ML14083A409
ML14083A409 | |
Person / Time | |
---|---|
Site: | Arkansas Nuclear |
Issue date: | 03/24/2014 |
From: | Dapas M NRC Region 4 |
To: | Jeremy G. Browning Entergy Operations |
G. Werner | |
References | |
71153, EA-14-008 IR-13-012 | |
Download: ML14083A409 (87) | |
See also: IR 05000368/2013012
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION IV
1600 E. LAMAR BLVD.
ARLINGTON, TX 76011-4511
March 24, 2014
Jeremy Browning, Site Vice President
Entergy Operations, Inc.
Arkansas Nuclear One
1448 SR 333
Russellville, AR 72802-0967
SUBJECT: ARKANSAS NUCLEAR ONE - NRC AUGMENTED INSPECTION TEAM
FOLLOW-UP INSPECTION REPORT 05000313/2013012 AND
05000368/2013012; PRELIMINARY RED AND YELLOW FINDINGS
Dear Mr. Browning:
On February 10, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed the
Augmented Inspection Follow-up Inspection at the Arkansas Nuclear One, Units 1 and 2. The
enclosed inspection report presents the results of this inspection. A final exit briefing was
conducted with you and other members of your staff on February 10, 2014.
The enclosed inspection report discusses two findings, one that has preliminarily been
determined to be Red with high safety significance for Unit 1, and one that has preliminary been
determined to be Yellow with substantial safety significance for Unit 2, that may require
additional regulatory oversight. As described in Section 4OA3.9 of the enclosed report, the
findings are associated with the March 31, 2013, Unit 1 stator drop that affected safety-related
equipment on both units.
The cause for the stator drop was not following a quality-related procedure, in that, the
overhead temporary hosting assembly was not properly designed; the associated calculation
was not reviewed; and the assembly was not load tested as required. During the movement of
the Unit 1 stator, the overhead temporary hoisting assembly collapsed, causing the 525-ton
stator to fall on and extensively damage portions of the Unit 1 turbine deck and subsequently to
fall over 30 feet into the train bay. The stator drop resulted in a Unit 1 loss of offsite power for
6 days and a Unit 2 reactor trip and loss of offsite power to one vital bus. The dropped stator
ruptured a common fire main header in the train bay, which caused flooding in Unit 1 and water
damage to the electrical switchgear for Unit 2. The alternate alternating current diesel generator
(station blackout) electrical supply cables to both units were pulled out of the electrical
switchgear and the diesel was therefore not available to either unit. In addition, there was one
fatality and eight individuals were injured. The Occupational Safety and Health Administration
(OSHA) conducted an independent inspection focusing on industrial safety aspects of the event
and issued four separate Citations and Notification of Penalties on September 26, 2013, with
proposed fines to the three involved contractors and Entergy Operations, Incorporated.
J. Browning -2-
Your staff conducted extensive reviews of this event in the root cause evaluation, documented
in Condition Report CR-ANO-C-2013-00888. Corrective actions included: repairing the
damaged Unit 1 turbine structure, fire main system, and both Unit 1 and Unit 2 electrical
systems; modifying procedures related to handling of heavy loads; training your staff on the
revised requirements for handling heavy loads; and providing additional oversight for the
subsequent Unit 1 replacement stator lift. The NRC inspectors observed many of the repair
activities, including the removal of the dropped stator and the subsequent Unit 1 replacement
stator lift. We noted that in your root cause evaluation, your staff did not address Entergys
oversight of the contractors involved with the stator lift. The NRC independently determined that
Entergy did not ensure adequate supervisory and management oversight of the contractors and
other supplemental personnel involved with the stator lift, and this contributed to the event.
These findings were assessed based on the best available information, using the applicable
Significance Determination Process. The final resolution of these findings will be conveyed in
separate correspondence. These findings also constitute an apparent violation of NRC
requirements which is being considered for escalated enforcement action in accordance with
the NRC Enforcement Policy, which appears on the NRCs Web site at:
http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html.
In accordance with NRC Inspection Manual Chapter 0609, Significance Determination
Process, we intend to complete our evaluation and issue our final determination of safety
significance within 90 days from the date of this letter. The NRCs significance determination
process is designed to encourage an open dialogue between your staff and the NRC; however,
the dialogue should not affect the timeliness of our final determination.
During the exit meeting, conducted on February 10, 2014, you requested a regulatory
conference to discuss these findings. As such, a regulatory conference to discuss the apparent
violation has been scheduled for Thursday, May 1, 2014, from 1 - 5 p.m. at the Nuclear
Regulatory Commission Region IV office in Arlington, Texas. We encourage you to submit
supporting documentation at least one week prior to the conference in an effort to make the
conference more efficient and effective. This conference will be open to public observation in
accordance with Section 2.4, Participation in the Enforcement Process, of the NRC
Enforcement Policy. The NRC will issue a public meeting notice and press release to announce
this conference. At the February 10th exit meeting, both you and your staff expressed concerns
that the NRC was not providing any credit for B.5.b mitigation equipment in the NRCs
preliminary risk analysis. As part of our risk analysis, we acknowledged that some credit may
be appropriate. We encourage you to be prepared to discuss, at the regulatory conference,
what range of credit should be applied and the supporting basis, to include such things as
procedures, training, pre-staging of equipment, etc.
Please contact Gregory Werner at 817-200-1574, and in writing, within 10 days from the issue
date of this letter to confirm your intentions to attend a regulatory conference as described
above. If we have not heard from you within 10 days, we will continue with our final significance
determination and enforcement decision.
Because the NRC has not made a final determination in this matter, no Notice of Violation is
being issued for these inspection findings at this time. In addition, please be advised that the
J. Browning -3-
number and characterization of the apparent violation may change based on further NRC
review.
In addition, the NRC inspectors documented three findings of very low safety significance
(Green) in this report. Two of these findings involve violations of NRC requirements. The NRC
is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the
If you contest these non-cited violations, you should provide a response within 30 days of the
date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory
Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the
Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Arkansas
Nuclear One.
If you disagree with a cross-cutting aspect assignment or a finding not associated with a
regulatory requirement in this report, you should provide a response within 30 days of the date
of this inspection report, with the basis for your disagreement, to the Regional Administrator,
Region IV; and the NRC resident inspector at the Arkansas Nuclear One.
In accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding,
a copy of this letter, its enclosure, and your response (if any) will be available electronically for
public inspection in the NRCs Public Document Room or from the Publicly Available Records
(PARS) component of the NRC's Agencywide Documents Access and Management System
(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-
rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Marc L. Dapas
Regional Administrator
Docket Nos: 50-313, 50-368
License Nos: DRP-51, NPF-6
Enclosure: Inspection Report 05000313/2013012 and 05000368/2013012
w/Attachment 1: Supplemental Information
w/Attachment 2: Unit 1 Outage Detailed Risk Evaluation
w/Attachment 3: Unit 2 At-Power Detailed Risk Evaluation
Electronic Distribution to Arkansas Nuclear One
J. Browning -4-
Electronic distribution by RIV:
Regional Administrator (Marc.Dapas@nrc.gov)
Deputy Regional Administrator (Steven.Reynolds@nrc.gov)
DRP Director (Kriss.Kennedy@nrc.gov)
DRP Deputy Director (Troy.Pruett@nrc.gov)
DRS Director (Acting) (Jeff.Clark@nrc.gov)
DRS Deputy Director Acting (Geoffery.Miller@nrc.gov)
Senior Resident Inspector (Brian.Tindell@nrc.gov)
Resident Inspector (Matthew.Young@nrc.gov)
Resident Inspector (Abin.Fairbanks@nrc.gov)
Acting Branch Chief, DRP/E (Greg.Werner@nrc.gov)
Senior Project Engineer, DRP/E (Michael.Bloodgood@nrc.gov)
Project Engineer, DRP/E (Jim.Melfi@nrc.gov)
ANO Administrative Assistant (Gloria.Hatfield@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)
Public Affairs Officer (Lara.Uselding@nrc.gov)
Project Manager (Michael.Orenak@nrc.gov)
Branch Chief, DRS/TSB (Ray.Kellar@nrc.gov)
ACES (R4Enforcement.Resource@nrc.gov)
OE (Roy.Zimmerman@nrc.gov)
OE (Nick.Hilton@nrc.gov)
OE (Lauren.Casey@nrc.gov)
NRR_OE (Carleen.Sanders@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
Branch Chief, ACES (Vivian.Campbell@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Technical Support Assistant (Loretta.Williams@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
RIV/ETA: OEDO (Ernesto.Quinones@nrc.gov)
ROPreports@nrc.gov
OEMail Resource@nrc.gov
RidsOeMailCenter Resource;
NRREnforcement.Resource
RidsNrrDirsEnforcement Resource
R:\REACTORS\ANO\2013\ANO2013012-LMW.docx ML
SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials GEW
Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials GEW
SRRA:NRR/
SRI:DRS/TSB SRI:DRS/EB1 PE:DRP/E RI:DRS/EB2 SRA:DRS/EB2
DRA/APOB
LWilloughby RLatta JMelfi NOkonkwo DLoveless JMitman
via email via email via email via email J.Dixon for Via email
3/13/14 3/6/14 3/5/14 3/4/14 3/12/14 3/10/14
SES:ACES C:ORA/ACES RC:ORA AC:DRP/E DD:DRP D:DRP
RBrowder VCampbell KFuller GWerner TPruett KKennedy
/RA/ /RA/ /RA/ /RA/ /RA/ /RA/
3/14/14 3/17/14 3/17/14 3/13/14 3/13/14 3/18/14
LCasey CSanders MDapas
via email via email /RA/
3/21/14 3/24/14 3/24/147
OFFICIAL RECORD COPY
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket: 05000313; 05000368
License: DRP-51; NPF-6
Report: 05000313; 05000368/2013012
Licensee: Entergy Operations, Inc.
Facility: Arkansas Nuclear One, Units 1 and 2
Location: Junction of Hwy. 64 West and Hwy. 333 South
Russellville, Arkansas
Dates: July 15, 2013 through February 10, 2014
Inspectors: Leonard Willoughby, Senior Reactor Inspector
Bob Latta, Senior Reactor Inspector
Jim Melfi, Project Engineer
Nnaerika Okonkwo, Reactor Inspector
Approved Gregory Werner
By: Acting Chief, Project Branch E
Division of Reactor Projects
-1- Enclosure
SUMMARY
IR 05000313; 05000368/2013012; 07/15/2013 - 02/10/2014; Arkansas Nuclear One;
Augmented Inspection Team Follow-up Report; Inspection Procedure 71153, Follow-up of
Events and Notices of Enforcement Discretion.
The inspection activities described in this report were performed by four inspectors from the
NRCs Region IV office. One preliminary finding of high safety significance (Red), one
preliminary finding of substantial safety significance (Yellow), and three findings of very low
safety significance (Green) are documented in this report. Both of the preliminary findings
constitute an apparent violation and two of the Green findings involved violations of NRC
requirements. The significance of inspection findings is indicated by their color (Green, White,
Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance
Determination Process. Their cross-cutting aspects are determined using Inspection Manual
Chapter 0310, Components Within the Cross-Cutting Areas. Violations of NRC requirements
are dispositioned in accordance with the NRC Enforcement Policy. The NRC's program for
overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, Reactor Oversight Process.
A. NRC-Identified Findings and Self-Revealing Findings
Cornerstone: Initiating Events
- Unit 1 Apparent Violation. The inspectors reviewed a self-revealing apparent
violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and
Drawings, which states, in part, that activities affecting quality shall be
prescribed by documented instructions, procedures, or drawings, of a type
appropriate to the circumstances and shall be accomplished in accordance with
these instructions, procedures or drawings. The licensee did not follow the
requirements specified in Procedure EN-MA-119, Material Handling Program, in
that, the licensee did not perform an adequate review of the subcontractors
lifting rig design calculation and the licensee failed to conduct a load test of the
lifting rig prior to use. The licensee initiated Condition Report
CR-ANO-C-2013-00888 to capture this issue in the corrective action program.
The licensees corrective actions included repairing damage to the Unit 1 turbine
deck, fire main system, and electrical system. In addition, changes were made to
various procedures including Procedure EN-DC-114, Project Management, to
provide guidance on review of calculations, quality requirements, and standards
associated with third party reviews.
The inspectors determined that the finding was more than minor because it was
associated with the procedural control attribute of the initiating event cornerstone,
and adversely affected the cornerstones objective to limit the likelihood of events
that upset plant stability and challenge critical safety functions during shutdown,
as well as power operations. The stator drop affected offsite power to Unit 1,
resulting in a loss of offsite power for approximately 6 days and a loss of the
alternate AC diesel generator. The inspectors used Inspection Manual
Chapter 0609, Attachment 0609.04, Initial Characterization of Findings, dated
June 19, 2012, to evaluate the significance of the finding. Since the plant was
shutdown, the inspectors were directed to Inspection Manual Chapter 0609,
Appendix G, Attachment 1, Shutdown Operations Significance Determination
-2-
Process Phase 1 Operational Checklists for Both PWRs and BWRs, Checklist 4,
dated May 25, 2004. Using Appendix G, Attachment 1, Checklist 4, the
inspectors concluded that this finding represented a degradation of the licensees
ability to add reactor coolant system inventory when needed since a loss of
offsite power occurred and therefore, this finding required a Phase 3 analysis. A
shutdown risk model was developed by modifying the at-power Arkansas Nuclear
One Unit 1 Standardized Plant Analysis Risk Model, Revision 8.19. The NRC
risk analyst assessed the significance of shutdown events by calculating an
instantaneous conditional core damage probability. The results were dominated
by two sequences. The largest risk contributor (approximately 97 percent) was
based on a failure of the emergency diesel generators without recovery. The
second largest risk contributor was the failure to recover decay heat removal.
The result of the analysis was an instantaneous conditional core damage
probability of 3.8E-4; therefore, this finding was preliminarily determined to have
high safety significance (Red).
This finding had a cross-cutting aspect in the area of human performance
associated with field presence, because the licensee did not ensure adequate
supervisory and management oversight of work activities, including contractors
and supplemental personnel. Specifically, the licensee did not provide a
sufficient level of oversight in that, the requirements in Procedure EN-MA-119, for
design approval and load testing of the temporary hoisting assembly, were not
followed [H.2] (Section 4OA3.9).
- Unit 2 Apparent Violation. The inspectors reviewed a self-revealing apparent
violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and
Drawings, which states, in part, that activities affecting quality shall be
prescribed by documented instructions, procedures, or drawings, of a type
appropriate to the circumstances and shall be accomplished in accordance with
these instructions, procedures or drawings. The licensee did not follow the
requirements specified in Procedure EN-MA-119, Material Handling Program, in
that, the licensee did not perform an adequate review of the subcontractors
lifting rig design calculation and the licensee failed to conduct a load test of the
lifting rig prior to use. The licensee initiated Condition Report
CR-ANO-C-2013-00888 to capture this issue in the corrective action program.
The licensees corrective actions included repairing damage to the Unit 1 turbine
deck, fire main system, and electrical system. In addition, changes were made to
various procedures including Procedure EN-DC-114, Project Management, to
provide guidance on review of calculations, quality requirements, and standards
associated with third party reviews.
The inspectors determined that this finding was more than minor because it was
associated with the procedural control attribute of the initiating event cornerstone,
and adversely affected the cornerstones objective to limit the likelihood of events
that upset plant stability and challenge critical safety functions during shutdown,
as well as power operations. The stator drop caused a reactor trip on Unit 2 and
damage to the fire main system which resulted in water intrusion into the
electrical equipment causing a loss of startup transformer 3. This resulted in the
loss of power to various loads, including reactor coolant pumps, instrument air
compressors, and the safety-related Train B vital electrical bus. The inspectors
used Inspection Manual Chapter 0609, Attachment 0609.04, Initial
-3-
Characterization of Findings, dated June 19, 2012, and Appendix A, The
Significance Determination Process (SDP) for Findings At-Power, dated
June 19, 2012, to evaluate the significance of the finding. Since this was an
initiating event, the inspectors used Exhibit 1 of Appendix A and determined that
Section C, Support System Initiators, was impacted because the finding
involved the loss of an electrical bus and a loss of instrument air. The inspectors
determined that Section E, External Event Initiators, of Exhibit 1 should also be
applied because the finding impacted the frequency of internal flooding. Since
Sections C and E were impacted, a detailed risk evaluation was required. The
NRC risk analyst used the Arkansas Nuclear One, Unit 2 Standardized Plant
Analysis Risk Model, Revision 8.21, and hand calculation methods to quantify the
risk. The model was modified to include additional breakers and switching
options, and to provide credit for recovery of emergency diesel generators during
transient sequences. Additionally, the analyst performed additional runs of the
risk model to account for consequential loss of offsite power risks that were not
modeled directly under the special initiator. The largest risk contributor
(approximately 96 percent) was a loss of all feedwater to the steam generators,
with a failure of once-through cooling. The result of the analysis was a
conditional core damage probability of 2.8E-5; therefore, this finding was
preliminarily determined to have substantial safety significance (Yellow).
This finding had a cross-cutting aspect in the area of human performance
associated with field presence, because the licensee did not ensure adequate
supervisory and management oversight of work activities, including contractors
and supplemental personnel. Specifically, the licensee did not provide a
sufficient level of oversight in that, the requirements in Procedure EN-MA-119, for
design approval and load testing of the temporary hoisting assembly, were not
followed [H.2] (Section 4OA3.9).
Cornerstone: Mitigating Systems
- Green. The inspectors reviewed a self-revealing, non-cited violation of Unit 1
Technical Specification 5.4.1.a and Unit 2 Technical Specification 6.4.1.a,
involving the licensees failure to develop and implement procedural controls for
response to internal flooding. Specifically, the licensee did not incorporate any
instructions for the operation of the permanently installed temporary fire pump
into procedures, which resulted in flooding due to the ruptured fire main header
and not securing the temporary fire pump for approximately 50 minutes. The
licensees corrective actions included changing Checklist 1104.032, Fire
Protection Systems, Revision 76, to include guidance for securing the temporary
fire pump in the event of a leak or rupture in the fire main header and provided
personnel training on this change. This issue was entered into the corrective
action program as Condition Reports CR-ANO-C-2013-01072 and
CR ANO-C-2013-01962.
The inspectors determined that the licensees failure to develop and implement
adequate procedural controls for the permanently installed temporary fire pump
was a performance deficiency. The performance deficiency was more than
minor because it was associated with the procedural quality attribute of the
mitigating systems cornerstone and affected the cornerstones objective to
ensure the availability, reliability, and capability of systems that respond to
-4-
initiating events to prevent undesirable consequences (i.e. core damage).
Specifically, if the necessary flood prevention/mitigation actions cannot be
completed in the time required, much of the stations accident mitigation
equipment could be adversely impacted.
Unit 1 Analysis:
Inspection Manual Chapter 0609, Attachment 0609.04, Initial Characterization of
Findings, dated June 19, 2012, Table 3, Section A, directs the user to
Appendix G. The inspectors used Inspection Manual Chapter 0609, Appendix G,
Attachment 1, Shutdown Operations Significance Determination Process
Phase 1 Operational Checklists for Both PWRs and BWRs, dated May 25, 2004,
Checklist 4, to evaluate the significance of the finding. The inspectors
determined that the finding was of very low safety significance (Green) because
the finding did not: (1) increase the likelihood of a loss of reactor coolant system
inventory, (2) degrade the licensees ability to terminate a leak path or add
reactor coolant system inventory when needed, or (3) degrade the licensees
ability to recover decay heat removal once it is lost.
Unit 2 Analysis:
Inspection Manual Chapter 0609, Attachment 0609.04, Initial Characterization of
Findings, dated June 19, 2012, Table 3, Section E, Step 2, directs the user to
Appendix F, Fire, Protection Significance Determination Process, dated
September 20, 2013. The inspectors used Appendix F, to evaluate the
significance of the finding. The finding involved a fixed fire protection system and
the fire water supply (temporary fire pump). The finding was screened against
the qualitative screening question in Appendix F, Task 1.3.1 and the inspectors
determined it was of very low safety significance (Green), because the reactor
was able to reach and maintain safe shutdown.
The finding had a cross-cutting aspect in area of the human performance
associated with documentation, because the licensee failed to create and
maintain complete, accurate, and up-to-date documentation for the use of the
temporary fire pump [H.7] (Section 4OA3.1).
- Green. The inspectors reviewed a self-revealing finding for the licensees failure
to provide appropriate work instructions for the replacement of the main
feedwater regulating valve 2CV-0748 linear variable differential transformer
2ZT-0748. Specifically, the licensee failed to translate vendor recommendations
for use of a thread sealant, and torqueing of the adjustment nuts on the linear
variable differential transformer 2ZT-0748 into procedural steps to be
accomplished and verified. The failure to follow these recommendations resulted
in the nuts falling off because of vibration. The licensee initiated Condition
Report CR-ANO-2-2013-00423 and Work Order WT-WTANO-2013-00039 to
update the work instructions and perform maintenance to repair the valve
position indication by adding thread sealant and torqueing the adjustment nuts to
prevent them from loosening.
