ML102150468

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IR 05000461-10-003, on 04/01/10 - 06/30/10; Clinton Power Station, Unit 1; Flood Protection Measures, Maintenance Risk Assessments and Emergent Work Control, Operability Evaluations, Emergency Response Organization Augmentation Testing..
ML102150468
Person / Time
Site: Clinton Constellation icon.png
Issue date: 08/03/2010
From: Ring M
NRC/RGN-III/DRP/B1
To: Pacilio M
Exelon Generation Co, Exelon Nuclear
References
IR-10-003
Download: ML102150468 (75)


See also: IR 05000461/2010003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

August 3, 2010

Mr. Michael J. Pacilio

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: CLINTON POWER STATION NRC INTEGRATED INSPECTION REPORT

05000461/2010-003

Dear Mr. Pacilio:

On June 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Clinton Power Station. The enclosed report documents the inspection results, which were

discussed on July 8, 2010, with Mr. M. Kanavos and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, one self-revealed and four NRC-identified findings of

very low safety significance were identified. Four of these findings were determined to involve

violations of NRC requirements. Additionally, five licensee-identified violations, which were

determined to be of very low safety significance, were reviewed by the inspectors and are listed

in this report. Because of the very low safety significance and because they were entered into

your corrective action program, the NRC is treating the above violations as non-cited violations

(NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy.

If you contest the subject or severity of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001,

with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at Clinton Power Station. In addition, if you disagree with the cross-cutting aspect

assigned to any finding in this report, you should provide a response within 30 days of the date

of this inspection report, with the basis for your disagreement, to the Regional Administrator,

Region III, and the NRC Resident Inspector at Clinton Power Station.

M. Pacilio -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket No. 50-461

License No. NPF-62

Enclosure: Inspection Report 05000461/2010-003

w/Attachment: Supplemental Information

cc: Distribution via ListServe

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-461

License No: NPF-62

Report No: 05000461/2010-003

Licensee: Exelon Generation Company, LLC

Facility: Clinton Power Station, Unit 1

Location: Clinton, IL

Dates: April 1 through June 30, 2010

Inspectors: B. Kemker, Senior Resident Inspector

D. Lords, Resident Inspector

J. Cassidy, Senior Health Physicist

E. Coffman, Reactor Engineer

D. Meléndez-Colón, Resident Inspector, Dresden

M. Mitchell, Health Physicist

R. Russell, Emergency Preparedness Inspector

S. Mischke, Resident Inspector, Illinois Emergency

Management Agency

Approved by: M. Ring, Chief

Branch 1

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ......................................................................................................... 1

REPORT DETAILS .................................................................................................................... 5

Summary of Plant Status ........................................................................................................ 5

1. REACTOR SAFETY ..................................................................................................... 5

1R01 Adverse Weather Protection (71111.01).......................................................... 5

1R04 Equipment Alignment (71111.04) .................................................................... 6

1R05 Fire Protection (71111.05) ............................................................................... 7

1R06 Flooding Protection Measures (71111.06) ....................................................... 8

1R07 Heat Sink Performance (71111.07) ................................................................14

1R11 Licensed Operator Requalification Program (71111.11) .................................14

1R12 Maintenance Effectiveness (71111.12) ..........................................................15

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ......16

1R15 Operability Evaluations (71111.15).................................................................21

1R19 Post-Maintenance Testing (71111.19) ............................................................25

1R22 Surveillance Testing (71111.22) .....................................................................26

1EP2 Alert and Notification System Evaluation (71114.02) ......................................27

1EP3 Emergency Response Organization Augmentation Testing (71114.03) ..........27

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ..............30

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

(71114.05)......................................................................................................31

1EP6 Drill Evaluation (71114.06) .............................................................................31

2. RADIATION SAFETY ..................................................................................................32

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) ............32

4. OTHER ACTIVITIES ...................................................................................................38

4OA1 Performance Indicator Verification (71151) ....................................................38

4OA2 Identification and Resolution of Problems (71152) .........................................41

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) .............45

4OA5 Other Activities ...............................................................................................48

4OA6 Management Meetings ...................................................................................50

4OA7 Licensee-Identified Violations .........................................................................51

SUPPLEMENTAL INFORMATION............................................................................................. 1

KEY POINTS OF CONTACT .................................................................................................. 1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ........................................................ 1

LIST OF DOCUMENTS REVIEWED ...................................................................................... 3

LIST OF ACRONYMS USED.................................................................................................14

Enclosure

SUMMARY OF FINDINGS

IR 05000461/2010-003, 04/01/10 - 06/30/10; Clinton Power Station, Unit 1; Flood Protection

Measures, Maintenance Risk Assessments and Emergent Work Control, Operability

Evaluations, Emergency Response Organization Augmentation Testing, and Identification and

Resolution of Problems.

This report covers a three-month period of inspection by the resident inspectors and

announced baseline inspections by regional inspectors. Two Severity Level IV non-cited

violations (NCVs) and three Green findings, two of which had an associated NCV, were

identified. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity

level after NRC management review. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Severity Level IV. The inspectors identified a finding of very low safety significance

with an associated Severity Level IV non-cited violation of the NRCs reporting

requirements in 10 CFR 50.72(a)(1), Immediate Notification Requirements for Operating

Nuclear Power Reactors, and 10 CFR 50.73(a)(1), Licensee Event Report System.

The licensee failed make a required 8-hour non-emergency notification call to the

NRC Operations Center and failed to submit a required Licensee Event Report within

60 days after discovery on October 7, 2009, of a condition that resulted in the plant

being in an unanalyzed condition that significantly degraded plant safety and could

have prevented fulfillment of the safety function of the emergency core cooling system.

No immediate corrective actions were taken to address this finding; however, the

licensee entered this issue into its corrective action program for evaluation.

This finding was of more than minor significance because the NRC relies on licensees

to identify and report conditions or events meeting the criteria specified in the

Technical Specifications and the regulations in order to perform its regulatory function.

Because this issue affected the NRC's ability to perform its regulatory function, the

inspectors evaluated it using the traditional enforcement process and assessed the

significance of the underlying issue using the SDP. The underlying technical issue

(i.e., interconnecting floor drains between the Residual Heat Removal A Pump Room

and the Radwaste Pipe Tunnel) was determined to be a finding of very low safety

significance during a Phase 3 Significance Determination Process evaluation.

