reading results and
expected monitor readings determined from laboratory sample measurements, to
ensure that the effluent RMS responded acceptably. The inspectors reviewed these
comparison results for liquid and gaseous effluent monitors during this inspection
and determined that the licensee's comparisons were in reasonably good
agreement.
. _ _ . __. . - - _ . , . __ .. . ._.
. .-.- - . . - - _ . - - - .
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27
c. Conclusions
The licensee has implemented effective programs for effluent RMS calibration and
reliability assessment.
R1.5 Air Cleanina Systems
a. Insoection Scope
The inspectors walked down systems, reviewed the licensee's most recent
surveillance test results, and interviewed the system engineer assigned to manage
the station air cleaning systems to determine the implementation of TS requirements
and the UFSAR commitments for: (1) the standby gas treatment system; (2) the
control room ventilation system; (3) technical support center system; and (4) the
radwaste building air cleaning system. j
b. Observation and Findinas
The inspectors reviewed the following surveillance test results:
e Visual inspection, j
e In-Place HEPA Leak Tests, 1
e in-Place Charcoal Leak Tests, 1
e Air Capacity Tests, I
e Pressure Drop Tests, and
e Laboratory Tests for the lodine Collection Efficiencies.
All test results were within the licensee's TS acceptance criteria. One individual
within the Engineering Department was assigned to manage the station ventilation
systems. All TS and UFSAR tests were conducted at the prescribed frequencies.
Unsatisfactory test results were analyzed and corrective actions were implemented
in a timely manner. The inspectors noted that attention given to the air cleaning
systems was excellent. The System Engineer monitored and trended the
performance of the air cleaning systems.
c. Conclusion
The licensee has implemented very good air filtration / ventilation system surveillance
programs for systems described in the TS and UFSAR. Attention placed on station
air cleaning systems by the engineering department was very good.
R5 Staff Training and Qualifications in RP&C
a. Inspection Scope (83522)
The inspector reviewed the training provided to both plant radiological workers and
health physics technicians. The inspector toured training facilities and also audited
one training class for health physics technicians.
1
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28
.
- b. Observations and Findinas
4
Since the last inspection in this area, the licensee constructed a new enhanced
7 radiation worker (ERW) training facility in the training center. As previously
! discussed (NRC Inspection Report 50-333/96-03) this training program was
.
developed to address concerns with the practices of plant radiation workers
,! observed during and immediately after the last refueling outage (RFO11). The new
'
training facility is a very close approximation of the environment typically
encountered in the plant, and stresses contamination control and radiological
condition awareness. All current plant employees have taken or will have taken this
training prior to the commencement of the next refueling outage (RFO12).
The inspector reviewed plant records and observed numerous plant workers l
entering and working in the reactor facility. A general improvement in worker l
practices was observed. j
!
The inspector also attended one training session for health physics technicians and i
supervisors. The session attended was on control of radiological activities on the !
refueling floor during an outage. Since the next refueling outage is scheduled to
commence at the end of October, this session was very timely. The session was i
set-up to encourage classroom participation and use the instructor in the role of I
discussion moderator.
c. Conclusions
Training activities continue to support and aid in improving plant radiological worker
practices. Additionally, specialized training for health physics technicians was both
timely and well presented.
R6 RP&C Organization and Administration
a. Insoection Scone (83522) .
The inspector reviewed management organization in the radiological controls
program, including maintaining occupational radiation exposure as low as is
reasonably achievable (ALARA), control of radiological work and radiological
housekeeping. The inspector made frequent tours of the radiologically controlled
area (RCA), and discussed specific radiological controls with the radiation protection
supervisors and various radiation protection technicians.
b. Observations and Findinas
in accordanca with plant Technical Specifications, responsibility for sate radiological
operations at the facility are the responsibility of the Plant Manager. The
Radiological and Environmental Services (RES) Manager serves as radiation
protection manager at the facility, and reports through the General Manager -
Support Services to the Plant Manager. The RES department is split between
chemistry and health physics groups. The health physics group consisted of a
_ -
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.
.
29
radiological engineering manager, health physics manager and technical staff.
Additionally the health physics manager has several supervisors reporting directly to
him relative to instrumentation and respiratory protection, decontamination and
shipping, ALARA and operational health physics. Recent modifications included
changing the supervisor for dosimetry, and placing the responsibility for RES under
the General Manager - Support Services. Previously the RES Manager reported to
the General Manager - Operations.
