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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M6631999-10-19019 October 1999 Forwards Insp Rept 50-277/99-07 & 50-278/99-07 on 990920.No Violations Noted ML20217K9241999-10-14014 October 1999 Forwards Amend 234 to License DPR-56 & Se.Amend Consists of Changes to TS in Response to Application & Suppls ,1001 & 06,which Will Support PBAPS Mod P00507,which Will Install Digital Pr Neutron Mining Sys ML20217F7391999-10-14014 October 1999 Requests Addl Info Re Peach Bottom Atomic Power Station Units 2 & 3 Appendix R Exemption Requests ML20217F6841999-10-13013 October 1999 Forwards Senior Reactor Operator Initial Exam Repts 50-277/99-302(OL) & 50-278/99-302(OL) Conducted on 990913- 16.All Applicants Passed All Portions of Exam ML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B4051999-10-0505 October 1999 Forwards Amend 233 to License DPR-56 & Safety Evaluation. Amend Changes Minimum Critical Power Ratio Safety Limit & Approved Methodologies Referenced in Core Operating Limits Report ML20217B3181999-10-0505 October 1999 Advises That Info Submitted in 990712 Application,Which Contained Attachment Entitled, Addl Info Re Cycle Spec SLMCPR for Peach Bottom 3 Cycle 13,dtd 990609, with Affidavit,Will Be Withheld from Public Disclosure ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20212J6851999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Peach Bottom Atomic Power Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl New Insps Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212J5751999-09-28028 September 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990913-16 at Licensee Facility.Without Encls ML20216J0191999-09-27027 September 1999 Forwards Request for Addl Info Re Util 990301 Request to Support Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long-term thermal- Hydraulic Stability Solution Hardware,For Plant ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20216H6751999-09-24024 September 1999 Forwards Amends 229 & 232 to Licenses DPR-44 & DPR-56, Respectively & Ser.Amends Will Delete SR Associated Only with Refueling Platform Fuel Grapple Fully Retracted Position Interlock Input,Currently Required by SR 3.9.1.1 ML20216H6451999-09-24024 September 1999 Forwards Notice of Withdrawal of Util 990806 Application for Amends to Fols DPR-44 & DPR-56.Proposed Change Would Have Involved Temporary Change to Increase Limit for Average Water Temp of Normal Heat Sink ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212E8661999-09-22022 September 1999 Discusses GL 98-01 Y2K Readiness of Computer Sys at NPPs & Supplement 1 & PECO Response for PBAPS Dtd 990630. Understands That at Least One Sys or Component Listed May Have Potential to Cause Transient During Y2K Transition ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212D1191999-09-17017 September 1999 Forwards SE Re Proposed Alternatives to ASME Section XI Requirements for Containment Inservice Insp Program at Plant,Units 2 & 3 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P2961999-09-0707 September 1999 Provides Authorization to Administer NRC Approved Initial Written Exams to Listed Applicants on 990913 at Peach Bottom Npp,Delta,Pennsylvania ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E6941999-08-26026 August 1999 Forwards Request for Addl Info Re Min Critical Power Ratio. Response Should Be Submitted within 30 Days of Ltr Receipt ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211Q4491999-08-25025 August 1999 Responds to Re Changes to PBAPS Physical Security Plan,Safeguards Contingency Plan & Guard Training & Qualification Plan Identified as Revs 13,11 & 9, Respectively.No NRC Approval Is Required,Per 10CFR50.54(p) ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211D5421999-08-23023 August 1999 Forwards Amends 228 & 231 to Licenses DPR-44 & DPR-56, Respectively & Se.Amends Revise TSs to Correct Typographical & Editorial Errors Introduced in TSs by Previous Amends ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20211A9721999-08-20020 August 1999 Forwards Request for Addl Info Re Third 10-year Interval Inservice (ISI) Insp Program Plan for Plant,Units 2 & 3 ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error 05000278/LER-1999-002, Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER1999-07-12012 July 1999 Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20209D9781999-07-0808 July 1999 Forwards Addl Info to Support EA of Proposed 990212 License Application ECR 98-01675,correcting Minor Administrative Errors in TS Figure Showing Site & Exclusion Areas Boundaries & Two TS SRs ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209C1201999-06-30030 June 1999 Informs of Util Intent to Request Renewed License for PBAPS, Units 2 & 3,IAW 10CFR54.Licensee Anticipates That License Renewal Application Will Be Submitted in Second Half of 2001 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20064A7171990-09-18018 September 1990 Comments on SALP Board Repts 50-277/89-99 & 50-278/89-99. Author Pledges Continued Mgt Support of & Attention to Rate of Improvement,Achievement of Goals & Performance of Routine Activities ML20065D4421990-09-14014 September 1990 Responds to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule. Proposed Schedules for Operator Licensing Exams, Requalification Exams & Generic Fundamental Exams Encl ML20059K3671990-09-14014 September 1990 Informs of Revised Commitments Re Crud Induced Localized Corrosion Related to Fuel Cladding Failures.Deep Bed Demineralizers Installation Activities Will Be Performed in Unit 1 Subsequent to Third Refueling Outage ML20064A7751990-09-13013 September 1990 Advises That Ba Stambauth No Longer Maintains Need to Hold Senior Operator License ML20065D3741990-09-11011 September 1990 Forwards Rev to Relief Request 10-VRR-2 Re RHR stay-fill Supply Check Valves,Per ML20064A5831990-09-0707 September 1990 Responds to Violations Noted in Insp Repts 50-352/90-17 & 50-353/90-16 Re Differential Pressure for Pumps.Corrective Actions:Licensee Will No Longer Use Expanded Ranges as Acceptance Criteria for Inservice Testing Program Tests ML20064A4821990-08-31031 August 1990 Forwards Rev 20 to Emergency Plan.Changes Necessitated by Annual Emergency Plan Update & Administrative in Nature ML20059F0541990-08-31031 August 1990 Responds to NRC Re Violations Noted in Safety Insp Repts 50-277/90-13 & 50-278/90-13.Corrective Actions: Training Will Be Provided for Personnel Re Requirements of Drawing E1317 & Administrative Procedures A-2 & A-6 ML20059E6071990-08-29029 August 1990 Forwards Semiannual Effluent Release Rept,Jan-June 1990 & Rev 8 to Odcm ML20028G8181990-08-27027 August 1990 Forwards Peach Bottom Atomic Power Station Semiannual Effluent Release Rept,Jan-June 1990. No Revs Made to ODCM During Rept Period ML20064A6471990-08-24024 August 1990 Forwards Public Version of Revised Epips,Consisting of Rev 10 to EP-101,Rev 2 to EP-112,Rev 13 to EP-208,Rev 11 to EP-230 & Rev 22 to EP-291 ML20059E9861990-08-24024 August 1990 Provides Justification for Applicability of Reload Methodology Topical Repts to Facility & Requests NRC Approval for Application of Reload Analysis Methodologies ML20059B0751990-08-24024 August 1990 Forwards Rev 0 to Updated FSAR for Limerick Generating Station,Units 1 & 2,Vols 1-19.W/one Oversize Encl. Proprietary Vol 7A (App 3B) Withheld (Ref 10CFR2.790) ML20059A6461990-08-15015 August 1990 Responds to Violation Noted in Insp Repts 50-277/90-200, 50-278/90-200,50-277/90-06 & 50-278/90-06 & Payment of Civil Penalty in Amount of $75,000.Corrective Actions:Emergency Svc Water Sys Restored to Operable Status ML20058N9591990-08-13013 August 1990 Forwards Revised Response to Violations Noted in Insp Repts 50-352/90-13 & 50-353/90-13.Corrective Actions:Ltr Issued to All Plant Personnel Providing Instructions on Proper Use & Handling of Controlled Documents in Controlled Locations ML20058N1771990-08-10010 August 1990 Responds to NRC Re Unresolved Items Noted in Insp Repts 50-352/90-80 & 50-353/90-80.Plant-specific Technical Guideline Has Been Revised to Ref Contingency Numbers Rather than Transient Response Implementation Plan Procedures ML20063P9461990-08-10010 August 1990 Provides Plans for Ultimate Disposition of Recirculation Inlet Nozzle to Safe End Weld Indication.Alternative Corrective Actions to Disposition Nozzle to Safe End Weld Indication Include Repair by Weld Overlay W/O Monitoring ML20058N1991990-08-0909 August 1990 Advises of Change of Address for Correspondence Re Util Operations.All Incoming Correspondence Must Be Directed to One of Listed Addresses ML20058P1261990-08-0909 August 1990 Forwards Monthly Operating Repts for Jul 1990 for Limerick Units 1 & 2 & Rev 1 to June 1990 Rept