Consistent with the guidance in Supplement I, Paragraph D.4, of the NRC Enforcement

Policy, the violation associated with this finding was determined to be a Severity Level IV

Violation. This finding affected the cross-cutting area of human performance because

the licensee did not use conservative assumptions in decision making while evaluating

the reportability of the unanalyzed condition with respect to the reporting requirements in

10 CFR 50.72(a)(1)(ii) and 50.73(a)(1). (IMC 0310 H.1(b)) (Section 1R06.1.b.(1))

1 Enclosure

Green. The inspectors identified a finding of very low safety significance associated with

the licensees failure to evaluate the functionality of multiple excess flow check valves

that had not been tested in accordance with the American Society of Mechanical

Engineers / American National Standards Institute (ASME/ANSI) Code Inservice Testing

requirements to establish whether the nonconforming condition warranted starting the

Technical Specification (TS) action time for the suppression pool makeup (SPMU)

system. In response to the inspectors questions, the licensee subsequently performed

an operability evaluation. No violation of regulatory requirements was identified because

subsequent testing by the licensee determined that the valves were functional.

The finding would become a more significant safety concern, if left uncorrected, and

was, therefore, more than a minor concern. Specifically, the failure to correctly evaluate

a degraded/nonconforming condition potentially affecting the operability of structures,

systems, and components (SSCs) required to be operable by TS could reasonably result

in an unrecognized condition of a SSC failing to fulfill a safety-related function. Because

the SPMU system was primarily associated with long term decay heat removal following

certain design basis accidents, the inspectors concluded that this issue was associated

with the Mitigating Systems Cornerstone. The finding was of very low safety significance

because the issue: (1) was not a design or qualification deficiency; (2) did not represent

an actual loss of safety function of a system; (3) did not represent an actual loss of

safety function of a single train for greater than its TS allowed outage time; (4) did not

represent an actual loss of safety function of one or more non-TS trains of equipment

designated as risk significant; and (5) did not screen as potentially risk significant due to

a seismic, flooding, or severe weather initiating event. The inspectors concluded that

this finding affected the cross-cutting area of human performance because the licensee

did not have a formal process in place with adequate guidance and training to enable

licensed senior reactor operators to properly and promptly evaluate operability in this

instance. As a result, senior reactor operators took it for granted that utilizing the relief

allowed by TS Surveillance Requirement 3.0.3 and performing a risk evaluation obviated

the need to address operability of the instrumentation supported by the excess flow

check valves for the ASME/ANSI Code noncompliance. (IMC 0310 H.1(a))

(Section 1R15.b.(1))

Cornerstone: Barrier Integrity

Severity Level IV. The inspectors identified a finding of very low safety significance with

an associated NCV of 10 CFR 50.59, Changes, Tests and Experiments. The licensee

failed to perform an adequate 10 CFR 50.59 evaluation and obtain a license amendment

prior to implementing CPS 3711.01, CPS [Clinton Power Station] Operations with the

Potential to Drain the Reactor Vessel [OPDRV], Revision 0 on January 11, 2010.

The procedure established a definition of an OPDRV for use in determining the

applicability of several TS requirements while in Modes 4 and 5. The licensee failed to

recognize that implementing this new procedure, in effect, constituted a change to the

TS incorporated into its licensing basis, which would, therefore, require a license

amendment pursuant to 10 CFR 50.59(c)(1)(i) and 10 CFR 50.90. No immediate

corrective actions were taken to address this finding; however, the licensee entered this

issue into its corrective action program for evaluation.

The finding was of more than minor significance because there was a reasonable

likelihood that the change requiring a 10 CFR 50.59 evaluation would require

NRC review and approval prior to implementation. Because this issue affected the

2 Enclosure

NRC's ability to perform its regulatory function, the inspectors evaluated it using the

traditional enforcement process and assessed the significance of the underlying issue

using the SDP. Based on the results of a modified Phase 2 SDP evaluation, this finding

was determined to be of very low safety significance. Consistent with the guidance in

Supplement I, Paragraph D.5, of the NRC Enforcement Policy, the violation associated

with this finding was determined to be a Severity Level IV Violation. The inspectors

concluded that this finding affected the cross-cutting area of human performance.

Specifically, the licensee did not use conservative decision making to demonstrate that

the proposed action did not require prior NRC approval. The inspectors noted that the

licensee was aware of potential concerns regarding the new procedure prior to

completing the initial 10 CFR 50.59 evaluation and again prior to revising the evaluation

in response to concerns raised by the inspectors; however, the incorrect conclusion was

reached in both revisions of the evaluation that the new procedure was not a change to

the TS and that a license amendment was not necessary. (IMC 0310 H.1(b))

(Section 1R13.b.(1))

Green. A finding of very low safety significance with an associated NCV of 10 CFR 50,

Appendix B, Criteria V, Instructions, Procedures, and Drawings, was self-revealed on

January 29, 2010, when the dryer cavity gate seal depressurized during the performance

of the containment and reactor vessel isolation functional surveillance procedure.

When the seal lost pressure, approximately 46,500 gallons of water leaked from the

dryer cavity pool into the reactor cavity. In response to the event, the licensee ensured

all personnel were out of the reactor cavity, entered its radioactive spill off-normal

procedure, and re-established air pressure to the dryer cavity gate seal. Subsequent

investigation revealed that during the gate seal inflation procedure, the proper valve

operation sequence was not followed. As a corrective action, the licensee revised many

of its procedures and included a special brief to the refueling outage preparation for

Reactor Services personnel.

The finding was of more than minor significance because the licensees failure to

correctly install the upper containment dryer cavity gate could be reasonably viewed as a

precursor to a significant event and, if left uncorrected, would potentially lead to a more

significant safety concern (i.e., increased dose or personnel contamination). In addition,

the finding was similar to Example 4c in IMC 0612, Power Reactor Inspection Reports,

Appendix E, Examples of Minor Issues, in that, data recorded during installation of the

dryer cavity gate seal was incorrect and resulted in backup air bottle supply pressure left

outside the acceptable range. Because the dryer cavity gate seal is intended to contain

highly radioactive fluids within containment, which supports the radiological barrier

functions to protect plant workers and the public following serious transients or

accidents, the inspectors concluded that this issue was associated with the Barrier

Integrity Cornerstone. Although this event resulted in a loss of inventory from the dryer

cavity pool and partial flooding of the lower reactor cavity and drywell, it was determined

to be of very low safety significance because there was no loss of inventory from the

reactor vessel and it could not result in the loss of reactor coolant system level

instrumentation. The inspectors concluded that this finding affected the cross-cutting

area of human performance. The licensee's Root Cause Report described the root

cause as the maintenance craftsman performed steps out of sequence and failed to

comply with the procedure. Therefore, as concluded by the Root Cause, in this

instance, the licensee did not effectively communicate expectations regarding procedural

compliance and, as a result, the Reactor Services maintenance craftsman did not

3 Enclosure

correctly follow the procedure by performing steps out of sequence and restoring a

system to service that was incorrectly aligned. (IMC 0310 H.4(b)) (Section 4OA2.3.b.(1))

Cornerstone: Emergency Preparedness

Green. The inspectors identified a finding of very low safety significance with an

associated NCV of 10 CFR 50.54(q) for the licensees failure to follow and maintain the

Emergency Plan, which meets the standards in 10 CFR 50.47(b) and the requirements

in Appendix E to 10 CFR 50. Specifically, the licensees Emergency Plan calls for the

performance of periodic drills to evaluate the ability to augment its Emergency

Response Organization (ERO). However, the Emergency Plan implementing procedure

used for the conduct of these augmentation drills exempts certain ERO members from

participation in these drills, a situation which prevents the licensee from fully

demonstrating its ability to augment all the ERO positions in a timely manner.