Discussions with various managers, supervisors and technicians indicated that all
had an appropriate awareness of previously identified problems within the RES
Department, and that all were aware of actions taken to address these issues.
These issues, previously identified and discussed in NRC Inspection Report No. 50-
333/95-10 included poor radiological worker practices, failure of the health physics
technicians to provide appropriate support to the plant staff, and a failure of the
health physics group to properly utilize or respond to findings and recommendations
made during quality assurance reviews. Interdepartmental communications
appeared to be the common problem still needing to be addressed. All personnel
contacted identified this as a key issue that still needed to be resolved.
Since the last inspection in this area (documented in NRC Inspection Report 50-
333/96-03), the unit has generally been operating at or near full power, while
continuing preparations for refueling outage 12 (RFO12) planned for late October
1996. During this inspection, several tours of various facilities located within the
radiologically controlled area (RCA) were conducted. Extensive efforts by the ,
licensee during the past year have led to notable improvement in the area of
l
radiological housekeeping. Especially notable was the condition of the areas on the '
refueling floor. Also observed during these tours was the significant amount of
scaffolding being erected in the reactor building in preparation for the RFO12 to
support snubber inspections taking place. These inspections are occurring before ,
the start of RFO12 in order to reduce the scope of work which must be performed !
during the outage, and consequently the outage length. Data from previous outages
indicates that 3-5 person-rem per day can be saved by minimizing the outage
length. Allinspections were taking place in locations not affected by power
operations, and therefore not leading to additional occupational exposure. j
l
For RFO 12, the licensee established goals of not more than 45 days and not mae i
than 168.8 person-rem. The ALARA goal was established at the end of 1995, and
is part of the annual site goal of not more than 260 person-rem. At the time of this
inspection, only four ALARA reviews in support of the refueling outage remained to
be completed. Data on total person-hours to be worked on four specific tasks had
not yet been provided by the appropriate working groups in order to complete these
associateci ALARA reviews. The licensee anticipated completing these remaining
reviews b/ mid-September. l
Current estimates by the ALARA staff show an anticipated total outage evposure of
184 person-rem, so that considerable exposure savings will have to be realized if
the licensee is to meet its outage exposure goal.
1
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30
J
. c. Conclusions
!
Plant management appears to have a good understanding of previously identified
problems involving radiation workers and health physics technicians, actions taken
to address these problems. Outage preparations appear appropriate in order for the
facility tc, meet its goals for outage duration and occupational exposure.
,
R7 Quality Assurance in RP&C Activities
i
a. Insoection Scope (83522)
!
'
The inspector reviewed audits, surveillances and RES self-assessments in order to
evaluate the effectiveness of quality assurance activities in the RES department.
, The inspector also discussed planned audits for the remainder of the year with
,
Quality Assurance (QA) personnel.
b. Observations and Findinas
Table R7 provides a listing of audits, surveillances and RES department self-
assessments reviewed bv the inspector. The scope and technical depth of these
reviews, especially in the self-assessments, was significantly improved over those
reviewed during previous inspections. More importantly was the acceptance of
I
findings and recommendations contained in these documents by RES management
and st sff. Findings and recommendations are now being promptly addressed and
the adequacy of responses verified i,y RES managerunt prior to submittal to QA.
i
'
An eadit of the health physics program by the QA department is scheduled to
co',imence in September,1996. The lead auditor is a QA engineer who has
i
r:eviously served as Radiological Engineering and Health Physics Manager within
.
the RES department. Several technical experts from outside the New York Power i
{ Authority have also been hired to assist in the audit. The self-assessment program
also is continuing, but will be temporarily suspended during the refueling outage.
4
- c. Conclusions
!
Audits and surveillances provided by the QA department continue to be of high
quality. The RES department had made significant improvements in the areas of j
{ self-assessment and acceptance of QA findings and recommendations.
l
l R8 Miscellaneous issues I
- R8.1 Evaluation of Unmonitored Release After September 16,1996 Scram
i
a. Insoection Scoce (71750) l
l
The inspector observed the performance of the EP radiological staff during the event
and reviewed radiological records and surveys. Survey results were reviewed to
4
determine the extent of radiological release.
.
