IR 05000220/2018003
ML18318A240 | |
Person / Time | |
---|---|
Site: | Nine Mile Point |
Issue date: | 11/14/2018 |
From: | Erin Carfang Reactor Projects Branch 1 |
To: | Bryan Hanson Exelon Generation Co, Exelon Nuclear |
References | |
1-2018-002 OI IR 2018003 | |
Download: ML18318A240 (30) | |
Text
UNITED STATES November 14, 2018
SUBJECT:
NINE MILE POINT NUCLEAR STATION - INTEGRATED INSPECTION REPORT 05000220/2018003 AND 05000410/2018003 AND NRC OFFICE OF INVESTIGATIONS REPORT 1-2018-002
Dear Mr. Hanson:
On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Nine Mile Point Nuclear Station (NMPNS), Units 1 and 2. On October 24, 2018, the NRC inspectors discussed the results of this inspection with Mr. Peter Orphanos, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented one finding of very low safety significance (Green) in this report.
This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
The NRCs Office of Investigations, Region I Field Office, conducted an investigation (Case No.
1-2018-002) to determine whether operators deliberately failed to follow a procedure required by technical specifications. Based upon the evidence developed during the investigation, the NRC did not substantiate that licensed operators deliberately failed to follow a technical specifications required procedure.
Please note that final NRC investigation documents, such as the OI report described above, may be made available to the public under the Freedom of Information Act (FOIA), subject to redaction of information appropriate under the FOIA. Requests should be made in accordance with 10 CFR 9.23, Requests for Records. Additional information is available on the NRC website at http://www.nrc.gov/reading-rm/foia-privacy.html.
If you contest the violation or significance of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at NMPNS. In addition, if you disagree with a cross-cutting aspect assignment, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at NMPNS. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Erin Carfang, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Numbers: 50-220 and 50-410 License Numbers: DPR-63 and NPF-69
Enclosure:
Inspection Report 05000220/2018003 and 05000410/2018003
Inspection Report
Docket Numbers: 05000220 and 05000410 License Numbers: DPR-63 and NPF-69 Report Numbers: 05000220/2018003 and 05000410/2018003 Enterprise Identifier: I-2018-003-0064 Licensee: Exelon Generation Company, LLC (Exelon)
Facility: Nine Mile Point Nuclear Station, LLC (NMPNS)
Units 1 and 2 Location: Oswego, New York Inspection Dates: July 1, 2018 to September 30, 2018 Inspectors: E. Miller, Senior Resident Inspector J. Dolecki, Resident Inspector B. Sienel, Resident Inspector J. Ambrosini, Senior Emergency Preparedness Inspector J. Furia, Senior Health Physicist J. Patel, Reactor Inspector R. Rolph, Health Physicist A. Rosebrook, Senior Project Engineer Approved By: E. Carfang, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at
NMPNS Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.
List of Findings and Violations Failure to Ensure that Thermal Power is Less Than or Equal to the Licensed Power Limit Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green NCV H.1 - Human 71111.22 Systems05000410/2018003-01 Performance,
Closed Resources The inspectors identified a Green finding and associated non-cited violation (NCV) of the NMPNS Unit 2 Operating License (NPF-69), Condition 2.C(1), Maximum Power Level, when Exelon did not ensure that thermal power was less than or equal to the licensed power limit of 3988 megawatts-thermal (MWth). Specifically, on multiple occurrences between May 22, 2018 and October 19, 2018, licensed operators in the main control room did not appropriately monitor and control 2-hour average thermal power at or below the licensed power limit. The inspectors determined the 2-hour average thermal power exceeded the licensed power limit outside of normal steady-state fluctuations, and did not take timely, effective corrective action to reduce thermal power below the licensed power limit when the 2-hour average was found to exceed the licensed power limit.
Additional Tracking Items Type Issue number Title Inspection Status Results Section LER 05000220/2017-002-01 Manual Reactor Scram Due to 71153 Closed Presesure Oscillations
PLANT STATUS
Unit 1 began the inspection period at rated thermal power. On September 8, 2018, operators reduced reactor power to 70 percent to perform surveillance testing and a control rod pattern adjustment. Operators restored Unit 1 to rated thermal power the same day. Unit 1 remained at or near rated thermal power for the remainder of the inspection period.
Unit 2 began the inspection period at rated thermal power. On August 27, 2018 the Unit 2 reactor automatically scrammed following a grid disturbance. On August 28, 2018, following evaluation of the event, operators commenced a reactor startup. Unit 2 reached rated thermal power on August 30, 2018. On August 31, 2018, operators reduced Unit 2 power to 80 percent to perform surveillance testing and to conduct a control rod pattern adjustment. Unit 2 was returned to rated thermal power on September 1, 2018, and remained at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection Summer Readiness
The inspectors evaluated summer readiness of alternating current offsite and alternate power systems.
External Flooding (1 Sample)
The inspectors evaluated readiness to cope with external flooding.
