LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint InstructionsML18039A314 |
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Browns Ferry |
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Issue date: |
04/09/1998 |
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From: |
Morrison G TENNESSEE VALLEY AUTHORITY |
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To: |
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Shared Package |
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ML18039A313 |
List: |
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References |
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LER-98-002, LER-98-2, NUDOCS 9804150349 |
Download: ML18039A314 (10) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150.0104 (4.96) EXPIRES 04I30/SS ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUFSTI 60.0 HRS. REPORTED LESSONS LICENSEE EVENT REPORT (LER) LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS AND FED BACK To INDUSTRY. FORWARD COMMENTS REGARDING BVRDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T.e F331, U.S.
(See reverse for. required number of NUCLEAR REGVLATORY COMMISSION, WASHINGTON, DC 2066&%01, AND To THE PAPERWORK REDUCTION PROJECT 13160%1041, OFRCE OF digits/characters for each block] MANAGEMENTAND BUDGET. WASHINGTON. DC 20603.
FACIUTY NAME ffI DOCKET NUMBER 12). PAGE l31 Browns Ferry Unit 3 05000296 1OF5 Engineered Safety Features Actuation As a Result of a Switch Failure EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED IB)
MONTH OAY YEAR YEAR SEOVENTIAL REVISION MONTH DAY YEAR FACIUTY NAME DOCKET NUMBER NUMBER NUMBER FACILITYNAME DOCKET NUMBER 03 10 1998 1998 002 00 04 09 98 OPERATING THIS REPORT IS SUBMITTED PURSUA NT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or morel MODE (9) 20. 2201 (b) 20.2203 (a) (2) (v) 50.73(a)(2)(i) 50.73(a)(2)(viii),
POWER 20.2203(a)(1) 20.2203(a) (3)(I) 50.73(a)(2)(ii) 50.73(a) (2)(x)
LEVEL (10) 100 20.2203(a) (2)(i) 20.2203(a) (3)(ii) 50.73(a) (2) (iii) 73.71 20.2203(a)(2)(ii) 20.2203(a) (4) X 50.73(a)(2)(iv) OTHER 20.2203(a) (2) (iii) 50.36(c) (1) 50.73(a) (2) (v) Specify in Abstract below 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii) or in NRC Form 366A LICENSEE CONTACT FOR THIS LER (12I TELEPHONE NUMBER (Include AIee Code)
G.M. Morrison, Industry Affairs Specialist (256) 729-7534 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE. SYSTEM COMPONENT MANUFACTURER REPORTABLE TO CAUSE SYSTEM COMPONENT MANVFACTURER REPORTABLE h
NPRDS TO NPRDS A ED '33. G080 NA SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH OAY YEAR YES No SUBMISSION DATE (15)
(If yes, complete EXPECTED SUBMISSION DATE). X ABSTRACT (Umit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On March 10, 1998, Surveillance Instruction (Sl) 3-SI-4.9.A.4.b(ll), 4KV Shutdown Board Undervoltage Start of Diesel Generator Division II Test, was in progress. At approximately 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br /> CST Operations personnel attempted to manually transfer 480V Shutdown Board 3B to its alternate supply in accordance with normal operating procedures. During the performance of the board transfer, the 480V Shutdown Board 3B alternate feeder breaker did not close as expected. This resulted in the momentary de-energization of 480V Shutdown Board 3B and all of its associated loads, including Reactor Protection System (RPS) bus B. The Primary Containment Isolation System groups associated with RPS bus B isolated as expected. Standby Gas Treatment System Trains A, B, and C and Control Room Emergency Ventilation System Train A automatically started as expected. The immediate cause of this event was the failure of the 480V Shutdown Board 3B alternate feeder breaker position switch to close. A mispositioned wire interfered with the proper operation of the switch close contacts. The most probable root cause of the. wire being mispositioned, was improper wire routing and/or improper removal or installation of the switch cover which caused the wire to interfere with the switch contacts. Corrective actions include continuity testing and visual inspections on additional breaker position switches to verify proper switch operation, and revision of the maintenance instruction(s) applicable to GE type SB-1 switches to include appropriate wire routing guidance.