The inspectors determined that the failure to provide instructions to properly
perform maintenance on linear variable differential transformer 2ZT-0748 was a
-5-
performance deficiency. The performance deficiency was more than minor
because it was associated with the procedure quality attribute of the mitigating
systems cornerstone. It adversely affected the cornerstone objective to ensure
the availability, reliability, and capability of systems that respond to initiating
events to prevent undesirable consequences and is therefore a finding. The
inspectors used Inspection Manual Chapter 0609, Attachment 0609.04, Initial
Characterization of Findings, dated June 19, 2012, and Appendix A, The
Significance Determination Process (SDP) for Findings At-Power, dated
June 19, 2012, to evaluate the significance of the finding. The inspectors
determined the finding was of very low safety significance (Green) because the
finding did not: (1) result in an actual loss of operability or functionality, (2)
represent a loss of system and/or function, (3) represent an actual loss of
function of a single train for greater than its technical specification allowed outage
time, (4) represent an actual loss of function of one or more non-technical
specification trains of equipment designated as high safety-significant for greater
than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and (5) involve the loss or degradation of equipment or function
specifically designed to mitigate a seismic, flooding, or severe weather event.
The finding had a cross-cutting aspect in the area of the problem identification
and resolution associated with operating experience, because although the
licensee had collected and evaluated the operating experience, it was not
implemented as procedural steps in linear variable differential transformer
replacement work instructions [P.5] (Section 4OA3.4).
- Green. The NRC identified a non-cited violation of 10 CFR 50.65(b)(2)(i) for the
licensees failure to monitor non-safety-related structures, systems, or
components that are relied upon to mitigate accidents or transients. Specifically,
the Unit 1 decay heat removal pump room level switches, which were credited for
mitigating the effects of internal flooding, were not being monitored as part of the
maintenance rule. The licensees corrective actions included developing a
preventative maintenance task to test the operation of the level switches. This
issue was entered into the corrective action program as Condition Report
CR-ANO-1-2013-03168.
The inspectors determined that the failure to effectively monitor the performance
of both Unit 1 decay heat removal room level switches in accordance with
10 CFR 50.65(a)(1) was a performance deficiency. The performance deficiency
was determined to be more than minor because it affected the equipment
performance attribute of the mitigating systems cornerstone and directly affected
the cornerstone objective of ensuring the availability and reliability of systems
that respond to initiating events to prevent undesirable consequences, in that it
called into question the reliability of flood mitigation equipment. The inspectors
used Inspection Manual Chapter 0609, Attachment 0609.04, Initial
Characterization of Findings, dated June 19, 2012, and Appendix A, The
Significance Determination Process (SDP) for Findings At-Power, dated
June 19, 2012, to evaluate the significance of the finding. The inspectors
determined the finding was of very low safety significance (Green) because the
finding did not: (1) result in an actual loss of operability or functionality, (2)
represent a loss of system and/or function (3) represent an actual loss of
function of a single train for greater than its technical specification allowed outage
time, (4) represent an actual loss of function of one or more non-technical
specification trains of equipment designated as high safety-significant for greater
-6-
than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and (5) involve the loss or degradation of equipment or function
specifically designed to mitigate a seismic, flooding, or severe weather event.
This finding did not have a cross-cutting aspect since the switches were installed
and evaluated in 2003, and therefore it is not indicative of current performance
(Section 4OA3.5.2).
-7-
REPORT DETAILS
4. OTHER ACTIVITIES
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)
.1 (Closed) Unresolved Item 05000313/2013011-001, Control of Temporary Modification
Associated with Temporary Fire Pump
The Augmented Inspection Team identified an unresolved item associated with operator
control of the water supply to the station fire suppression system and the control of a
temporary fire pump modification. Specifically, following the stator drop, a significant fire
water leak occurred in the turbine building train bay as a result of a ruptured eight-inch
fire water header. The Augmented Inspection Team determined that additional
inspection was needed to assess the timeliness of the licensees actions to secure the
fire pumps and terminate the supply of water to the fire main rupture in the turbine
building train bay.
Observations and Findings
Introduction. The Augmented Inspection Team, Follow-up Team (inspectors) reviewed a
self-revealing, Green non-cited violation of Unit 1 Technical Specification 5.4.1.a and
Unit 2 Technical Specification 6.4.1.a, involving the licensees failure to develop and
implement procedural controls for response to internal flooding.
Description. In 1999, the licensee installed a temporary fire pump that could be used
during outages or other times when the permanently installed fire pumps were out of
service. The power supply for this electric fire pump was from the London 13.8 kV line,
which is an additional offsite power source not included in the plant Technical
Specifications. This temporary fire pump allowed the licensee to perform maintenance
on installed fire pumps and still maintain fire water suppression capability for the site. At
the time of the event, the temporary electric fire pump was in service and supplying
water from the intake canal to the station fire suppression system.
The collapse of the temporary hoisting assembly and the drop of the generator stator
ruptured an eight-inch fire main in the train bay. As designed, the diesel-driven fire
pump started when the system pressure dropped below 95 psig. The permanently
installed electric fire pump was not available due to the loss of offsite power, but the
temporary electric fire pump continued to operate since the London 13.8 kV line was
unaffected by the event. The two operating pumps were each capable of supplying
approximately 2,500 gpm at rated system pressure.
At 8:03 a.m., an entry in the control room log stated that all firewater pumps, including
the temporary firewater pump were secured. However, several subsequent log entries
reflected significant water flow from the fire suppression system in the turbine building
and into the Unit 1 auxiliary building. A log entry, made 67 minutes after the event,
stated that fire hydrant 1 was cycled opened then shut in an attempt to lower fire header
-8-
pressure and slow firewater into the train bay. A log entry five minutes later stated that
the temporary fire pump was secured.
The Augmented Inspection Team confirmed through interviews with the operators that
the diesel-driven pump was secured first, and the temporary pump was secured at a
later time following the cycling of fire hydrant 1. The Augmented Inspection Team
reviewed video taken inside the turbine building following the event and confirmed that
the diesel-driven pump was secured at a time consistent with the entry in the station log.
However, the Augmented Inspection Team also identified indications of system pressure
consistent with an operating pump approximately 40 minutes after the event.
Based on uncertainties associated with the time line for operator response, the
inspectors examined the licensees revised sequence of events for securing the supply
of water to the fire main rupture in the turbine building train bay, conducted system walk
downs, and reviewed the available video records of the stator drop event. As a result of
these reviews, the inspectors determined that the initial timeline for securing the
temporary firewater pump, documented in Corrective Action 1, of Condition Report
CR-ANO-C-2013-01072, was at least 10 minutes longer than the previously estimated
time of 8:19 a.m. Specifically, review of video evidence established that the temporary
firewater pump was secured between 8:29 a.m. and 8:38 a.m. This time frame was
predicated on observed flow in the video recording at 8:24 a.m. with pressure beginning
to drop at approximately 8:29 a.m. and no firewater flow from the ruptured pipe evident
at 8:38 a.m.
The inspectors also reviewed the temporary fire pump installation procedure,
the associated 10 CFR 50.59 evaluation, the associated operations training material,
and the corrective actions identified in Condition Report CR-ANO-C-2013-01072. From
these reviews, the inspectors determined that subsequent to the event, extensive
corrective actions had been developed to address the prolonged operator response time
for securing the temporary fire pump. However, the inspectors determined that prior to
the event, there were no specific procedural controls, guidance, or standing orders which
directed operations personnel to secure firewater pumps in the event of flooding
caused by a fire system leak. The licensees corrective actions included changing
Checklist 1104.032, Fire Protection Systems, Revision 76, to include guidance for
securing the temporary fire pump in the event of a rupture in the fire main and provided
training on this change. This issue was entered into the corrective action program as
Condition Reports CR-ANO-C-2013-01072 and CR-ANO-C-2013-01962.
Analysis. The inspectors determined that the licensees failure to develop and
implement adequate procedural controls for the permanently installed temporary fire
pump was a performance deficiency. The performance deficiency was more than minor
because it impacted the procedural quality attribute of the mitigating systems
cornerstone and affected the cornerstones objective to ensure the availability, reliability,
and capability of systems that respond to initiating events to prevent undesirable
consequences (i.e. core damage). Specifically, if the necessary remedial actions cannot
be completed in the time required, some of the stations accident mitigation equipment
could be adversely impacted.
-9-
Unit 1 Analysis:
Inspection Manual Chapter 0609, Attachment 0609.04, Initial Characterization of
Findings, dated June 19, 2012, Table 3, Section A, directs the user to Appendix G. The
inspectors used Inspection Manual Chapter 0609, Appendix G, Attachment 1,
Shutdown Operations Significance Determination Process Phase 1 Operational
Checklists for Both PWRs and BWRs, dated May 25, 2004, Checklist 4, to evaluate the
significance of the finding. The inspectors determined that the finding was of very low
safety significance (Green) because the finding did not: (1) increase the likelihood of a
loss of reactor coolant system inventory, (2) degrade the licensees ability to terminate a
leak path or add reactor coolant system inventory when needed, and (3) degrade the
licensees ability to recover decay heat removal once it is lost.
Unit 2 Analysis:
Inspection Manual Chapter 0609, Attachment 0609.04, Initial Characterization of
Findings, dated June 19, 2012, Table 3, Section E, Step 2, directs the user to
Appendix F, Fire, Protection Significance Determination Process dated September 20,
2013. The inspectors used Appendix F, to evaluate the significance of the finding. The
finding involved a fixed fire protection system and the fire water supply (temporary fire
pump). The finding was screened against the qualitative screening question in
Appendix F, Task 1.3.1 and the inspectors determined it was of very low safety
significance (Green), because the reactor was able to reach and maintain safe
shutdown.
The finding had a cross-cutting aspect in area of the human performance associated
with documentation, because the licensee failed to create and maintain complete,
accurate, and up-to-date documentation for the use of the temporary fire pump [H.7]
(Section 4OA3.1).
Enforcement. Unit 1 Technical Specification 5.4.1.a and Unit 2 Technical
Specification 6.4.1.a, state that, Written procedures shall be established, implemented,
and maintained covering the following activities: The applicable procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation),
February 1978, Appendix A, Section 6.r, requires, in part, implementation of approved
procedures for combating emergencies and other significant events, including other
expected transients that may be applicable. Contrary to the above, since 1999, the
licensee failed to establish a procedure to address the requirements of Regulatory
Guide 1.33, Appendix A, Section 6.r. Specifically, Procedure 1104.032, Fire Protection
Systems, Revision 75, did not contain specific controls or guidance to secure the
temporary fire pump in the event of flooding caused by a fire system leak. Since this
finding is of very low safety significance and has been entered into the corrective action
program as Condition Reports CR-ANO-C-2013-01072 and CR-ANO-C-2013-01962,
this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of
the NRC Enforcement Policy: NCV 05000313/20130012-01; 05000368/20130012-01;
Failure to Adequately Develop and Implement Adequate Procedural Controls to
Remediate the Anticipated Effects of Internal Flooding for Either Unit.
- 10 -
.2 (Closed) Unresolved Item 05000313/2013011-002; 05000368/2013011-002, Damage to
Unit 1 and Unit 2 Structures, Systems and Components
The Augmented Inspection Team concluded that the licensee had appropriate plans in
place to identify affected equipment, control access to the affected areas, and
commence debris removal and repair activities after the stator drop occurred. However,
since a full assessment of the damage to Unit 1 and Unit 2 structures, systems,
components following the dropped stator was not possible until debris had been
removed, an unresolved item was opened to assess the damage.
Observations and Findings
The inspectors reviewed Condition Reports CR-ANO-1-2013-00868 and
CR-ANO-2-2013-00620, and performed visual inspections of walls, floors, structural
supports, and ceilings. The inspectors visually inspected support beams, conduit, cable
raceways, ventilation ducting, hydrogen piping, carbon dioxide piping, instrument air
piping, and equipment in the affected areas.
The inspectors discussed with the licensee the effect of the dropped stator on electrical
busses, raceways and cabling, and the acceptance testing the licensee performed on
the affected cables. The inspectors also reviewed and discussed the post-installation
testing the licensee performed on the repaired Unit 1 4160 Vac switchgear.
The inspectors toured affected areas, looking at the turbine building structures and
components. Acceptance testing of the repaired switchgear was ongoing, but was
mostly completed by the time of the inspection. The inspectors concluded that the
turbine building structures were repaired to the same condition as they were prior to the
stator drop, with exceptions, that included:
The non-load bearing masonry block wall between the machine shop and the
train bay was not replaced. The licensee relocated the machine shop equipment
to a different facility outside the protected area, and intends to use the area
between the train bay and former machine shop as a storage area during future
refueling outages.
The inspectors concluded that the repairs to the turbine building structures and
components were effective.
No findings were identified.
.3 (Closed) Unresolved Item 05000313/2013011-003, Procedural Controls Associated with
Unit 1 Steam Generator Nozzle Dams
The Augmented Inspection Team identified an unresolved item associated with the
procedural controls for the backup air supply systems to the Unit 1 nozzle dams. The
inspectors concluded that additional inspection was required to assess the procedural
controls associated with the primary and backup pressure sources for the steam
generator nozzle dams.
- 11 -
a. Observations and Findings
On March 28, 2013, the Unit 1 steam generator nozzle dams were installed. The nozzle
dams consisted of one rigid plug and two inflatable dams, installed in the reactor coolant
system piping that provided access for work inside the steam generators while
maintaining water inventory in the reactor coolant system. The inflatable nozzle dams
are pressurized to a normal operating pressure of approximately 75 psig. On a loss of
seal pressure, the design of the nozzle dams limits the maximum leakage through the
seals to approximately 2 gpm. The normal system lineup included a regulated 90 psig
primary supply with an independent 80 psig backup pressure source. At the time of the
stator drop event, the primary supply for the nozzle dams consisted of a portable electric
air compressor with the backup supply provided by a second portable electric air
compressor powered by a different train of non-safety-related electrical power. In the
event of loss of both air supplies, the licensees contingency plan provided for the use of
the instrument air system.
The stator drop event resulted in the loss of offsite electrical power to Unit 1 and most of
the power to the containment building, including loss of power to both air compressors
for the nozzle dams. The nozzle dams began to lose pressure, due to the check valves
on the air supply lines leaking. At approximately 9:30 a.m., personnel entered
containment and observed nozzle dam pressure was approximately 50 psig and falling.
The licensees steam generator engineer requested nitrogen bottles be brought into
containment. While waiting for the nitrogen bottles, nozzle dam pressures approached
25 psig, at which point the nozzle dam seals were subject to reactor coolant system
leakage. The steam generator engineer connected the local instrument airline to the
nozzle dams; however, instrument air pressure was reduced to approximately 50 psig
due to the trip of the instrument air compressors following the startup transformer 3
lockout and partial loss of offsite power to Unit 2. Compressed nitrogen bottles were
subsequently taken into containment and aligned to the nozzle dam consoles and seal
pressure was restored to approximately 70 psig. However, as a result of degraded seal
pressure, a small amount of reactor coolant system inventory leaked past the nozzle
dam seals.
Recovery efforts also included connecting a line to the nozzle dams from a distribution
air center supplied by the refueling air compressor. The refueling air compressor was
located outside the containment building and was powered from the London 13.8kV line,
which was not affected by the stator drop event. The refueling air compressor was
placed into service as the primary source of air for nozzle dam seal pressurization with
the nitrogen bottles as the backup source. The licensee established local nozzle dam
checks on a two-hour frequency. The inspectors determined the licensees response to
this event was appropriate.
The inspectors reviewed design documents and industry information associated with the
nozzle dam design. Unit 1 Safety Analysis Report Section 4.2.2.2, Steam Generator,
indicated that the nozzle dams prevent water from entering the steam generators.
Section 4.2.2.2 also stated that the nozzle dams serve no safety function. Engineering
Evaluation ER981203 E101, Engineering Evaluation of the ANO-1 Steam Generator
Nozzle Dams, dated January 1999, documented that the nozzles dam structure
consisted of two redundant inflatable seals and one passive emergency backup seal.
The design of the seals was for the inflatable seals to provide the primary and normal
backup seal and in the unlikely event of both inflatable seals failing, the passive seal
- 12 -
would limit leakage to less than 2 gpm, as stated above. The design of the seal was
consistent with industry guidance to limit leakage on the event of a catastrophic
inflatable seal failure. The inspectors reviewed the original procurement Specification
ANO-M-434, Specification for Arkansas Nuclear One Russellville, Arkansas OTSG
[Once-Through Steam Generator] Nozzle Dams, dated April 20, 1990. The nozzle
dams, including the seals, were procured as non-quality related.
As documented in Condition Report CR-ANO-1-2013-00917, the corrective actions
included leak testing of the nozzle dam check valves and having nitrogen bottles as a
backup source of air in case of loss of electrical power to the air compressors. One of
the contributors to the loss of seal pressure was that in 2010, Procedure OP-5120.504,
OTSG Nozzle Dam Training, Testing and Installation/Removal, Revision 6, was revised
to allow various options for maintaining seal pressure, and nitrogen bottles were no
longer used based on the operational convenience of not bringing the bottles into
containment. The inspectors determined that the change in 2010, to remove the
nitrogen bottles, was non-conservative.
No findings were identified.
.4 (Closed) Unresolved Item 05000368/2013011-004, Main Feedwater Regulating Valve
Maintenance Practices
The Augmented Inspection Team identified an unresolved item associated with licensee
maintenance practices involving the main feedwater regulating valves. The inspectors
concluded that additional inspection was required to assess the effectiveness of the
licensee maintenance practices for the main feedwater regulating valves.
Following the Unit 2 reactor trip on March 31, 2013, operators identified that main
feedwater regulating valve A failed to indicate closed. This indication resulted in the
operators tripping main feedwater pump A and manually initiating the emergency
feedwater actuation system. Operators subsequently placed the auxiliary feedwater
system in service, which required operators to manually inhibit the emergency feedwater
system, rendering both trains of emergency feedwater inoperable and requiring entry
into Technical Specification 3.0.3 for a short period of time. The licensee later
determined that the regulating valve actually had closed, and the valve indication was in
error.
Observations and Findings
Introduction. The inspectors reviewed a Green self-revealing finding associated with a
failure to provide sufficient work instructions for the replacement of the main feedwater
regulating valve 2CV-0748 linear variable differential transformer 2ZT-0748.
Specifically, the licensee failed to translate vendor recommendations to use a thread
sealant and torqueing the adjustment nuts on the linear variable differential transformer
2ZT-0748, into procedural steps to be accomplished and verified. The failure to use
thread sealant and torque the adjustment nuts resulted in the nuts loosening and falling
off because of vibration. The licensee initiated corrective actions, Condition Report
CR-ANO-2-2013-00423 and Work Order WT-WTANO-2013-00039 to perform
maintenance to add thread sealant, and torque the nuts to prevent the nuts from
loosening.
- 13 -
Description. Following the Unit 2 reactor trip on March 31, 2013, operators identified
that main feedwater regulating valve 2CV-0748 went closed; however, the digital
indications provided from the valve linear variable differential transformer and limit
switches falsely showed the valve to be 7.7 percent open. These indications resulted in
the operators tripping main feedwater pump A and manually initiating the emergency
feedwater actuation system in accordance with Procedure 2002-001, ANO standard
Post Trip Action, Revision 13. Operators subsequently placed the auxiliary feedwater
system in service, which required operators to manually inhibit the emergency feedwater
system, rendering both trains inoperable and requiring entry into Technical Specification
3.0.3 for a short period of time. This complicated operator response to the trip.
The licensee later determined that the regulating valve actually had closed, and the
valve indication was in error. Based on its investigation, the licensee determined that
the lower nut, which holds the LVDT 2ZT-0748, MFW 2P-1A DISCH MAIN REG LVDT
on a support plate on which the limit switches were also mounted, was missing. The
missing nut caused the linear variable differential transformer and the valve limit switch,
which provide digital indication for feedwater loop A main regulating valve position, to
show an incorrect valve position indication.
The linear variable differential transformer was replaced during refueling outage 2R22,
which occurred in the fall of 2012. Maintenance work order MWO-5024186-01 had a
note that required thread sealant for the linear voltage differential transformer rod. The
work order did not provide steps for the application of thread sealant for the upper and
lower nuts that hold the linear variable differential transformer rod. The use of a note
was contrary to Procedure EN-AD-101-01, Nuclear Management Manual Procedure
Writer Guide, Section I, Item 7, which specified that, notes are to be used for clarifying
information and are not to contain action instructions.
As corrective actions, the licensee torqued and added thread sealant to the nuts that
held the linear variable differential transformer rod; modified the work order to add steps
to install thread sealant; and, torqued the upper and lower nuts of the linear variable
differential transformer rod. The linear variable differential transformer was also
calibrated and tested.
Analysis. The inspectors determined that the failure to provide instructions to properly
perform maintenance on linear variable differential transformer 2ZT-0748 was a
performance deficiency. The performance deficiency was more than minor because it
was associated with the procedure quality attribute of the mitigating systems
cornerstone. It adversely affected the cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences, and is therefore a finding. The inspectors used Inspection
Manual Chapter 0609, Attachment 0609.04, Initial Characterization of Findings, dated
June 19, 2012, and Appendix A, The Significance Determination Process (SDP) for
Findings At-Power, dated June 19, 2012, to evaluate the significance of the finding.