The licensees approved Emergency Plan does not provide for such an exemption.

The licensee entered the finding into the corrective action program.

The use of an implementing procedure that causes the conduct of an activity to be

inconsistent with the associated requirements in the licensees Emergency Plan results

in a failure to follow and maintain the Emergency Plan and is a performance deficiency.

As a result of the limitations in the procedure, the licensee failed to conduct call-in drills

to demonstrate timely augmentation of ERO positions filled by skilled/technical

personnel. The deficiency did not impact the NRCs regulatory process or contribute to

actual safety consequences; therefore, the performance deficiency was screened using

the Emergency Preparedness Significance Determination Process as a failure to

comply. The deficiency was determined to be more than minor because the deficiency

adversely affected the Emergency Preparedness Cornerstone objective and had the

attribute associated with ERO readiness in the area of ERO augmentation testing.

The inspector evaluated the finding using the IMC 0609, Appendix B, Sheet I, Failure to

Comply Flowchart. The inspector evaluated the finding as a degraded planning

standard function since the licensees conduct of the augmentation exercises did not

include all ERO positions. The finding was determined to be of very low safety

significance. The inspector determined the finding had a cross-cutting aspect in the

problem identification and resolution area with a component in self and independent

assessments. The licensees augmentation call-in drills were not comprehensive to

include all ERO augmentation staffing positions. (IMC 0310 P.3(a)) (Section 1EP3.1)

B. Licensee-Identified Violations

Violations of very low safety significance that were identified by the licensee have been

reviewed by the inspectors. Corrective actions planned or taken by the licensee have

been entered into the licensees corrective action program. The violations and corrective

action tracking numbers are listed in Section 4OA7 of this report.

4 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 was operated at or near full power during the inspection period with one exception.

On May 16, 2010, the licensee reduced power to about 71 percent to perform control rod

pattern adjustments and main steam isolation valve channel functional testing. The licensee

returned the unit to full power later the same day.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness For Impending Hot Summer Weather Conditions

a. Inspection Scope

The inspectors evaluated the licensees preparations for hot summer weather

conditions, focusing on the auxiliary power system and the control room ventilation

system. During the week of April 19, 2010, the inspectors performed a detailed review

of severe weather and plant de-winterization procedures and performed general area

plant walkdowns. The inspectors focused on plant-specific design features and

implementation of procedures for responding to or mitigating the effects of hot summer

weather conditions on the operation of the plant. The inspectors reviewed system health

reports and system engineering summer readiness review documents for the above

systems.

Additionally, the inspectors reviewed selected action requests for the identification and

resolution of procedure and equipment deficiencies associated with adverse weather

mitigation.

This inspection constituted one seasonal extreme weather readiness inspection sample

as defined in Inspection Procedure (IP) 71111.01.

b. Findings

No findings of significance were identified.

.2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems

a. Inspection Scope

The inspectors evaluated the licensees plant features and procedures for operation and

continued availability of offsite and alternate AC power systems. The inspectors

interviewed plant personnel and reviewed the licensees communications protocols

between the Transmission System Operator (TSO) and the plant to verify that the

appropriate information was being exchanged when issues arose that could impact the

offsite power system. Aspects considered in the inspectors review included:

The actions to be taken when notified by the TSO that the post-trip voltage of the

offsite power system at the plant will not be acceptable to assure the continued

5 Enclosure

operation of the safety-related loads without transferring to the onsite power

supply;

The compensatory actions identified to be performed if it is not possible to predict

the post-trip voltage at the plant for the current grid conditions;

The required re-assessment of plant risk based on maintenance activities that

could affect grid reliability, or the ability of the transmission system to provide

offsite power; and

The required communications between the plant and the TSO when changes at

the plant could impact the transmission system, or when the capability of the

transmission system to provide adequate offsite power is challenged.

The inspectors performed a walkdown of the switchyard with a plant operator and a TSO

electrician to observe the material condition of the offsite power sources. The inspectors

also reviewed the status of outstanding work orders to assess whether corrective actions

for any degraded conditions were scheduled with the TSO with the appropriate priority.

This inspection constituted one offsite and alternate AC power systems readiness

inspection sample as defined in IP 71111.01.

b. Findings

No findings of significance were identified.

.3 Readiness For Impending Adverse Weather Condition - Tornado/High Winds

a. Inspection Scope

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility for the week of April 5, 2010, the inspectors reviewed the licensees overall

preparations/protection for the expected conditions. The inspectors toured the plant

grounds in the vicinity of the main power transformers, unit auxiliary transformers,

reserve auxiliary transformers, emergency reserve auxiliary transformer, and static VAR

compensators to look for loose debris, which, if present, could become missiles during

a tornado or with high winds. During the inspections, the inspectors focused on

plant-specific design features and the licensees procedure used to respond to tornado

and high winds conditions.

This inspection constituted one readiness for impending adverse weather condition

inspection sample as defined in IP 71111.01.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.4 Quarterly Partial System Walkdowns (71111.04Q)

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

6 Enclosure

Reactor Core Isolation Cooling (RCIC) System (single train risk-significant

system;

Division 2 Emergency Diesel Generator (DG) during maintenance on Division 1

safety systems;

Residual Heat Removal (RHR) Train 'B' during maintenance on RHR Train 'A.'

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones. The inspectors reviewed operating procedures, system

diagrams, Technical Specification (TS) requirements, and the impact of ongoing work

activities on redundant trains of equipment. The inspectors verified that conditions did

not exist that could have rendered the systems incapable of performing their intended

functions. The inspectors also walked down accessible portions of the systems to verify

system components were aligned correctly and available, as necessary.

In addition, the inspectors verified that equipment alignment problems were entered into

the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted three partial system walkdown inspection samples as defined

in IP 71111.04.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors performed fire protection tours in the following plant areas:

Fire Zone A3-g, Containment Electrical Penetration Area (West) -

Elevation 781'-0";

Fire Zones CB-3b & 3d, Division 4 NSPS [Nuclear System Protection System]

Inverter and Battery Rooms - Elevation 781'-0";

Fire Zone F-1i, Fuel Pool Cooling Pump Room - Elevation 712'-0";

Fire Zone F-1n, Fuel Pool Cooling Heat Exchanger Room - Elevation 737'-0";

and

Fire Zone R-1n, Paint and Oil Storage Room - Elevation 737'-0."