ML20058N1281990-08-0909 August 1990 Forwards Correction to Rev 10 to EPIP EP-234, Obtaining Containment Gas Samples from Containment Leak Detector During Emergencies ML20058M9951990-08-0808 August 1990 Responds to NRC Re Violations Noted in Insp Repts 50-352/90-15 & 50-353/90-14.Corrective Actions:Personnel Counseled on Importance of Procedure Compliance & Operations Manual Revised ML20058Q4051990-08-0606 August 1990 Forwards Public Version of Revised Emergency Response Procedures,Including Rev 12 to ERP-140,App 2,Rev 13 to ERP-140,App 3,Rev 4 to ERP-230,Rev 3 to ERP-305 & Rev 3 to ERP-660 ML20058M6631990-08-0303 August 1990 Responds to NRC 890406 Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81.Based on Encl Schedule,Overall Projected Implementation Date Will Be 901119 ML20056A9611990-08-0303 August 1990 Notifies That Be Saxman Terminated Employment & Operating Responsibilities W/Util on 900706 ML20081E1581990-07-30030 July 1990 Forwards List of 1990 QA Program Changes for Plant.List Identifies Page & Paragraph Number,Brief Description & Type of Change ML20056A0421990-07-27027 July 1990 Forwards Updated Human Resource Status Rept for Jan-Jul 1990 for Areas Identified in Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81 ML18095A3661990-07-26026 July 1990 Forwards Decommissioning Repts for Hope Creek,Peach Bottom & Salem Nuclear Generating Stations ML18095A3761990-07-26026 July 1990 Forwards Decommissioning Repts & Certification of Financial Assurance for Plants ML20055J0241990-07-26026 July 1990 Forwards Response to NRC Regulatory Effectiveness Review Rept for Plant.Response Withheld Per 10CFR73.21 ML20056A9731990-07-25025 July 1990 Forwards Facility Written Exam Comments for NRC Insp Repts 50-352/90-10 & 50-353/90-11.Written Exam for Reactor Operator & Senior Reactor Operator Considered Comprehensive & Thorough ML18095A3721990-07-24024 July 1990 Forwards Rept & Certification of Financial Assurance for Decommissioning for Plants,Per 10CFR50.75 ML20055H8511990-07-24024 July 1990 Responds to NRC 900720 Request for Addl Info Re Util 900516 Request for Exemption from Full Participation During 1990 Onsite/Offsite Emergency Exercise.Nrc Region I & FEMA Support Feb 1991 Exercise,Per 900718 Telcon ML20055H8331990-07-20020 July 1990 Submits Change of Addresses for Correspondence Re Util Nuclear Operations ML20055H0231990-07-12012 July 1990 Forwards Public Version of Revised Epips,Including Rev 10 to EP-210,Rev 19 to EP-231 & Rev 13 to EP-237 ML20044B2621990-07-12012 July 1990 Forwards Annual Progress Rept on Implementation of Control Room Enhancements,Per NUREG-0737.Corrective Actions for All Priority 1 Human Engineering Discrepancies Completed for Unit.Remaining Priority 2 Discrepancies Under Reevaluation ML20055G5481990-07-11011 July 1990 Forwards Public Version of Revised Epips,Including Rev 12 to ERP-140,App 3 & Revs 3 to ERP-310 & ERP-317 ML20044A1041990-06-22022 June 1990 Forwards Application for Amends to Licenses NPF-39 & NPF-85, Consisting of Tech Spec Change Requests 90-03-0 & 90-04-0, Revising Surveillance Requirement 4.9.6.1 for Section 3.9.6 Refueling Platform Re Main Hoists/Auxiliary Hoists ML20043H7041990-06-21021 June 1990 Forwards Endorsements 143-146 to Nelia Policy NF-140 & Endorsements 93-96 to Maelu Policy MF-67 ML20044A2961990-06-21021 June 1990 Submits Revised Response to NRC Bulletin 89-002 Re safety- Related Swing Check Valves to Be Installed on Emergency Diesel Generator.Bolts Will Not Be Replaced Because Valves W/Original Internal Bolts Meet Requirements of Bulletin ML20043J0371990-06-20020 June 1990 Forwards Description,Scope,Objectives for Plant 1990 Annual Emergency Exercise Scheduled for 900920,per 890809 Ltr.Util Will Submit Revised Objectives for Exercise to Reflect Limited Participation,If Exemption Request Approved ML20043H6081990-06-19019 June 1990 Corrects 900427 Response to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing - 10CFR55 & Conforming Amends. ML20055C7621990-06-18018 June 1990 Informs NRC of Plans Re Licensing of Senior Reactor Operators (Sros) Limited to Fuel Handling at Plants.Util in Process of Implementing New Program for Establishment & Maint of Licensed SROs Limited to Fuel Handling at Plants ML20055C7471990-06-15015 June 1990 Requests That Listed Operator Licenses Be Discontinued ML20043G1331990-06-14014 June 1990 Responds to NRC 900614 Ltr Re