The inspectors determined that the finding was of very low safety significance (Green)
because the finding did not: (1) result in an actual loss of operability or functionality, (2)
represent a loss of system and/or function, (3) represent an actual loss of function of a
single train for greater than its technical specification allowed outage time, (4) represent
an actual loss of function of one or more non-technical specification trains of equipment
designated as high safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and (5) involve the loss
or degradation of equipment or function specifically designed to mitigate a seismic,
- 14 -
flooding, or severe weather event. The finding had a cross-cutting aspect in the area of
problem identification and resolution associated with operating experience, because
although the licensee had collected and evaluated the operating experience, it was not
implemented as procedural steps in linear variable differential transformer replacement
work instructions [P.5].
Enforcement. This finding does not involve a violation, because there is no regulatory
requirement associated with this finding. As such, and because the associated
performance deficiency is of very low safety significance (Green), it is identified as a
finding: FIN 05000368/2013012-002, Main Feedwater Regulating Valve Maintenance
Practices.
.5 (Discussed) Unresolved Item 05000313/2013011-005, Flood Barrier Effectiveness
The Augmented Inspection Team noted that following the stator drop, a significant fire
water leak occurred in the train bay from a ruptured eight-inch fire header. Due to the
approximately 50 minute time before the pipe rupture was isolated, fire water sprayed
into the auxiliary building and accumulated in the general area access at the 317 foot
elevation. Water also accumulated in the flood protected decay heat vault B, which is
also on the 317 foot elevation. The Augmented Inspection Team concluded that
additional inspection was required to determine the causes and impact of the failed flood
hatches and the partially open decay heat vault B, drain isolation valve.
a. Inspection Scope
Background of Unit 1 and Unit 2 Flood Protection Features
The Arkansas Nuclear One facility was built at a plant grade elevation of 354 feet. The
design basis flood water level for both Unit 1 and Unit 2 has a projected flood elevation
of 361 feet at the site. Safety-related structures, systems, and components necessary
for reaching and maintaining safe shutdown are protected against the design basis flood
level. The flood protection features for both units are similar, but Unit 2 has a more
robust design.
Both units have safety-related structures, systems, and components necessary to
maintain safe shutdown for above the design basis flood water level, including the
emergency diesel generators, 4160 Vac vital and non-vital switchgear, service water
pump motors, and offsite power feeds. Some of this equipment is located in the auxiliary
building below the projected flood level and requires protection. Both units auxiliary
building designs incorporate features to keep water out, such as watertight doors,
equipment hatches, and concrete plugs with a neoprene seal to prevent water from
entering. The incorporated barriers include reinforced concrete walls designed to resist
the static and dynamic forces of the projected flood, with special water-stops at
construction joints to prevent in-leakage. Pipe penetrations through the walls have
special rubber boots or other protective features. In addition, both units have required
safety-related structures, systems, and components on the 317 foot elevation partitioned
into separate rooms to provide protection in the event of flooding. The partition walls are
designed to withstand hydrostatic loading over their full height.
- 15 -
Watertight Rooms in Unit 1 and Unit 2
Unit 1 has two watertight rooms on the 317 foot elevation. Each room contains a train of
safety-related equipment, consisting of a decay heat removal pump, a reactor building
spray pump, a decay heat removal heat exchanger, and a room cooler. Other Unit 1
safety-related pumps, including the high pressure injection pumps and emergency
feedwater pumps, are on the 335 foot elevation and are not in watertight rooms.
Similarly, Unit 2 has watertight rooms for protection of safety-related equipment. Unit 2
has the emergency feedwater pumps protected in watertight rooms located on the 335
foot elevation. Unit 2 has separate trains of low pressure safety injection pumps, high
pressure safety injection pumps, and containment spray pumps in separate vaults on the
317 foot elevation. Unit 2 also has a swing high pressure safety injection pump and
associated room cooler in a separate vault on the 317 foot elevation.
Any water leakage into the auxiliary building would flow into various floor drains and
openings, down to the 317 foot level of each auxiliary building. This leakage would
either go into each units respective dirty waste storage tank or into the units auxiliary
building sump. Sump pumps are provided to remove any small leakage that could seep
through exterior concrete walls and discharge into the dirty waste storage tank. The
water can then be transferred out of the dirty waste storage tank to be processed and
safely disposed of via each units radioactive waste cleanup system. The auxiliary
building sump pumps and dirty waste system are non-safety-related. One sump pump
will automatically start on Unit 1 at a specified level, and a second pump that could be
started manually is available. Unit 2 sump pumps will both start automatically,
depending on Unit 2 sump level.
Augment Inspection Follow-up Team Review
The inspectors reviewed the licensees Condition Report ANO-C-2013-01304 written to
address the condition of water entering the Unit 1 auxiliary building, walked down
various design features of the auxiliary building, interviewed staff, reviewed records, and
associated drawings. Due to the equipment in the turbine building impacted by the
stator drop, non-safety-related power was lost and there was no power to the auxiliary
building sump pumps and dirty waste storage tank system. The licensee identified about
an inch of water in decay heat removal room B and on the general access area of the
317 foot level of the auxiliary building. When water from the broken fire main reached
the removable floor plugs, the water leaked past the plugs into the lower auxiliary
building elevations, because the plug seals were degraded. The water subsequently
reached the 317 foot level of the auxiliary building and filled the auxiliary building sump.
Each decay heat removal room has an isolation valve that allows water in the decay
heat removal room to be drained to the auxiliary building sump. The isolation valve for
the drain from decay heat removal room B was not fully shut and water from the auxiliary
building sump flowed back into the room.
b. Observations and Findings
.1 Flood Mitigation Barriers
The inspectors have not completed their evaluation of the licensees extent of condition
for the degraded flood barriers. As such, this unresolved item will remain open and will
include the consideration of the following items:
- 16 -
(a) Floor Plugs are designed to allow for access and the movement of components into
and out of the lower levels of the auxiliary building. Flood protection for these plugs
was provided by a neoprene seal. The licensee had no specified frequency for seal
replacement. The seal was either too old and it did not seal, or the design was
inadequate in that the seal rolled out of place when the plug was set into the floor.
(b) The decay heat removal room drain valves are manually closed to prevent water
from entering the vault. During the event, one drain valve indicated closed, but the
valve was partially open, allowing water to enter the room. On several occasions
after the event, operators attempted to shut the valve, but it did not fully shut. The
lack of maintenance on the associated reach rods, and/or position indication not
being correct, or a combination of these two conditions, resulted in plant operators
not being able to consistently close the train B decay heat removal vault drain valve.
(c) From its extent of condition review, the licensee identified other paths for water to get
into the auxiliary building. These included: drains in the turbine building, a sump
from the solid radioactive waste storage building (located in the switchyard) to the
Unit 1 auxiliary building sump, unprotected penetrations in the auxiliary building
annex, unprotected electrical conduits entering into the auxiliary building, unsealed
holes in the auxiliary building from the turbine building, and the tendon gallery access
hatches. On March 5, 2014, the licensee submitted a non-emergency 10 CFR 50.72
notification, Event Number 49873, to the NRC for the discovery of pathways that
could bypass flood barriers. For immediate corrective actions, the licensee installed
barriers in the pathways or implemented compensatory measures.
(d) The NRC needs to determine why these items identified in the extent of condition
walk down for the flooding event, caused by the stator drop, were not identified as
part of the flooding walk downs described in Arkansas Nuclear One letters, dated
November 27, 2012 (ML 12334A008 and ML ML12334A006), in response to the
NRCs Request for Information letter, Request for Information Pursuant to Title 10 of
the Code of Federal Regulations 50.54(f) Regarding Recommendations 2.1, 2.3,
and 9.3 of the Near-Term Task Force Review of Insights form the Fukushima Dai-ichi
Accident, dated March 12, 2012 (ML12053A340).
(e) The safety classification of the vault drain valves as non-safety-related does not
appear commensurate with its importance in mitigating a flooding event.
.2 Decay Heat Removal Rooms Flood Level Switches not Scoped into the Maintenance
Rule
Introduction. The inspectors identified a Green non-cited violation of
10 CFR-50.65(b)(2)(i) associated with the licensees failure to monitor non-safety-related
structures, systems, and components that are relied upon to mitigate accidents or
Description. During inspection of the water intrusion into Unit 1, the inspectors noted
that both Unit 1 decay heat removal rooms contain high level alarm switches that are
credited, in part, with mitigating the effects of internal flooding caused by a moderate
energy line break. Specifically, if there is internal flooding in one of the Unit 1 decay
heat removal rooms as indicated by the room level switch, operators are dispatched to
- 17 -
ensure that the other Unit 1 train decay heat removal room is isolated. The inspectors
noted that the failure of these switches could result in operators failing to take actions to
mitigate internal flooding.
The level switches associated with Unit 1 decay heat removal rooms provide a control
room alarm. The annunciator response Procedure 1203.012H, Annunciation K09
Corrective Action, Revision 43, directs the operators to verify that the opposite train
room floor drain valve is closed. This action helps ensure that two trains of safety-
related equipment are not affected by the flooding.
The licensee installed new level switches in 2003, but determined that no preventive
maintenance activity was necessary for these switches. Based on their understanding
that these non-safety-related switches are credited with mitigating an accident, and the
knowledge that the maintenance rule scoping documents did not identify these level
alarm switches, the inspectors questioned how they were being controlled and what type
of preventative maintenance was being performed. The licensees corrective actions
included developing a preventive maintenance task to test the operation of the level
switches and the switches operated properly. The licensee entered this issue into the
corrective action program as Condition Report CR-ANO-2013-03168.
The inspectors, as part of their independent extent of condition review, looked at how the
licensee treats the room level switches in Unit 2 and noted that the licensee had
established preventive maintenance tasks to test the operation of the level switches.
Analysis. The failure to effectively monitor the performance of both Unit 1 decay heat
removal room level switches in accordance with 10 CFR 50.65(a)(1) was a performance
deficiency. The inspectors determined that the performance deficiency was more than
minor because it affected the equipment performance attribute of the mitigating systems
cornerstone, and directly affected the cornerstone objective of ensuring the availability
and reliability of systems that respond to initiating events to prevent undesirable
consequences, in that it called into question the reliability of flood mitigation equipment.
The inspectors used Inspection Manual Chapter 0609, Attachment 0609.04, Initial
Characterization of Findings, dated June 19, 2012, and Appendix A, The Significance
Determination Process (SDP) for Findings At-Power, dated June 19, 2012, to evaluate
the significance of the finding. The inspectors determined the finding was of very low
safety significance (Green) because it did not: (1) result in an actual loss of operability or
functionality, (2) represent a loss of system and/or function, (3) represent an actual loss
of function of a single train for greater than its technical specification allowed outage
time, (4) represent an actual loss of function of one or more non-technical specification
trains of equipment designated as high safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and
(5) involve the loss or degradation of equipment or function specifically designed to
mitigate a seismic, flooding, or severe weather event. This finding did not have a cross-
cutting aspect since the switches were installed and evaluated in 2003, and therefore it
is not indicative of current performance
Enforcement. Title 10 CFR 50.65(b)(2)(i) requires, in part, that the scope of the
monitoring program specified in paragraph (a)(1) shall include non-safety-related
structures, systems, and components that are relied upon to mitigate accidents or
transients. Contrary to the above, from initial maintenance rule scoping in 1996 to the
present, the Unit 1 decay heat removal room level alarm switches (non-safety-related)
were not included in the scope of the monitoring program specified in
- 18 -
10 CFR 50.65(a)(1). The inclusion of the Unit 1 decay heat removal room level alarm
switches in the scope of the monitoring program is necessary because these
components are relied upon to mitigate accidents or transients. Since this finding is of
very low safety significance and has been entered into the corrective action program as
Condition Report CR-ANO-1-2013-03168, this violation is being treated as a non-cited
violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:
NCV 05000313/2013013-003, Failure to Scope Required Components in the Stations
Maintenance Rule Monitoring Program.
.6 (Closed) URI 05000313; 368/2013011-006, Compensatory Measures for Firewater
System Rupture
The Augmented Inspection Team identified an unresolved item associated with the
licensees compensatory measures for fire suppression prior to the restoration of the
damaged firewater system. The inspectors concluded that additional inspection was
needed to fully assess the effectiveness of the compensatory measures and the
timeliness of the firewater system restoration.
Observations and Findings
The inspectors conducted interviews with on-shift licensee personnel assigned to
establish compensatory measures for the damaged fire main. The inspectors toured the
areas impacted by the damaged fire main and reviewed the Unit 1 and Unit 2 Technical
Requirements Manual.
The Unit 1 stator drop caused damage to an eight-inch fire main pipe that feeds various
fire stations. To control flooding, the fire suppression system was secured until the
damaged piping could be isolated.
The licensee did establish compensatory measures while isolating and repairing the
damaged fire main system. In addition, before the Unit 2 startup, the licensee
established compensatory measures to meet conditions specified in the Unit 2 Technical
Requirements Manual. The inspectors reviewed the compensatory measures
implemented by the licensee and determined that they were appropriate.
No findings were identified.
.7 (Closed) URI 05000368/2013011-007, Timeliness of Emergency Action Level
Determination
The Augmented Inspection Team identified an unresolved item involving the timeliness
of the emergency declaration of a Notification of Unusual Event based on the information
available to the control room operators. The inspectors concluded that additional follow-
up inspection was required to assess the timeliness of the emergency classification
given the information available to the control room operators.
Observations and Findings
The inspectors conducted interviews with on-shift licensee personnel and physically
observed the damaged electrical area in order to make an independent assessment of
the information needed to determine if criteria was met for an emergency declaration.
- 19 -
The inspectors concluded that a correct and timely emergency declaration was made by
the licensee.
The Unit 1 stator drop caused damage to an eight-inch fire main and a wall adjacent to
the Unit 2 4160 Vac non-vital switchgear. The spray from the damaged fire main piping
impacted the Unit 2 switchgear breaker enclosures and accumulated on the floor. The
water spray and/or the water accumulation caused breaker 2A-113 to short and explode,
vaporizing the components within the breaker cubicle.
The initial report to the control room at 9:25 a.m. was that one of the breaker doors on
switchgear bus 2A1 has been knocked open, but licensee personnel were unable to
determine at that time which breaker had been impacted. Light smoke with no visible
fire, from the back of one breaker in switchgear bus 2A2, was reported. There was
standing water around the switchgear. The March 31, 2013, dayshift Unit 2 Shift
Manager walked the inspectors around the Unit 2 non-vital switchgear explaining the
conditions observed in the area after the Unit 1 stator drop event. At the time of the
event, the licensee determined that it was unsafe for personnel to approach the breaker.
Approximately one hour later, conditions were such that licensee personnel could
observe the breaker cubicle to make a preliminary assessment. The licensee noted
metal splatter on the inside of the door that would indicate a high-energy event, i.e.
explosion, from possible water intrusion into the breaker cubicle. According to the Unit 2
station logs, when these observations were reported to the control room operators, the
shift manager declared an emergency declaration of a Notice of Unusual Event at 10:34
a.m. Initial notifications of the Notice of Unusual Event were completed at 10:48 a.m.
per the logs. The inspectors determined that upon identification of the explosion of
breaker 2A-113, the shift manager made the emergency declaration notification to offsite
parties within 15 minutes of the initial emergency declaration.
No findings were identified.
.8 (Closed) Unresolved Item 05000313/2013011-008, Effectiveness of Shutdown Risk
Management Program
The Augmented Inspection Team determined that additional inspection was necessary
to assess the effectiveness of the licensees risk mitigating measures associated with
the stator move.
Observations and Findings
The inspectors reviewed Condition Reports CR-ANO-1-2013-00132 and
CR-ANO-1-2013-01028, as well as Procedures EN-FAP-OU-100, Refueling Outage
Preparation and Milestones, Revision 1 and EN-OU-108, Shutdown Safety
Management Program, Revision 5. These procedures provided a process to assess
the overall impact of plant maintenance on plant risk to satisfy the requirements
of 10 CFR 50.65(a)(4) during the cold shutdown and refueling modes of reactor
operation. Procedure EN-OU-108, Step 5.4, described two types of contingency plans
that needed to be developed. The stator move fell under the definition of an outage risk
contingency plan. Procedure EN-FAP-OU-100 also described the level of contingency
planning necessary based on the probability of an issue/problem occurring and the
potential impact the issue/problem could have. Plant history, industry experience, and
worker knowledge were used to evaluate probability and impact. Probabilities of an
- 20 -
issue/problem were further delineated into High, Medium, or Low, and the impacts
of an issue were also delineated as High, Medium, or Low.
The movement of the stator was a high impact, but low probability event. The inspectors
noted that Procedure EN-FAP-OU-100, Section 7.7, did not require a contingency plan
because of the low probability of the event. The inspectors reviewed Regulatory
Guide 1.182, Assessing and Managing Risk before Maintenance Activities at Nuclear
Power Plants, dated May 2000, which endorses NUMARC 93-01, Industry Guideline
for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, dated
February 11, 2000, Section 11, Assessment of Risk Resulting from Performance of
Maintenance Activities. NUMARC 93-01, Section 11, references NUMARC 91-06,
Guidelines for Industry Actions to Assess Shutdown Management, Section 4.0,
Shutdown Safety Issues.
The inspectors determined that while no specific contingency plan for the stator move
was developed, the licensee did develop a contingency plan for the protection of spent
fuel cooling. The inspectors concluded that no contingency plans were procedurally
required to be developed by the licensee for the stator move and this was consistent
with NUMARC 93-01.
No findings were identified.
.9 (Closed) Unresolved Item 05000313/2013011-009, Effectiveness of Material Handling
Program
The Augmented Inspection Team identified an unresolved item associated with the
licensees implementation of Procedure EN-MA-119, Material Handling Program. The
inspectors determined that the design and test process applied to the crane did not
conform to applicable procedures and standards. However, the inspectors concluded
that additional inspection was needed to assess the effectiveness of the material
handling program implementation in mitigating risk associated with the stator movement
activities.
a. Observations and Findings
Introduction. The NRC identified an apparent violation of 10 CFR 50, Appendix B,
Criterion V, Instructions, Procedures and Drawings, applicable to both Unit 1 and
Unit 2. Criterion V states, in part, that activities affecting quality shall be prescribed by
documented instructions, procedures, or drawings, of a type appropriate to the
circumstances and shall be accomplished in accordance with these instructions,
procedures or drawings. The licensee did not follow the requirements specified in
Procedure EN-MA-119, in that, the licensee did not perform an adequate review of the
subcontractors lifting rig design calculation, and the licensee did not conduct a load test
of the lifting rig prior to use. The licensee initiated Condition Report
CR-ANO-C-2013-00888 to capture this issue in its corrective action program. The
licensee's corrective actions included repairing damage to the Unit 1 turbine deck, fire
main system, and electrical system. In addition, changes were made to various
procedures including Procedure EN-DC-114, Project Management, to provide
guidance on review of calculations, quality requirements, and standards associated with
third party reviews.
- 21 -
Description. The Augmented Inspection Team evaluated the effectiveness of measures
to reduce the potential for a load drop consistent with the program requirements
specified in Procedure EN-MA-119. They determined through interviews and
documentation reviews, that the licensees pre-outage evaluations were primarily
focused on ensuring that the temporary hoisting assembly did not overload the existing
plant structures. The Augmented Inspection Team also established that the project
management organization considered the temporary crane installed by the subcontractor
in the turbine building to be a temporary hoisting assembly. Procedure EN-MA-119,
Section 5.2, Load Handling Equipment Requirements, Item 7, stated, in part, that the
following measures were to be used to establish the temporary hoisting assemblies
structural integrity:
- Licensee engineering support personnel shall approve the design of vendor
supplied temporary overhead cranes.
- The temporary overhead crane shall be designed for 125 percent of the projected
hook load and shall be load tested in all configurations for which it will be used.
- Load bearing welds are required to be inspected before and after the load test.
Section 5.2, Item 7, also included a note indicating that specially designed lifting devices
may be designed and tested to other approved standards.
Based on the results of the Augmented Inspection Teams evaluation of the material
handling program, the inspectors determined that the temporary hoisting assembly had
not been load tested. The Augmented Inspection Team also established that although
the note in Procedure EN-MA-119 allowed the use of alternate standards in lieu of load
testing, the licensee could not identify objective evidence to demonstrate that an
alternate approved standard had been used for the design and testing of the temporary
hoisting assembly.
The inspectors, based on their independent review, determined that the temporary
hoisting assembly design was based, in part, on an incorrect assumption, and the frame
was not designed to support the stator load. The licensee concluded that one of the root
causes for the temporary lift assembly collapse was that the sub-contractors design did
not ensure that the lift assembly north tower could support the loads anticipated for the
lift.
In addition, the licensee, based on its root cause evaluation, concluded that the
subcontractor failed to conduct the required load testing of their modified temporary lift
assembly before its use. Specifically, the licensee concluded that:
- The north tower structure of the temporary lift assembly had not been subject to
a load test or previously used in lifts of equal or greater capacity to that of the
Unit 1 stator.