The inspectors verified that transient combustibles and ignition sources were

appropriately controlled and assessed the material condition of fire suppression

systems, manual firefighting equipment, smoke detection systems, fire barriers and

emergency lighting units. The inspectors verified that fire hoses and extinguishers were

in their designated locations and available for immediate use; that fire detectors and

sprinklers were unobstructed; that transient material loading was within the analyzed

limits; that the licensees fire plan was in alignment with actual conditions; and that fire

doors, dampers, and penetration seals appeared to be in satisfactory condition.

7 Enclosure

In addition, the inspectors verified that fire protection related problems were entered into

the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted five quarterly fire protection inspection samples as defined in

IP 71111.05AQ.

b. Findings

No findings of significance were identified.

1R06 Flooding Protection Measures (71111.06)

.1 Unanalyzed Condition of Interconnecting Floor Drains Between the RHR A Pump Room

and Radwaste Pipe Tunnel

(Closed) Unresolved Item (URI)05000461/2009004-01, Interconnecting Floor Drains

Between the RHR A Pump Room and Radwaste Pipe Tunnel

a. Inspection Scope

The inspectors had previously identified that floor drains in the RHR A Pump Room and

the Radwaste Pipe Tunnel were interconnected, which resulted in an unanalyzed

condition. This issue was reviewed by the inspectors during this inspection period to

resolve open questions regarding the licensees evaluation of the extent of condition and

the reporting requirements. The extent of condition involved interconnecting floor drains

between the RHR C Pump Room and the Auxiliary Building Floor Drain Tank Room

and Pump Room.

The inspectors discussed the licensees evaluation of the extent of condition and the

reporting requirements with the licensee. The inspectors reviewed the flood analyses

and design documents, including the Updated Final Safety Analysis Report (UFSAR),

plant drawings, and engineering calculation IP-M-0782, Suppression Pool Equalization

Levels, Revision 0.

This inspection constituted one internal flood protection inspection sample as defined in

IP 71111.06.

b. Findings

(1) Failure to Satisfy 10 CFR 50.72 and 50.73 Reporting Requirements

Introduction

The inspectors identified a finding of very low safety significance (Green) with an

associated Severity Level IV non-cited violation of the NRCs reporting requirements in

10 CFR 50.72(a)(1), Immediate Notification Requirements for Operating Nuclear Power

Reactors, and 10 CFR 50.73(a)(1), Licensee Event Report System. The licensee

failed to make a required 8-hour non-emergency notification call to the NRC Operations

Center and also failed to submit a required Licensee Event Report (LER) within 60 days

after discovery of a condition that resulted in the plant being in an unanalyzed condition

8 Enclosure

that significantly degraded plant safety and could have prevented fulfillment of the safety

function of the emergency core cooling system (ECCS).

Discussion

During review of plant drawings for floor drain system piping in the ECCS and RCIC

Pump Rooms on the 7070 elevation of the Auxiliary Building, the inspectors identified

that floor drains in the RHR A Pump Room appeared to be connected via permanent

4-inch pipe embedded in the floor to floor drains in the Radwaste Pipe Tunnel, which is

located along the western wall of the (adjacent) Control Building at the 7200 elevation.

The inspectors noted that each of the separate pump rooms was supposedly designed

to be isolated from other areas of the plant and not susceptible to flooding from sources

external to the pump rooms.

The inspectors discussed this floor drain configuration with the licensee and questioned

the adequacy of the design with respect to the potential for flooding. The inspectors

noted that Section 3.8.4.1.1 of the UFSAR stated that the ECCS Pump Rooms are in

flood protection compartments with watertight doors. In the event of a pipe rupture, the

flooding in one compartment will not result in the flooding of any other compartment, and

the failure of a pump suction line will not drain the suppression pool. Section D3.6.4 of

the UFSAR stated that a postulated failure of any of the non-isolable portions of the

ECCS pump suction lines to the suppression pool could result in flooding of a single

ECCS cubicle to the high water level in the suppression pool (7315 elevation). Due to

the interconnecting floor drain piping, if flooding in the RHR A Pump Room (from the

suppression pool) were to occur, then the potential existed that cross-flooding could

occur between the RHR A Pump Room and the Radwaste Pipe Tunnel. Flooding could

potentially continue until the suppression pool level was below the Control Building floor

drain level (7206 elevation).

The inspectors discussed this issue in greater detail and documented a finding with an

associated NCV of 10 CFR 50, Appendix B, Criteria III, Design Control, in

NRC Inspection Report 05000461/2010002, regarding the licensees failure to correctly

translate the design basis into the design of the Auxiliary Building floor drain system with

appropriate margin. To address the immediate operability concern, the licensee plugged

the two floor drains in the Radwaste Pipe Tunnel to prevent communication with the floor

drain system in the RHR A Pump Room. The exposed vertical section of the drain line

in the low pressure core spray (LPCS) Pump Room was then cut and a solid steel plate

welded into the pipe per an engineering design change to permanently isolate the floor

drains between the two rooms.

The inspectors reviewed the licensees evaluation of the as-found condition with the

interconnecting floor drains between the RHR A Pump Room and Radwaste Pipe

Tunnel. The licensee concluded in its evaluation that, while the interconnecting floor

drains represented an unanalyzed condition, that was not consistent with the licensing

basis, safe shutdown would still be assured. The licensee evaluated the concern with

potential flooding in the RHR A Pump Room in terms of 10 CFR 50, Appendix A,

General Design Criteria. For a pipe break, General Design Criteria (GDC) 4,

Environmental and Missile Design Bases, and NUREG-800, Standard Review Plan,

require that the break be evaluated coincident with the functional failure of any single

active component, a seismic event the level of the safe shutdown earthquake, and a loss

of offsite power. This is consistent with UFSAR Section 3.6.1.3.1, which states, in part,

9 Enclosure

that [i]n the plant design, consideration was given to the effects of postulated piping

breaks with respect to the limits of acceptable damage/loss of function, to assure that,

even with coincident single loss of active component, and earthquake equal to the safe

shutdown earthquake, and loss of offsite power, the remaining structures, systems, and

components would be adequate to safely shutdown the plant. The RHR A pump has

multiple safety functions, and, consistent with the design basis assumptions, all of these

functions would be lost in the event of a pipe break in the pump room. The suppression

pool supports the functions of all three divisions of the ECCS and, if the suppression

pool were impacted by a single failure, that single failure could render multiple divisions

incapable of performing their design safety functions. That would be contrary to the

current licensing basis. The suppression pool also supports the pressure suppression

function of the primary containment. If the suppression pool level were to drain below

the minimum vent cover level of 151 (7271 elevation), an insufficient amount of water

would be available to adequately condense the steam from the safety/relief valve

quenchers, main vents, or RCIC turbine exhaust lines.