Violations Noted in Insp Repts 50-352/90-13 & 50-353/90-12.Corrective Actions:Boxes of Completed Procedures Improperly Stored Shipped to Util Storage Vault by 900406 ML20043G8131990-06-13013 June 1990 Responds to NRC 900515 Ltr Re Violations Noted in Insp Repts 50-277/90-06 & 50-278/90-06.Corrective Actions:Surveillance Test 6.16, Motor Driven Fire Pump Operability Test, Will Be Revised ML20043G9981990-06-12012 June 1990 Forwards, Core Operating Limits Rept for Unit 1 Reload 2, Cycle 3 & Core Operating Limits Rept for Unit 2,Cycle 1. Repts Submitted in Support of Tech Spec Change Request 89-13 Re Parameter Limits,Per Generic Ltr 88-16 ML20043H0111990-06-12012 June 1990 Advises That AR Wargo Reassigned from Operating Shift Responsibilities & Will Be Resigning License,Effective on 900514 ML20043G7311990-06-0808 June 1990 Provides Addl Response to Generic Ltr 88-01, NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping. Welds Examined During Last Refueling Outage Addressed ML20043F8021990-06-0808 June 1990 Forwards Monthly Operating Repts for May 1990 for Limerick Units 1 & 2 & Revised Pages to Mar 1990 Rept for Unit 2 & Apr 1990 Rept for Units 1 & 2 ML20055D1141990-06-0808 June 1990 Forwards Public Version of Revs to Emergency Response Procedures,Including Rev 9 to ERP-140 & Rev 3 to ERP-315 1990-09-07
[Table view] |
Text
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'10 CFR-50.54(f)
- GL 89-13
- PHILADELPHI A ELECTRIC COMPANY NUCLEAR GROUP HEADQUARTERS 955-65 CHESTERBROOK BLVD.-
WAYNE, PA 19087 5691 (215) 640-6650 D AVID R. HELWlO
. vics Passioswv ucci. san ornveces January 29, 1990 Docket Nos. 50r277-50-278 50-352 50-353 License Nos. DPR-44 DPR -
NPF-39 NPF-85 U.S. Nuclear Regulatory. Commission Attn: Document Control Desk Washington, DC 20555
SUBJECT:
Peach Bottom Atomic Power Station, Units 2 and 3 Limerick Generating Station, Units l~and 2 Response to NRC Generic Letter 89-13, " Service Water System Problems =Affecting Safety-Related-Equipment" Gentlemen:
NRC' Generic Letter (GL) 89-13, " Service Water System Problems:Affecting Safety-Related Equipment," dated July 18, 1989, required licensees to perform recommended actions presented in the-letter or equally effective-alternative = actions to ensure that their service water systems are in compliance and will be maintained in compliance with 10 CFR 50, Appendix A, General. Design Criteria 44, 45,.and 46,-and Appendix'B,-Section XI.- GL 89-13 required a -
response.to be submitted within-180 days-from receipt of the letter advising the NRC whether the-licensee has established programs to
' implement theLrecommendations of the letter or that it has pursued an equally; effective alternative course of action, including schedules of plans-for implementation of the various actions.
Philadelphia Electric Company received GL 89-13 on August 1, 1989. j h.
Our responses for Peach Bottom Atomic Power Station (PBAPS) //
Units 2 and 3 and Limerick Generating Station (LOS) Units 1 and 2, provided in Attachments 1 and 2, describe our current programs and planned actions in response to recommended actions I - V of GL 89-
-13. -j 9002080367 900129 /
3PDR ADOCK 05000277 P PDC n/1[Jloh j
a documsnt Control D3sk January 29, 1990-
.GL.89-13 Page 2 A summary of each recommended action, I-V, of GL 89-13 is
.provided in Attachment 3 to this letter.
A report' confirming that the actions presented in this response have been implemented will be submitted within.30 days of completion for each station. The reports are expected to be submitted in April, 1992 for PBAPS Units 2 and 3, and September, 1991 for LGS Units 1 and 2.
If you have any questions, or require additional information, please contact us.
Very truly yours, i
/
Attachments cc: W. T. Russell, Administrator, Region I, USMRC J. J. Lyash, USNRC Senior Resident Inspector, PBAPS T. J. Kenny, USNRC Senior Resident Inspector, LGS
COMMONWEALTH OF-PENNSYLVANIA :
3
- ss.
COUNTY OF CHESTER :
D. R. Helwig, being first duly sworn, deposes and says:
That'he is Vice President of Philadelphia Electric Company, that he has read the response to Generic Letter No. 89-13, and knows the contents thereof; and that the statements:and matters-set forth therein-are true and correct to the best of his knowledge, information and belief.
l Vice Pres nt Subscribed and sworn to before me this.1f.aday of 74 W 4fl990. 'l b4%W b4 Notary Public-9 .