- Occupational Safety and Health Administration (OSHA) regulation
CFR 29.1910.179 (k)(1) required that prior to initial use of a new or altered crane,
the crane shall be tested to insure compliance with this section.
- 22 -
- The industry consensus standard, American Society of Mechanical Engineers
NQA-1-2008, to which the subcontractor designed the temporary lift assembly,
required load testing to ensure the structural and mechanical capacity of new or
modified cranes.
Based on the results of their review, the inspectors concluded that the licensee failed to
properly implement the requirements specified in Procedure EN-MA-119. Specifically,
the inspectors identified that the licensee failed to:
- Adequately review and approve the subcontractors design
Calculation 27619-C1 as required by Section 5.2[7](a).
- Ensure that a load test of the assembly to at least 125 percent of the projected
hook load was conducted, and that the assembly be load tested in all
configurations for which it will be used, as required by Section 5.2[7](b).
The licensee initiated Condition Report CR-ANO-C-2013-00888 to capture this issue in
its corrective action program. The licensees corrective actions included repairing
damage to the Unit 1 turbine deck, fire main system, and electrical system. In addition,
changes were made to various procedures including Procedure EN-DC-114, Project
Management, to provide guidance on review of calculations, quality requirements, and
standards associated with third party reviews.
Unit 1:
Analysis. The inspectors determined that the failure to implement the requirements of
Procedure EN-MA-119 was a performance deficiency. Specifically, the licensee failed
to: (1) independently review the subcontractors calculation for the design of the
temporary hoisting assembly as specified in Procedure EN-MA-119, Section 5.2[7](a),
and (2) perform a load test of the assembly to 125 percent of the projected hook load
and load test the assembly in all configurations for which it will be used, as required by
Procedure EN-MA-119 Section 5.2[7](b). The finding was more than minor because it
was associated with the procedural control attribute of the initiating event cornerstone,
and adversely affected the cornerstones objective to limit the likelihood of events that
upset plant stability and challenge critical safety functions during shutdown, as well as
power operations. The stator drop affected offsite power to Unit 1, resulting in a loss of
offsite power for approximately 6 days and a loss of the alternate AC diesel generator.
The inspectors used Inspection Manual Chapter 0609, Attachment 0609.04, Initial
Characterization of Findings, dated June 19, 2012, to evaluate the significance of the
finding. Since the plant was shutdown, the inspectors were directed to Inspection
Manual Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance
Determination Process Phase 1 Operational Checklists for Both PWRs and BWRs,
Checklist 4, dated May 25, 2004. Using Appendix G, Attachment 1, Checklist 4, the
inspectors concluded that this finding degraded the licensees ability to add reactor
coolant system inventory when needed since a loss of offsite power occurred, and
therefore, this finding required a detailed risk analysis. A shutdown risk model was
developed by modifying the at-power Arkansas Nuclear One Unit 1 standardized plant
analysis risk (SPAR) model, Revision 8.19. The NRC risk analyst assessed the
significance of shutdown events by calculating an instantaneous conditional core
damage probability. The results were dominated by two sequences. The largest risk
contributor (approximately 97 percent) was from a failure of the emergency diesel
- 23 -
generators without recovery. The second largest risk contributor was the failure to
recover decay heat removal. The result of the analysis was an instantaneous
conditional core damage probability of 3.8E-4; therefore, this finding was preliminarily
determined to have high safety significance (Red). Refer to Attachment 2 for the Unit 1
outage detailed risk evaluation.
This finding had a cross-cutting aspect in the area of human performance associated
with field presence, because the licensee did not ensure adequate supervisory and
management oversight of work activities, including contractors and supplemental
personnel. Specifically, the licensee did not provide a sufficient level of oversight in that,
the requirements in Procedure EN-MA-119, for design approval and load testing of the
temporary hoisting assembly, were not followed [H.2].
Unit 2:
Analysis. The inspectors determined that the failure to implement the requirements of
Procedure EN MA-119 was a performance deficiency. Specifically, the licensee failed
to: (1) independently review the subcontractors calculation for the design of the
temporary hoisting assembly as specified in Procedure EN-MA-119, Section 5.2[7](a),
and (2) perform a load test of the assembly to 125 percent of the projected hook load
and load test the assembly in all configurations for which it will be used, as required by
Procedure EN-MA-119 Section 5.2[7](b). The finding was more than minor because it
was associated with the procedural control attribute of the initiating event cornerstone,
and adversely affected the cornerstones objective to limit the likelihood of events that
upset plant stability and challenge critical safety functions during shutdown, as well as
power operations. The stator drop caused a reactor trip on Unit 2 and damage to the
fire main system which resulted in water intrusion into the electrical equipment causing a
loss of startup transformer 3. This resulted in the loss of power to various loads,
including reactor coolant pumps, instrument air compressors, and the safety-related
Train B vital electrical bus. The inspectors used Inspection Manual Chapter 0609,
Attachment 0609.04, Initial Characterization of Findings, dated June 19, 2012, and
Appendix A, The Significance Determination Process (SDP) for Findings At-Power,
dated June 19, 2012, to evaluate the significance of the finding. Since this was an
initiating event, the inspectors used Exhibit 1 of Appendix A and determined that
Section C, Support System Initiators, was impacted because the finding involved the
loss of an electrical bus and a loss of instrument air. The inspectors determined that
Section E, External Event Initiators, of Exhibit 1 should also be applied because the
finding impacted the frequency of internal flooding. Since Sections C and E were
impacted, a detailed risk evaluation was required. The NRC risk analyst used the
Arkansas Nuclear One, Unit 2 Standardized Plant Analysis Risk Model, Revision 8.21,
and hand calculation methods to quantify the risk. The model was modified to include
additional breakers and switching options, and to provide credit for recovery of
emergency diesel generators during transient sequences. Additionally, the analyst
performed additional runs of the SPAR model to account for consequential loss of offsite
power risks that were not modeled directly under the special initiator. The largest risk
contributor (approximately 96 percent) was a loss of all feedwater to the steam
generators, with a failure of once-through cooling. The result of the analysis was a
conditional core damage probability of 2.8E-5; therefore, this finding was preliminarily
determined to have substantial safety significance (Yellow). Refer to Attachment 3 for
the Unit 2 at-power detailed risk evaluation.
- 24 -
This finding had a cross-cutting aspect in the area of human performance associated
with field presence, because the licensee did not ensure adequate supervisory and
management oversight of work activities, including contractors and supplemental
personnel. Specifically, the licensee did not provide a sufficient level of oversight in that,
the requirements in Procedure EN-MA-119, for design approval and load testing of the
temporary hoisting assembly, were not followed [H.2].
Enforcement (Unit 1 and Unit 2). Title 10 of the Code of Federal Regulations (CFR)
Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, states, in
part, that activities affecting quality shall be prescribed by documented instructions,
procedures, or drawings, of a type appropriate to the circumstances and shall be
accomplished in accordance with these instructions, procedures, or drawings. Quality
Procedure EN-MA-119, Material Handling Program, Section 5.2[7], Temporary
Hoisting Assemblies, Step (a) states, in part, that vendor supplied temporary overhead
cranes or supports, winch-driven hoisting or swing equipment, and other assemblies are
required to be designed or approved by engineering support personnel. The design is
required to be supported by detailed drawings, specifications, evaluations, and/or
certifications. Quality Procedure EN-MA-119, Material Handling Program,
Section 5.2[7] Temporary Hoisting Assemblies, Step (b) states, in part, that the
assembly shall be designed for at least 125 percent of the projected hook load and
should be load tested and held for at least five minutes at 125 percent of the actual load
rating before initial use. The assembly shall be load tested in all configurations for which
it will be used.
Contrary to the above, on March 31, 2013, the licensee did not accomplish the stator lift
and move, an activity affecting quality, as prescribed by documented instructions and
procedures. Specifically:
a. The licensee approved a design for the temporary hoisting assembly that was
not supported by detailed drawings, specifications, evaluations, and/or
certifications. In addition, the temporary hoisting assembly was not
adequately designed for at least 125 percent of the projected hook load. The
licensee failed to identify the load deficiencies in vendor
Calculation 27619-C1, Heavy Lift Gantry Calculation, and the incorrectly
sized component in the north tower structure of the temporary hoisting
assembly.
b. The licensee failed to perform a load test in all configurations for which the
temporary hoisting assembly would be used.
As a result, on March 31, 2013, while lifting and transferring the main generator stator,
the temporary overhead crane collapsed, causing the 525-ton stator to fall on and
extensively damage portions of the plant.
For Unit 1:
The Unit 1 finding has been preliminary determined to be of high safety significance
(Red) and will be treated as an apparent violation and tracked as
AV 05000313/20130012-004; Unit 1 - Failure to Follow the Materials Handling Program
during the Unit 1 Generator Stator Move.
- 25 -
For Unit 2:
The Unit 2 finding has been preliminary determined to be of substantial safety
significance (Yellow) and will be treated as an apparent violation and tracked as
AV 05000368/20130012-005; Unit 2 - Failure to Follow the Materials Handling Program
during the Unit 1 Generator Stator Move.
.10 (Closed) URI 05000313/2013011-010, Causes and Corrective Actions Associated with
the Dropped Heavy Load Event
The Augmented Inspection Team identified an unresolved item associated with the
licensees identified causes and planned corrective actions for the March 31, 2013,
temporary crane failure. The root cause evaluation effort was still in progress at the
conclusion of the inspection. The Augmented Inspection Team concluded additional
follow-up inspection was necessary to assess the adequacy of the licensees identified
causes and corrective actions when completed.
Observations and Findings
Condition Report CR-ANO-C-2013-00888, documented the root cause evaluation for the
Unit 1 Main Turbine Generator Stator, drop that occurred on March 31, 2013. The
licensee identified a total of two root causes and four contributing causes, with the two
root causes and two of the four contributing causes being attributed to the contractor
performance. The report was finalized on July 22, 2013.
The stator contractor, Siemens Energy, Inc. (Siemens), and their heavy lift
subcontractor, Bigge Crane and Rigging Co. (Bigge), declined to participate on the root
cause evaluation team. The root cause team concluded that, if it had full access to
material, personnel, and records from the two vendors, the team might have identified
additional contributing causes along with corrective actions. However, the root cause
team did conclude that enough information was available to it and that information was
sufficiently adequate to identify why the event occurred and to establish the associated
corrective actions.
The root cause team evaluated a number of different areas, including: extent of
condition, extent of cause, operating experience, safety culture, vendor oversight, and
organizational and programmatic weakness. Actual nuclear safety and radiological
safety were also evaluated. The licensee concluded that the event was mitigated by
safety-related equipment and appropriate operator response. Control room operators, in
both units, were able to respond and take necessary corrective actions to mitigate the
effects of equipment damage from the stator drop. The structures, systems, and
components for both units responded as designed with no significant challenge to
nuclear or radiological safety.
The root causes were:
1. The root cause of the temporary lift assembly collapse was that the Bigge design
did not ensure the lift assembly north tower could support the loads anticipated
for the lift.
- 26 -
2. Bigge failed to perform required load testing of the temporary lift assembly prior
to its use in accordance with OSHA regulation.
The four contributing causes were:
1. Siemens and Bigge inaccurately represented that the hoist assembly had been
used at other electric power stations to lift components that exceeded the
anticipated weight of the Unit 1 stator.
2. Siemens failed to provide adequate oversight and control of Bigges
performance.
3. Procedure EN-MA-119 does not provide clear guidance regarding independent
reviews of special lift equipment.
4. Supplemental Project personnel lacked sufficient knowledge of OSHA and ASME
NQA-1 application to temporary lift assemblies and accepted Bigges assertion
that load testing was not required based on a combination of engineering
analysis and previous use.
The inspectors determined that the root causes did identify why the temporary hoisting
assembly failed. The inspectors noted that contributing causes identified various
inadequacies in procedures, oversight of the subcontractor by the primary contractor,
and knowledge of applicable standards by supplemental personal. However, it was not
clear to the inspectors that the root causes or contributing causes addressed the
licensees oversight of contractors. The NRC conducted an independent review of the
event, and as part of its review of Unresolved Item 2013011-009, Effectiveness of
Material Handling Program, the NRC identified a cross-cutting aspect H.2, Field
Presence, associated with the licensee not ensuring adequate supervisory and
management oversight of work activities, including contractors and supplemental
personnel.
The licensee implemented appropriate corrective actions to ensure the subsequent lift of
the dropped stator and the Unit 1 replacement stator were performed safely considering
lessons-learned from the root cause evaluation. Actions were implemented to ensure
the safety of personnel and equipment during the lift of the replacement stator from the
train bay to the generator pedestal.
No findings were identified.
4OA6 Meetings, Including Exit
Exit Meeting Summary
On February 10, 2014, the inspectors presented the inspection results to Mr. J. Browning, Site
Vice President, and other members of the licensee staff. The licensee acknowledged the issues
presented. Proprietary information was provided to the team and the information is being
handled in accordance with NRC policies.
- 27 -
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
J. Browning, Site Vice President
J. McCoy, Engineering Director
D. Perkins, Maintenance Manager
L. Blocker, Nuclear Oversight Manager
D. James, Regulatory and Performance Improvement Director
S. Pyle, Regulatory Assurance Manager
N. Mosher, Licensing Specialist
C. ODell, Production Manager
R. Byford, Training Manager
B. Gordon, Projects and Maintenance Services Manager
T, Evans, Production General Manager
T. Sherrill, Chemistry Manager
R. Harris, Emergency Plan Manager
J. Tobin, Security Manager
P. Williams, Operations Manager
T. Chernivec, Performance Improvement Manager
B. Daibu, Design and Program Engineering Manager
NRC Personnel
K. Kennedy, Division Director (telephonically)
L. Willoughby, Senior Reactor Inspector
B. Latta, Senior Reactor Inspector
J. Melfi, Reactor Inspector
N. Okonkwo, Reactor Inspector
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000313/2013012- AV Unit 1 - Failure to Follow the Materials Handling Program during
004 the Unit 1 Generator Stator Move
05000368/2013012- AV Unit 2 - Failure to Follow the Materials Handling Program during
005 the Unit 1 Generator Stator Move
Opened and Closed
05000313;368/ NCV Failure to Adequately Develop and Implement Adequate
2013012-001 Procedural Controls to Remediate the Anticipated Effects of
Internal Flooding for Either Unit
05000368/2013012- FIN Main Feedwater Regulating Valve Maintenance Practices
002
A1-1 Attachment 1
Opened and Closed
05000313/2013012- NCV Failure to Scope Required Components in the Stations
003 Maintenance Rule Monitoring Program
Closed
05000313/2013011- URI Control of Temporary Modification Associated with Temporary
001 Fire Pump
05000313;368/ URI Damage to Unit 1 and Unit 2 Structures, Systems and
2013011-002 Components
05000313/2013011- URI Procedural Controls Associated with Unit 1 Steam Generator
003 Nozzle Dams
05000368/2013011- URI Main Feedwater Regulating Valve Maintenance Practices
004
05000313:368/ URI Compensatory Measures for Firewater System Rupture
2013011-006
05000368/2013011- URI Timeliness of Emergency Action Level Determination
007
05000313/2013011- URI Effectiveness of Shutdown Risk Management Program
008
05000313/2013011- URI Effectiveness of Material Handling Program
009
05000313/2013011- URI Causes and Corrective Actions Associated with the Dropped
010 Heavy Load Event
Discussed
05000313/2013011- URI Flood Barrier Effectiveness
005
LIST OF DOCUMENTS REVIEWED
Calculations
NUMBER TITLE REVISION/DATE
27619-C1 Bigge - Heavy Lift Gantry - ANO Stator Replacement 0
Project
83-D-1140-05 Flooding Potential Due to Sprinkler System 'F' December 8,
1982
83-D-2038-01 Flooding Potential Due to Sprinkler System Actuation at December 8,
Elev 317', 335' and 354' 1982
83-D-2057-03 Corridor 2104 Flooding Chronology October 19,1983
A1-2
83E-0062-11 Ponding Level Estimation at Elev. 317'-0 0
83E-0062-12 Ponding Evaluation Fire Zone 105-T & 144-D 1
83-E-0062-13 Summary Calc. 0 Flooding Depths Due to Fire Protection July 15, 1985
Discharges and Know Elevations of Safety Related
Electrical Equipment
CALC-89-D-1011- OTSG Nozzle Dam Safety Evaluation 0
05
83-D-2057-03 Corridor 2104 Flooding Chronology October 19,
1983
Procedures
NUMBER TITLE REVISION
1005.002 Control of Heavy Loads 25
1015.048 Shutdown Operations Protection Plan 9
2201.001 Standard Post Trip Action 13
2203.034 Fire or Explosion 14
1203.012H Annunciator K09 Corrective Action 43
2304-262 Unit 2 Feedwater Control System LOOP A Calibration 12
COPD-24 Risk Assessment Guidelines 46
EN-DC-114 Project Management 14
EN-DC-150 Condition Monitoring of Maintenance Rule Structures 4
EN-FAP-OU-100 Refueling Outage Preparation and Milestones 5
EN-FAP-OU-105 Refueling Outage Execution 1
EN-HU-104 Engineering Task Risk & Rigor 3
EN-LI-102 Corrective Action Process 21
EN-MA-119 Material Handling Program 16
EN-MA-126 Control of Supplemental Personnel 15
EN-OU-108 Shutdown Safety Management Program 5
EN-OU-108 Shutdown Safety Management Program 6
EN-WM-104 Online Risk Assessment 7
OP-1104.032 Fire Protection Systems 75
A1-3
OP-5120.504 OTSG Nozzle-Dam Training, Testing & 6
Installation/Removal
Drawings
NUMBER TITLE REVISION
1000.028-A Temporary Alteration Form -Fire Water System 024-00-0
83E3719 28 Inch OTSG Nozzle Dam 7
A-2441-20-1 Dirty Waste Drain Tank Item T-20 Shop Fabrication 3
Details Bechtel for Arkansas Power
A-411 Radiation Zones Plant Elevation 3170 11-4 6
A-412 Radiation Zones Plant Elevation 3350 11-5 8
A-413 Radiation Zones Plant Elevation 3540 11-6 1
C-202 Auxiliary Building Plan at Elevation 335'-0 14
C-2202 Auxiliary Building Plan at Elevation 335'-0 15
E-001 Station Single Line Diagram
E-2673, Sh. 12 Connection Diagram Terminal Box 4
E-2680, Sh. 3 Connection Diagram Feedwater and Condensate System 13
Console 2CO2
E-2728, Sh. 2 Schematic Diagram Feedwater Control System Train A 10
E-2728, Sh. 4 Schematic Diagram Feedwater Control System Train A 11
E-383 Schematic Diagram Auxiliary Building Sump Pumps 5
E-389 Schematic Diagram - Dirty Liquid and Laundry Radwaste 3
Drain Pumps
LW-321 Overflow Piping to flow Drain Dirty Waste Drain Tank 1
T-20
M-002 Equipment Location Fuel Handling Floor Plan 24
M-003 Equipment Location Operating Floor Plan 40
M-004 Equipment Location Intermediate Floor Plan 37
M-005 Equipment Location Ground Floor Plan 36
M-006 Equipment Location Plan Below Grade 32
M-007 Equipment Location Sections A-A and F-F 18
M-008 Equipment Location Section B-B 32
M-009 Equipment Location Section C-C 13
A1-4
M-010 Equipment Location Section D-D 14
M-011 Equipment Location Misc. Plans and Sections 15
M-0213, Sh. 1 Dirty Radioactive Waste Drainage & Filtration 60
M-0213, Sh. 2 Laundry Waste and Containment & Aux Building Sump 28
Drainage
M-0215 Gaseous Radioactive Waste