71111.04 - Equipment Alignment Partial Walkdown
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 Division II standby gas treatment system on July 23, 2018
- (2) Unit 1 emergency diesel generator 103 following surveillance testing on September 10, 2018
- (3) Unit 2 Division II emergency diesel generator during 115 kV Line 5 planned outage on September 10, 2018
71111.05AQ - Fire Protection Annual/Quarterly Quarterly Inspection
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Unit 1 261 emergency diesel generator 102 room, fire area 22 on September 14, 2018
- (2) Unit 1 261 emergency diesel generator 103 room, fire area 19 on September 14, 2018
- (3) Unit 1 turbine building 261 emergency diesel generator power board 102, fire area 5 on September 14, 2018
- (4) Unit 1 turbine building 261 emergency diesel generator power board 103, fire area 5 on September 14, 2018
- (5) Unit 1 reactor building 281 east, fire area 1, on September 28, 2018
- (6) Unit 1 reactor building 298 east, fire area 1, on September 28, 2018
71111.06 - Flood Protection Measures Internal Flooding
The inspectors evaluated internal flooding mitigation protections in the following areas:
- (1) Unit 1 102 and 103 emergency diesel generators on September 14, 2018
- (2) Unit 1 102 and 103 emergency power boards on September 14, 2018
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification
- (1) The inspectors observed a Unit 1 simulator evaluation that involved a drywell pressure transmitter failure, a control rod drive pump failure, an un-isolable steam leak in emergency condenser piping, and a loss of reactor pressure vessel level indication on July 24, 2018
- (2) The inspectors observed a Unit 2 simulator evaluation that involved an offsite chlorine spill, a recirculation pump failure, multiple control rods drifting into the core, a loss of one offsite power line and emergency diesel generator failures, and fuel damage on
July 31, 2018 Operator Performance (2 Samples)
- (1) The inspectors observed Unit 1 operations personnel during reactor downpower manipulations to 90 percent and control rod scram time testing on September 8, 2018
- (2) The inspectors observed Unit 2 operations personnel during a startup following a reactor scram and turbine trip on August 27, 2018
71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 1 reactor protection system uninterruptible power supplies
- (2) Unit 2 standby gas treatment system
71111.13 - Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 2 emergent high pressure core spray unit cooler maintenance on July 6, 2018
- (2) Unit 1 unplanned actuation of automatic transfer switch to alternate power supply for main transformer cooling on August 2, 2018
- (3) Unit 1 planned core spray 121 system valve maintenance on August 21, 2018
- (4) Unit 2 unplanned main generator unit Phase 1 differential relay maintenance on August 28, 2018
- (5) Unit 2 elevated risk due to Division II emergency diesel generator failure to start on August 30, 2018
- (6) Unit 2 power rate ascension rate limitation during startup on August 30, 2018
- (7) Unit 2 reserve station transformer 2RTX-XSR1A during planned maintenance on September 4, 2018
- (8) Unit 2 planned 115 kv Line 5 outage on September 10, 2018
71111.15 - Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Unit 2 drywell floor drain leak rate instrumentation on July 20, 2018
- (2) Unit 1 emergency diesel generator 102 emergency shutdown on July 23, 2018
- (3) Unit 2 D service water pump failed start logic surveillance on August 14, 2018
- (4) Unit 1 missed surveillance of core spray 111 inboard discharge isolation valve on September 28, 2018
71111.18 - Plant Modifications
The inspectors evaluated the following temporary or permanent modifications:
- (1) Unit 1 auxiliary control room panel doors IS19 and IS21 in the open position on August 21, 2018
- (2) Unit 1 temporary modification for scaffold installation near emergency diesel generator 102 to support maintenance on September 11, 2018
71111.19 - Post Maintenance Testing
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
- (1) Unit 1 containment spray loop 122 electrical preventive maintenance on July 12, 2018
- (2) Unit 2 drywell floor drain system maintenance to unclog suction strainers on July 23, 2018
- (3) Unit 2 Division II emergency diesel generator replacement of air relays and lube oil pressure switch on August 31, 2018
- (4) Unit 2 rod worth minimizer power supply replacement on August 28, 2018
71111.20 - Refueling and Other Outage Activities
The inspectors evaluated the Unit 2 forced outage (N2FO18-01) activities to address an electrical grid disturbance and corrective maintenance to main generator trip system relays from August 27, 2018, to August 30, 2018.
71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: Routine
- (1) Unit 1 N1-ST-22, Diesel Fire Pump Instrument Air Test and Flow Verification, on July 2, 2018
- (2) Unit 2 N2-OSP-LOG-S001, Shift Checks, on July 26, 2018
- (3) Unit 1 N1-ISP-036-006, Emergency Cooling System - High Steam Flow Instrument Trip Channel Test/Calibration, on August 9, 2018
- (4) Unit 2 N2-OSP-RSP-Q001, RPS Turbine Stop Valve Closure Logic, Control Valve Fast Closure Scram Functional Tests and Turbine Valve Cycling, on August 31, 2018
- (5) Unit 2 N2-OSP-EGS-R002, Operating Cycle Diesel Generator 24-Hour Run Division I and II, on September 19, 2018
Inservice (2 Samples)
- (1) Unit 2 N2-OSP-SLS-Q001, Standby Liquid Control Pump, Check Valve, Relief Valve Operability Test and ASME XI Pressure Test, on July 30, 2018
- (2) Unit 2 N2-OSP-RHS-Q@006, Quarterly Operability Flow Rate Test on Loop C of Division II LP ECCS, on August 2, 2018
71114.02 - Alert and Notification System Testing
The inspectors evaluated the maintenance and testing of the alert and notification system from July 2016 to July 2018.
71114.03 - Emergency Response Organization Staffing and Augmentation System
The inspectors conducted a review of Exelons emergency response organization augmentation staffing requirements and the process for notifying and augmenting the emergency response organization.
71114.05 - Maintenance of Emergency Preparedness
The inspectors reviewed a number of activities to evaluate the efficacy of Exelons efforts to maintain the NMPNS emergency preparedness programs.
71114.06 - Drill Evaluation Emergency Planning Drill
The inspectors evaluated the conduct of a Unit 2 emergency planning drill on July 31,
RADIATION SAFETY
71124.05 - Radiation Monitoring Instrumentation Walkdowns and Observations
The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.
Calibration and Testing Program (1 Sample)
The inspectors evaluated Exelons calibration and testing program.
71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation Radioactive Material Storage
The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Exelon had established a process for monitoring the impact of long-term storage of the waste.
Radioactive Waste System Walk-down (1 Sample)
The inspectors walked down the following:
- (1) Accessible portions of liquid and solid radioactive waste processing systems to verify current system alignment and material condition
- (2) Abandoned in place radioactive waste processing equipment to review the controls in place to ensure protection of personnel
- (3) Changes made to the radioactive waste processing systems since the last inspection
- (4) Processes for mixing and transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers
- (5) Current methods and procedures for dewatering waste
Waste Characterization and Classification (1 Sample)
The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.
Shipment Preparations (1 Sample)
The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and Exelon verification of shipment readiness.
Shipment Records (1 Sample)
The inspectors reviewed selected non-excepted package shipment records.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified Exelons performance indicator submittals listed below for the period from July 1, 2017, through March 31, 2018: (3 Samples)
- (1) EP01, Drill and Exercise Performance
- (2) EP02, Emergency Response Organization Drill Participation
- (3) EP03, Alert and Notification Reliability The inspectors verified Exelons performance indicator submittals listed below for Units 1 and 2 for the period from July 1, 2017, through June 30, 2018: (12 Samples)
- (4) MS05, Unit 1 Safety System Functional Failures
- (5) MS05, Unit 2 Safety System Functional Failures
- (6) MS06, Unit 1 Emergency Alternating Current Power System
- (7) MS06, Unit 2 Emergency Alternating Current Power System
- (8) MS07, Unit 1 High Pressure Injection System
- (9) MS07, Unit 2 High Pressure Injection System
- (10) MS08, Unit 1 Heat Removal System
- (11) MS08, Unit 2 Heat Removal System
- (12) MS09, Unit 1 Residual Heat Removal System
- (13) MS09, Unit 2 Residual Heat Removal System
- (14) MS10, Unit 1 Cooling Water System
- (15) MS10, Unit 2 Cooling Water System
71152 - Problem Identification and Resolution (PI&R) Annual Follow-up of Selected Issues
The inspectors reviewed Exelons corrective actions associated with the following issues:
- (1) Unit 1 - Issue Report 03987066, March 20, 2017 reactor scram following reactor pressure oscillations
- (2) Unit 2 - Issue Report 04128779, Division II emergency diesel generator loss of offsite power/loss of coolant accident testing failure to maintain voltage within the limit specified in Technical Specifications
71153 - Follow-up of Events and Notices of Enforcement Discretion Events
The inspectors evaluated response to the following event:
- (1) Unit 2 reactor scram due to turbine trip on August 27, 2018
Licensee Event Reports (1 Sample)
The inspectors evaluated the following licensee event reports:
- (1) Licensee Event Report 05000220/2017-002-01, Manual Reactor Scram Due to Presesure Oscillations (ADAMS Accession No. ML18242A071). The circumstances surrounding this licensee event report are documented in report section Inspection Results.