NOTARIAL SEAL i
. CATHERINE A. MENDEZ. Notary Public Tredyttdn Twp.. Chester County My Commission Expres Sect. 4.1993 i
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j ATTACHMENT 1 l PEACH BOTTOM ATOMIC POWER STATION, UNITS 2 AND 3 l RESPONSE TO GENERIC LETTER 89-13,
" SERVICE WATER SYSTEM PROBLEMS AFFECTING SAFETY-RELATED EQUIPMENT" !
l The Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3,. service ~ water systems consist of the Service Water (SW),
Emergency Service Water (ESW) and High Pressure Service Water (HPSW) I systems. The ESW and HPSW systems are the service water systems I which function to transfer heat from safety-related equipment to an ,
ultimate heat sink. The SW system supplies cooling water required for normal plant operations and has no safety-related function. The SW system removes heat from heat exchangers in the turbine and reactor buildings including the Fuel Pool Cooling and Cleanup system and transfers the heat to the Conowingo Pond. During normal operation, the SW system supplies cooling water to various heat exchangers and coolers associated with the ESW system. In the event of a loss of offsite power, the ESW system supplies cooling water from the Conowingo Pond to safety-related heat exchangers consisting of room unit coolers for the Residual Beat Removal (RHR), Core Spray
-(CS), Reactor Core Isolation Cooling (RCIC), and High Pressure Coolant Injection (HPCI) systems, CS pump motor oil coolers, RHR pump seal coolers, and the emergency diesel generators. The HPSW system supplies cooling water from the conowingo Pond to safety- 1 related RHR heat exchangers. The ESW and HPSW systems are common to Units 2 and 3. In response to a seismic event, resulting in the loss of-the Conowingo Dam, the ESW and HPSW systems are aligned to 4 the Emergency Cooling Tower'to provide safe-shutdown cooling to both units.
The existing programs and planned actions in response to Recommended Actions I-V of Generic Letter (GL) 89-13 are provided below.
Recommended Action I PBAPS will implement programs consistent with those described in Enclosure 1 to GL 89-13, as described below.
PBAPS has an established Preventive Maintenance (PM)
Program for the Intake Structure. The program includes visual inspection of the inner Intake Structure by a diver each refueling outage and removal of accumulated mud and debris as necessary.
, Diver inspections are also performed for the ESW and HPSW Intake L Pump Structure Sump at the same frequency. The sump is sounded on a quarterly basis to determine accumulated mud levels.
l Planned improvements to the Intake Structure PM program l include trending of the inspection findings and review of the outer Intake Structure surveillance for improvements.
PBAPS has an established program for routine treatment of the service water systems with blocide to control biofouling by 1
-,e ,-a -_ - .,u .a - .-s.. - aa - -. ~n..
t
Attachment' 1 Page 2 1
. Asiatic clams. These systems are currently treated once.a year during the most probable spawning periods. A chlorinatica program l has also been established for the SW system and some ESW components to help mitigate other biofouling. The current chlorination program is controlled by compliance with our National Pollutant Discharge Elimination. System (NPDES) permit. Another program in place that I
- addresses potential silting and macrofouling is continuous treatment l of the'ESW systems with dispersant and corrosion inhibitors.
Planned improvements to our current chemical treatment programs will be based upon:
1
- 1) evaluation of the chemical treatment program for ESW system to develop improvements to increase the chlorination system's reliability, and
- 2) evaluation.of the need to chemically treat the HPSW system.
In addition, completion of the Unit 2 ESW pipe replacement modification to provide bypass lines at each Emergency Core Cooling System (ECCS) room unit cooler will ensure a constant supply of chemically treated water to piping and coolers when there is no operational requirement for cooling water flow. This improvement was completed on Unit 3 during the last refueling outage.
Most of the redundant and infrequently used cooling loops and components are flushed at test pressures-and flows during <
routine testing. The' existing test programs will be evaluated and revised as necessary to ensure that the infrequently used equipment is adequately flushed to prevent fouling and blockage related problems.-
The current lay-up practices for systems using service water as a source will be evaluated and improved as appropriate to help mitigate corrosion and-fouling.
The activities for developing improvements to existing programs to reduce the incidence of fouling problems, as described above, are expected to be completed prior to startup following the next (eighth) refueling outages for Units 2 and 3, which are currently projected to be April, 1991 and December, 1991 respectively.
Recommended Action II PBAPS will conduct a test program to verify the heat transfer capabilities of safety-related heat exchangers cooled by the ESW and HPSW systems. The total test program will consist of an initial test program and a periodic retest program, with periodic test frequencies based upon previous test results to assure the equipment will perform their intended safety functions during the interval between tests.
i
' Attachment 1 I Page 3 1 The test program will be based upon the program described' l
in Enclosure 2 to GL 89-13 and test techniques developed in conjunction with Electric Power Research Institute (EPRI) and other i utilities. The plans for the test program currently include: i J
a) heat transfer testing of heat exchangers which can be practically tested, b) use of equipment temperature monitoring and trending during -
performance of ECCS pump tests and emergency _ diesel generator testing, and c)- alternative preventive maintenance for certain heat exchangers with maintenance frequency based on hydraulic performance.