TVA is submitting this report pursuant to 10 CFR 50.73(a)(2)(iv) as an event or condition that resulted in a manual or automatic actuation of any engineered safety feature.
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION I4-96)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 2OF5 Btowns Ferry Unit 3 05000296 1998 002 00 TEXT fifmore space is required, use additional copies of NRC Form 366AI (17)
I. PLANT CONDITIONS At the time the event occurred, Units 2 and 3 were in the Run Mode at 100 percent power. Unit 1 was shutdown Bnd defueled.
11 ~ DESCRIPTION OF EVENT A. Event:
On March 10, 1998 surveillance instruction (Sl) 3-SI-4.9.A.4.b(ll), 4KV Shutdown Board Undervoltage Start of Diesel Generator Division II Test, was in progress. This test is performed to verify that an undervoltage condition on a 4KV Shutdown Board [ED) will start the associated diesel as required by Technical Specification Section 4.9.A.4.b. Prior to establishing an undervoltage condition on 4KV Shutdown Board 3EC, the Sl provides for the transfer of loads normally supplied by the 4KV Shutdown Board to an alternate power supply to minimize the impact of the test on plant operations.
At approximately 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br /> operations personnel attempted to manually transfer 480V Shutdown Board 3B to its alternate supply in accordance with normal operating procedures. During the performance of the board transfer, the 480V Shutdown Board 3B alternate feeder breaker did not close as expected. The normal feeder breaker was immediately reclosed. This resulted in the momentary de-energization of 480V Shutdown Board 3B and all of its associated loads, including Reactor Protection System (RPS)[JC] motor-generator set 3B. Upon the'loss of power to RPS bus 3B, Unit 3 received a RPS half-scram and Primary Containment Isolation System (PCIS)[JM) groups 2, 3, 6 and 8 isolated as expected. Standby Gas Treatment System [BH) Trains A, B, and C and Control Room Emergency Ventilation System [Vl] Train A automatically started as expected. Operations personnel immediately recognized the failure of the 480V Shutdown Board to transfer as the cause of the engineered safety features actuation. Operator response to the event proceeded in accordance with the plant abnormal operating instruction for loss of one RPS bus. Recovery from the event was completed at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> when all components were returned to the state which existed prior to the beginning of the Sl.
On March 10, 1998, at 1348 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.12914e-4 months <br /> (CST), TVA made a four-hour non-emergency notification to the NRC via the Emergency Notification System pursuant to 10 CFR 50.72(b)(2)(ii).
This report is submitted pursuant to 10 CFR 50.73(a)(2)(iv) as an event or condition which resulted in a manual or automatic actuation of any engineered safety feature.
B. Ino erable Structures Com onents or S stems that Contributed to the Event:
None.
C. Dates and A roximate Times of Ma or Occurrences:
May 10, 1998 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br /> CST While performing a transfer of 480V Shutdown Board 3B to its alternate supply, the alternate feeder breaker fails to close. The deenergization of 480V Shutdown Board 3B results in a loss of power to RPS bus 3B.
NRC FORM 366 I4ISEI
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NRC FORM 366A U.s. NUCLEAR REGULATORY COMMISSION I4-SS) s LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 3 OF 5 Browns Ferry Unit 3 05000296 1998 002 00 TEXT (Il more space is required, use addirional copies of hfRC Form 366A/ I17I C. Dates and A roximate Times of Ma or Occurrences continued:
PCIS Groups 2, 3, 6 and 8 isolate as expected and SBGT Trains A,
-B, and C and CREV Train A autostart.
March 10, 1998 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> CST. Recovery from the event is completed. All components were returned to their pre-event status.
March 10, 1998 1348 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.12914e-4 months <br /> CST A four-hour non-emergency report is made to the NRC pursuant to 10 CFR 50.72(b)(2)(ii) .
D. Other S stems or Seconda Functions Affected:
None.
E. Method of Discove Loss of RPS B was received in the Unit 3 control room at 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br /> CST.
F. O erator Actions:
.No operator actions contributed to occurrence of this'event. Operator actions in response to the event were proper and in accordance with plant instructions.
G. Safet .S stem Res onse:
All safety systems responded as expected.