INSPECTION RESULTS
Failure to Ensure that Thermal Power is Less Than or Equal to the Licensed Power Limit Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green NCV H.1 - Human 71111.22 Systems05000410/2018003-01 Performance, Closed Resources The inspectors identified a Green finding and associated NCV of the NMPNS Unit 2 Operating License (NPF-69), Condition 2.C(1), Maximum Power Level, when Exelon did not ensure that thermal power was less than or equal to the LPL of 3988 MWth. Specifically, on multiple occurrences between May 22, 2018 and October 19, 2018, licensed operators in the main control room did not appropriately monitor and control 2-hour average thermal power at or below the licensed power limit. The inspectors determined the 2-hour average thermal power exceeded the licensed power limit outside of normal steady-state fluctuations and did not take timely, effective corrective action to reduce thermal power below the licensed power limit when the 2-hour average was found to exceed the licensed power limit.
Description:
During a Unit 2 main control room walkdown on July 26, 2018, the inspectors identified the 2-hour average thermal power to be above the 3988 MWth operating license limit. Following additional review, the inspectors identified the 3988 MWth operating license limit was exceeded periodically between May 22, 2018 and October 19, 2018. Among the instances, some of the longest durations include the following 19 instances where the 2-hour average thermal power was continuously above 3988 MWth:
May 22, 2018, for 56 minutes (1:42 AM to 2:38 AM)
May 22, 2018, for 70 minutes (6:50 AM to 8:00 AM)
May 22, 2018, for 96 minutes (10:07 AM to 11:43 AM)
May 27, 2018, for 72 minutes (9:02 PM to 10:14 PM)
June 24, 2018, for 72 minutes (7:52 AM to 9:04 AM)
June 30, 2018 for 78 minutes (1:41 AM to 2:58 AM)
July 8, 2018, for 103 minutes (11:41 AM to 1:24 PM)
July 9, 2018, for 75 minutes (4:03 AM to 5:18 AM)
July 10, 2018, for 55 minutes (4:27 AM to 5:22 AM)
July 10, 2018, for 61 minutes (9:37 AM to 10:38 AM)
July 13, 2018, for 56 minutes (7:51 PM to 8:47 PM)
July 15, 2018, for 61 minutes (2:05 PM to 3:06 PM)
July 26, 2018, for 74 minutes (6:04 AM to 7:18 AM)
July 26, 2018, for 61 minutes (5:29 PM to 6:30 PM)
September 19, 2018, for 60 minutes (6:01 PM to 7:01 PM)
September 20, 2018, for 86 minutes (2:00 AM to 3:29 PM)
September 22, 2018, for 73 minutes (5:16 AM to 6:29 AM)
October 9, 2018, for 38 minutes (4:23 AM to 4:51 AM)
October 19, 2018, for 48 minutes (3:03 PM to 3:51 PM)
Additionally, on May 21, 2018, at 3:01 PM, June 29, 2018, at 10:56 PM, July 9, 2018, at 12:19 AM, July 10, 2018, at 6:51 AM, and twice on September 19, 2018, at 4:05 AM and 9:48 AM, the 2-hour average thermal power was below the licensed power limit during steady-state operation then operators started to further open a recirculation flow control valve, which resulted in the 2-hour average thermal power subsequently exceeding the licensed power limit. This is noteworthy because Exelons procedures state steady-state is only applicable when no operator action is taken.
N2-OP-101D, Power Changes, Revision 02800, Section F, states that if any of the following points are reached immediate operator action is required to ensure thermal power is trending below 3988 MWth:
1-second instant = 4028 MWth 1-minute average = 4008 MWth 10-minute average = 3998 MWth On June 24 from 7:44 AM to 7:55 AM the 10-minute average thermal power was above 3998 MWth, peaking at 3999 MWth. Contrary to N2-OP-101D, operators did not take timely effective action to reduce reactor power once the 10-minute average exceeded 3998 MWth.
Further, the following procedural steps are provided in N2-OP-101D for monitoring and controlling 2-hour average core thermal power during normal operations:
(F.2.1) CLOSELY MONITOR 2-hour average core thermal power during Steady State operation with goal of maintaining rolling two-hour thermal power average between 3984 MWth AND 3988 MWth.
(F.2.2) IF 2-hour average core thermal power is found to exceed 3988 MWth THEN TAKE ACTION to ensure thermal power is reduced to less than or equal to 3988 MWth AND CLOSELY MONITOR 2-hour average, to ensure it remains less than 3988 MWth for the shift.
Contrary to the requirements for monitoring the 2-hour average in accordance with N2-OP-101D, on June 30, 2018, from 1:41 AM to 2:58 AM, July 8, 2018, from 11:41 AM to 1:00 PM, July 10, 2018, from 4:27 AM to 5:22 AM, July 26, 2018, from 6:04 AM to 7:18 AM, September 19, 2018, from 6:01 PM to 7:01 PM, and October 19, 2018, from 3:03 PM to 3:51 PM, the operators did not perform any action to maintain thermal power less than the licensed power limit while the 2-hour average was above the licensed power limit.
The inspectors compared the N2-OP-101D procedure to the Nuclear Energy Institute (NEI)
Position Statement, associated NRC Safety Evaluation, and NRC RIS 2007-21, Revision 1.
The inspectors determined Exelon revised N2-OP-101D in April 2010 following the issuance of NRC RIS 2007-21, Revision 1. Specifically, Revision 00800 included the below listed precaution and limitation while Revision 00900 did not include direction to perform immediate operator action if the 2-hour average thermal power exceeded the licensed power limit or include commensurate steps to what exists in the current revision of the procedure:
If the 10 minute smoothed thermal power indication exceeds 3467 MWth [(previous licensed power limit prior to April 2012)], take immediate action to reduce power to less than licensed limit, monitor 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> average thermal power indication taking actions to maintain less than licensed limit, initiate a Condition Report noting highest power achieved (instantaneous and 10 minute smoothed) and make notification as required by administrative procedures.
The inspectors concluded the supplemental documentation discussed above was not adequately translated into N2-OP-101D in order to ensure adherence to the licensed power limit. Specifically, as stated below, NEI Position Statement Guidance to Licensees on Complying with the Licensed Power Limit, as endored by the NRC Safety Evaluation Step 4.2(2) discusses timely operator action in Section 4.2(2):
Closely monitor thermal power during steady state power operation with the goal of maintaining the two-hour thermal power average at or below the LPL. If the core thermal power average for a 2-hour period is found to exceed the LPL, take timely action to ensure that thermal power is less than or equal to LPL.