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31
b. Observations and Findinas
After the September 16,1996, plant scram, turbine building ventilation was isolated
while there were steam leaks from a blown low pressure turbine and a reactor feed
pump rupture disk. Pressure in the turbine building resulted in steam exiting from
the turbine building, indicating an unmonitored release. During the event, onsite I
surveys were conducted by survey teams which indicated that no release occurred. l
Calculations were performed using conservative assumptions which showed that if I
any release occurred, it was negligible. The EP radiological coordinator directed
appropriate surveys and remained cognizant of radiological activities. Subsequent ;
to the event, environmental monitoring samples were collected and surveyed and l
direct reading radiation monitors were read. The result was that no increase in
radiation levels was observed as a result of the plant transient. Analysis results for
the environmental samples were less than detectable for all plant related
radionuclides. I
c. Conclusions
During the event, EP radiological activities were well coordinated. Based on surveys
and environmental radiation monitoring results, there was no indication of any
increased radiation levels associated with the September 16,1996 event.
P1 Conduct of Emergency Preparedness (EP) Activities
a. Insoection Scope (71750)
The inspectors observed the EP organization performance during the September 16, l
1996, plant event. A review of EP staffing, event classification and notification and
facilities using LAP-1, Emergency Plan Implementation Checklist and IAP-2,
Classification of Emergency Condition, and review of the technical support center l
(TSC) and operational support center (OSC) logs and activities were also performed.
b. Observations and Findinas .
1
At 1:40 p.m. on September 16, approximately 36 minutes after the initial plant
scram, the event was classified as a notification of unusual event (NUE) in
accordance with emergency action level (EAL) 7.2.1, main turbine failure resulting
in casing penetration or damage to turbine seals or generator seals. The event
notifications were completed by 2:16 p.m. and additional followup notifications
were made as necessary. The NRC entered the monitoring phase at the incident
response center. The licensee staffed the TSC and OSC to provide support to
operations and the EP organizations were operational at 2:10 p.m. At 2:36 a.m. on
September 17, the NUE was terminated upon restoration of the main condenser and
verification of cooldown capability.
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c. Conclusions l
The implementation of the emergency plan was a sound decision. The event was l
il appropriately classified, notifications made and the TSC and OSC were properly
staffed and provided assistance to operators in a timely manner. EP procedures,
i
j logs and status boards were in use and significant EP facility discrepancies were not
j evident.
l
j P3 EP Procedures and Documentation
}
j An in-office review of revisions to the emergency plan implementing procedures
. submitted by the licensee was completed. A list of the specific revisions reviewed
.! are included in Attachment 1 to this inspection report. The inspector concluded
l that the revisions did not reduce the effectiveness of the emergency plan and were
i acceptable.
i
1 F8 Miscellaneous Fire Protection issues j
J
! F8,1 Performance of the Fire Suooression System durina the September 16 Plant
$
l a. Inspection Scope
t
l
l During the September 16,1996, plant transient, fire suppression sprinkler systems !
! within the turbine building condenser area actuated, and the fire header above the
I
'
turbine bearings charged, but did not actuate. The inspectors reviewed the
licensee's evaluation of the fire protection system performance during the event,
j and the work requests (WRs) associated with the replacement of the affected
i sprinkler heads. Additionally, discussions were held with the fire protection
} engineer, and the fire protection system engineer regarding the system
j performance, post transient plant inspections and restoration of fire protection
! equipment.
i-
l b. Observations and Findinas
i
j '
During the September 16 plant transient, both the reactor feed water pump (RFP)
!. turbine exhaast header and the main turbine hood disc ruptured, causing local
! temperatures to increase. The increase in temperature resulted in the actuation of
- the fire suppression sprinkler system within the turbine building condenser area, and
l the fire water header above the turbine bearings charged. During the recovery from
j the event, operators appropriately secured the fire suppression system.
!
I Following the event, the system engineer walked down portions of the fire
- protection systems, including the sprinklers, fire detection panels and emergency
i lights, and determined that fire protection equipment responded as designed to the
j event. In areas that were wetted by the fire water released, the licensee performed
- inspections of the electrical panels, cabinets and junction boxes for water intrusion
- with no problems identified.
!
!
l
4
,-m .. . ..- - - , , - - - , - . - - - - - - - -- n.,. ., , r..----- ,,
..