The test program will differ from the program described ini ;
Enclosure 2 to GL 89-13 in that not every safety-related heat exchanger cooled by ESW and HPSW will be subjected to heat transfer testing. .For certain room unit cooler groups subject to the same sources of fouling, such as the CS unit coolers, an engineering analysis will'be performed to determine the one heat exchanger of. '
each similar group which is most subject to reduction in heat-transfer capability and which can be practically tested. These 3 "most limiting" heat exchangers will be tested, and the: test data will then be applied to the hydraulic _ performance of the other similar heat exchangers in the cooling loops to establish heat -
transfer capabilities. This testing method will establish the heat >
transfer capabilities of each safety-related heat exchanger and also ,
maintain plant personnel dose ALARA and reduce the manpower and economic burden of the test program.
The initial test program for Unit 2 is expected to be
. completed ~by April 1992. This twelve (12) month extension to the period requested in GL 89-13 is proposed in order to allow testing of the ESW system components during-the period of lowest cooling water temperatures after the completion of the ESW pipe replacement
' modification work during the eighth refueling outage. Testing during:this period will provide the most useful results because the larger temperature differences on both the air and water side of the L heat exchangers will reduce the significance of instrument l~~
- inaccuracies. The initial test program for Unit 3 is expected to be
' completed prior to startup following the eighth refueling outage.
-Recommended Action III PBAPS has established PM programs for the Intake Structure,
-ESW and HPSW system components and the majority of safety-related heat exchangers-cooled by ESW and HPSW. Corrective maintenance is ;
performed as required.
The existing PM programs at PBAPS will be reviewed and upgraded to include additional inspection and maintenance of system I
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1 4
Attachment 1 Page 4 .j pipin'g and. components includin 1 heat exchangers,-as necessary,g tothe remainder ensure of the safety-related that corrosion, erosion, j silting, and biofouling do not degrade the required performance of l safety-related systems supplied by the ESW and HPSW systems.
Protective coating failure will not be addressed in the PM programs because the service water system piping is'not protected ]
I with internal coatings.
The program improvements will be established prior to '
startup following the eighth refueling outage for each unit.
Recommended Action IV An independent activity to confirm that the ESW and HPSW systems will perform their intended functions in accordance with the licensing basis for the PBAPS, including a review of single active component failures, will be completed as part of a. Configuration Management design baseline document review of these systems which is scheduled to be completed in late 1990. The task will include:
a) review of original design documents, calculations, specifications, and licensing documents, and ,
b) review of the current Updated Final Safety Analysis Report (UFSAR),. Other licensing documents,_ rodification documentation, and system drawings.
Accessible portions of the ESW and HPSW. systems will be walked down to ensure that the as-built configurations are in accordance with the appropriate licensing basis documentation. However, walkdowns.
are not planned for the portions of the ESW system recently replaced on Unit 2 and Unit 3 because confirmation of the as-built system was performed as part of the modification process.
Recommended Action:V PBAPS will confirm that the maintenance practices, operating and emergency operating procedures, and training which-
- involve the ESW and HPSW systems are adequate to ensure that safety-related equipment cooled by these systems will function as intended and that the opportunity for human error is minimized prior to startup following the eighth refueling outage for PBAPS Unit 2.
r ATTACHMENT 2 LIMERICK GENERATING STATION, UNITS 1 AND 2 RESPONSE TO GENERIC LETTER 89-13, !
" SERVICE WATER SYSTEM PROBLEMS AFFECTING SAFETY-RELATED EQUIPMENT" The Limerick Generating Station (LGS), Units 1 and 2, i service water systems consist of the Service Water (SW), Emergency !
Service systems.Water (ESW) and Residual Deat Removal Service Water (RHRSW) I The ESW and RHRSW systems are the service water systems which function to transfer heat from safety-related equipment to an ultimate heat sink. The SW system supplies cooling water required for normal plant operation and has no safety-related function. The SW system removes heat from heat exchangers in the turbine, reactor, l
and radwaste enclosures and transfers the heat to the cooling towers. During normal operation, the SW system supplies cooling !
water to various heat exchangers and coolers associated with the ESW system. In the event of a loss-of-offsite power or loss-of-coolant accident, the ESW system supplies cooling water from the Spray Pond (Ultimate Beat Sink) to safety-related_ heat exchangers consisting of room unit coolers for the Residual Heat Removal (RHR), Core Spray (CS), Reactor Core Isolation Cooling (RCIC), and High Pressure Coolant Injection (HPCI) systems, motor oil and seal coolers for the RHR pumps, control room chillers, and the emergency diesel generators. The ESW system is common to Units 1 and 2 and consists of two (2) independent loops. The RHRSW system supplies cooling 1 I
water from the Spray Pond to the safety-related RBR heat exchangers. i The system is common to Units 1 and 2 and consists of two (2) independent loops, each servicing one RHR heat exchanger in each unit.