N2-OP-101D does not include a timeliness component to perform action to reduce thermal power whenever the 2-hour thermal average is discovered to be above the licensed power limit. There is no timeliness direction provided in N2-OP-101D for the operators to take action (e.g., prompt or immediate operator action) until 3998 MWth on the 10-minute average is reached (i.e., 10 MWth above the LPL). As a result, the inspectors determined N2-OP-101D allows operators to operate the reactor above the licensed thermal power limit for unspecified periods of time.
Further, the NRC Safety Evaluation states, RIS 2007-21 states that slight changes in thermal power may occur due to expected variances in plant parameters. Specifically, NEI demonstrated to the NRC at a public meeting held June 12, 2008, that for short durations (1-minute average for thermal power) some peaks which lasted for less than one second exceed the thermal power limit but the average was below the licensed power limit. One of the specific examples provided in the supplemental documentation is bi-stable flow.
Following the refueling outage in May 2018, a change in the severity of power oscillations due to bi-stable flow was observed as noted by Issue Report (IR) 04141573. These bi-stable flow oscillations result in a power change greater than the 4 MWth range goal provided for the operators in N2-OP-101D. Based on this information, the inspectors concluded the changes in power due to these more severe bi-stable flows are not considered to be consistent with the definition of small fluctuations described in the supplemental documentation.
Unit 2s Renewed Facility Operating License (NPF-69), Condition 2.C(1), Maximum Power Level, states, Exelon Generation is authorized to operate the Unit 2 facility at reactor core power levels not in excess of 3988 MWth (100 percent rated power). Given the increased severity of bi-stable flow and duration of the instances where thermal power is above the licensed power limit, the inspectors concluded the power excursions above the licensed power limit were not small, short-term fluctuations and not due to normal fluctuations of plant parameters while operating under steady-state conditions at or near the licensed power limit.
The inspectors determined the operators did not adequately maintain power below the licensed power limit when the 2-hour average exceeded the licensed power limit.
Corrective Actions: As an immediate corrective action, on July 30, 2018 Exelon generated IR 04160054 and subsequently IR 04187330 on October 24, 2018, to capture the inspectors concerns regarding maintaining core thermal power at or below the licensed power limit.
Exelon performed a benchmark with the rest of the Exelon fleet regarding power management. Exelon updated N2-OP-101D to direct operators to manage power using the 1-hour average for thermal power. Exelon also adjusted the thermal power operating band established in N2-OP-101D to establish additional margin to the licensed power limit.
Corrective Action Reference: IR 04160054 and IR 04187330 Performance Assessment Performance Deficiency: The inspectors determined that licensed operators did not ensure that thermal power was less than or equal to the licensed power limit when the 2-hour average exceeded the licensed power limit was contrary to the NMPNS Unit 2 Operating License (NPF-69), Condition 2.C(1), Maximum Power Level, and was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because if left uncorrected the performance deficiency had the potential to lead to a more significant safety concern. Specifically, operation above the licensed power limit reduced the analyzed margins to fuel cladding failure and could result in unanalyzed consequences during an initiating event. The inspectors reviewed the examples of minor issues in IMC 0612, Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues, dated August 11, 2009, and noted there were two examples that were applicable to screening this issue of concern. Consistent with Example 8b, the operators non-compliance with the Unit 2 license condition to operate the reactor at or below rated thermal power could have the potential to lead to a more significant safety concern. Also, consistent with Example 8c, the inspectors determined operator actions to raise and maintain thermal power above rated thermal power, and the failure to promptly restore Unit 2 to rated thermal power once exceeded could have the potential to lead to a more significant safety concern.
Significance: The inspectors assessed the significance of the finding using IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012. The inspectors performed a Phase 1 SDP review of this finding using the guidance provided in IMC 0609, Appendix A, Exhibit 2, Mitigating System Screening Questions, and determined this finding would require evaluation using IMC 0609, Appendix M, because the finding was the result of a mismanagement of reactivity by licensed reactor operators (e.g., reactor power exceeding the licensed power limit, inability to anticipate and control changes in reactivity during operations). The finding screened as very low safety significance (Green) based on a qualitative evaluation of the conditions and consequences of the performance issue not resulting in a violation of the core thermal limits.
This assessment is consistent with those documented for similar issues in Prairie Island Nuclear Generating Plant Integrated Inspection Report 05000282/2009002, 05000306/2009002 and Fermi Power Plant Integrated Inspection Report 05000341/2015001.
The maximum power reached at Unit 2 was 100.28 percent (3999 MWth/3988 MWth). The inadequate monitoring and control of reactor power did not result in exceeding the two percent reactor thermal power allowance contained in the safety analysis. Therefore, the safety analysis remained bounded for all instances described herein when the licensed power limit was exceeded.
Cross-Cutting Aspect: The inspectors determined that the finding had a cross-cutting aspect of Resources within the cross-cutting area of Human Performance because Exelon did not provide adequate guidance in N2-OP-101D to take timely action to restore and maintain reactor power at or below the licensed power limit. [H.1]
Enforcement Violation: Nine Mile Point Nuclear Station Unit 2 Operating License (NPF-69), Condition 2.C(1), Maximum Power Level, specifies, in part, Exelon Generation is authorized to operate the facility at reactor core power levels not in excess of 3988 megawatts thermal (100 percent rated power).
Contrary to the above, between May 22, 2018, and October 19, 2018, Exelon operated Unit 2 at reactor core power levels in exceedance of the LPL, 3988 MWth. Specifically, the inspectors identified numerous instances when the 3988 MWth operating license limit was exceeded between May 22, 2018 and October 19, 2018, on multiple occasions for extended periods of time.
Disposition: Exelon entered this issue into the corrective action program as IR 04160054 and IR 04187330, and this violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.
Observations 71152 Annual Followup of Selected Isssues March 20, 2017 reactor scram following reactor pressure oscillations The inspectors conducted a problem identification and resolution inspection sample to review the cause evaluation for IR 03987066, regarding a reactor scram that occurred on March 20, 2017 due to a mechanical pressure regulator malfunction. The inspectors reviewed the evaluation for adequacy and if corrective actions were timely.
Inspectors reviewed the timeline established in operator logs during the time of the event and reported in LER 05000220/2017-002-00, Manual Reactor Scram due to Pressure Oscillations on May 18, 2017. Following the event Exelon wrote IR 03987066 and conducted a Corrective Action Program Evaluation (CAPE), which is a Level 2 cause evaluation in accordance with PI-AA-120, Issue Identification and Screening Process, Revision 008.
On March 19, 2017, at 7:25 PM, the electronic pressure regulator was removed from service, due to a known degraded condition at lower power, placing Unit 1 on the mechanical pressure regulator, the second of two pressure control systems. The Unit 1 main generator was offline and main turbine trip testing was being conducted as part of the scheduled reactor shutdown, which was in-progress at the time of the scram. Following the second main turbine trip on March 20, 2017, at 2:06 AM, with reactor power at approximately 14 percent, the main turbine bypass valves began cycling due to an issue with the mechanical pressure regulator, resulting in 2-3 psig reactor pressure oscillations. Throughout the power oscillations, licensed operators continued to insert control rods as part of the shutdown. At approximately 4 percent reactor power, Unit 1 operators recognized the mechanical pressure regulator oscillations resulted in reactor pressure changes, turbine bypass valve movement, and corresponding power oscillations visible on the average power range monitors and the intermediate range monitors instruments. On March 20, 2017, at 2:27 AM, operators at Unit 1 inserted a manual reactor scram due to pressure oscillations exceeding procedural limits, established in N1-SOP-31.2, Pressure Regulator Malfunction, Revision 00300.