M-0219, Sh. 1 Fire Water 83
M-0262, Sh. 4 Piping & Instrument Diagram Areas H.V.A.C. Aux. Bldg. - 3
Rad. Waste
M1-H-35 Sodium Thiosulfate Stg Tank - 99 ID 35'-11 on Side 3
M-2001-N1-71, Sh. Loop A FWCS Demand 0
1
M-2002 Equipment Location Fuel Handling Floor Plan 30
M-2003 Equipment Location Operating Floor Plan 53
M-2004 Equipment Location Intermediate Floor Plan 24
M-2005 Equipment Location Ground Floor Plan 39
M-2006 Equipment Location Plan Below Grade 40
M-2007 Equipment Location Section A-A & F-F 17
M-2008 Equipment Location Section B-B 20
M-2009 Equipment Location Section C-C 14
M-2010 Equipment Location Section D-D 16
M-2011 Equipment Location Misc. Plans & Sections 19
M-2044 Plant Design Drawing Area 24 Containment Auxiliary 32
Building Plan at Elev. 354-0 to 372-0
M-2045 Plant Design Drawing Area 24 Containment Auxiliary 45
Building Plan at Elev. 335-0 to 354-0
M-2046 Plant Design Drawing Area 24 & 26 Containment 26
Auxiliary Building Plan at Elev. 335-0 3
M-2047 Plant Design Drawing Area 24 Containment Auxiliary 34
Building Section A24-A24
M-2048 Plant Design Drawing Area 24 Containment Auxiliary 33
Building Section B24-B24
M-2049 Plant Design Drawing Area 24 Containment Auxiliary 32
Building Section C24-C24
A1-5
M-2050 Plant Design Drawing Area 24 Containment Auxiliary 30
Building Section D24-D24 & J24-J24
M-2063 Plant Design Drawing Area 26 Containment Auxiliary 23
Building Plan Above Grade
M-2064 Plant Design Drawing Area 26 Containment Auxiliary 23
Building Plan Below Grade
M-2065 Plant Design Drawing Area 26 Containment Auxiliary 13
Building Misc. Plans & Sections
M-2066 Plant Design Drawing Area 26 Containment Auxiliary 24
Building Section A26-A26
M-2067 Plant Design Drawing Area 26 Containment Auxiliary 30
Building Misc. Sections
M-2119 Piping and Instrument Diagram, Unit 1/Unit 2, Fire Water, 83
Sheet 1
M-2201-229, Sh. 2CO2 Wiring Diagram 21
06
M-2201-229, Sh. 2CO2 Wiring Diagram 20
10
M-2204, Sh. 1 Piping & Instrumentation Diagram Condensate and 98
M-2204, Sh. 2 Piping & Instrumentation Diagram Condensate and 82
M-2204, Sh. 3 Piping & Instrumentation Diagram Condensate and 46
M-2204, Sh. 4 Piping & Instrumentation Diagram Condensate and 67
M-2204, Sh. 5 Piping & Instrumentation Diagram Condensate and 14
M-2213, Sh. 1 Liquid Radioactive Waste System 60
M-2213, Sh. 2 Liquid Radioactive Waste System 49
M-2213, Sh. 3 Liquid Radioactive Waste System 13
M-2213, Sh. 4 Liquid Radioactive Waste System - Auxiliary Building 15
Elevation 317'-0
M-2213, Sh. 5 Liquid Radioactive Waste System - Auxiliary Building 15
Elevation 335'-0
M-2213, Sh. 6 Liquid Radioactive Waste System - Auxiliary Building 15
Elevations 354'-0 & 372'-6
A1-6
M-2213, Sh. 7 Liquid Radioactive Waste System - Auxiliary Building 5
Elevations 385'-0, 404'-0 & 422'-0
M-2219 Piping and Instrument Diagram, Fire Water, Sheet 1 61
M-2219 Piping and Instrument Diagram, Outside Fire Water, Unit 50
1 One/Unit Two, Sheet 5
M-2219 Piping and Instrument Diagram, Fire Water, Sheet 1 61
M-2219 Piping and Instrument Diagram, Outside Fire Water, Unit 50
1 One/Unit Two, Sheet 5
M-2219, Sh. 1 Fire Water 1
Work Orders
280093 272329 52355991 52380738 50234186-01
Condition Reports Reviewed
CR-ANO-C-2013-01072 CR-ANO-C-2013-00888 CR-ANO-C-2013-01962
CR-ANO-1-2013-00917 CR-ANO-C-2013-01074 CR-ANO-C-2013-00891
CR-ANO-1-2013-00132 CR-ANO-1-2013-01028 CR-ANO-1-2013-01286
WT-WTANO-2013-00039 CR-ANO-2-2012-01432
Condition Reports Generated During the Inspection
CR-ANO-C-2013-01985 CR-ANO-1-2013-01286 CR-ANO-C-2013-01304
CR-ANO-2-2013-00423 CR-ANO-2-2013-01945
Miscellaneous
REVISION/
NUMBER TITLE DATE
1104.032 Fire Protection Systems 75
1CAN111202 Flooding Walkdown Report - Entergy Response to NRC November 27,
Request for Information (RFI) Pursuant to 10 CFR 50.54(f) 2012
Regarding the Flooding Aspects of 0Recommendation 2.3 of
the Near-Term Task Force Review of Insights from the
Fukushima Dai-ichi Accident Aransas Nuclear One - Unit 1
1-OPG-002 Tank Volume Book 3
A1-7
Miscellaneous
REVISION/
NUMBER TITLE DATE
2CAN111202 Flooding Walkdown Report - Entergy Response to NRC November 27,
Request for Information (RFI) Pursuant to 10 CFR 50.54(f) 2012
Regarding the Flooding Aspects of 0Recommendation 2.3 of
the Near-Term Task Force Review of Insights from the
Fukushima Dai-ichi Accident Aransas Nuclear One - Unit 2
A1LP-AO-FPS Fire Protection Systems 12
EC-0044229 Provide Flooding Protection of Room 83 and Room 2079 (Unit 0
1 and Unit 2 Void Areas) Procedures 1203.025 and 2203.008
for Natural Emergencies
Engineering General Flooding of Unit 1 Aux Building April 21, 2013
Review
ER-981203E101 Engineering Evaluation of ANO-1 Steam Generator Nozzle December 7,
Dams 1998
ER-991909 Engineering Request - Connect Temporary Pump to Fire E301-0
System Test Header
ER-991909 Temporary Fire Pump Alteration E101-0
ER-991909 Temporary Fire Pump Alteration E101-1
ER-991909 Temporary Fire Pump Alteration E101-2
ER-ANO-2002- Evaluation for PM requirements for Decay Heat Vaults Level October 20,
1223-001 Switches 2002
Information Notice Deficiencies in Outside Containment Flooding Protection October 9,
No. 87-49 1987
Letter Letter, Phillps to Giambusso, Flooding of Safety Related October 20,
Equipment 1972
LIC-068-27 Pipe Rupture Leakage Criteria June 20,1988
Operator Round Waste Control Operator Rounds, March 20-April 16, 2013
Data
PMCD 2002-3701- PM Evaluation for DHR Room Flood Alarm Level Switches February 20,
P101 2003
ANO Stator Replacement Lift Plan letter from: Bigge Crane & February 8,
Rigging Co. to: Siemens Entergy 2013
EN-S Nuclear Management Manual, 50.59 Review Form- 055-06-0
Attachment 9.1
A1-8
Miscellaneous
REVISION/
NUMBER TITLE DATE
Repetitive Maintenance Task, Calibration of PDT4410
OPS-A3 Unit 1 WCO Log sheet 22
ANO-1 Stator Recovery Slides, Restart Challenge
Presentation 1, Structural & Mechanical Damage
Assessment & Repair
ANO-1 Stator Recovery Slides, Restart Challenge
Presentation 2, Electrical Damage Assessment
ANO-1 Stator Recovery Slides, Restart Challenge
Presentation 3, Electrical Testing
Unit 1 Outage schedule 0
EOOS Chart, ANO Unit 2, July 25, 2013
P.O. 31028-0159- Purchase Order for Replacement of Cubicle for Unit 1-A2 May17, 2013
PO Switchgear NSR/PP
TRM-U1 Technical Requirements Manual 44
TRM-U2 Technical Requirements Manual 52
2A-113_1.jpg Picture of 2A-113 Breaker Door
2A-113_3.jpg Picture of 2A-113 Breaker Door
Fire water system status 4-2-13 0502
Fire water system status 4-3-13 0609
Fire water system status 4-3-13 1109
Fire water system status 4-3-13 1800
Fire water system status 4-4-13 0451
Fire water system status 4-4-13 1800
Fire water system status 4-7-13 0600
Fire water system status 4-11-13 1245
Fire water system status 4-12-13 0400
Fire water system status
Log Entries Report for Fire Water up to 4-12-13 0400
Sequence of Events up to 4-12-13
A1-9
Miscellaneous
REVISION/
NUMBER TITLE DATE
Tagout 1R24-1 - FS-009-B-FS RUPTURE with P&ID Markup
Tagout 1R24-1 - FS-009-C-FS RUPTURE with P&ID Markup
Tagout 1R24-1 - FS-009-D-FS RUPTURE and 2C23-1 -
FS 019-2HR-36 with P&ID Markup
Tagout 1R24-1 - FS-009-FS RUPTURE with P&ID Markup
Vendor Documents
NUMBER TITLE REVISION
TDF130 0320 Fisher Control Systems Instruction Manual Actuators Types 5
470, 471, 475 & 478 Series
TDG200 0080 For Model 3172 Aux Bldg Sump Pumps
TDO045 210 OMEGA Level Switch Series LV-70 - Maintenance Section
TDR340.0060 Installation and Maintenance Instruction McCannaflow 0
Flanges Ball Valves Class 150 & 300 1 Thru 4
Engineering Information Records
NUMBER TITLE REVISION
DCP 94-2008 Feedwater Control Systems Upgrade July 26,1995
ECT-44312-02 SU 1 A1 & A2 Live Bus Test July 21, 2013
ECT-44312-03 Functional Testing for Breaker 2A-903 July 20, 2013
ECT-44312-04 Functional Testing for Breaker 2A-901 July 24, 2013
ECT-44312-05 Functional Testing for Startup Transformer #2 A-1 Feeder July 8, 2013
breaker A-111
System Training Manuals
NUMBER TITLE REVISION
STM 1-52 Dirty Liquid Radwaste 7
STM 2-33 System Training Manual Alternate AC Diesel Generator 22
STM 2-69 System Training Manual Feedwater System Control 13
STM 2-19 System Training Manual Main Feedwater System 14
A1-10
Unit 1
Outage Detailed Risk Evaluation
(Phase 3 Risk Assessment Loss of Offsite Power)
Revision 1b
Probabilistic Risk Assessment (PRA) Analyst: Jeff Mitman, Senior Reliability and Risk
Analyst, NRR/DRA/APOB
Independent Reviewer Donald Chung, Reliability And Risk Analyst,
NRR/DRA/APOB
Region IV Reviewer David Loveless, Senior Risk Analyst
A2-1 Attachment 2
1.0 Introduction
On March 31st 2013, at 7:50 am, Arkansas Nuclear One Unit 1 (ANO1) experienced a
loss of offsite power (LOOP). This LOOP event occurred because while lifting and
transferring the Unit 1 main generator stator to the train bay, the hoist assembly failed.
The dropped stator fell on to the turbine deck and into the train bay. This event resulted
in multiple damages in the turbine building including damage to electrical buses
supplying offsite power to Unit 1, and damage to the fire suppression piping.
At the time of this event, Unit 1 was in a refueling outage. It had been shutdown for
approximately 7 days. Fuel was in the reactor vessel, the reactor cavity was flooded up,
and both trains of decay heat removal system were in service. With the loss of offsite
power, both Unit 1 emergency diesel generators (EDG) started and loaded their
respective buses. Decay heat removal was quickly restored. Once decay heat removal
was restored the unit was quasi stable, with no offsite power available due to damage to
the non-vital electrical buses, with EDGs powering the vital busses and the decay heat
removal system operating and providing decay heat removal to the reactor vessel.
Dropping the generator stator caused the following damage:
- Offsite power was lost - it took six days to recover
- The station blackout diesel generators (called the AAC) connection to the plant
was severed rendering the ACC non-functional
- Fire watering piping was damaged requiring shutdown of the fire protection
system. The damage to the piping also caused flooding in the Unit 1 and 2
structures with tens of thousands of gallons of water challenging critical
equipment
2.0 Discussion of the Performance Deficiency
The licensee failed to properly implement Engineering Procedure EN-MA-119, Material
Handling Program. The following two examples are presented:
The licensee failed to adequately review and approve Bigge Calculation 27619-C1 as
required by Section 5.2[7] (a)
Engineering Procedure EN-MA-119, Section 5.2[7] requires temporary hoisting
assemblies to be designed or approved by Engineering Support Personnel (ESP). The
design calculation did not adequately consider the loads that would be experienced by
the lift. Entergys review and approval process failed to identify the calculation
deficiencies and the weak component in the north tower structure. Specifically,
Entergys ESP failed to adequately review and identify the flaw in Calculation 27619-C1
consistent with the requirements of procedure Section 5.2[7] (a) which states that
temporary hoisting assemblies are required to be designed or approved by ESP.
The licensee failed to ensure that a load test of the assembly to at least 125 percent of
the projected hook load or to another approved standard was performed as required by
Section 5.2[7](b) and associated note.
A2-2
3.0 Plant Conditions Prior to the Event
Plant equipment and conditions were as follows:
- Unit was in refueling outage with fuel in the reactor, head removed, and refueling
canal flooded
- Estimated time to boil (TTB) was 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />
- Estimated time to core uncovery was 4 days
- Both trains of reactor shutdown cooling (SDC) were in service
- Plant electrical lineup was in a plant shutdown configuration to support
maintenance and testing as follows:
o 6900 Volt Bus H2 was de-energized.
o 6900 Volt Bus H1 was energized.
o 4160 Volt Bus A2 was de-energized.
o Safety-related 4160 Volt Buses A3 and A4 were cross tied and supplied
power via non-safety-related 4160 Volt bus A1.
o 480 Volt buses B5 and B6 were cross tied.
o Green train battery D06 had been disconnected from D02 bus.
o D04 battery charger was supplied from Swing MCC B56 to provide power
to Green train DC bus D02.
o B56 was aligned to B5.
4.0 Plant Conditions after Initiating Event Initiated
Time to boil was estimated at eleven hours and time to core uncovery without mitigation
was estimated at four days.
The following equipment was unavailable after event initiation:
- Offsite power
- Station blackout diesel generator - ACC
- Fire water
- All balance of plant equipment
- Gravity feed from the borated water storage tank (BWST) as water
level in the BWST was lower than water level in reactor coolant
system (RCS)
- Instrument air (IA) was unavailable - the analyst assumed that all
air operated valves failed in a safe direction, i.e., the systems IA
supported remained available (Note: 1) the DHR heat exchanger
bypass valves fail shut on loss of air, 2) the service water supply
valve to the DHR heat exchanger fails full open on loss of air)
- Starting air compressors for the emergency generators
- Normal lighting
A2-3
The following equipment was available after the event initiation to mitigate
the event:
- Both emergency diesel generators and their respective electrical
distribution systems
- Both decay heat removal trains (two pumps)
- Both high pressure injection (HPI) trains (three pumps)
- Reactor building spray systems - note these were not credited in
the analysis, however, the non-crediting had no effect on the
quantitative results
5.0 Significance Determination Process (SDP) Phase 2 Summary
No Phase 2 was conducted.
6.0 Initiation of a Phase 3 SDP Risk Assessment
A Phase 3 SDP risk assessment was performed by the Office of Nuclear Reactor
Regulation (NRR).
The analysts used the following generic references in preparing the risk assessment:
- NUMARC 91-06, Guidelines for Industry Actions to Assess Shutdown
Management. December 1991
- NUREG/CR-6883, The SPAR-H Human Analysis Method. August 2005
- NUREG-1842, Good Practices for Implementing Human Reliability Analysis.
April 2005
- NUREG/CR-6595 Revision 1, An Approach for Estimating the Frequencies of
Various Containment Failure Modes and Bypass Events. October 2004
- INL/EXT-10-18533 Revision 2, SPAR-H Step-by-Step Guidance. May 2011
- RASP Manual Volume 1 - Internal Events, Revision 2.0 date January 2013
- NUREG/CR-1278, Handbook of HRA with Emphasis on Nuclear Power Plant
Applications. August 1983
The analyst used the following plant specific references:
- EOP: 1202.007, Degraded Power
- AOPs:
o 1203.024, Loss of Instrument Air
o 1203.028, Loss of Decay Heat Removal
o 1203.050, Unit 1 Spent Fuel Pool Emergencies
- Calculation: 89-E-0017-01, Time to Boiling and Time to Core Uncovery after Loss
of Decay Heat Removal, Unit 1, Revision 7
A2-4
- Procedure: 1103.018, Maintenance of RCS Water Level
7.0 Development of the Model
No Low Power/Shutdown (LP/SD) SPAR model exists for ANO Unit 1. Therefore, the at-
power ANO1 SPAR model was modified to allow analysis of the LOOP event. A new
event tree (ET) was created to analyze the event.
This ET is shown in Figure A-1 of Appendix A. The ET was linked to a mix of existing
at-power fault trees (FT) and new FTs, as applicable. The existing FTs were modified as
necessary to appropriately describe system dependencies during shutdown conditions
and the different success criterion. The ET and high level FTs are shown in Appendix A.
Modeling Assumptions
- PRA mission time is normally assumed to be 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. However,
after the event was initiated it took approximately six days to
recovery offsite power. If the emergency diesel generators failed
after running successfully for three days the time to core uncovery
was over three days after loss of DHR. Thus the emergency
diesel generator mission time was modified to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.
- The Division 2 normal AC power is from 4Kv bus A2. However,
bus A2 was unavailable for maintenance and bus A4 was
receiving power from 4Kv bus A3 via breaker A-310 and A-410. A
model change was made to reflect this alternative alignment and
the associated interlocks and their failure probabilities.
- As identified above, the Green train battery D06 had been
disconnected from D02 bus. D02 DC bus was being fed from a
battery charger supplied from Div. 1 AC power. With this
arrangement, the Div. 2 DC system would (and did) de-energize
on a loss of Div. 1 AC power. If the Div. 1 AC power is restored
with an EDG start then Div.2 DC power would be (and was)
restored. However, if the Div. 1 EDG did not restore AC power to
the battery charger, the Div. 2 DC power would remain de-
energized. The consequence of this is that without DC power
from a Div. 1 battery charger the Div. 2 EDG would not start
normally. In fact, during the event, the Div.2 EDG start was
delayed about 10 seconds until the Div. 1 EDG restored Div.2 DC
power. The model was modified to allow for a manual realignment
of Div. 2 DC power directly to the Div. 1 battery. This human
action (HFE) was given a failure probability of 4E-3 (DCP-XHE-
XM-DD11D12). Notes: 1) An alternative means of re-energizing
the Div. 2 DC system would be to restore the Div. 2 battery from
its maintenance status. The licensee indicated that this could be
accomplished in about 30 minutes once the problem and solution
were identified and the decision made to proceed. This recovery
method was not modeled as it is assumed that the failure
probability of the primary method was adequately low to negate
A2-5
the need for the additional recovery method. 2) Both EDGs can
be manually started without DC power during a proceduralized
process that the licensee estimates would take about 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.
This capability was not explicitly modeled as the analyst assumed
that this procedure is adequately credited as part of the diesel
recovery analysis incorporated into the event tree.
- As noted above, instrument air failed during the event. Without
instrument air, there is no means to recharge the EDG start air
receiver tanks. The receiver tanks have sufficient capacity for
about 10 normal starts of the EDGs. Thus if the EDGs did not
start initially, there would be a limited number of starts before the
tanks deplete. This dependency was modeled.
- On loss of instrument air the DHR heat exchanger bypass valves
fails full closed, i.e., in the safe direction. Also the service water
supply valves to the DHR heat exchangers fail full open also in the
safe direction. These attributes were not modeled.
- As discussed above, the RCS level at the beginning of the event
was higher than the BWST level. Therefore, at the beginning of
the event there was no capability to gravity feed the RCS from the
BWST. The licensee asserted that they have capabilities to refill
the Unit 1 BWST from the Unit 2 RWT. However, once the BWST
was refilled RCS level would still be higher than the BWST level.
However, if RCS boiling were to commence, then the level in the
RCS would decrease. Level would decrease below the Unit 1
BWST level at which point level would allow gravity feeding of the
Unit 1 RCS. However, boiling would cause the Unit 1 reactor
building (i.e., containment) to pressurize. This elevated pressure
would preclude gravity feed. The licensee could depressurize the
reactor building. These capabilities are un-proceduralized and
were not credited in the modeling.
- Time to boil (TTB) was changed from 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />. Time
to core uncovery was changed from 3 to 4 days to 4 days. Both
changes are based on revised calculations from the licensee.
These changes had no impact on the HRA analysis. However,
the change in the core uncovery time did lower the non-recovery
probabilities marginally.
HRA Analysis
Shutdown operation is highly dependent on operator actions as most of the required
actions are manual (e.g., initiating feed of the RCS). HRA analysis was conducted to
properly characterize the required manual actions. The human error probabilities
(HEPs) were calculated using the Low Power Shutdown SPAR-H worksheets from
NUREG/CR-6883, The SPAR-H Human Reliability Analysis Method
and INL/EXT-10-18533 and SPAR-H Step-by-Step. Consideration was given to the
following:
A2-6
- available time to perform the manual actions,
- stress levels of the crew during the event,
- complexity of the diagnoses and required recovery actions,
- crew experience and applicable and relevant training,
- quality and thoroughness of procedures,
- ergonomics,
- fitness of duty issues, and
- available work processes
Table 1 shows a summary of the dominant HEPs, a detailed discussion of the HEPs is
given in Appendix B.
In addition to the calculation of specific HEPs for this condition, sequences or cutsets
which involved multiple operator actions were examined for human action dependency.
For the dominant HEPs no dependent couplets were found.
In addition, the cutsets were reviewed to find those that contained two or more HEPs in
a single sequence of cutset. For those cutset with multiple HEPs, the HEPs were
reviewed to determine if the product of the HEPs was less than 1E-6. For those cutsets
a floor, or cutoff, was applied as directed by RASP Manual Volume 4 - Shutdown
Events, Revision 1 Appendix B. Because of the long times to core damage, a cutoff of
1E-7 was applied. This conservative assumption did not materially affect the results.