The existing programs and planned actions in response to Recommended Actions I-V of Generic Letter (GL) 89-13 are provided below.
Recommended Action I LGS will implement programs consistent with those described in Enclosure 1 to GL 89-13 with the exception of intake structure inspections, as described below.
LGS has an established inspection program for the Spray Pond and cooling tower basins. The Spray Pond and cooling tower basins are currently inspected once each refueling cycle, and accumulated sludge is removed as necessary. This practice of inspection is considered to be as effective as intake structure inspections because these structures provide large settling areas, and are the locations where service water enters plant systems. A planned improvement to the existing inspection practice will be to trend the inspection findings.
LGS currently does not have Asiatic clams in its plant intake vicinity, however, Asiatic clams are present in the source water bodies. The source water bodies are currently surveyed for
-Page 2 Asiatic clams annually. We plan to increase the frequency of i
surveys in the general plant vicinity to semi-annuallys The I surveying program will be discontinued when Asiatic clams are identified to be in the plant intake vicinity. A clam biocide treatment program similar to the program currently being implemented at the Peach Bottom Atomic Power Station (PBAPS) is being evaluated for use at LGS when it becomes necessary. The implementation of this program will be contingent upon revision of our National '
Pollutant Discharge Elimination System (NPDES) permit.
l i LGS has an established chlorination program to help i' mitigate biofouling in the nonsafety-related SW system. The program treats some ESW system components due to normal system line-ups during the treatment.
Planned improvements to the chlorination program will be based upon:
- 1) evaluation of the current method of chlorination and the locations of chemical injection, and ,
}
- 2) evaluation of changes to systems' operations and line-ups '
during chemical treatment to ensure adequate treatment for l' ESW system components.
In addition, we intend to pursue an increase of the current periods of chemical treatment, while remaining in compliance with our NPDES permit.
Most of the redundant and infrequently used cooling loops and components are flushed at test pressures and flows during routine testing. The existing test programs will be evaluated and revised as necessary to ensure that the infrequently used equipment ;
is flushed on a routine basis to prevent fouling and blockage '
related problems.
The lay-up practices for ESW system components will be evaluated and improved as appropriate to help mitigate corrosion and ,
fouling. The RERSW heat exchangers are currently laid up with demineralized water when taken out of service. Lay-up practices for
'the remainder of the RHRSW system will be evaluated and improved as necessary. .
The activities for developing improvements to exi7 ting programs to reduce the incidence of fouling problems, as d5 scribed above, are expected to be completed prior to startup fnilowing the next (third) refueling outage for' Unit 1 and the next (first) refueling outage for Unit 2, which are currently projected to be December, 1990 and July, 1991, respectively.
Attachment 2 Page 3 t
Recommended Act3on II LGS will conduct a t7st program to verify the heat transfer capabilities of safety-related heat exchangers cooled by the ESW and MRRSW systems. The total test program will consist of an initial test program and a periodic retest program, with periodic test frequencies based upon previous test results to assure the equipment '
will perform their intended safety functions during the interval between tests.
The test program will be based upon the program described in Enclosure 2 to GL 89-13 and test techniques developed in conjunction with the Electric Power Research Institute (EPRI) and other utilities. The plans for the test program currently includes a) heat transfer testing of heat exchangers which can be !
practically tested, >
b) use of equipment temperature monitoring and trending during performance of Emergency Core Cooling System (ECCS) pump -
tests and emergency diesel generator tests, and c) alternative preventive maintenance for certain heat exchangers with maintenance frequency based on hydraulic performance.
- The test program will differ from the program described in Enclosure L to GL 89-13 in that not every safety-related heat i exchanger cooled by the ESW and RERSR systems will be subjected to heat transfer testing. For certain room unit cooler groups subject to the same sources of fouling, such as the CS unit coolers, an engineering analysis will be performed to determine the one heat exchanger of each similar oroup which is most subject to reduction in heat transfer capabilit and which can be practically tested.
l These "most limiting" heat exchangers will be wested, and the test !
data will then be applied to the hydraulic performance of the other i similar heat exchangers in the cooling loops to establish heat transfer capabilities. This testing method will establish the heat .
transfer capabilities of each safety-related heat exchanger and also maintain plant personnel dose ALARA and reduce the manpower and i
economic burden of the test program.
l The initial test program for Unit 1 is expected to be completed within four (4) months following the third refueling outage. This four (4) month extension to the period requested in GL l 89-13 is proposed in order to allow testing of the ESW system components during the next period of lowest cooling water temperatures. Testing during this period will provide the most useful results because the larger temperature differences on both the air and water side of the heat exchangers will reduce the significance of instrument inaccuracies. The initial test program for Unit 2 la expected to be completed within one (1) month following the first refueling outage. This extension is proposed in order to allow for the performance of corrective maintenance and i
Attachment 2 !