N1-SOP-31.2, has an override to scram the reactor if > 2 psi pressure oscillations are experienced after transfer to the standby pressure regulator. Or, > +/- 3 % average power range monitor oscillations are experienced after transfer to the standby pressure regulator.
Additionally following the flow chart in N1-SOP-31.2, if both the EPR and MPR are not controlling pressure and, Pressure is not under control, the operators are also directed to scram the reactor. The logs stated that at 2:10 AM operators entered N1-SOP-31.2 due to indications of pressure oscillations of 2-3 psi. The inspectors questioned why the action to scram the reactor was not taken until 2:27 AM, given the post transient review written operator statements and CAPE stated the observed conditions, which met the scram override in the first step of N1-SOP-31.2.
Following the scram, Exelon conducted a post transient review and did not identify any issues with crew performance. Based on the inspectors concerns that operators did not take timely actions as required by procedures based upon the operator logs, post transient review written operator statements, CAPE and confirmed by LER 05000/2017-002-00 which contained the same statements, the NRC launched an Office of Investigations investigation (1-2018-002) to determine if operators willfully did not follow N1-SOP-31.2 instructions to scram the reactor.
Based upon the evidence developed during the investigation, the NRC did not substantiate that licensed operators deliberately failed to follow a Technical Specifications required procedure. Operator logs and the LER 05000220/2017-002-00 were determined to be incorrectly documented, which was captured in IR 04187343.
The inspectors identified the following performance deficiencies during their review:
Operator logs and basic event timeline were inaccurate and out of order Operators did not identify entry criteria were met for N1-SOP-31.2 for 14 minutes while indications were available in the main control room, and some of those indications were noted by operators based on post transient review written operator statements Operators did not enter N1-SOP-1.5, Unplanned Rx Power Change, Revision 00500, when unplanned power change of more than 2% was occurring Operators did not conduct an adequate 4.0 Critique, in accordance with OP-AA-101-113-1006, 4.0 Crew Critique Guidelines, Revision 009 These performance deficiencies were reviewed using NRC IMC 0612, Appendix B and determined to be minor since operators did eventually enter the appropriate procedure and did manually scram Unit 1 when the conditions were recognized based on testimony under oath.
Inspectors noted that N1-SOP-31.2 lacked clarity regarding which path to take when a pressure regulator is already out of service and there is no backup available. The inspectors also noted that there was no additional visual indication to aid operators in recognizing the reactor pressure oscillations in a timely manner due to the narrow range pressure indication being out of service due to the reactor being at a reduced power during the shutdown. Also, the turbine trip and HPCI actuation at 2:16 AM was a distraction which contributed to operators not entering N1-SOP 31.2 in a timely manner. The HPCI initiation was documented in operator logs, however this was not captured in LER 05000220/2017-002-00.
Exelon entered the resident inspectors observations (IR 04070755) into the corrective action program and evaluated the usage of N1-SOP-31.2. Based upon this review, the procedure was revised to expand the range of pressure oscillation to 4 psig before taking action to scram the reactor. Exelon also entered the resident inspectors observations concerning an inadequate 4.0 critique of operator actions during the post trip review (IR 04073439) and conducted an evaluation. Exelon recognized during the OI investigation that the timeline was not adequate, and generated IR 04091110 on January 7, 2018. Exelon updated the event timeline and issued LER 05000220/2017-002-01 on August 18, 2018 to reflect the revised timeline after the NRC OI completed on-site interviews.
Inspectors determined the causal evaluation lacked the expected level of self-criticality needed to identify performance issues related to the March 2017 scram. In conclusion, while inspectors identified numerous performance deficiencies with both operator performance and the subsequent causal evaluation, the underlying issues are considered minor, after a new timeline was established for the scram.
Observations 71152 Annual Followup of Selected Isssues Division II Emergency Diesel Generator Loss of Offsite Power/Loss of Coolant Accident testing failure to maintain voltage within the limit specified in Technical Specifications The inspectors reviewed the work group evaluation, the corrective actions taken, the failure analysis, and the past operability regarding the deficiencies discovered on the Division II emergency diesel generatorautomatic voltage regulator. The inspectors concluded that the evaluation was adequate, the extent of condition was reasonable, and the corrective actions were timely.
Minor Violation 71153 Follow-up of Events and Notices of Enforcement Discretion This violation of minor significance was identified by inspectors and has been entered into the licensees corrective action program, consistent with the NRC Enforcement Policy.
Mnior Violation: During the review of Licensee Event Report (LER) 05000220/2017-002-01, Manual Reactor Scram Due to Presesure Oscillations, the inspectors identified a minor violation of 10 CFR 50.9, Completeness and accuracy of information. The LER was found to be inaccurate. Specifically, the LER timeline contained inaccurancies regarding the time operators entered a special operating procedure and did not include an actuation of high-pressure coolant injection (HPCI). The timeline stated at 2:10 AM operators entered the special operating procedure for Pressure Regulator Malfunction, due to reactor pressure oscillations of 2-3 psig. At 2:27 AM operators inserted a manual scram of the reactor due to pressure oscillations exceeding procedural limits.
This information was confirmed by a review of the operational logs for March 20, 2017.
During OI Investigation 1-2018-002, it was determined that this entry was not accurate and although an exact time could not be established is was estimated to have been at 2:20 AM vice 2:10 AM. Additionally the timeline did not include a mention that at 2:16 AM unexpected turbine trip signal was received and HPCI was initiated due to a tagging error. Operators reset HPCI at 2:18 AM and restored main feedwater flow to restore Reactor Vessel water level. A sixty day telephone notification instead of a written licensee event report was conducted for this invalid initiation of HPCI was completed on May, 11, 2017, as EN 52747 as allowed by 10 CFR 50.73(a)(2)(iv).
Screening: Violations involving the submittal of inaccrurate or incomplete information are evaluated under Traditional Enforecement because they impact the NRCs regulatory process. Accordingly, the inspectors evlauted this issue against the example violations in Section 6.9 of the NRC Enforcement Policy. Inspectors concluded that the violation is of minor safety significance because the inaccurate information did not change the NRCs review of the licensee event report.
Enforcement:
10 CFR 50.9 requires that information provided to the Commission by a licensee shall be complete and accurate in all material respects. Contrary to the above, on June 22, 2015, Entergy provided information to the Commission that was not complete and accurate in all material respects. In the licensee event report, Exelon documented incorrect information that resulted in the NRC launching a substation further inquiry (OI investigation),but did not substantiate that licensed operators deliberately failed to follow a Technical Specifications required procedure.