Normal lighting was impacted by the LOOP. This could have an impact on the ability of
the equipment operators to perform tasks outside of the main control. This impact was
not assessed.
A detailed description of the HEPs is given in Appendix B.
Table 1
Summary of Dominant HRA Results
Human Description Time Time Mean Mean Total
Error Needed Available Diagnosi Action Mean
SD-XHE-D-LOSDC Operator Fails to Diagnose 5 minutes 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> 2E-5 n/a 2E-5
Loss of SDC before boiling
SD-XHE-XL-LOSDC Operator Fails to Recover 30 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> n/a 4E-4 4E-4
Loss of SDC before Boiling minutes
SD-XHE-XL-MINJ Operator Fails to Inject (AC 30 4 days n/a 2E-5 2E-5
power available) before minutes
Level Reaches TAF
SD-XHE-XL-LPR Operator Fails to Initiate 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 5 days 2E-5 2E-4 2.2E-4
Low Pressure Recirc
SD-XHE-XM-BWST Operator Fails to Refill 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 5 days n/a 2E-5 2E-5
BWST during Shutdown
DCP-XHE-XM-DD11D12 Operator Action to Align 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 2E-3 2E-3 4E-3
125VDC Panel D11 to
Feed 125VDC Panel D21
A2-7
8.0 Conditional Core Damage Probability (CCDP) Assessment Results
A detailed Phase 3 Significance Determination Process risk analysis was performed
consistent with NRC Inspection Manual Chapter (IMC) 0609 Appendix G. Step 4.3.8 of
this procedure directs the analyst to assess the significance of shutdown events by
calculating an instantaneous conditional core damage probability (ICCDP). (Throughout
this assessment, the analyst has used the terminology of CCDP instead of ICCDP for
simplicity.) This assessment was performed by setting the initiating event frequency
(IEF) for loss of offsite power to 1.0 and all other IEF to zero. The above described
SPAR model was evaluated using the SAPHIRE code version 8.0.9.0.
As this SDP evaluates an actual event in which no external events occurred, there was
no risk from external events. As discussed in the above paragraph, this would include
setting any external event IEF to zero.
The truncation limit was set at 1E-16.
The result of the CCDP analysis is 3.8E-4; based on these results the finding is
preliminary Red. The top cutsets are in Appendix C. The analyst did not perform
uncertainty analysis.
Table 2
CCDP Results
Sequence Point Estimate Cut Set Count
4 1.6E-5 6784
6 2.1E-8 2072
8 3.3E-7 13225
11 1.0E-7 553
13 4.3E-9 79
15 7.2E-9 359
19 3.7E-4 3955
Total 3.8E-4 27027
The results are dominated by two sequences. The largest contributor is from Sequence
19 which comprises a failure of the emergency diesel generators (EDG) without
recovery. Both the EDG and EDG non-recovery failure probabilities were calculated
using the standard SPAR methods and models. Sequence 4 is also a significant
contributor. Sequence 4 cutsets are dominated by failure to recover DHR.
The numeric results above quantify to a preliminary Red finding. However, given the
time to core damage, recovery may be possible with temporary systems such as B.5.b
equipment. The analyst is unaware of procedures or training to cool the RCS during
these conditions. In addition, condition in the reactor building may become difficult if not
life threatening once boiling begins. In conclusion, some credit for these types of actions
may be warranted. However, neither SPAR-H nor any other HRA method was ever
intended to quantify these types of scenarios. However, using SPAR-H yields failure
probabilities between 0.1 and 0.5. If significant credit were given, this could reduce the
finding into the Yellow range.
A2-8
9.0 Conditional Large Early Release Probability (CLERP) Assessment
The figure of merit for this analysis is incremental conditional large early release
probability (ICLERP). This ICLERP analysis is based on the method for shutdown
described in NUREG/CR-6595 Revision 1, An Approach for Estimating the Frequencies
of Various Containment Failure Modes and Bypass Events, dated 10/2004. This report
supplies simplified containment event trees (CET) to determine if the core damage
sequence contributes to LERF. NUREG/CR-6595 presents its analysis in terms of
LERF, which is interpreted here as ICLERP.
NUREG/CR-6595 defines LERF as the frequency of those accidents leading to
significant, unmitigated releases from containment in a time frame prior to effective
evacuation of the close-in population such that there is a potential for early health
effects. This is identical to the definition of LERF in IMC 0609 Appendix H. Figure 4.2
(PWR Large Dry and Sub-atmospheric Containment Event Tree) from NUREG/CR-6595
is applicable to the ANO1 event.
This event occurred seven days after shutdown. The earliest core damage could occur
would be four days after event initiation. Thus core damage would not occur until 11
days after shutdown. Based on this time and the recommended approach given by
NUREG/CF-6595 no large early release could occur.
10.0 Sensitivity Analysis
Several sensitivity cases were conducted to further understand the event risk
significance. The cases are described below.
Case 1: Loss of Instrument Air
The LOOP event on Unit 1 in combination with the partial LOOP in Unit 2 combined to
cause a loss of instrument air on Unit. There does not appear to be any impact on
Unit 1 from the loss of air. However, instrument air was being supplied to the steam
generator nozzle dams. If the nozzle dams had failed, water level could have drained to
the bottom of the steam generator openings. The nozzle dam design appears to
preclude a significant inventory on loss of air. The design limits the leakage to 2 gpm on
each nozzle dam. With several hundred thousand gallons of water above the nozzle
dams this leakage rate is insignificant.
Case 2: HRA No Cutoff
A case was conducted to verify the sensitivity of the results to the cutoff value. This
case was run with truncation level of 1E-16. The calculated CCDP was 1.6E-4. This
indicates that the cutoff implementation is a second order effect only.
A2-9
Sequence Point Estimate
4 1.6E-05
6 1.7E-08
8 3.3E-07
11 6.0E-10
13 6.1E-13
15 1.8E-10
19 3.7E-04
Total 3.8E-04
Case 3: DC Flooding
The stator drop severed a fire water header pipe. It took approximately 45 minutes to
stop this leakage. Before the leakage was stopped, water accumulated into the Unit 1
and 2 turbine buildings where it caused a small Unit 2 kV fire/explosion. This caused a
loss of offsite power to one division of Unit 2 AC power which was mitigated by the
associated emergency diesel generator. Water also started to accumulate into the
Unit 1 SDC/DHR B pump vault. If this accumulation continued it could have failed the
pump. Potentially it could have impacted other Unit 1 equipment. Sensitivity cases were
conducted with various flooding probabilities and various combinations of impacted
equipment. Those combinations and their impacts are presented in the below table.
These analyses assume that the flooding could not impact the Unit 1 emergency diesel
generator or their associated 4kV switch gear and 480 v MCCs.
This analysis shows that if the flooding had not been terminated in a timely manner it
could have had a significant impact on plant safety.
Impacted Equipment
Flood Probability = 0.1 Flood Probability = 1.01
Both LPI/SDC/DHR pumps 1E-3 5E-2
A single HPI pump (either
no impact no impact
A, B or C)
Any combination of two HPI
no impact no impact
pumps
All three HPI pumps no impact no impact
All of HPI and SDC/DHR 1E-3 1E-1
Notes:
1) If the associated basic events are set to True instead of 1.0 the CCDPs are somewhat
lower as would be expected.
2) These sensitivity cases were run with truncation set to 1E-8.
A2-10
Case 4: Impact of Loss of EDG Starting Air Compressors
The LOOP caused a loss of normal EDG starting air. If multiple starts of the EDG were
required this could impact the restoration of the emergency power. While it is difficult to
quantify the change in the EDG non-recovery probability, it is straight forward to
calculate the impact of non-recovery probabilities on the CCDP. The analyst assumed
that the non-recovery probability was double from 4.0E2 (for 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br />) to 8.0E-2. The
new CCDP is 7.5E-4.
Case 5: Impact of EDG 2 in Maintenance
When the generator stator was dropped, the licensee was making plans to start
maintenance on the Div. 2 emergency diesel generator. This maintenance was
imminent. No licensee restrictions were in place to delay this maintenance until after the
generator stator lifts had been completed. If this EDG maintenance had been started
and sufficiently progressed to preclude restoration this would have significantly
increased the risk. This sensitivity case places the Div. 2 EDG in maintenance. The
new CCDP is 3.5E-3.
A2-11
Appendix A: Model Figures
A2-12
Figure A-1: Loss of Offsite Power Event Tree
LOOP Event Occurs EMERGENCY POWER OPERATOR FAILS TO DIAGNOSIS LOSS OF Recover RHR/SDC Gravity or Forced Feed GRAVITY FEED (without LOW PRESSURE BWST REFILL OPERATOR FAILS TO LATE RECOVERY OF # End State
during Mode 6 AVAILABLE RECOVER OFFSITE RHR/DHR BEFORE DURING SHUTDOWN (with AC power) after AC Power) before TAF RECIRCULATION during RECOVER EMERGENCY SDC/DHR COOLIING (Phase - CD)
POWER IN 72 HOURS BOILING (11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />) before Boiling (11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />) Loss of SDC/DHR Shutdown DIESEL IN 96 HOURS
IE-M6-LOOP EPS OPR-72H LORHR-D SDC-REC MINJ G-FEED LPR-SD REFILL DGR-96H LTREC
1 OK
2 OK
3 OK
6 Days
4 CD
LTREC-6D
5 OK
5 Days
6 CD
LTREC-5D
7 OK
4 Days
8 CD
9 OK
10 OK
6 Days
11 CD
LTREC-6D
12 OK
5 Days
13 CD
LTREC-5D
14 OK
4 Days
15 CD
Undeveloped Branch as Probability is 0.0
16 OK
0% (Undeveloped branch as given failure)
17 OK
1.95E-3
100%
18 OK
100 %
4E-2 4 Days
19 CD
A2-13
Figure A-2: Emergency Power Failure Fault Tree
EMERGENCY POWER FAILS
FAILURE OF AC POWER FROM
SWITCHGEAR A3
ACP-SWGR-A3 Ext
FAILURE OF AC POWER FROM
SWITCHGEAR A4
ACP-SWGR-A4 Ext
Figure A-3: Offsite Power Recovery Fault Tree
OPERATOR FAILS TO
RECOVER OFFSITE POWER IN
24 HOURS
OPR-24H
OPERATOR FAILS TO
RECOVER OFFSITE POWER IN
24 HOURS
OEP-XHE-XL-NR24H 2.31E-02
Note that the non-recovery probability was set to one in a change set
A2-14
Figure A-4: Diagnose Loss of RHR/DHR Fault Tree
DIAGNOSIS LOSS OF RHR
BEFORE BOILING
LORHR-D
Operator Fails to Diagnose
Loss of SDC before boiling
SD-XHE-XD-LOSDC 2.00E-05
A2-15
Figure A-5: Recovery RHR/SDC Fault Tree
Recover RHR/SDC DURING
SHUTDOWN
SDC-REC
DHR HARDWARE FAILURES Operator Fails to Recover Loss
of SDC/DHR before Boiling
DHR3 SD-XHE-XL-LOSDC 4.00E-04
FAILURE OF DHR SUCTION INSUFFICIENT FLOW TO RCS
PATH FROM RCS INLET INLET HEADERS DURING DHR
DHR02 DHR03
RCS Suction MOV CV-1404 to DHR TRAIN A FAILS
LPI Fails
LPI-MOV-OC-CV1404 8.13E-07 DHR-TRAINA Ext
RCS Suction MOV CV-1410 to DHR TRAIN B FAILS
LPI Fails
LPI-MOV-OC-CV1410 8.13E-07 DHR-TRAINB Ext
LPI Fails
LPI-MOV-OC-CV1050 8.13E-07
A2-16
Figure A-6: Gravity and Forced Feed Fault Tree
Gravity or Forced Feed (with AC
power) after Loss of SDC/DHR
MINJ
Operator Fails to Inject (AC
power available) before Level
Reaches TAF
F-FEED-LATE3 SD-XHE-XL-MINJ 2.00E-05
HIGH PRESSURE INJECTION
during Shutdown
HPI-SD Ext
LOW PRESSURE INJECTION
LPI-SD Ext
Gravity Feed before Core
Damage
G-FEED-1 Ext
Note the gravity feed portion of this FT is set to fail as gravity feed will not work because the physical level of the
BWST is lower than the refueling canal
A2-17
Figure A-7: Gravity Feed (without AC Power) Fault Tree
GRAVITY FEED (without AC
Power) before TAF
G-FEED
Gravity Feed before Core Operator Fails to Gravity Feed
Damage (without power) before Level
Reachs TAF
G-FEED-1 Ext SD-XHE-XL-GRAVITY 4.00E-04
Note this FT is set to fail as gravity feed will not work because the physical level of the BWST is lower than the refueling canal
A2-18
Figure A-8: Low Pressure Recirculation Fault Tree
LOW PRESSURE
RECIRCULATION during
Shutdown
LPR-SD
HARDWARE FAILURES Operator Fails to Initiate Low
DURING LOW PRESSURE Pressure Recirc
RECIRCULATION
LPR2 SD-XHE-XL-LPR 2.20E-04
INSUFFICIENT FLOW TO RCS
INLET HEADERS DURING LPR
LPR01
INSUFFICIENT FLOW TO RCS INSUFFICIENT FLOW TO RCS
INLET HDR A (VIA CKV 14A) INLET HDR B (VIA CKV 14B)
DURING LPR
LPR002 LPR003
INSUFFICIENT FLOW FROM CCF OF RCS INLET CHECK INSUFFICIENT FLOW FROM COMMON CAUSE FAILURE OF
DHR TRAINS TO RCS HEADER VALVES DH-14A&DH-14B TO DHR TRAINS TO RCS HEADER CFS TANK DISCHARGE CKV
A REACTOR VESSEL B CF-1A & DH-14B
LPR0004 LPI-CKV-CF-DH14AB 2.49E-07 LPR0015 CFS-CKV-CF-1A14B 2.49E-07
RCS DISCHARGE CHECK CCF OF RCS INLET CHECK
VALVE DH-14A FAILS VALVES DH-14A&DH-14B TO
REACTOR VESSEL
NO FLOW FROM DHR TRAIN A NO FLOW FROM DHR TRAIN B LPI-CKV-CC-DH14A 1.07E-05 NO FLOW FROM DHR TRAIN A NO FLOW FROM DHR TRAIN B LPI-CKV-CF-DH14AB 2.49E-07
TO RCS HEADER A DURING LPI TO RCS HEADER A DURING LPI TO RCS HEADER B DURING TO RCS HEADER B DURING RCS DISCHARGE CHECK
LPR LPR VALVE DH-14B FAILS
LPR00002 LPR00003 LPR00102 LPR00103
LPI-CKV-CC-DH14B 1.07E-05
NO FLOW FROM SUMP (HDR LPI TRAIN A INJECTION CHECK NO FLOW FROM SUMP (HDR CCF OF INJECTION CHECK NO FLOW FROM SUMP (HDR LPI TRAIN A INJECTION CHECK NO FLOW FROM SUMP (HDR LPI TRAIN B INJECTION
A) TO DHR/LPR TRAIN A VALVE DH-13A FAILS B) TO DHR/LPR TRAIN B VALVES INTO RCS HDR A (13A, A) TO DHR/LPR TRAIN A VALVE DH-17 FAILS B) TO DHR/LPR TRAIN B CHECK VALVE DH-13B FAILS
18)
LPR000004 LPI-CKV-CC-DH13A 1.07E-05 LPR000013 LPI-CKV-CF-HDRA 2.49E-07 LPR000004 Int LPI-CKV-CC-DH17 1.07E-05 LPR000013 Int LPI-CKV-CC-DH13B 1.07E-05
CCF OF INJECTION CHECK DHR TRAIN B INJECTION CCF OF INJECTION CHECK CCF OF INJECTION CHECK
VALVES INTO RCS HDR A (13A, CHECK VALVE DH-18 FAILS VALVES INTO RCS HDR B (17, VALVES INTO RCS HDR B (17,
18) 13B) 13B)
ANO 1 PWR D NO OR NO FLOW FROM SUMP (HDR CCF OF SUMP ISOLATION LPI-CKV-CF-HDRA 2.49E-07 ANO 1 PWR D NO OR NO FLOW FROM SUMP (HDR CCF OF SUMP ISOLATION LPI-CKV-CC-DH18 1.07E-05 LPI-CKV-CF-HDRB 2.49E-07 LPI-CKV-CF-HDRB 2.49E-07
INSUFFICIENT CCOLING FROM A) TO DHR/LPR TRAIN A MOVs 1406 AND 1405 CCF OF LPI INLET CHECK INSUFFICIENT COOLING FROM B) TO DHR/LPR TRAIN B MOVs 1406 AND 1405 CCF OF LPI INLET CHECK
DHR TRAIN A VALVES DH-13A & DH-13B TO DHR TRAIN B VALVES DH-13A & DH-13B TO
DHR-TRNA-COOL Ext LPR0000007 HPI-MOV-CF-CV14056 1.86E-05 REACTOR VESSEL DHR-TRNB-COOL Ext LPR0000107 HPI-MOV-CF-CV14056 1.86E-05 REACTOR VESSEL
480V MCC BUS B51 AC POWER SUMP ISOLATION MOV CV-1405 LPI-CKV-CF-DH13AB 2.49E-07 480V MCC BUS B61 AC POWER SUMP ISOLATION MOV CV-1406 LPI-CKV-CF-DH13AB 2.49E-07
FAILURES FAILS TO OPEN FAILURES FAILS TO OPEN
ACP-MCCB51 Ext HPI SUCTION CHECK VALVE HPI-MOV-CC-CV1405 9.63E-04 ACP-MCCB61 Ext HPI-MOV-CC-CV1406 9.63E-04
BW-3 FAILS (SUCTION HEADER LPI DISCHARGE MOV CV-1401 LPI DISCHARGE MOV CV-1400
A) FAILS TO CLOSE FAILS TO OPEN FAILS TO OPEN
LPR00000022 HPI-CKV-OC-BW3 1.31E-07 LPR00001022 LPR00001025
LPI-MOV-CC-CV1401 9.63E-04 LPI-MOV-CC-CV1400 9.63E-04
SUMP ISOLATION MOV CV-1414 SUMP ISOLATION MOV 1415
FAILS TO REMAIN OPEN FAILS TO REMAIN OPEN
COMMON CAUSE FAILURE OF COMMON CAUSE FAILURE OF CCF OF HPI (MAKEUP) PUMPS
BWST ISOL MOVs 1407 AND HPI-MOV-OC-CV1414 8.13E-07 BWST ISOL MOVs 1407 AND SUCTION CHECK VALVES HPI-MOV-OC-CV1415 8.13E-07
1408 1408 (BW-2/3)
LPI-MOV-CF-BWST 7.78E-06 LPI-MOV-CF-BWST 7.78E-06 HPI-CKV-CF-BW23 2.49E-07
BWST ISOLATION VALVE CV- BWST ISOLATION VALVE CV- HPI SUCTION CHECK VALVE
1407 FAILS TO CLOSE 1408 FAILS TO CLOSE BW-2 FAILS (HEADER B)
LPI-MOV-OO-CV1407 9.63E-04 LPI-MOV-OO-CV1408 9.63E-04 HPI-CKV-CC-BW2 1.07E-05
A2-19
Figure A-9: BWST Refill Fault Tree
BWST REFILL
REFILL
OPERATOR FAILS TO REFILL HARDWARE FAILURE TO
BWST during Shutdown REFILL BWST (undeveloped)
SD-XHE-XM-BWST 2.00E-05 HPI-VCF-FC-BWST 1.00E-03
Figure A10: Diesel Generator Recovery Fault Tree
OPERATOR FAILS TO
RECOVER EMERGENCY
DIESEL IN 72 HOURS
DGR-72H
OPERATOR FAILS TO
RECOVER EMERGENCY
DIESEL IN 72 HOURS
EPS-XHE-XL-NR72H 7.14E-02
A2-20
Figure A-11: SDC/DHR Late Recovery Fault Tree
LATE RECOVERY OF SDC/DHR
COOLIING
LTREC
Late Recovery of SDC/DHR (3
Days)
LTREC-DHR-3D 1.90E-01
Note the value of the late recovery basic event varies with the time available
A2-21
Appendix B: HRA Analysis
A2-13
Human Error Probabilities
A high level discussion of the Human Reliability Analysis (HRA) is presented above in Section 7
on Model Development. Also included above is a summary of the HRA results. The following
discusses the Human Failure Events (HFE), the derivation of the in individual Human Error
Probabilities (HEP). This HRA analysis was done consistent with the guidance of
NUREG/CR-6883, The SPAR-H Human Reliability Analysis Method, dated August 2005.
The Human Error Probabilities (HEPs) for this analysis were calculated using the Low Power
Shutdown SPAR-H worksheets from NUREG/CR-6883. Consideration was given to the
available time to perform the action, the stress levels of the crew during the event, complexity of
the action, crew experience and applicable and relevant training, quality and thoroughness of
procedures, ergonomics, fitness of duty issues, and the available work processes.