Page 4 potential modification activities during the outage prior to establishing the baseline tests. ,
Recommended Action III LGS has established PM programs for the cooling tower [
basin, ESW and RHRSW system components including the ESW side of the i diesel generator heat exchangers and the RHR pump seal and motor oil ;
coolers. Corrective maintenance is performed as required.
1 The existing PM programs at LGS will be reviewed and upgraded to include additional PM tasks, as necessary, for 1
inspection and maintenance of system components and piping to ensure i that corrosion, erosion, silting, and biofouling do not degrade the J required performance of safety-related systems supplied by the ESW and RHRSW systems.
Protective coating failure will not be addressed in the PM programs because the service water system piping is not protected with internal coatings. ,
The program improvements will be establiohed prior to startup following the third refueling outage for Unit 1 and the
, first refueling outage for Unit 2.
Recommended Action IV An independent activity to confirm that the ESW and RHRSW !
systems will perform their intended functions in accordance with the
' licensing basis for LGS, including a review of single active component failures, will be completed as part of a Configuration Management design baseline document review of these systems which is scheduled to be completed in late 1990. The task will includes i a) review of original design documents, calculations, specifications, and licensing documents, and b) review of the Final Safety Analysis Report (PSAR), other licensing documents, modification documentation and system drawings. '
System walkdowns and performance testing were recently ,
completed for the ESW and RRRSW systems during the preoperational test programs conducted in 1984 for Unit 1 and 1988 for Unit 2. The programs included reviews of system design and as-built configuration and testing to verify the systems' capability to perform in accordance with their licensing basis. Additional walkdowns will be performed to resolve discrepancies identified during the design baseline document review.
The LGS modification process, which was implemented prior to the startup of Unit 1, ensures that any design changes made to
[
Attachment 2 -
Page 5 ;
i.
safety-related equipment and systems are subjected to a 10 CPR 50.59 evaluation and a review of the Technical Specifications and the i PSAR. Administrative controls are also established to ensure that maintenance, troubleshooting, testing, and modification activities are performed in a manner which does not degrade plant design. Each activity is governed by a specific plant procedure.
Philadelphia Electric Company (PECo) plans to conduct a :
Safety System Functional Inspection (SSF1) of the LGS ESW system in
Recommended Action V LCS will confirm that the maintenance practices, operating and emergency operating procedures, and training which involve the ;
ESW and RHRSW systems are adequate to ensure that safety-related 1 equipment cooled by these systems will function as intended and that the opportunity for human error is minimize <3 prior to startup following the third refueling outage for LCL Unit 1.
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ATTACHMENT 3 I i
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SUMMARY
OF RECOMMENDED ACTIONS j I-V OF GENERIC LETTER 89-13, !
" SERVICE WATER SYSTEM PROBLEMS AFFECTING j SAFETY-RELATED BQUIPMENT" i I. For open-cycle service water systems, implement and I maintain an ongoing program of surveillance and control :
techniques to significantly reduce the incidence of flow :
blockage problems as a result of biofouling.
II. Conduct a test program to verify the heat transfer j capability of all safety-related heat exchangers cooled by service water. The total test program should consist of an )
initial test program and a periodic retest program. Both I the initial test program and periodic retest program should i include heat exchangers connected to or cooled by one or ;
more open-cycle systems. An example of an alternative '
action that would be acceptable to the NRC la frequent regular maintenance of a heat exchanger in lieu of testing for degraded performance of the heat exchanger. j III. Ensure by establishing a routine inspection and maintenance l program for open-cycle service water system piping and .
components that corrosion, erosion, protective coating !
failure, silting, and biofouling cannot degrade the ;
performance of the safety-related systems suppled by '
service water.
IV. Confirm that the service water system will perform its '
intended function in accordance with the licensing basis 'I for the plant. Reconstitution of the design basis of the system is not intended. This confirmation should include a review of the ability to perform required safety functions in the event of failure of a single active component. To ensure that the as-built system is in accordance with the e appropriate licensing basis documentation, this ;
confirmation should include recent (within the past 2 years) system walkdown inspections.
+
, V. Confirm that maintenance practices, operating and emergency procedures, and training that involves the service water
- l system are adequate to ensure that safety-related equipment t t
cooled by the service water system will function as ,
intended and that operators of this equipment will perform effectively. This confirmation should include recent (within the past 2 years) reviews of practices, procedures, '
and training modules. The intent of this action is to reduce human errors in the operation, repair, and maintenance of the service water system. ,
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.__ - . , _ . ~ < - < . -