Exelon identified the inaccuracy and entered the issue into the corrective action program (IR 04091110) on January 7, 2018, and submitted LER 05000220/2017-002-01 on August 18, 2018, revising the timeline to show operators entering N1-SOP-31.2 at 2:20 AM vice 2:10 AM.
The disposition of this violation closed Licensee Event Report 05000220/2017-002-01.
EXIT MEETINGS AND DEBRIEFS
The inspectors confirmed that proprietary information was controlled to protect from public disclosure.
On October 24, 2018, the inspectors presented the quarterly resident inspection results to Mr. Peter Orphanos, Site Vice President, and other members of the Exelon staff.
DOCUMENTS REVIEWED
Procedures
N2-MSP-GEN-V001, Revetment Ditch Structure Inspection, Revision 00501
N2-OP-70-LINEUPS, Station Electrical Feed and 115 kV Switchyard - Lineups, Revision 00000
N2-OP-70, Station Electrical Feed and 115 kV Switchyard, Revision 02400
Issue Report
04056415
Work Orders
C92770203
C93625607
Drawing
EE-MO001A, Piping & Instrumentation Diagram (P&ID) Plant Master One Line Diagram Normal
Power Distribution, Revision 23
Miscellaneous
Unit 2 USAR, Section 2.5, Revision 22
Procedures
N1-OP-45, Emergency Diesel Generators, Revision 04600
N2-OP-61B, Standby Gas Treatment System, Revision 01600
N2-OP-100A, Standby Diesel Generators, Revision 02500
N2-OP-100A-LINEUPS, Standby Diesel Generators - LINEUPS, Revision 00500
Issue Report
04171115
Drawings
PID-61B, P&ID Primary Containment Purge and Standby Gas Treatment, Revision 23
PID-104A, Standby Diesel Gen System, Revision 28
Procedures
N1-FPM-FPE-A001, Annual Inspection of Portable Fire Extinguishers, Revision 01900
N1-FPM-FPE-M005, Fire Protection Equipment Monthly Inspection, Revision 00700
N1-FST-FPL-A001, Low Pressure Carbon Dioxide System Functional Test, Revision 01500
N1-FST-FPP-D002, Daily Fire Door Inspection, Revision 00500
N1-PFP-0101, Unit 1 Pre-Fire Plans, Revision 00500
Miscellaneous
DCD-805, Nine Mile Point Unit 1 NFPA 805 Design Criteria, Revision 1
FPEE0-03-002, Evaluation of Interim Action Taken to Prevent Personnel Injury From CO2,
Revision 1
FPEE 1-91-003, Excessive Door Gap at Floor for Fire Doors, Revision 1
Miscellaneous
Unit 1 Probabilistic Risk Assessment, Revision 1
Procedures
N1-SOP-5.1, Loss of Control Rod Drive, Revision 00500
N1-ST-R1, Control Rod Scram Insertion Time Test, Revision 02500
N2-OP-101A, Plant Start-Up, Revision 04700
Procedures
N1-ARP-A8, 3-4, Transformer No. 1 Off Normal, Revision 01100
N1-OP-33C, Main Transformer XF-TB01, Revision 00600
N2-OP-72, Standby and Emergency AC Distribution System, Revision 01900
N2-OP-100A, Standby Diesel Generators, Revision 02500
N2-OSP-EGS-M@001, Diesel Generator and Diesel Air Start Valve Operability Test - Division I
and II, Revision 01600
OP-AA-108-117, Protected Equipment Program, Revision 005
OP-NM-108-117, Protected Equipment Program at Nine Mile Point, Revision 00500
Issue Reports
04153112 04159345 04161364 04161702
04162590 04162686 04167980 04168453
04168767
Drawings
Drawing No. 0001040209048, Control Diagram Shutdown System, Revision 9
EE-001A, Main One Line Diagram Generator and Main Transformer, Revision 26
ESK-08SPU001, Sheet 1,
Revision 16
PID-104A, Standby Diesel Gen System, Revision 28
Work Orders
C90937645 C92862878 C93455910 C93470881
C93471031
Procedure
N1-OP-40, Reactor Protection and ATWS Systems, Revision 02700
Issue Reports
2698136 02699078 02739808 03963439
03965701 03976658 03982372 04006367
04022391 04028534 04061183 04062507
Miscellaneous
Maintenance Rule System Basis Document for Nine Mile Point 1 120V AC Distribution on
March 23, 2018
Maintenance Rule Basis Document, Nine Mile Point Unit 2, Standby Gas Treatment System
Procedures
N1-ARP-A4, Control Room Panel A4, Revision 01400
N1-ST-M4A, Emergency Diesel Generator 102 and PB 102 Operability Test, Revision 02300
N1-ST-Q1A, CS Pump, Valve and SDC Water Seal Check Valve Operability Test,
Revision 01600
N1-ST-Q1A, CS Pump, Valve and SDC Water Seal Check Valve Operability Test,
Revision 01800
N1-ST-Q1B, CS 121 Pump, Valve and SDC Water Seal Check Valve Operability Test, Revision
2000
N2-OP-11, Service Water System, Revision 01301
OP-NM-102-1001, Operations On-Line Work Management, Revision 00000
WC-AA-101, On-Line Work Control Process, Revision 28
WC-AA-111, Surveillance Program Requirements, Revision 6
Issue Reports
04132680 04156899 04158124 04158821
04161880 04162540 04177972
Drawings
C-19410-C, Sheet 1, Elementary Wiring Diagram 4.16kV Emergency Power Boards and Diesel
Generators (#102 and #103 Control Circuits), Revision 32
C-19410-C, Sheet 2, Elementary Wiring Diagram 4.16kV Emergency Power Boards and Diesel
Generators (#102 and #103 Control Circuits), Revision 21
C-19410-C, Sheet 3, Elementary Wiring Diagram 4.16kV Emergency Power Boards and Diesel
Generators (#102 and #103 Control Circuits), Revision 9
LSK-23-6C, Logic Diagram Reactor Building Floor Drains, Revision 13
TL2DFR-001, Test Loop Diagram Drywell Floor Drn Tank TK1 Level 2DFR-LT106/-FT137,
Revision 2
Work Orders
C93432297 C93441998 C93548675 C93665070
C93432297 C93441998 C93548675 C93625381
C93548634 C93625384
Miscellaneous
SDBD-804, Emergency Diesel Systems, Revision 04
PCR-18-04221
PCR-18-04222
Procedures
CNG-MN-1.01-1005, Scaffold Control, Revision 00400
MA-AA-796-024, Scaffold Installation, Inspection, and Removal, Revision 011
NES-MS-04.1, Seismic Prequalified Scaffolds, Revision 7
Issue Reports (*initiated in reponse to inspection)
2084606
2466423
04166573*
Work Order
C92998294
Miscellaneous
1-SCAFFOLD-TB-261-296, EDG 103 Room for VESDA Fire Detection Modification Upgrade,
July 16, 2018
1-SCAFFOLD-TB-261-297, EDG 102 Room for VESDA Fire Detection Modification Upgrade,
