ML19165A024

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Reactor Vessel Level Monitoring System Special Report
ML19165A024
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 06/12/2019
From: Laura Smith
Exelon Generation Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
Download: ML19165A024 (2)


Text

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~:) Exelon Generation Larry D. Smith Regulatory Assurance Manager Calvert Cliffs Nuclear Power Plant 1650 Calvert Cliffs Parkway Lusby, MD 20657 410 495 5219 Office 410 610 9729 Mobile www.exeloncorp.com larry.smith2@exeloncorp.com TS 3.3.10 and 5.6.7 June 12, 2019 U.S. Nuclear Regulatory Commission ATIN: Document Control Desk Washington, DC 20555 Calvert Cliffs Nuclear Power Plant, Unit No. 2 Renewed Facility Operating License No. DPR-69 NRC Docket No. 50-318

Subject:

Reactor Vessel Level Monitoring System Special Report This special report is submitted in accordance with Calvert Cliffs Nuclear Power Plant Technical Specification 3.3.10. The report is required due to the Unit 2 Reactor Vessel Level Monitoring System having less than the required minimum number of operable channels.

ACTION TAKEN On May 1, 2019 at 00:10 am the CCNPP Unit 2 Reactor Vessel Water Level Monitoring System (RVLMS),

Channel A experienced a total loss of cabinet power. Calvert Cliffs Technical Specification "Post-Accident Monitoring (PAMS) Instrumentatio n," section 3.3.10-1 function 5, requires two channels of RVLMS to be operable. Because of the subject failure, CCNPP entered Technical Specification 3.3.10, Condition A. This failure resulted in Channel A being declared inoperable. When the Completion Time of Condition A expired, CCNPP entered Technical Specification 3.3.10, Condition B.l, which requires submission of this report in accordance with Technical Specification 5.6.7.

PREPLANNED ALTERNATE METHOD OF MONITORING The Reactor Vessel Water Level Monitoring System instrumentatio n is designated for post-accident monitoring use. It provides the plant operator with information to assess void formation in the reactor vessel head region and the trend of liquid level in the reactor vessel plenum. The Reactor Vessel Water Level Monitoring System consists of two redundant channels. Reactor Vessel Water Level Monitoring Channel B remains operable with all eight of its sensors functioning normally. The removal of Channel A from operable status eliminates a means of redundant indication. However, alternate methods of monitoring for core and Reactor Coolant System voiding, using pressurizer level, Reactor Coolant System subcooling, hot and cold leg temperature, and core exit thermocouple instrumentatio n, have been initiated as required by plant procedures.

Document Control Desk June 12, 2019 Page 2 CAUSES OF INOPERABILITV The cause of inoperability is the failure of channel A RVLMS line filter and bulk 300 VDC power distribution modules. The most probable cause of these failures is age related due to run to maintenance system.

PLANS AND SCHEDULES FOR RESTORING THE SYSTEM TO OPERABLE STATUS Calvert Cliffs Nuclear Power Plant performed troubleshooting an.d determined a blown fuse interrupted the source power to the RVLMS cabinet A. The source power was tagged out and additional troubleshootin g with temporary power was performed locally at the cabinet. The HMI computer powered up properly, but each time the power supply chassis was energized it immediately tripped the breaker.

This indicates the line filter and bulk 300 vdc power distribution modules are the cause of the failure. The parts are ordered and expected to be received by June 28, 2019. Repairs will take place once the parts are received.

There are no regulatory commitments contained in this correspondence.

Should you have questions regarding this matter, please contact me at (410) 495-5219.

Respectfully, Larry D. Smith Regulatory Assurance Manager LDS/MJF/lmd cc: NRC Project Manager, Calvert Cliffs D. Tancabel, MD-DNR NRC Regional Administrator, Region I NRC Resident Inspector, Calvert Cliffs