ML19350F148

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LER 81-034/03L-0:on 810602,during Testing,Control Rod Driveline J-3 Overtravel Alarm Came Up & Rod Position Indication Was Lost.Probably Caused by Detached Inner filter.J-3 Recoupled
ML19350F148
Person / Time
Site: Dresden Constellation icon.png
Issue date: 06/10/1981
From: Holland P
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19350F147 List:
References
LER-81-034-03L, LER-81-34-3L, NUDOCS 8106240267
Download: ML19350F148 (1)


Text

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R"TTI i During nor nal operations, with DTS 300-2 in progress, J-3 CRD was tested for overtravel.l r.usi l The overtravel alarm came up and rod position indication was lost. This was of minimal l g l safety significance since the rod was i= mediately recoupled. There was no effect on l ll o t s i l public health or safety. Previous events of this type during cycle 7 on Dresden 2; l ge,,,l R.O.: 2-80-9/03L, 2-80-28/03L, 2-80-37/03L, 2-80-62/03L, and 2-80-64/03L, Docket l

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