July 16, 2018
ECP-14-000378, RPIS Panel Door Modification Needed to Allow For the Closure of the Doors
on PNL-1S19 and PNL-1S21, Revision 1
Procedures
N1-ST-Q6D, Containment Spray System Loop 122 Quarterly Operability Test, Revision 01300
N1-ST-Q6D, Containment Spray System Loop 122 Quarterly Operability Test, Revision 01400
N1-ST-Q6D, Containment Spray System Loop 122 Quarterly Operability Test, Revision 01500
N2-OP-67, Drywell Equipment and Floor Drains System, Revision 00201
N2-OP-95A, Rod Worth Minimizer System, Revision 00604
N2-OP-100A, Standby Diesel Generators, Revision 02500
N2-OP-101A, Plant Start-Up, Revision 04700
N2-OSP-EGS-M@001, Diesel Generator and Diesel Air Start Valve Operability Test -
Division I and II, Revision 01600
N2-PM-@031, Control Rod Venting and Stroking, Revision 01400
Issue Reports
04131863 04141764 04168453 04168767
Work Orders
C93613030 C93615251 C93678891 C93679300
Drawing
0007.221-001-025, Elementary Diagram Reactor Manual Control System, Revision 7
Procedures
N2-OP-101A, Plant Start-Up, Revision 04700
N2-OP-30, Control Rod Drive, Revision 02400
N2-OP-3, Condensate and Feedwater, Revision 05100
Issue Reports
04167387
04167969
Miscellaneous
Reactivity Maneuver Plan NM2C17-SU-1, Startup Sequence, Revision 1, approved
July 13, 2018
Special Reactivity Maneuver Plan NMC17-6-1, Revision 0, approved August 29, 2018
Unit 2 USAR, Section 5.2, Revision 22
Procedures
HU-AA-104-101, Procedure Use and Adherence, Revision 5
N1-ISP-036-006, Emergency Cooling System - High Steam Flow Instrument Trip Channel
Test/Calibration, Revision 01100
N1-OP-21A, Fire Protection System - Water, Revision 02400
N1-PM-M9, Monthly Operation of Fire Pumps, Revision 02
N1-ST-22, Diesel Fire Pump Instrument Air Test and Flow Verification, Revision 00500
N2-OP-101D, Power Changes, Revision 02800
N2-OSP-EGS-R002, Operating Cycle Diesel Generator 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Run Division 1 and 2,
Revision 01000
N2-OSP-LOG-S001, Shift Checks - Mode 1, Revision 03500
N2-OSP-RHS-Q@006, RHR System Loop C Pump and Valve Operability Test and System
Integrity Test, Revision 00500
N2-OSP-RSP-Q001, RPS Turbine Stop Valve Closure Logic, Control Valve Fast Closure Scram
Functional Tests and Turbine Valve Cycling, Revision 01100
N2-OSP-EGS-M@001, Diesel Generator and Diesel Air Start Valve Operability Test - Division II
and II, Revision 01600
OP-AA-1, Conduct of Operations, Effective Date August 21, 2014
Issue Reports
2649114 03974806 04141573 04153004
04155406 04160054 04168442 04173901
04174986
Work Order
C93629226
Drawings
C-18017-C, Sheet 1, Emergency Cooling System P&ID, Revision 56
C-18030-C, Sheet 3, Fire Protection Water System P&ID, Revision 37
C-19841-C, Sheet 2, Elementary Wiring Diagram 125 VDC Battery Boards 11 and 12 Control
Circuits, Revision 12
Miscellaneous
DCD-805, NMPNS Unit 1 NFPA 805 Design Criteria, Revision 1
Information Notice No. 86-110: Anomalous Behavior of Recirculation Loop Flow in Jet Pump
BWR Plants, dated December 31, 1986
NEI Position Statement Guidance to Licensees on Complying with the Licensed Power Limit,
dated June 12, 2008
NRC Regulatory Issue Summary 2007-21, Adherence to Licensed Power Limits, Revision 1,
dated February 9, 2009
NRC Safety Evaluation Regarding Endorsement of NEI Guidance for Adhering to the Licensed
Thermal Power Limit, dated October 8, 2008
PCR-18-03986
PCR-18-04021
PCR-18-04573
PCR-18-04819
Issue Reports
03993592
04115422
04126142
Miscellaneous
Nine Mile Point Nuclear Generating Stations and James A. FitzPatrick Nuclear Power Plant
Public Alert and Notification Design Report, Revision 2 (February 2017)
Procedure
TQ-AA-113, ERO Training and Qualification, Revision 32
Issue Reports
2735527 04040124 04043130 04069096
Procedures
NOSA-NMP-17-03, 2017 Emergency Preparedness Audit Report
NOSA-NMP-18-03, 2018 Emergency Preparedness Audit Report
Issue Reports
03974715
04099960
04111306
Work Orders
C93596864
C93603725
C93614859
Miscellaneous
KLD TR-823 Nine Mile Point Nuclear Station Units 1 and 2 Evacuation Time Estimates
(February 8, 2016)
KLD TR-846, Nine Mile Point and James
- A. FitzPatrick, 2016 Population Update Analysis
(September 10, 2016)
KLD TR-928, Nine Mile Point and James
- A. FitzPatrick, 2017 Population Update Analysis
(September 9, 2017)
Procedure
N-NM-EP-ID-U2JUL2018, Revised July 25, 2018
Issue Report
04163950
Procedures
N1-ISP-077-005, Off Gas Sample/System Flow Instrumentation Cannel Calibration,
Revision 00301
N1-ISP-112-005, Stack Flow Instrumentation Calibration, Revision 0700
N1-ISP-112-008, OGE SMS Flow Instrumentation Calibration, Revision 00500
N1-RSP-9C, Instrument Channel Calibration of Emergency Consdenser Vent Radiation Monitor,
Revision 00601
N1-RSP-10C, The Use and Routine Calibration of the General Atomic High Range Gamma
Radiation Monitoring System, Revision 00501
N1-RSP-13, Stack Radiation Monitor Calibration Check and Channel Test, Revision 00300
N2-IPM-GEN-@001, Safety Related Loop Calibration, Revision 00800 and Revision 00900
N2-ISP-CWS-A101, Calibration Test of the Circulating Water Cooling Tower Blowdown Lines
Flow Instrument Channel, Revision 00500
N2-ISP-LWS-R101, Liquid Radwaste Discharge Flow to Lake Insturment Channel Calibration,
Revision 00501
N2-ISP-SWP-R112, Service Water Effluent Lines A and B Flow Instrument Channel
Calibration, Revision 01000
N2-RSP-RMS-R001, Main Stack Wide Range Gas Monitor System Calibration, Revision 01100
N2-RSP-RMS-R100, Operating Cycle Channel Calibration of the Flow System on the DRMS
Gaseous/Particulate Process Radiation Monitors, Revision 00700
N2-RSP-RMS-R103, Channel Calibration Test of the Standby Gas Treatment System Exhaust