During review of the licensees evaluation and discussion with engineering staff,

the inspectors identified that a postulated failure of the 20 suction piping between the

remote manual containment isolation valve, 1E12-F004A, and the RHR A pump under

the requirements of GDC 4 would result in non-isolable flooding into the RHR A Pump

Room, and hence into the Radwaste Pipe Tunnel through the floor drains, that would

drain the suppression pool below the suppression pool high water level assumed in

Section D3.6.4 of the UFSAR since the flood level in the room would not equalize with

the suppression pool above the suppression pool high water level. This particular

scenario had not been considered by the licensee in the evaluation. This portion of

the piping system is within the moderate-energy portion of the fluid system.

The licensee determined that a break or crack in the line, when calculated per

UFSAR Section 3.6.2.1.5.b, would result in a 206 gallons-per-minute (gpm) leak.

In its evaluation of the unanalyzed condition, the licensee concluded that it was not

reportable to the NRC under the requirements of 10 CFR 50.72(b)(3)(ii)(B) or

50.73(a)(2)(ii)(B) as a condition that results (or resulted) in the nuclear power plant being

in an unanalyzed condition that significantly degrades (or degraded) plant safety.

The licensee also concluded that the non-conforming condition was not reportable to the

NRC under the requirements of 10 CFR 50.72(b)(3)(v)(D) or 50.73(a)(2)(v)(D) as a

condition that could have prevented the fulfillment of the safety function of structures

or systems needed to mitigate the consequences of an accident. The inspectors

questioned this conclusion. The licensee wrote action request (AR) 01031977 to

address the open questions and subsequently submitted a voluntary LER

(LER 05000461/2010-001-00, Unanalyzed Leakage Pathway Affecting Residual Heat

Removal A Pump Room Flooding Analysis). However, the LER was submitted after

the 60-day reporting period and, as discussed below, the licensee reached an incorrect

conclusion in the LER because it did not take into consideration those safety functions

that would still be required after safe shutdown has initially been achieved.

During this inspection period, the inspectors concluded that the unanalyzed condition

met the 10 CFR 50.72(b)(3)(ii)(B), 50.73(a)(2)(ii)(B), 50.72(b)(3)(v)(D), and

50.73(a)(2)(v)(D) reporting criteria. According to the licensees evaluation, the

postulated sequence of events for the above non-isolable pipe break scenario would

progress slowly and safe shutdown could be achieved after about 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />. However,

the inspectors concluded that the postulated event would still significantly degrade

10 Enclosure

plant safety and it could still result in the loss of safety function of the low pressure

injection/spray ECCS subsystems. Technical Specification 3.5.2 requires that two

ECCS injection/spray subsystems be operable in Modes 4 and 5, except with the

reactor cavity to steam dryer pool gate removed and water level 228 over the top of

the reactor pressure vessel flange. Assuming the suppression pool continues to drain

into the Radwaste Pipe Tunnel, with suppression pool level below the TS 3.5.2 minimum

level of 129 (7249 elevation), the low pressure injection/spray ECCS subsystems

would not be capable of fulfilling their safety function. According to Emergency

Operating Procedure (EOP)-6, Table Z, NPSH [Net Positive Suction Head] / Vortex

Limits, the minimum suppression pool level required to maintain NPSH to the

ECCS pumps is 110. While operators may be able to bring the plant to safe shutdown

before the suppression pool reaches the minimum vent coverage level of 151, the

suppression pool would still continue to drain due to the non-isolable pipe break and,

without the addition of water, would eventually reach the level that would not support the

ECCS pumps. The inspectors concluded that by this point in the scenario, plant safety

would be significantly degraded. There are available makeup sources of water for the

suppression pool, even with a loss of offsite power. Dumping the upper containment

pool to the suppression pool and/or addition of water from the RCIC storage tank using

the high pressure core spray pump would provide additional time before reaching 129

(or 110) for the licensee to locate the two floor drains in the Radwaste Pipe Tunnel and

plug them to stop the suppression pool drain down. However, plugging floor drains in

this infrequently accessed plant area would involve operator manual actions not

considered or credited in the current licensing basis.

Because the condition existed (i.e., it was occurring) at the time of discovery on

October 7, 2009, the inspectors concluded that the 10 CFR 50.72(b)(3) criteria for an

8-hour notification call to the NRC were met and the licensee should have made the

appropriate notification call. The licensee corrected the floor drain condition on the

following day, October 8, 2009.

Analysis

The inspectors determined that the licensees failure to report this issue as a condition

that results (or resulted) in the nuclear power plant being in an unanalyzed condition that

significantly degrades (or degraded) plant safety, and as a condition that could have

prevented the fulfillment of the safety function of structures or systems needed to

mitigate the consequences of an accident, was a licensee performance deficiency

warranting a significance evaluation. Consistent with the guidance in IMC 0612,

Power Reactor Inspection Reports, Appendix B, Issue Screening, because these

violations of the NRCs reporting requirements affected the NRC's ability to perform its

regulatory function, the inspectors evaluated the violations using the traditional

enforcement process in accordance with the NRC Enforcement Policy and assessed the

significance of the underlying issue using the SDP. The inspectors reviewed the

examples of minor issues in IMC 0612, Power Reactor Inspection Reports,

Appendix E, Examples of Minor Issues, and found no examples related to this issue.

The inspectors determined that this finding was of more than minor significance because

the NRC relies on licensees to identify and report conditions or events meeting the

criteria specified in the TS and the regulations in order to perform its regulatory function.

The inspectors previously determined that the underlying issue was a finding of very low

safety significance (Green) during a Phase 3 SDP review and documented the finding in

NRC Inspection Report 05000461/2010002 (NCV 05000461/2010002-03, Unanalyzed

11 Enclosure

Condition of Interconnecting Floor Drains Between the RHR A Pump Room and

Radwaste Pipe Tunnel). Consistent with the guidance in Supplement I, Paragraph D.4,

of the NRC Enforcement Policy, the violation associated with this finding was determined

to be a Severity Level IV Violation.

Cross-Cutting Aspects

The inspectors concluded that this finding affected the cross-cutting area of human

performance. Specifically, the licensee did not use conservative assumptions in

decision making while evaluating the reportability of the unanalyzed condition with

respect to the reporting requirements in 10 CFR 50.72(a)(1)(ii) and 50.73(a)(1).

Specifically, the licensee did not take into consideration those safety functions that would

still be required after safe shutdown has initially been achieved. (IMC 0310 H.1(b))

Enforcement

Title 10 CFR 50.72(a)(1)(ii) required, in part, that the licensee shall notify the

NRC Operations Center via the Emergency Notification System of those

non-emergency events specified in Paragraph (b) that occurred within three years of

the date of discovery. Title 10 CFR 50.72(b)(3) required, in part, that the licensee shall

notify the NRC as soon as practical and in all cases within eight hours of the occurrence

of any of the applicable conditions. Title 10 CFR 50.72(b)(3)(ii)(B) required, in part,

that the licensee report any event or condition that results in the nuclear power plant

being in an unanalyzed condition that significantly degrades plant safety.