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33
i
Subsequently, the licensee drained the fire header above the turbine bearings and I
returned it to service. Additionally, the fire suppression sprinkler headers that had
actuated, and surrounding sprinkler heads which the licensee determined may have !
degraded due to the increased temperatures experienced during the event, were
replaced under WR 96-04792-00. A total of 41 sprinkler heads were replaced with 1
an equivalent model head as evaluated in Design Equivalent Modification D1-92- '
197. The system was subsequently leak tested under WR 96-04792-02, and
returned to service. The inspector reviewed portions of the completed WRs and the
design equivalent modification, and determined them to be appropriate.
c. Conclusions
The fire suppression system equipment performed as designed during the
Septemtier 16 plant transient. The licensee's inspections of wetted equipment
resulting from the actuation of the sprinkler system, and subsequent sprinkler head
replacernent were reviewed by the inspector and determined to be appropriate.
S1 Conduct of Security and Safeguards Activities
a. Insoection Scope (71750)
The inspector observed security force member support during the September 16 ;
event. j
b. Observations and Findinas
The September 16 transient resulted in the loss of normal plant communications and
vital area doors failed in the locked position. Security personnel were assigned to ;
-
strategic areas in the plant to help with access and communication for operations - !
personnel. '
c. Conclusions ;
i
Security force members responded in a timely manner to assist with plant
communications and vital area access.
V. Manaaement Meetinos
X1 Exit Meeting Summary
The inspectors presented the inspections results to raembers of the licensee
management at the conclusion of the inspection on October 10,1996. The
licensee acknowledged the findings presented and nc.ted that none of the materials
examined during the inspection was considered prop ietary information.
.
.
34
PARTIAL LIST OF PERSONS CONTACT
T
New York Power Authority
M. Colon.b, Plant Manager
R. Locy, Operations Manager
D. Ruddy, Director, Design Engineering
A. Zaremba, Licensing Manager :
1
NRC .
l
C. Cowgill, Chief, Projects Branch 2
R. Keimig, Chief, Emergency Preparedness and Safeguards Branch i
W. Rutand, Chief, Electrical Engineering 3 ranch
J. Shannon, Reactor Engineer, Electrical Engineering Branch
G. Smith, Senior Physical Security inspector
.
l
I
l
l
-. - - -_ - -. - - _. - -.-
.
.
35
INSPECTION PROCEDURES USED
37551 Onsite Engineering
62703 Maintenance Observations
61726 Surveillance Observations
71707 Plant Operations
71750 Plant Support
,
83522 Radiation Protection Organization and Management Controls
84750 Radioactive Waste Treatment, and Effluent and Environmental
Monitoring
ITEMS OPENED, CLOSED, AND DISCUSSED
Ooened
50-333/96006-001 VIO Maintenance planning and work associated with WR 96-
02875-00 to perform calibration of 71-59N-1UPRN05 was
improperly performed resulting in a reverse power scram and
plan transient
50-333/96006-002 URI Condenser response related to September 16,1996 reverse
power scram (i.e. MSIV isolation signal input on low condenser
vacuum)
50-333/96006-003 IFl Seismic qualification process for commercial grade equipment
50-333/96006-004 URI Failure of a TIPS power supply resulting in opening three
containment isolation valves
50-333/96006-005 NCV Documentation of environmental qualification of fuses were
not in an auditable form
Closed
50-333/9521-002 URI EQ fuse discrepancies and resulting corrective actions to
prevent recurrence
50-333/96-001 LER Failure to implement radiation monitoring instrumentation
setpoint changes following revision to the offsite dose
calculation manual (ODCM)
. . . - _ _ _
.
'
,
36
50-333/96-009 LER Incorrect Time Delay Relay Installation for Emergency Diesel 1
Generator
l
l
Discussed
'
None
4
4
1
l
I
1
.
.
.
e
ATTACHMENT 1
EP Implementing Procedures Reviewed ,
!
)
Document Document Title Revision
E-Plan Appendix H 19 ,
EAP-3 Fire 18 I
'
EAP-5.3 Onsite/Offsite Downwind Surveys and
Environmental Monitoring 4
EAP-8 Personnel Accountability 32
EAP-17 Emergency Organization Staffing 71 l
EAP-22 Operation and Use of Radio Paging Device 25 !
EAP-43 Emergency Facilities Long Term Staffing 32 l
SAP-2 Emergency Equipment inventory 20
SAP .3 Emergency Communications Testing 49
SAP-7 Monthly Surveillance Procedure for On-Call
Employees 29
SAP-8 Prompt Notification System Failure / Siren
System False Activation 9
l
1
-. _ -.