Process Radiation Monitor, Revision 06
N2-RSP-RMS-R104, Channel Calibration Test of the Off Gas Process Radiation Monitors,
Revision 01100
N2-RSP-RMS-R106, Channel Calibration Test of the Drywell High Range Area Radiation
Monitor, Revision 00701
N2-RSP-RMS-R106, Channel Calibration Test of the Drywell High Range Area Radiation
Monitors, Revision 00900
N2-RSP-RMS-R112, Channel Calibration Test of the Cooling Tower Blowdown Line Liquid
Process Radiation Monitor, Revision 00700
N2-RSP-RMS-R113, Channel Calibration Test of the Service Water Effluent Line Process
Radiation Monitors 2SWP*CAB146A and 2SWP*CAB146B, Revision 00800
N2-RSP-RMS-R116, Channel Calibration Test of the Liquid Radwaste Effluent Line Liquid
Process Radiation Monitor, Revision 00700
Issue Reports
2422411 02422931 04035349 04035349
Work Orders Title Date
C93594663 Stack Flow Instrumentation Calibration June 6, 2018
C93315144 May 22, 2017
C93515685 OGE SMS Flow Instrumentation Calibration August 8, 2017
C93137950 August 7,2016
C92936275 Off Gas Sample/System Flow Instrumentation June 8, 2017
Calibration December 11, 2014
C93050182 Calibration of the High Range Gamma Monitor March 29, 2017
C91990615 Calibration of the High Range Gamma Monitor April 1, 2014
C93625652 Stack Radiation Monitor Calibration July 17, 2018
C93563705 January 22, 2018
C93330540 Calibration of Emergency Condenser Vent Monitor September 25,2017
C92188924 June 23, 2015
C90926779 Liquid Radwaste Discharge Flow to Lake Instrument July 13,2011
C90776169 Calibration (Note: Monitor not in use.) August 26, 2010
C93326176 Service Water Effluent Lines A and B Flow Instrument January 13, 2017
C92763149 Calibration January 19, 2016
C93462398 January 25, 2018
C92795227 March 17, 2016
C93587633 Circulating Water Cooling Tower Flow Instrument December 11, 2017
C92894774 Calibration December 18, 2014
C93589633 Safety Related Loop Calibration May 31, 2017
C92894774 September 23, 2015
C93457436 DRMS Gaseous/Particulate Flow System Calibration April 25, 2018
C92741553 April 19, 2016
C93457438 April 27, 2018
C92741642 April 20, 2016
C93363246 June 7, 2018
C92326679 December 17, 2015
C93457473 Drywell High Range Area monitor Calibration May 3, 2018
C93502206 Service Water Effluent Monitor (A) Calibration August 17, 2017
C93491426 Service Water Effluent Monitor (B) Calibration January 5, 2018
Work Orders Title Date
C93614340 Cooling Tower Blowdown Line Monitor Calibration July 12, 2018
Miscellaneous
Portable Radiation Protection Instrument Calibrations
Instrument Model Instrument ID Calibration Date
AMP-100 5013-074 April 10, 2018
AMS-4 1742 March 7, 2018
BC-4 135 August 22, 2017
BC-4 945 March 13, 2018
Frisktech A734x July 30, 2017
Gillian 202004 April 2, 2018
Micro Rem Meter B503B March 23, 2018
PM-7 630 January 26, 2017
PNR-4 4464 September 19, 2017
September 19, 2018
RO-2 1558 April 2, 2017
SAC-4 689 March 5, 2018
Telepole 6610-036 November 27, 2017
Whole Body Counter Calibration Records
Number Title Date
Calib-17- Calibration of the Canberra Accuscan II WBC System September 13, 2017
000586 at the Exelon Nine Mile Point Nuclear Power Plant
Calib-17- Calibration of the Canberra FASTSCAN WBC System September 12, 2017
000585 at the Exelon Nine Mile Point Nuclear Power Plant
NNA* 2016 Recalibration of the Accuscan II Counting System September 9, 2016
at Nine Mile Point Nuclear Stations
NNA 2016 Recalibration of the Extended FASTSCAN September 9, 2016
Counting System at Nine Mile Point Nuclear Station
- No Number Assigned
Miscellaneous
Shipments 15-2022; 17-2043; 17-2042; 17-2033; 16-2020
71151
Procedures
EP-AA-125-1001, EP Performance Indicator Guidance, Revision 10
ER-AA-600-1047, Mitigating Systems Performance Index Basis Document, Revision 11
LS-AA-2200, Mitigating System Performance Index Data Acquisition and Reporting, Revision 6
N1-MSPI-001, Nine Mile Point Unit 1 MSPI Basis Document, Revision 11
N1-ST-M4A, Emergency Diesel Generator 102 and PB 102 Operability Test, Revision 02000
N2-MSPI-001, Nine Mile Point Unit 2 MSPI Basis Document, Revision 15
N2-OP-35, Reactor Core Isolation Cooling, Revision 01500
Work Order
C93215271
Miscellaneous
NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7
71152
Procedures
N2-OSP-EGS-R004, Operating Cycle Diesel Generator Simulated Loss of Offsite Power With
and Without ECCS Division 1/2, Revision 01800
PI-AA-120, Issue Identification and Screening Process, Revision 8
PI-AA-125, Corrective Action Program (CAP) Procedure, Revision 6
Issue Report
04128779
Drawings
0001.040-209-010, Control Schematic, Revision 6
0001.040-209-065A, System Schematic Division I & II Diesel Generator Voltage Regulator,
Revision 1
213000710, Schematic - Remote S.
- V.S. Regulator 3 Phase with Paralleling, Revision E
C7206600710, Synchronous Motor Pull-Out Relay, Revision C
Work Orders
C93663763
C93664220
Miscellaneous
1011108, Portrec (NEI Peebles) Voltage Regulators for Emergency Diesel Generators, dated
December 2004
5059-2018-136, Remove Division 1 and 2 Synchronous Motor Pull-Out Relay, dated
April 22, 2018
ECP-18-000259, Design Equivalent Change Package for Removal of Division I and II Diesel
Synchronous Motor Pullout Relay, Revision 0
Exelon Power Labs Report, Failure Analysis of a Pullout Relay, dated May 11, 2018
PORC Presentation Form, Surveillance Test Interval (STI) Evaluation NM-15-001, dated
March 14, 2016
71153
Procedures
N2-ARP-851200, 2CEC-PNL851 Series 200 Alarm Response Procedures, Revision 00900
N2-EOP-RPV, RPV Control - Flowchart, Revision 01500
N2-SOP-08, Unplanned Power Changes, Revision 01300
N2-SOP-21, Turbine Trip, Revision 00900
N2-SOP-101C, Reactor Scram, Revision 01300
Miscellaneous