A2-14
B1 Operator Fails to Diagnose Loss of SDC before Boiling
HRA Worksheets for LPSD
SPAR HUMAN ERROR WORKSHEET
Plant: ANO1 Initiating Event: Basic Event: SD-XHE-XD-LOSDC
Basic Event Description: Operator Fails to Diagnose Loss of SDC before boiling
Part I. DIAGNOSIS WORKSHEET
PSFs PSF Levels Multiplier for Selected Please note specific reasons for
Diagnosis PSF PSF level selection in this
column.
Available Time Inadequate time P(failure) = 1.0 5 minutes required, 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> available
Barely adequate time (2/3 Nominal) 10
Nominal time 1
Extra time (between 1 and 2 x nominal and > than 30 min) 0.1
Expansive time (> 2 x nominal and > 30 min) 0.01 X
Insufficient information 1
Stress Extreme 5
High 2 X
Nominal 1
Insufficient information 1
Complexity Highly 5
Moderately Complex 2
Nominal 1
0.5
Obvious diagnosis 0.1 X Pump stop with loss of power is
Insufficient information 1 obvious
Experience/ Low 10
Training Nominal 1 X
High 0.5
Insufficient information 1
Procedures Not available 50
Incomplete 20
Available, but poor 5
Nominal 1 X
Diagnostic/symptom oriented 0.5
Insufficient information 1
Ergonomics/HMMissing/Misleading 50
Poor 10
Nominal 1 X
Good 0.5
Insufficient information 1
Fitness for Unfit P(failure) = 1.0
Duty Degraded Fitness 5
Nominal 1 X
Insufficient information 1
Work Poor 2
Processes Nominal 1 X
Good 0.8
Insufficient information 1
NHEP = 2.00E-05
Negative PSFs adjustment ( >3 negative PSFs) NA
Final Diagnosis
2.00E-05
A2-15
B2 Operator Fails to Recover Loss of SDC/DHR before Boiling
HRA Worksheets for LPSD
SPAR HUMAN ERROR WORKSHEET
Plant: ANO1 Initiating Event: Basic Event: SD-XHE-XL-LOSDC
Basic Event Description: Operator Fails to Recover Loss of SDC before boiling
Part II. ACTION WORKSHEET
PSFs PSF Levels Multiplier for Selected Please note specific reasons
Action PSF for PSF level selection in
this column.
Available Time Inadequate time P(failure) = 1.0 30 minutes required, 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />
Time Available is the time required 10 available. SDC/DHR pumps are
Nominal time 1 located in the containment one
Time available is 5x the time required 0.1 X boiling occurs into containment
Time available is 50x the time required 0.01 operation of pumps will be effected
Insufficient information 1
Stress Extreme 5
High 2 X
Nominal 1
Insufficient information 1
Complexity Highly 5
Moderately 2 X
Nominal 1
Insufficient information 1
Experience/Training Low 3
Nominal 1 X
High 0.5
Insufficient information 1
Procedures Not available 50 .
Incomplete 20
Available but poor 5
Nominal 1 X
Insufficient information 1
Ergonomics/HMI Missing/Misleading 50
Poor 10
Nominal 1 X
Good 0.5
Insufficient information 1
Fitness for Duty Unfit P(failure) = 1.0
Degraded Fitness 5
Nominal 1 X
Insufficient information 1
Work Processes Poor 5
Nominal 1 X
Good 0.5
Insufficient information 1
Final Action HEP 4.00E-04
A2-16
B3 Operator Fails to Inject (AC power available) before Level Reaches TAF
HRA Worksheets for LPSD
SPAR HUMAN ERROR WORKSHEET
Plant: NMP1 Initiating Event: Basic Event: SD-XHE-XL-MINJ
Basic Event Description: Operator Fails to Inject after Level Reaches Scram Setpoint and before it Reaches TAF
Part II. ACTION WORKSHEET
PSFs PSF Levels Multiplier for Selected Please note specific reasons for
Action PSF PSF level selection in this
column.
Available Time Inadequate time P(failure) = 1.0
Time Available is the time required 10
Nominal time 1
Time available is 5x the time required 0.1
Time available is 50x the time required 0.01 X
Insufficient information 1
Stress Extreme 5
High 2 X
Nominal 1
Insufficient information 1
Complexity Highly 5 This assumes that condensate
Moderately 2 continues to run on loss of DC. If
Nominal 1 X racking in core spray is required this
Insufficient information 1 would be moderate.
Experience/Training Low 3
Nominal 1 X
High 0.5
Insufficient information 1
Procedures Not available 50 .
Incomplete 20
Available but poor 5
Nominal 1 X
Insufficient information 1
Ergonomics/HMI Missing/Misleading 50
Poor 10
Nominal 1 X
Good 0.5
Insufficient information 1
Fitness for Duty Unfit P(failure) = 1.0
Degraded Fitness 5
Nominal 1 X
Insufficient information 1
Work Processes Poor 5
Nominal 1 X
Good 0.5
Insufficient information 1
NHEP = 2.00E-05
Negative PSFs adjustment (>3 negative PSFs) NA
Final Action HEP 2.00E-05
A2-17
B4a Operator Fails to Diagnose Need for Low Pressure Recirc
HRA Worksheets for LPSD
SPAR HUMAN ERROR WORKSHEET
Plant: ANO1 Initiating Event: Basic Event: SD-XHE-XL-LPR
Basic Event Description: Operator Fails to Initiate Low Pressure Recirc
Part I. DIAGNOSIS WORKSHEET
PSFs PSF Levels Multiplier for Selected Please note specific reasons for
Diagnosis PSF PSF level selection in this
column.
Available Time Inadequate time P(failure) = 1.0 Feed has been started therefore there
Barely adequate time (2/3 Nominal) 10 is at least 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to restart SDC
Nominal time 1
Extra time (between 1 and 2 x nominal and > than 30 min) 0.1
Expansive time (> 2 x nominal and > 30 min) 0.01 X
Insufficient information 1
Stress Extreme 5
High 2 X
Nominal 1
Insufficient information 1
Complexity Highly 5
Moderately Complex 2
Nominal 1 X
0.5
Obvious diagnosis 0.1
Insufficient information 1 Scram setpoint is an obvious cue
Experience/ Low 10
Training Nominal 1 X
High 0.5
Insufficient information 1
Procedures Not available 50
Incomplete 20
Available, but poor 5
Nominal 1 X
Diagnostic/symptom oriented 0.5
Insufficient information 1
Ergonomics/HMMissing/Misleading 50
Poor 10
Nominal 1 X
Good 0.5
Insufficient information 1
Fitness for Unfit P(failure) = 1.0
Duty Degraded Fitness 5
Nominal 1 X
Insufficient information 1
Work Poor 2
Processes Nominal 1 X
Good 0.8
Insufficient information 1
NHEP = 2.00E-4
Negative PSFs adjustment ( >3 negative PSFs) NA
Final Diagnosis HEP = 2.00E-4
A2-18
B4b Operator Fails Action for Low Pressure Recirc
HRA Worksheets for LPSD
SPAR HUMAN ERROR WORKSHEET
Plant: ANO1 Initiating Event: Basic Event: SD-XHE-XL-LPR
Basic Event Description: Operator Fails to Initiate Low Pressure Recirc
Part II. ACTION WORKSHEET
PSFs PSF Levels Multiplier for Selected Please note specific reasons for
Action PSF PSF level selection in this
column.
Available Time Inadequate time P(failure) = 1.0
Time Available is the time required 10
Nominal time 1
Time available is 5x the time required 0.1
Time available is 50x the time required 0.01 X
Insufficient information 1
Stress Extreme 5
High 2 X
Nominal 1
Insufficient information 1
Complexity Highly 5
Moderately 2
Nominal 1 X
Insufficient information 1
Experience/Training Low 3
Nominal 1 X
High 0.5
Insufficient information 1
Procedures Not available 50 .
Incomplete 20
Available but poor 5
Nominal 1 X
Insufficient information 1
Ergonomics/HMI Missing/Misleading 50
Poor 10
Nominal 1 X
Good 0.5
Insufficient information 1
Fitness for Duty Unfit P(failure) = 1.0
Degraded Fitness 5
Nominal 1 X
Insufficient information 1
Work Processes Poor 5
Nominal 1 X
Good 0.5
Insufficient information 1
NHEP = 2.00E-05
Negative PSFs adjustment (>3 negative PSFs) NA
Final Action HEP 2.00E-05
A2-19
B5a Operator Fails Diagnoses for Aligning Alternate DC Power
HRA Worksheets for LPSD
SPAR HUMAN ERROR WORKSHEET
Plant: ANO1 Initiating Event: Basic Event: DCP-XHE-XM-DD11D21
Basic Event Description: Operator Action to Align 125VDC Panel D11 to Feed 125VDC Panel D21
Part I. DIAGNOSIS WORKSHEET
PSFs PSF Levels Multiplier for Selected Please note specific reasons for
Diagnosis PSF PSF level selection in this
column.
Available Time Inadequate time P(failure) = 1.0 30 minutes required, aasumed 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />
Barely adequate time (2/3 Nominal) 10 battery depletion time is time available.
Nominal time 1
Extra time (between 1 and 2 x nominal and > than 30 min) 0.1 X
Expansive time (> 2 x nominal and > 30 min) 0.01
Insufficient information 1
Stress Extreme 5
High 2 X
Nominal 1
Insufficient information 1
Complexity Highly 5
Moderately Complex 2
Nominal 1 x
0.5
Obvious diagnosis 0.1
Insufficient information 1
Experience/ Low 10
Training Nominal 1 X
High 0.5
Insufficient information 1
Procedures Not available 50
Incomplete 20
Available, but poor 5
Nominal 1 X
Diagnostic/symptom oriented 0.5
Insufficient information 1
Ergonomics/HMMissing/Misleading 50
Poor 10
Nominal 1 X
Good 0.5
Insufficient information 1
Fitness for Unfit P(failure) = 1.0
Duty Degraded Fitness 5
Nominal 1 X
Insufficient information 1
Work Poor 2
Processes Nominal 1 X
Good 0.8
Insufficient information 1
NHEP = 2.00E-03
Negative PSFs adjustment ( >3 negative PSFs) NA
Final Diagnosis
2.00E-03
A2-20
B5a Operator Fails Action for Aligning Alternate DC Power
HRA Worksheets for LPSD
SPAR HUMAN ERROR WORKSHEET
Plant: ANO1 Initiating Event: Basic Event: DCP-XHE-XM-DD11D21
Basic Event Description: Operator Action to Align 125VDC Panel D11 to Feed 125VDC Panel D21
Part II. ACTION WORKSHEET
PSFs PSF Levels Multiplier for Selected Please note specific reas
Action PSF for PSF level selection in
this column.
Available Time Inadequate time P(failure) = 1.0 30 minutes required, aasumed 4
Time Available is the time required 10 hour battery depletion time is t
Nominal time 1 X available.
Time available is 5x the time required 0.1
Time available is 50x the time required 0.01
Insufficient information 1
Stress Extreme 5
High 2 X
Nominal 1
Insufficient information 1
Complexity Highly 5
Moderately 2
Nominal 1 X
Insufficient information 1
Experience/Training Low 3
Nominal 1 X
High 0.5
Insufficient information 1
Procedures Not available 50 .
Incomplete 20
Available but poor 5
Nominal 1 X
Insufficient information 1
Ergonomics/HMI Missing/Misleading 50
Poor 10
Nominal 1 X
Good 0.5
Insufficient information 1
Fitness for Duty Unfit P(failure) = 1.0
Degraded Fitness 5
Nominal 1 X
Insufficient information 1
Work Processes Poor 5
Nominal 1 X
Good 0.5
Insufficient information 1
Final Action HEP 2.00E-03
A2-21
Appendix C: Cutsets
A2-22
Top 40 Cutsets:
Top 20 Cutsets from Sequence 4
Prob/ Total
- Cut Set Description
Freq. %
Total 1.54E-5 100 Displaying 20 of 6784 Cut Sets.
1 3.22E-6 20.9 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
9.63E-4 LPI-MOV-CC-CV1400 LPI DISCHARGE MOV CV-1400 FAILS TO OPEN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
2 3.18E-6 20.6 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
9.51E-4 SWS-AOV-CC-CV3841 FAILURE OF SWS MOV CV-3841 TO PMP P34A TO OPEN
3 3.17E-6 20.5 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
9.47E-4 LPI-MDP-FS-P34B LPI MDP P34B FAILS TO START
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
4 1.21E-6 7.84 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
3.62E-4 LPI-MDP-FR-P34B LPI MDP P34B FAILS TO RUN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
5 1.04E-6 6.75 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
2.48E-5 SWS-AOV-CF-CV38401 CCF OF SWS AOVs CV-3840/3841 TO PUMPS P34A/B TO OPEN
6 9.95E-7 6.44 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.37E-5 LPI-MDP-CF-STRT LPI PUMP COMMON CAUSE FAILURES TO START
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
7 7.70E-7 4.99 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
Common Cause failure of DHR Unit Coolers VUC-1A,1B, 1C & 1D to
1.83E-5 LPI-ACX-CF-VC1XR
RUN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
8 5.31E-7 3.44 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
1.26E-5 LPI-MDP-CF-RUN LPI PUMP COMMON CAUSE FAILURES TO RUN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
9 3.18E-7 2.06 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
9.50E-5 LPI-ACX-CF-VC1CDR Common Cause failure of DHR Unit Coolers VUC-1C and 1D to Run
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
10 1.22E-7 0.79 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
Common Cause failure of DHR Unit Coolers VUC-1A,1B, 1C & 1D to
2.89E-6 LPI-ACX-CF-VC1XS
Start
A2-23
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
11 1.17E-7 0.76 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.89E-3 EPS-DGN-FS-DG1 DIESEL GENERATOR 1 FAILS TO START
9.63E-4 LPI-MOV-CC-CV1400 LPI DISCHARGE MOV CV-1400 FAILS TO OPEN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
12 1.15E-7 0.75 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.89E-3 EPS-DGN-FS-DG1 DIESEL GENERATOR 1 FAILS TO START
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
9.51E-4 SWS-AOV-CC-CV3841 FAILURE OF SWS MOV CV-3841 TO PMP P34A TO OPEN
13 1.15E-7 0.75 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.89E-3 EPS-DGN-FS-DG1 DIESEL GENERATOR 1 FAILS TO START
9.47E-4 LPI-MDP-FS-P34B LPI MDP P34B FAILS TO START
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
14 1.00E-7 0.65 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
1.00E-7 SD-CUTOFF HFE Cutoff Value for Shutdown
1.00E+0 SD-XHE-XL-LOSDC-C Operator Fails to Recover Loss of SDC/DHR before Boiling (cutoff)
1.00E+0 SD-XHE-XL-LPR-C Operator Fails to Initiate Low Pressure Recirc (cutoff)
15 9.68E-8 0.63 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.39E-3 ACP-CRB-OO-1A308 4160V AC BREAKER 152-308 FAILS TO CLOSE
9.63E-4 LPI-MOV-CC-CV1400 LPI DISCHARGE MOV CV-1400 FAILS TO OPEN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
16 9.55E-8 0.62 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.39E-3 ACP-CRB-OO-1A308 4160V AC BREAKER 152-308 FAILS TO CLOSE
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
9.51E-4 SWS-AOV-CC-CV3841 FAILURE OF SWS MOV CV-3841 TO PMP P34A TO OPEN
17 9.52E-8 0.62 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.39E-3 ACP-CRB-OO-1A308 4160V AC BREAKER 152-308 FAILS TO CLOSE
9.47E-4 LPI-MDP-FS-P34B LPI MDP P34B FAILS TO START
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
18 6.69E-8 0.43 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
2.00E-5 LPI-ACX-CF-VC1CDS Common Cause failure of DHR Unit Coolers VUC-1C and 1D to Start
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
19 4.40E-8 0.28 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.89E-3 EPS-DGN-FS-DG1 DIESEL GENERATOR 1 FAILS TO START
3.62E-4 LPI-MDP-FR-P34B LPI MDP P34B FAILS TO RUN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
20 4.05E-8 0.26 M6-LOOP2 : 04
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
1.00E-3 EPS-XHE-XR-DG1 OP FAILS TO RESTORE DIESEL GENERATOR 1
9.63E-4 LPI-MOV-CC-CV1400 LPI DISCHARGE MOV CV-1400 FAILS TO OPEN
4.20E-2 LTREC-DHR-5D Late Recovery of SDC/DHR (5 Days)
A2-24
Top 20 Cutsets from Sequence 19
Prob/ Total
- Cut Set Description
Freq. %
Total 3.62E-4 100 Displaying 20 of 3955 Cut Sets.
1 2.53E-4 70 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
7.96E-2 EPS-DGN-FR-DG2 DIESEL GENERATOR 2 FAILS TO RUN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
2 4.33E-5 12 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
1.08E-3 EPS-DGN-CF-DG12R CCF OF DIESEL GENERATORS DG1&DG2 TO RUN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
3 9.20E-6 2.54 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
2.89E-3 EPS-DGN-FS-DG2 DIESEL GENERATOR 2 FAILS TO START
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
4 9.20E-6 2.54 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG2 DIESEL GENERATOR 2 FAILS TO RUN
2.89E-3 EPS-DGN-FS-DG1 DIESEL GENERATOR 1 FAILS TO START
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
5 7.61E-6 2.1 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.39E-3 ACP-CRB-OO-1A308 4160V AC BREAKER 152-308 FAILS TO CLOSE
7.96E-2 EPS-DGN-FR-DG2 DIESEL GENERATOR 2 FAILS TO RUN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
6 7.61E-6 2.1 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.39E-3 ACP-CRB-OO-1A408 4160V AC BREAKER 152-408 FAILS TO CLOSE
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
7 7.00E-6 1.94 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
Operator Action to Align 125VDC Panel D11 to Feed 125VDC Panel
2.20E-3 DCP-XHE-XM-DD11D21
D21
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
8 4.31E-6 1.19 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
9.93E-1 SWS-4C-RUNNING SWS MDP P4C IS RUNNING; 4B ALIGNED TO RED TRAIN
1.36E-3 SWS-MDP-FS-P4C SERVICE WATER MDP P4C FAILS TO START
9 3.23E-6 0.89 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
8.09E-5 ACP-CRB-CF-A3A4-12 CCF OF A3-TO-A4 XTIE BREAKERS TO OPEN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
10 3.18E-6 0.88 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
A2-25
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
1.00E-3 EPS-XHE-XR-DG2 OP FAILS TO RESTORE DIESEL GENERATOR 2
11 3.18E-6 0.88 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG2 DIESEL GENERATOR 2 FAILS TO RUN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
1.00E-3 EPS-XHE-XR-DG1 OP FAILS TO RESTORE DIESEL GENERATOR 1
12 3.07E-6 0.85 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG1 DIESEL GENERATOR 1 FAILS TO RUN
9.63E-4 EPS-MOV-CC-CV3807 SWS SUPPLY MOV CV-3807 TO DGN 2 COOLING FAILS TO OPEN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
13 3.07E-6 0.85 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
7.96E-2 EPS-DGN-FR-DG2 DIESEL GENERATOR 2 FAILS TO RUN
9.63E-4 EPS-MOV-CC-CV3806 SWS SUPPLY MOV CV-3806 TO DGN 1 COOLING FAILS TO OPEN
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
14 1.45E-6 0.4 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
3.61E-5 EPS-DGN-CF-DG12S CCF OF DIESEL GENERATORS DG1&DG2 TO START
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
15 9.47E-7 0.26 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.37E-5 EPS-MDP-CF-P16ABS CCF of EDG Fuel Oil Pump to Start
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
16 7.43E-7 0.21 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
1.86E-5 EPS-MOV-CF-SWS CCF OF SWS SUPPLY MOVs 3806 AND 3807
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
17 5.06E-7 0.14 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
1.26E-5 EPS-MDP-CF-P16ABR CCF of EDG Fuel Oil Pump to Run
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
18 3.34E-7 0.09 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.89E-3 EPS-DGN-FS-DG1 DIESEL GENERATOR 1 FAILS TO START
2.89E-3 EPS-DGN-FS-DG2 DIESEL GENERATOR 2 FAILS TO START
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
19 2.77E-7 0.08 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.39E-3 ACP-CRB-OO-1A308 4160V AC BREAKER 152-308 FAILS TO CLOSE
2.89E-3 EPS-DGN-FS-DG2 DIESEL GENERATOR 2 FAILS TO START
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
20 2.77E-7 0.08 M6-LOOP2 : 19
1.00E+0 IE-M6-LOOP LOOP Event Occurs during Mode 6
2.39E-3 ACP-CRB-OO-1A408 4160V AC BREAKER 152-408 FAILS TO CLOSE
2.89E-3 EPS-DGN-FS-DG1 DIESEL GENERATOR 1 FAILS TO START
4.00E-2 EPS-XHE-XL-NR96H OPERATOR FAILS TO RECOVER EMERGENCY DIESEL IN 4 Days
A2-26
Unit 2
At-Power Detailed Risk Evaluation
Probabilistic Risk Assessment (PRA) Analyst: David Loveless, Senior Risk Analyst
Independent Reviewer Jeff Mitman, Senior Reliability and Risk
Analyst, NRR/DRA/APOB
A3-1 Attachment 3
A. Summary of Issue:
At the time of the event, ANO Unit 2 was operating at 100 percent power.