.
.
.
ATTACHMENT 2
Procedures Reviewed Related to September 16,1996 Event
Document Document Title Revision
EOP-2 Reactor Pressure Vessel Control 2
EOP-4 Primary Containment Control 2
AOP-31 Loss of Condenser Vacuum 10
AOP-57 Recovery from Residual Bus Transfer 2
OP-4 Circulating Water System 33
.
9
4
d
I
i
)
$
9
l
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A
4
4
,
. . . _ _ _ -- ._ _ -__ ___ _ . _ . . . . _ _
.
~.
>a
ATTACHMENT 3
4
,
September 16,1996 Seauence of Events
1
3
1304 While performing 345 KV relay maintenance, l&C technicians shorted across relay
contacts which simulated a main generator neutral bus ground fault.
Output breakers trip, main turbine and generator trip, reactor scram on turbine
i control valve fast closure.
! Residual bus transfer results in loss of balance of plant loads and uninterruptible
, power supply.
All 4 emergency diesel generators start but do not load (as designed).
,
The "G" safety relief valve opens, reactor pressure peaks at 1082 psig.
l High pressure coolant injection and reactor core isolation cooling start at low reactor
I
vessel level. i
Recirc pumps trip and alternate rod insertion on low reactor vessel level.
Lowest indicated reactor vessel level at 126" (normal reactor vessel operating level l
is 201.5 "). !
Operators entered EOP-2, reactor pressure vessel (RPV) Control, on low RPV water l
level. 1
I
1305 Turbine bypass valves close on loss of electro-hydraulic control (EHC). '
The reactor feed pumps trip on low suction pressure due to loss of condensate
pumps.
1311 (Approx time) B LP turbine rupture disc ruptures. Turbine building pressure reached
3 psig. Also, B RFP rupture disc ruptured at 5 psig.
1313 Loss of A and B RPS during manual transfer, MSIVs close.
1323 The "B" RPS was restored.
1327 The "A" RPS was restored.
1329 Operators attempt to restore UPS.
i
1335 TlP isolation valves open.
1340 The E-plan was entered and an unusual event was declared.
1353 Operators started the B RHR pump for torus cooling, D RHR pump failed to start.
- _ . . . _ _ _ _ _ _ . . _ - - _ ___ . _ _ _ _ _ _ _ . _ . . _ . - _ _ _ _ . _ . .
i
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Attachment 3 2
1415 Blown rupture disk confirmed on B LP turbine.
1417 Operators successfully restored the UPS.
1421 Reset PCIS isolation and verified all rods in via full core display. j
!
1623 Fuel pool cooling restored, i
1658 Cycled D RHR pump breaker, started D RHR pump.
2016 Restored circ water system.
2022 rupture disc on LP turbine installed.
2356 MSIVs opened.
0205 Condenser vacuum reestablished. BPV used for RPV control.
I
0236 Exited unusual event.
'
0544 Started shutdown cooling on B RHR pump. i
0600 Coolant temperature less than 212 degrees. !
0614 Mode switch in refuel.
1
1
. - _ _ -- .. . -. - .. . . - . - _. .-
o
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TABLE R7
Listino of Audits, Surveillances and
Self-Assessments Reviewed
Action Plan to improve Radiological Performance, Rev 1, July 12,1996
Review of the JAF Radiation Protection Program, January - July 1996, August 9,1996
RES Department Six Month Self Assessment, August 26,1996
JRES-SAR-96-008, Sealed Source Leak Rate Testing, May 22,1996
JRES-SAR-96-009, Radiation Worker Practices, July 17,1996
JRES-SAR-96-011, Informational Content of ALARA, Dosimetry and Radiation Protection i
Records, Logs and Reviews, July 30,1996
QA-SR-1865, Yankee Atomic Environmental Laboratory TLD Processing Review, May 13,
1996
QA-SR-1873, Review of the Action Plan to improve Radiological Performance, Action Plan
No. JRES-APL-95-015, June 28,1996
QA-SR-1879, Radwaste Shipment No. 0696-6061, July 12,1996
QA-SR-1892, Receipt inspection of HIC L-490261-55, August 8,1996
QA-SR-1898, inspection of the Capping and Storage of HlC Line L-490261-55 and Receipt
inspection of HIC Liner L-490261-40, August 14,1996
QA-SR-1902, inspection of the Capping of HIC Liner L-490261-40, August 21,1996
__