Title 10 CFR 50.72(b)(3)(v)(D) required, in part, that the licensee report any event or

condition that at the time of discovery could have prevented the fulfillment of the safety

function of structures or systems that are needed to mitigate the consequences of an

accident.

Title 10 CFR 50.73(a)(1) required, in part, that the licensee submit an LER for any event

of the type described in this paragraph within 60 days after the discovery of the event.

Title 10 CFR 50.73(a)(2)(ii)(B) required, in part, that the licensee report any event or

condition that resulted in the nuclear power plant being in an unanalyzed condition that

significantly degraded plant safety. Title 10 CFR 50.73(a)(2)(v)(D) required, in part, that

the licensee report any event or condition that could have prevented the fulfillment of the

safety function of structures or systems that are needed to mitigate the consequences of

an accident.

Contrary to the above:

1. The licensee failed to notify the NRC Operations Center via the Emergency

Notification System of a non-emergency event specified in Paragraph (b) within

eight hours after discovery of an event on October 7, 2009. The event involved the

discovery of interconnecting floor drains between the RHR A Pump Room and the

Radwaste Pipe Tunnel, which resulted in the plant being in an unanalyzed condition

that significantly degraded plant safety and at the time of discovery could have

prevented fulfillment of the safety function of the ECCS.

2. The licensee failed to submit a required LER within 60 days after discovery of an

event on October 7, 2009. The event involved the discovery of interconnecting floor

drains between the RHR A Pump Room and the Radwaste Pipe Tunnel, which

12 Enclosure

resulted in the plant being in an unanalyzed condition that significantly degraded

plant safety and could have prevented fulfillment of the safety function of the ECCS.

This Severity Level IV violation of the NRC reporting requirements is associated with a

Green SDP finding and will be treated as a NCV consistent with Section VI.A of the

NRC Enforcement Policy. (NCV 05000461/2010003-01, Failure to Satisfy

10 CFR 50.72 and 50.73 Reporting Requirements). The licensee entered this finding

into its corrective action program as AR 01080117.

(2) Extent of Condition Review - Interconnecting Floor Drains Between the RHR C Pump

Room and the Auxiliary Building Floor Drain Tank Room and Pump Room

During its extent of condition review, the licensee also discovered that a similar

arrangement existed with floor drains on the west side of the Auxiliary Building in that

the RHR C Pump Room floor drain piping communicates with the floor drains in the

Auxiliary Building Floor Drain Tank Room and Pump Room. Those rooms are located

south of the RHR C Pump Room on the other side of the watertight door, at the 7120

elevation. The licensee evaluated this configuration and concluded that draining the

suppression pool through this drain path in the event of a pipe break in RHR C Pump

Room was not a concern. The licensee noted that the combined volume of the RHR C

Pump Room, Auxiliary Building Floor Drain Tank Room, and Auxiliary Building Floor

Drain Pump Room was about the same as the LPCS Pump Room. Therefore, the

licensee concluded that in the event of a pipe break in RHR C Pump Room, the

suppression pool could not be drained below the equalization elevation for the LPCS

Pump Room, which was already believed to be acceptable.

However, during review of the licensees evaluation, the inspectors noted that the

equalization level for the LPCS Pump Room, as stated in Table 2 of CPS 4304.01,

Flooding, Revision 4e, was 121. This level is well below the minimum vent cover

level of 151 and also below the TS 3.5.2 minimum suppression pool level of 129 for

operability of the ECCS subsystems with the unit in Modes 4 and 5. The inspectors

questioned whether the results of the existing Flood Analysis for the LPCS Pump Room

was acceptable based on having the equalization level below the minimum vent cover

level in the event of a non-isolable suction pipe break and similarly whether the above

evaluation for the RHR C Pump Room was acceptable. In response to the inspectors

questions, the licensee wrote AR 01039042 to address apparent discrepancies with the

suppression pool equalization levels in Table 2 of CPS 4304.01 and the possible impact

on the Flood Analysis for the ECCS Pump Rooms. From this action request, the

licensee identified the need to complete a formal calculation confirming the flooding

equalization levels and issue it with an engineering evaluation that includes an

operating procedure review and identification of any necessary operations training.

This is important because licensed operators would utilize information from this table in

evaluating actions to be taken under the emergency operating procedures in the event of

ECCS pump room flooding.

During this inspection period, the inspectors reviewed the licensees calculation

and associated engineering evaluation and found no additional issues of concern.

The equalization levels for the LPCS and RHR C Pump Rooms are below the 151

minimum vent cover level at 144 and 1410, respectively. However, the licensing basis

does not assume a loss of coolant accident coincident with a non-isolable pump room

flooding event and there is sufficient margin to the TS 3.5.2 minimum suppression pool

13 Enclosure

level of 129 to support operability of the ECCS pumps. The equalization level for the

RHR C Pump Room was calculated to include the volume of the Auxiliary Building Floor

Drain Tank Room and Pump Room because the interconnecting floor drains have been

accepted as-is.

The inspectors concluded that the licensees failure to have an accurate supporting

calculation for the flooding equalization levels in Table 2 of CPS 4304.01 constituted a

violation of 10 CFR 50, Appendix B, Criteria III, Design Control, of minor significance

and is not subject to enforcement action in accordance with the NRCs Enforcement

Policy. The licensee entered this violation into its corrective action program as

AR 01039042.

Unresolved Item 05000461/2009004-01 is closed.

1R07 Heat Sink Performance (71111.07)

.1 Annual Heat Sink Performance (71111.07A)

a. Inspection Scope

The inspectors reviewed the licensees maintenance activities for the RHR system.

Specifically, the review included the program for testing and analysis of the RHR Pump

Room Ventilation Cooling Unit (heat exchanger) and RHR Heat Exchanger Room

Ventilation Cooling Unit, which were cleaned, inspected, and evaluated. The inspectors

assessed the as-found and as-left condition of the heat exchangers by direct observation

and document reviews to verify that no deficiencies existed that would adversely impact

the heat exchangers' ability to transfer heat to the shutdown service water (SX) system

and to ensure that the licensee was adequately addressing problems that could affect

the performance of the heat exchangers. The inspectors observed portions of inspection

and cleaning activities, and reviewed documentation to verify that the inspection

acceptance criteria specified in procedure ER-AA-340-1002, Service Water Heat

Exchanger and Component Inspection Guide, Revision 4, were satisfactorily met.

This inspection constituted two annual heat sink inspection samples as defined in

IP 71111.07.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

The inspectors observed licensed operators during simulator training on June 9, 2010.

The inspectors assessed the operators response to the simulated events focusing

on alarm response, command and control of crew activities, communication practices,

procedural adherence, and implementation of Emergency Plan requirements.