III. CAUSE OF, THE EVENT A. Immediate Cause:
The immediate cause of this event was the failure of the 480V Shutdown Board 3B alternate feeder breaker position switch to close. A mispositioned wire interfered with the proper operation of the switch close contacts; B. Root Cause 'e The most probable root cause of the wire being mispositioned, was improper wire routing and/or improper removal or installation of the switch cover which caused the wire to interfere with the contacts.
C. Contributin Factors:
None.
'NRC FORM 366 I4-95)
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-96]
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISION NUMBER 4OF5 Browns Ferry Unit. 3 05000296 1998 002 00 TEXT llfmore space is required, use additional copies of NRC Form 366A/ (17I IV. ANALYSIS OF THE EVENT The event was uncomplicated operationally. The half-scram event occurred on Unit 3 and involved the Unit 3 RPS bus 3B. A full scram was not initiated because RPS bus 3A remained energized throughout the event. The only.
impact of this event on Units 1 and 2 were Refuel Zone isolations and the autostart of the SGT and CREV systems which are the expected responses to the loss of RPS bus 3B. Operations personnel immediately recognized the cause of the.ESF actuation and took appropriate actions in accordance with plant procedures. Proper communications and coordination took place between the Operations personnel in the Units 1, 2, and 3 control rooms.
All initiations and actuations/isolations were consistent with and to be expected with the loss of RPS bus 3B.
V. ASSESSMENT OF THE SAFETY CONSEQUENCES There were no actual or potential safety consequences associated with this event. The 480V Shutdown Board alternate feeder breaker position switch which failed does not perform a safety function. The failure of this switch would not have prevented the 480V Shutdown Board from performing its safety function. This event did not adversely affect the safety of plant personnel or the public.
VI. CORRECTIVE ACTIONS A. Immediate Corrective Actions:
The wiring interference with the 480V Shutdown Board 3B alternate feeder breaker, position switch was corrected and proper operation of the switch was verified.
B. Corrective Actions to Prevent Recurrence:
Continuity testing and visual inspections will be performed on a sample of breaker position switches on the remaining 480V Shutdown Boards to verify proper breaker position switch operation. Testing and inspections of additional switches may be performed based on the sample results.'he maintenance instruction(s) applicable to GE type SB-1 switches will be revised to ensure appropriate wire routing guidance is incorporated.
VII ADDITIONALINFORMATION
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A. Failed Com onents:
Troubleshooting revealed that a wire was interfering with the proper operation of the alternate feeder breaker position switch closing contacts. The switch is a General Electric (GE) [G080] control and instrument switch, type SB-1. The type SB-1 switches are multi-stage rotary switches with cam-operated contacts. Each stage consists of a insulating barrier carrying one or two moving contacts and two or three cams on the operating shaft which move the contacts. The switch is provided with a protective cover which is removable for access to the switch terminals and contacts.
'TVA does not consider these corrective actions regulatory commitments. The completion of these items will be tracked in TVA's Corrective Action Pro ram.
NRc FQRM 366 I4-95I
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-9SI LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 YEAR SEQUENTIAL REVISIOI4 NUMBER 5OF5 Browns Ferry Unit 3 05000296 1998 002 00 TEXT fffmore spece is required, use edditionel copies of NRC Form 366A/ (17)
A. Failed Com onents continued:
Inspection of switch revealed a wire which was landed on the ¹2C switch terminal was in close proximity to the ¹2 moveable contact. The moveable contact was observed to move the wire out of the way when the switch was operated with the cover removed. However, with the cover installed sufficient interference was present to prevent contact closure. No maintenance or modification history was discovered relevant to condition of the switch. It was concluded that the most probable root cause of the event was improper wire routing and/or removal or replacement of the switch cover which caused the wire to interfere with the contacts. The absence of maintenance or modification history prevented the evaluation of human performance issues.
Figure 1:shows the, wire impact point with moveable contact ¹2.
B. Previous Similar Events:
No previous LERs have resulted from GE type SB-1 switch failures at Browns Ferry.
VIII. COMMITMENTS None.
Figure 1 Wire Interference With Alternate Feeder Breaker Position Switch Moveable Contact
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'RC FORM 366 (4-95)
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