At approximately 0750 hours0.00868 days <br />0.208 hours <br />0.00124 weeks <br />2.85375e-4 months <br /> on March 31, 2013, the temporary hoist assembly used to lift
and transport the Unit 1 stator from the turbine building failed resulting in the ~524 ton stator
dropping onto the Unit 1 turbine deck (Elev. 386) and then rolling and falling onto the
transport vehicle parked in the train bay (Elev. 354).
The impact of the stator on the Unit 1 turbine deck resulted in substantial damage to turbine
building structural members and to the turbine deck floor in the vicinity of the impact. The
4160 VAC switchgear A1 and A2 located immediately below where the stator impacted the
turbine deck were damaged, rendering offsite power sources from startup #1 and startup #2
transformers inoperable.
Falling components impacted the north wall of the train bay causing structural damage and
damage to the fire suppression system, causing substantial fire water spray into the train
bay area. The stator came to rest against the south wall of the train bay on top of the
transport vehicle. Both the north and south non-structural concrete masonry unit walls of
the train bay suffered substantial damage.
The shock from the stator contacting the turbine building, and temporary lift assembly
components falling into the turbine building, caused relays in the Unit 2 switchgear area
located just adjacent to the train bay to actuate resulting in the trip of 2P-32B reactor coolant
pump. This resulted in a trip to the Unit 2 reactor. The Unit 2 post-trip response was normal
except it was complicated by Feedwater Loop A man feedwater regulating valve 2CV- 0748
position indication discrepancy. This caused the operators to trip the main feedwater pumps
and manually initiated Emergency Feedwater.
The stator drop caused a rupture of an eight-inch fire main in the turbine building train bay.
Water from the fire suppression system migrated to several areas of the turbine building on
Unit 2. Offsite power to Unit 2 from startup transformer 3 was lost after water from the
ruptured fire main caused an electrical fault inside the Unit 2 non-safety-related switchgear
in the turbine building. The loss of power from startup transformer 3 resulted in a loss of
train B vital electrical bus (safety-related,) a trip of the running reactor coolant pumps and
charging pump on Unit 2, and a trip of the running instrument air compressors maintaining
instrument air header pressure for both units. Unit 2 emergency diesel generator 2 started
and energized the train B vital electrical bus, while the train A vital and non-vital electrical
buses were re-energized from startup transformer 2. Operators took appropriate actions to
stabilize Unit 2, restore the instrument air system and subsequently cooled Unit 2 to cold
shutdown conditions on natural circulation.
B. Statement of the Performance Deficiency:
The licensee failed to accomplish actions specified in plant procedures. Procedure
EN MA 119, Material Handling Program is a quality-related procedure that controls the
licensees activities for handling and moving loads and rigging equipment at all Entergy
sites. The procedure requires the licensee to review and approve the lifting rig design and
verify that a load test is conducted. The licensee approved an inadequate design and did
not conduct a load test.
A3-2
C. Significance Determination Basis:
1. Reactor Inspection for IE, MS or BI Cornerstones
(a) Screening Logic
Minor Question: In accordance with NRC Inspection Manual Chapter 0612,
Appendix B, Issue Screening, the finding was determined to be more than
minor because it was associated with the procedural control attribute of the
initiating event cornerstone, and adversely affected the cornerstones objective to
limit the likelihood of events that upset plant stability and challenge critical safety
functions during shutdown as well as power operations. The stator drop affected
Unit 2 by causing a complicated reactor trip.
Initial Characterization: Using Manual Chapter 0609, Attachment 4, Initial
Characterization of Findings, the inspectors determined that the finding could be
evaluated using the significance determination process. In accordance with
Table 3, SDP Appendix Router, the inspectors determined that the subject
finding should be processed through Appendix A, The Significance
Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events
Screening Questions, dated June 19, 2012.
Issue Screening: Using Appendix A, Exhibit 1, the inspectors determined that
the finding did not affect loss of coolant accident initiators. The inspectors then
determined that the finding did cause a reactor trip and the loss of mitigation
equipment relied upon to transition the plant from the onset of the trip to a stable
shutdown condition. This mitigation equipment, lost or degraded, included one
source of offsite power, main feedwater, and the alternate ac diesel generator.
Therefore, a detailed risk evaluation was required.
Results: The Region IV senior reactor analyst performed a detailed risk
evaluation in accordance with Appendix A, Section 6.0, Detailed Risk
Evaluation. The detailed risk evaluation result is a preliminary finding of
substantial safety significance (Yellow). The calculated change in core damage
frequency of 2.8 x 10-5 was dominated by the internal event initiated by the stator
drop on March 31, 2013. The analyst determined that the external event risk was
negligible and that the finding would not involve a significant increase in the risk
of a large, early release of radiation.
(b) Detailed Risk Evaluation:
(1) The Phase 3 model revision and other PRA Tools used
The analyst utilized the Standardized Plant Analysis Risk Model for
Arkansas Nuclear One, Unit 2 (SPAR), Revision 8.21 and hand
calculation methods to quantify the risk of the subject performance
deficiency. The model was modified by the analyst and Idaho National
Laboratories to include additional breakers and switching options, and to
provide credit for recovery of emergency diesel generators during
transient sequences. Additionally, the analyst performed additional runs
of the SPAR model to account for consequential loss of offsite power
risks that were not modeled directly under the special initiator.
A3-3
(2) Influential assumptions
1. The subject performance deficiency directly resulted in the Unit 2
event on March 31, 2013. This event would not have occurred had
the performance deficiency not existed. Therefore, the performance
deficiency caused an increase in the nominal initiating event
frequency of 1 over the assessment period.
2. Given Assumption 1, the exposure time was set to the 1-year
assessment period. The actual exposure time that the performance
deficiency existed is not critical.
3. The best available initiating event to model the subject performance
deficiency is the loss of main feedwater initiator. The actual event
was initiated by a general transient. However, a failure of the
indication for Regulating Valve 2CV-748 prevented the main
feedwater system from initiating a reactor trip override. As a result,
operators tripped the operating main feedwater pump and initiated the
emergency feedwater actuation system.
4. The analyst noted that the SPAR model does not model offsite power
to a level sufficient to show failures within the offsite circuits.
Therefore, the failure of Bus 2A2 is an appropriate surrogate for the
Lockout of Startup Transformer 3. This surrogate was considered
appropriate because Bus 2A2 was de-energized for approximately
44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> following the event.
5. The alternate ac diesel generator was unavailable to respond at any
point throughout its mission time because the stator drop caused
significant damage to the control and power cabling associated with
this generator.
6. The analyst noted that Version 8.21 of the SPAR model had not yet
been updated to evaluate the risk of a postulated consequential loss
of offsite power given a reactor trip. Based on NUREG/CR-6890,
Reevaluation of Station Blackout Risk at Nuclear Power Plants, the
conditional probability of a loss of offsite power given a reactor trip at
a large nuclear power plant during times of higher grid loading is
3.91 x 10-3/ trip. Multiple runs of the SPAR model can be made to
quantify the change in risk for these postulated events.
A3-4
(4) Calculation discussion
A detailed risk evaluation performed consistent with NRC Inspection
Manual Chapter (IMC) 0609 Appendix A, Section 6.0, Detailed Risk
Evaluation. To conduct a risk assessment and determine the change in
core damage frequency (CDF) an analyst must solve the following
equation:
CDF = [(IEFcase * CCDPcase) - (IEFbase * CCDPbase)] * EXP
Where:
- IEFcase Initiating Event Frequency of the case being
evaluated
- CCDPcase Conditional Core Damage Probability of the case
- IEFbase Initiating Event Frequency of the baseline
- CCDPbase Conditional Core Damage Probability of the
baseline
- EXP The Exposure Period including repair time
Conditional Core Damage Probability of the Event
The analyst used several surrogate basic events to model the event that
occurred on March 31, 2013. First, the analyst modeled the event as a
loss of main feedwater. The actual event was initiated by a transient.
However, a failure of the indication for Regulating Valve 2CV-748
prevented the main feedwater system from initiating a reactor trip
override. As a result, operators tripped the operating main feedwater
pump and initiated the emergency feedwater actuation system. The
analyst determined that a best estimate analysis would result from using
the Loss of Main Feedwater initiator to model the risk of this event.
The analyst noted that the SPAR model does not model offsite power to a
level sufficient to show failures within the offsite circuits. Therefore, the
analyst used the failure of Bus 2A2 as a surrogate for the Lockout of
Startup Transformer 3. This surrogate was considered appropriate
because Bus 2A2 was de-energized for approximately 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> following
the event.
As a final surrogate, the analyst modeled the gross failure of cabling
associated with the AAC as an operator failure to start the machine. This
surrogate provided the correct logic for the failure while indicating that the
machine could not be recovered within the stated mission time.
The change set developed for the quantification of risk is documented in
Table 1. The total change in core damage frequency calculated was
2.8 x 10-5. This included additional runs performed to account for
consequential loss of offsite power sequences not directly modeled in the
current version of the SPAR.
A3-5
Table 1
SPAR Change Set
Basic Event Event Description Original Modified
Value Value
ACP-BAC-LP-2A2 Division B AC Power 4160V Bus 2A2 Fails 3.34E-05 True
ACP-CRB-OO-152113 Failure of CRB 152-113 to close 2.39E-03 True
EPS-XHE-XM-SBO Operator Fails to Start SBO Diesel 2.00E-02 True
Generator
IE-******** All Initiating Events various False
IE-LOMFW Loss of Main Feedwater 6.89E-02 1.0
The above described SPAR model was evaluated using the SAPHIRE
code Version 8.0.9.0. The truncation limit was set at 1E-12. The result of
the model run was a conditional core damage probability of 2.74 x 10-5.
The analyst noted that Version 8.21 of the SPAR model had not yet been
updated to evaluate the risk of postulated consequential loss of offsite
power given a reactor trip. Based on NUREG/CR-6890, Reevaluation of
Station Blackout Risk at Nuclear Power Plants, the conditional probability
of a loss of offsite power given a reactor trip at a large nuclear power
plant during times of higher grid loading is 3.91 x 10-3/ trip.
Using the same basic event modifications and truncation limit, the analyst
set the loss of offsite power frequency to 3.91 x 10-3 and re-quantified the
model. The result of the model run was a conditional core damage
probability of 7.46 x 10-7. Being mutually exclusive core damage
sequences, the conditional core damage probabilities from the loss of
offsite power and loss of main feedwater sequences can be summed.
The analyst added the sequences to determine the total conditional core
damage probability for the event of 2.8 x 10-5.
Exposure Period
This SDP evaluation is an initiating event that occurred as a result of a
performance deficiency. The calculation is a conditional core damage
probability estimate and exposure time does not apply.
To show that the use of a conditional core damage probability estimate
was appropriate, the analyst assumed that the exposure period started at
March 31, 2013, when the stator was first lifted and ended on April 22,
2013, when the last of the major components affected were returned to
service. This represented approximately 22 days of exposure and repair
time. This exposure time corresponds to the time period that the
condition being assessed was reasonably known to have existed plus the
repair time (per the usage rules of IMC 0308, Attachment 3, Appendix A).
SPAR model basic event IE-LOMFW, representing a Loss of Main
Feedwater initiator would then be set to a frequency corresponding to one
event during the 22 days. The basis for the initiating event frequency
change is that analyst noted, given the conditions of the temporary lift
crane, the load would have always fallen at the time the load was rotated
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to align with the truck bay. Therefore, the frequency of the loss of main
feedwater, given a stator drop, was assumed to be 1.0 over the 22 day
exposure time.
NOTE: This method of calculation is essentially equivalent to performing
a conditional core damage probability assessment for a loss of main
feedwater event and then subtracting the baseline core damage
probability. Given that the core damage probability is approximately the
integral of core damage frequency over time, at the point in time on
March 31, 2013, where the initiating event occurred, this integral is equal
to the conditional core damage probability multiplied by the integral of the
Dirac delta function. This integral is the numerical equivalent to the
conditional core damage probability.
Initiating Event Frequency
As discussed under Exposure Period above, the analyst determined that
the best method to estimate the change in core damage frequency for the
subject performance deficiency was by quantifying the conditional core
damage probability for the event.
To continue the rough calculation of change in conditional core damage
frequency the analyst increased the number of loss of main feedwater
initiators by one over the exposure time (22-days). Therefore, the
initiating event frequency was set as 4.55 x 10-2 /day.
Baseline Risk
As discussed under Exposure Period above, the analyst determined that
the best method to estimate the change in core damage frequency for the
subject performance deficiency was by quantifying the conditional core
damage probability for the event.
However, for illustrative purposes, the analyst quantified the baseline loss
of main feedwater conditional core damage probability. This value was
5.86 x 10-7. The analyst noted that the SPAR model provides a baseline
initiating event frequency for a loss of main feedwater at 6.89 x 10-2/year.
Change in core damage frequency quantified
Given these calculations and assumptions, the analyst calculated the
change in core damage frequency as follows:
CDF = [(4.55 x 10-2/day * 2.8 x 10-5)
- (6.89 x 10-2/year ÷ 365 days/year * 5.86 x 10-7)] * 22 days
= [1.27 x 10-6 /day - 1.11 x10-10 /day] * 22 days
= 2.79 x 10-5
(5) Analysis of Dominant Cut-sets / Sequences
The dominant accident sequence cutsets involved a loss of main
feedwater, loss of auxiliary feedwater, loss of emergency feedwater, and
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the failure of once-through cooling. The evaluation of consequential loss
of offsite power provided a dominant accident sequence involving a
transient with consequential loss of offsite power, the loss of all feedwater
to the steam generators and failure of once-through cooling.
Table 2
Core Damage Sequences
Sequence Description Point % of Cut Set
Estimate Total Count
MFW-14 IEMFW-FW-OTC 2.69E-5 95.6 6,036
LOOP-19 IELOOP-EFW-OTC 3.79E-7 1.3 1,733
LOOP-20-09-10 IELOOP-SBO(EPS)-RSUB-OPR08H- 2.74E-7 1.0 527
DGR08H-EFWMAN-SGDEPLT
MFW-15-10 IEMFW-RPS-FWATWS 1.25E-7 0.4 157
MFW-13 IEMFW-FW-SSRC-HPR 8.98E-8 0.3 1,679
LOOP-20-30 IELOOP-SBO-EFW-OPR08H-DGR08H 8.00E-8 0.3 959
MFW-02-09-04 IEMFW-LOSC-RCPT-HPI 6.14E-8 0.2 814
MFW-15-11 IEMFW-RPS-RCSPRESSURE 3.99E-8 0.1 18
MFW-15-09 IEMFW-RPS-BORATION 3.79E-8 0.1 16
MFW-12 IEMFW-FW-SSCR-CSR 2.63E-8 0.1 560
Others All Additional Sequences Combined 1.33E-7 0.5 3,886
Total CCDP All Sequences 2.81e-5 100.0 16,385
Abbreviations
BORATION Failure of Emergency Boration
CBO Controlled Bleedoff Isolated
CSR Containment Spray Recirculation
DGR08H Nonrecovery of Diesel Generator in 8 Hours
EFWMAN Manual Control of Emergency Feedwater
EPS Emergency Power System
FW Feedwater System (MFW, EFW, and auxiliary feedwater)
FWATWS Feedwater System under ATWS Conditions
HPI High Pressure Injection
HPR High Pressure Recirculation
IELOOP Initiating Event: Loss of Offsite Power
IEMFW Initiating Event: Loss of Main Feedwater
LOSC Loss of RCP Seal Cooling
OPR08H Nonrecovery of Offsite Power in 8 Hours
OTC Once-Through Cooling
RCPT Reactor Coolant Pumps Tripped
RCSPRESS RCS Pressure Limited
RSUB Reactor Coolant Subcooling Maintained
SBO Station Blackout
SGDEPLT Late Depressurization of Steam Generators
SSCR Secondary Cooling Recovered
The dominant accident sequence cutsets involved a loss of main
feedwater, loss of auxiliary feedwater, loss of emergency feedwater, and
the failure of once-through cooling. The top ten sequence cutsets are
provided in Table 2 of the detailed risk evaluation. The top 100 cutsets
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for each of two model runs are provided as attachments to this
evaluation.
The results are dominated by one core damage sequence. The largest
contributor is Sequence 14 from the loss of main feedwater tree. The
sequence comprises a failure of all feedwater to the steam generators,
including main feedwater, auxiliary feedwater, and emergency feedwater,
with a loss of once-through cooling. The remainder of the sequences are
dominated by failure of the emergency diesel generators without recovery
of ac power.
(6) Sensitivity Analysis
The SRA performed a variety of uncertainty and sensitivity analyses on
the internal events model as shown below. The results confirm the
recommended Yellow finding.
Sensitivity Analysis 1 - Transient without Loss of Main Feedwater.
The SRA ran the model using a transient as the initiator. The change in
core damage frequency was 1.10 x 10-5 (Yellow).
Sensitivity Analysis 2 - No consequential loss of offsite power.
The SRA ran the model without including the additional runs to calculate
the change in risk from a postulated consequential loss of offsite power.
The change in core damage frequency was 2.74 x 10-5 (Yellow).
Sensitivity Analysis 3 - Potential Recovery of Bus 2A2
The SRA ran the model with the failure of Bus 2A2 probability set to
6.79 x 10-1. This value, calculated using SPAR-H methodology,
represented the probability that operators would fail to recover the bus
prior to core damage, given the adverse and unknown conditions of site
electrical supply. The change in core damage frequency was 1.97 x 10-5
(Yellow).
(7) Contributions from External Events (Fire, Flooding, and Seismic)
Manual Chapter 0609, Appendix A, Section 6.0 requires, when the
internal events detailed risk evaluation results are greater than or equal to
1.0E-7, the finding should be evaluated for external event risk
contribution. The analyst noted that this detailed risk assessment
evaluates an actual event in which no external events occurred.
Additionally, the period of time that the events impacted plant equipment
was small enough that the probability of an external initiator occurring
during this time would be negligible. Therefore, the analyst assumed that
the risk from external events, given the subject performance deficiency
was essentially zero.
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(8) Potential Risk Contribution from LERF
In accordance with the guidance in NRC Inspection Manual
Chapter 0609, Appendix H, Containment Integrity Significance
Determination Process, this finding would not involve a significant
increase in risk of a large, early release of radiation because Arkansas
Nuclear One, Unit 2 has a large, dry containment and the dominant
sequences contributing to the change in the core damage frequency did
not involve either a steam generator tube rupture or an inter-system loss
of coolant accident.
(9) Total Estimated Change in Core Damage Frequency
The total change in risk caused by this performance deficiency is the sum
of the internal and external events change in core damage frequencies.
This value was 2.8 x 10-5 (YELLOW).
(10) Licensees Risk Evaluation
The licensee provided an assessment of the risk related to the March 31,
2013 event. With similar modeling assumptions, the licensees at-power
probabilistic safety assessment provided a conditional core damage
probability of 2.94 x 10-5/year. This corroborated the NRC analysts
evaluation. However, the licensee calculated per component repair times
for the major components affected by the performance deficiency and
stated that the change in core damage frequency, after removing
qualitative modeling conservatisms was less than 1 x 10-6, resulting in a
Green finding.
Using the licensee's method, the exposure period defined by the licensee
affected the time following the plant transient. However, the licensee did
not adjust the initiating event likelihood to address the increased rate of
failure over this new exposure time.
(11) Summary of Results and Impact
The NRCs quantitative risk assessment was determined to represent a
risk estimate in the Yellow region. Region IV recommends a preliminary
finding of substantial safety significance (Yellow based on change in core
damage frequency).
(d) Peer Review:
Jeff Mitman, Senior Reliability and Risk Analyst, NRR/DRA/APOB
(e) References:
The analysts used the following generic references in preparing the risk
assessment:
- NUREG/CR-6890, Reevaluation of Station Blackout Risk at Nuclear Power
Plants
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- NUREG/CR-6883, The SPAR-H Human Analysis Method. August 2005
- NUREG-1842, Good Practices for Implementing Human Reliability Analysis.
April 2005
- NUREG/CR-6595 Revision 1, An Approach for Estimating the Frequencies
of Various Containment Failure Modes and Bypass Events. October 2004
- INL/EXT-10-18533 Revision 2, SPAR-H Step-by-Step Guidance. May 2011
- RASP Manual Volume 1 - Internal Events, Revision 2.0 date January 2013
- Risk Assessment of Operational Events, Volume 2 - External Events,
Revision 1.01, January 2008
- NUREG/CR-1278, Handbook of HRA with Emphasis on Nuclear Power Plant
Applications, August 1983
The analysts used the following plant specific references:
Version 8.21
- Arkansas Nuclear One, Unit 2, Final Safety Analysis Report Page 8.3-12
- EOP: 1202.007, Degraded Power
- AOPs:
o 1203.024, Loss of Instrument Air
o 1203.028, Loss of Decay Heat Removal
o 1203.050, Unit 1 Spent Fuel Pool Emergencies
- Calculation: 89-E-0017-01, Time to Boiling and Time to Core Uncovery after
Loss of Decay Heat Removal, Unit 1, Revision 7
- Procedure: 1103.018, Maintenance of RCS Water Level
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