The inspectors also observed the post-training critique to assess the ability of licensee

evaluators and operating crews to self-identify performance deficiencies. The crews

14 Enclosure

performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements.

This inspection constituted one quarterly licensed operator requalification inspection

sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated the licensee's handling of selected degraded performance

issues involving the following risk-significant structures, systems, and components

(SSCs):

Feedwater System Primary Containment Isolation Valves 1B21F032A and

1B21F032B;

Reactor Recirculation System Flow Control Valves 1B33F060A and 1B33F060B.

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the SSCs. Specifically, the inspectors independently verified

the licensee's handling of SSC performance or condition problems in terms of:

Appropriate work practices;

Identifying and addressing common cause failures;

Scoping of SSCs in accordance with 10 CFR 50.65(b);

Characterizing SSC reliability issues;

Tracking SSC unavailability;

Trending key parameters (condition monitoring);

10 CFR 50.65(a)(1) or (a)(2) classification and reclassification; and

Appropriateness of performance criteria for SSC functions classified (a)(2) and/or

appropriateness and adequacy of goals and corrective actions for SSC functions

classified (a)(1).

In addition, the inspectors verified that problems associated with the effectiveness of

plant maintenance were entered into the licensee's corrective action program with the

appropriate characterization and significance. Selected action requests were reviewed

to verify that corrective actions were appropriate and implemented as scheduled.

This inspection constituted two maintenance effectiveness inspection samples as

defined in IP 71111.12.

b. Findings

No findings of significance were identified.

15 Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Maintenance Risk Assessments and Emergent Work Control

.a Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for

maintenance and emergent work activities affecting the risk significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

Planned maintenance on March 25th to drain the RHR A Heat Exchanger;

Planned maintenance and testing on April 22nd on the High Pressure Core

Spray System;

Planned maintenance on the Emergency Reserve Auxiliary Transformer (ERAT)

for a system outage window the week of May 3rd.

These activities were selected based on their potential risk significance relative to

the Reactor Safety Cornerstones. As applicable for each of the above activities, the

inspectors reviewed the scope of maintenance work in the plants daily schedule,

reviewed Control Room logs, verified that plant risk assessments were completed as

required by 10 CFR 50.65(a)(4) prior to commencing maintenance activities, discussed

the results of the assessment with the licensees Probabilistic Risk Analyst and/or Shift

Technical Advisor, and verified that plant conditions were consistent with the risk

assessment assumptions. The inspectors also reviewed TS requirements and walked

down portions of redundant safety systems, when applicable, to verify that risk analysis

assumptions were valid, that redundant safety related plant equipment necessary to

minimize risk was available for use, and that applicable requirements were met.

The inspectors also completed a review of the licensees procedure for determining what

constitutes an operation with the potential to drain the reactor vessel (OPDRV) and

resolved open questions with the licensees 10 CFR 50.59 evaluation.

In addition, the inspectors verified that maintenance risk related problems were

entered into the licensees corrective action program with the appropriate significance

characterization. Selected action requests were reviewed to verify that corrective

actions were appropriate and implemented as scheduled.

This inspection constituted three maintenance risk assessment inspection samples as

defined in IP 71111.13.

16 Enclosure

b. Findings

(1) Failure to Perform an Adequate 10 CFR 50.59 Evaluation For Clinton Power Station

(CPS) Procedure 3711.01

(Closed) URI 05000461/2010002-06, Questions Regarding 10 CFR 50.59 Evaluation

for CPS Procedure 3711.01 Involving Operations with the Potential to Drain the Reactor

Vessel (OPDRV)

Introduction

The inspectors identified a finding of very low safety significance (Green) with an

associated Severity Level IV non-cited violation of 10 CFR 50.59, Changes, Tests and

Experiments, for the licensees failure to perform an adequate 10 CFR 50.59 evaluation

and obtain a license amendment prior to implementing CPS 3711.01, CPS Operations

with the Potential to Drain the Reactor Vessel, Revision 0. Specifically, the licensee

failed to recognize that implementing this new procedure, in effect, constituted a change

to the TS incorporated into its licensing basis, which would, therefore, require a license

amendment pursuant to 10 CFR 50.59(c)(1)(i) and 10 CFR 50.90.

Discussion

On January 11, 2010, the licensee approved procedure CPS 3711.01, which established

how it chose to define an OPDRV. OPDRV is a term used in a number of TS, including

CPS TSs 3.3.6.1, 3.6.1.2, 3.6.1.3, 3.6.4.1, 3.6.4.2, 3.6.4.3, 3.7.3, and 3.7.4. The term is

also important in the action statements of TS Limiting Conditions for Operation (LCOs)

3.5.2, 3.8.2, and 3.8.10.

Notably, the new procedure changed how control rod drive mechanism (CRDM)

replacement was classified by the licensee. Prior to the change, this evolution had been

treated as an OPDRV; however, once the procedure was approved, the evolution was

no longer considered an OPDRV. During the refueling outage that began the following

day on January 12th, there was no longer a licensee procedural requirement to enter a

number of TS LCO action statements during CRDM replacements.

In CPS 3711.01, the licensee, among other things, chose to define a maximum hole

diameter size of 1.92 inches below normal water level, which was to be considered to

have no potential to drain the reactor vessel. This number was based upon the

licensees ability to provide non-safetyrelated makeup measures to compensate for

reactor coolant system (RCS) inventory loss and, therefore, maintain reactor vessel

water level above the vessel flange. The licensee performed an evaluation

(CL-2010-E-001, CPS Procedure 3711.01, Revision 0) to address the requirements of

10 CFR 50.59 prior to implementing the new procedure. The licensees evaluation

concluded that the procedure change did not involve a revision to the TS and that the

impact of the change could not be more than minimal; therefore, a license amendment

was not required prior to its approval.

In the initial revision of CL-2010-E-001, the licensee stated that a 17-hour period is

established to take action to restore reactor vessel water level before irradiated fuel

could become uncovered based upon the 1.92 inch hole diameter size. After the

inspectors identified potential event scenarios introduced by the procedure change that

were not analyzed, the licensee revised the evaluation. In the revised evaluation, the

17 Enclosure

licensee concluded that 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and 58 minutes would be available to take action in a

loss of offsite power scenario to restore water level before uncovering irradiated fuel.

Despite the significantly less response time available (17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> versus approximately

7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />), the licensee again concluded that a license amendment request was not

required. In response to additional questions from the inspectors, the licensee also

analyzed a possible scenario involving the removal of a control rod that is relied upon to

isolate leakage for a removed CRDM. In this instance, the licensee concluded that

7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> and 36 minutes would be available to respond to the event.

No detailed discussion was provided in either version of the 10 CFR 50.59 evaluation as

to how station personnel would respond to a potential drain down event in the absence

of any procedural guidance. In the initial evaluation, the licensee generally assumed

that the 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> considered to be available for event response would be sufficient.

Notably, this initial evaluation did not attempt to credit the availability of the ECCS as a

makeup source; however, the revised evaluation did. Technical Specification 3.5.2,

ECCS - Shutdown, contains the requirements for the operability of the ECCS

subsystems while shutdown. In the applicability statement, it states that the TS does not

apply when in Mode 5 with water level greater than 22 8 over the reactor vessel flange

and the gate removed between the reactor cavity and the steam dryer pool. Therefore,

under the possible event conditions during refueling operations, there would be no TS

requirement for any ECCS subsystem to be operable. The licensee, however, credited

the ECCS in its revised evaluation for each possible event scenario by stating that an

ECCS subsystem and an emergency diesel generator was required by Clinton

procedure OU-CL-104, Shutdown Safety Management Program Clinton Power Station.

While this procedure did state in Step 4.3.3.5 that as a general guideline at least one

ECCS pump should be available anytime the cavity gate is removed, it was not a

requirement. In Attachment 2 of the procedure under the inventory control requirements

for Mode 5 with the reactor cavity flooded, the procedure clearly stated that this was a

requirement only for a Green shutdown risk condition. A Green shutdown risk

condition is a condition of the least or minimal plant risk. For any other inventory control

shutdown risk condition entered by the licensee, it would be incorrect to credit the

availability of the ECCS for response to these possible event scenarios.

Technical Specification 3.5.2 contains the action statement to suspend all operations

that have a potential for draining the reactor vessel under the applicable conditions.

Since the conversion of CPS from TS to improved Standard Technical Specifications

(NUREG-1434, Standard Technical Specifications - General Electric Plants, BWR/6,

Revision 1), the respective LCO action statement now directs the licensee to

suspend operations with a potential for draining the reactor vessel. During this

conversion of TS, no discussion was documented in the CPS licensing basis regarding

this difference in phrasing of the respective LCO action statements; therefore, the

meaning of the action statements necessarily remains unchanged. Plain language

understanding of suspend all operations that have a potential to drain the reactor

vessel does not imply the inclusion of any qualifying statements and criteria such as

those included in CPS 3711.01 prior to entering those corresponding TS LCO action

statements. In addition to an un-isolable hole diameter size of 1.92 inches, many other

criteria and conditions were assigned by the licensee before an evolution could be

considered an OPDRV. This new process by which the licensee chose to define

OPDRV is in contrast to the plain language that is the CPS licensing basis. Therefore,

implementation of CPS 3711.01 involved a change to the TS that required prior

approval of the NRC.

18 Enclosure

Analysis

The inspectors determined that the licensees failure to perform an adequate

10 CFR 50.59 evaluation and obtain a license amendment prior to implementing

CPS 3711.01 was a licensee performance deficiency warranting a significance

evaluation. Consistent with the guidance in IMC 0612, Power Reactor Inspection

Reports, Appendix B, Issue Screening, because this issue affected the NRC's ability to

perform its regulatory function, the inspectors evaluated it using the traditional

enforcement process and assessed the significance of the underlying issue using the

SDP. The inspectors reviewed the examples of minor issues in IMC 0612,

Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues, and found

no examples related to this issue. The inspectors determined that this finding was of

more than minor significance because there was a reasonable likelihood that the change

requiring a 10 CFR 50.59 evaluation would require Commission review and approval

prior to implementation.

The inspectors and the Regional Senior Reactor Analyst used IMC 0609, Appendix G,

Shutdown Operations Significance Determination Process, to evaluate the significance

of this finding. The applicable Phase 1 checklist was Checklist 7, BWR [Boiling Water

Reactor] Refueling Operation with RCS level > 23. The finding did not screen as very

low safety significant in Phase 1 because it was a finding that increased the likelihood of

a loss of RCS inventory. A modified Phase 2 SDP evaluation was conducted using

Worksheet 3, SDP Worksheet for a BWR Plant - Loss of Inventory in [Plant Operating

State] POS-3 (Cavity Flooded) and the associated event tree in Figure 4, Event Tree

for Loss of Inventory - BWR POS-3.

The Phase 2 worksheet was modified because it generally assumes that the

RHR system is available for decay heat removal and that a loss of inventory would

threaten the decay heat removal functions. During this period of CRDM maintenance,

the common suction line for RHR shutdown cooling was isolated and the fuel pool

cooling system was providing the decay heat removal function. In addition, the

worksheet does not anticipate that auto initiation of ECCS would be available during

cavity flooded conditions. Therefore, the analysis needs to account for this deviation

from the methodology.

The first sequence that needs to be solved (labeled Sequence 3) involves loss of

inventory (LOI), recovery of RHR in shutdown cooling (RHRREC) and long term

makeup (LCOOL). Because the common suction line for RHR is in maintenance,

the RHR system cannot be recovered. However, in this sequence level is recovered by

successful short term injection. This level recovery allows decay heat removal via the

fuel pool cooling system to be recoverable. Long term inventory source can be from

multiple sources including RHR service water, condensate storage tank, demineralized

water tank, the suppression pool and the condenser hotwell. Because the sequence

involves successful injection into the RCS in the near term, a long time is available

before the core cooling is interrupted by depletion of the source of water for the injection

systems (the suppression pool is assumed to be the source of water for this near term

injection).

The other sequences in the Phase 2 worksheet were solved assuming that

approximately 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> was available to isolate the drain path before the level in the

reactor cavity reached the reactor flange. The licensee provided information that both

19 Enclosure

RHR trains and at least one train of LPCS were available for automatic injection in the

event of a loss of RCS inventory. These systems could also be started manually if the

automatic initiation were to fail. Adequate level indication was available to identify a loss

of RCS inventory event.

This finding was determined to be a precursor finding, as defined in IMC 0609,

Appendix G. Table 2 was used to estimate the Initiating Event Likelihood (IEL) for a

LOI precursor. Given 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> to isolate, adequate level indication, and the ability to

identify the leak path and stop it, the estimated IEL was 4. Maximum mitigation credit

was applied for the RCS injection (both automatic and manual injection were available),

and long term cooling functions because of the amount of time available for operators to

respond and the number of RCS injection systems available. No credit was given for the

isolation function given that this drain path would not be automatically isolated. This is

conservative, given that the drain path is isolable with reasonable operator action, but is

accounted for in the estimated IEL. Given these assumptions, three sequences of 8

were estimated, which is equivalent to a 7, or a change in core damage frequency of

1E-7/year. The dominant sequence is a loss of inventory event followed by the failure of

RCS injection.

Based on the results of the modified Phase 2 SDP evaluation, this finding was

determined to be of very low safety significance (Green). Consistent with the guidance

in Supplement I, Paragraph D.5, of the NRC Enforcement Policy, the violation

associated with this finding was determined to be a Severity Level IV Violation.

Cross-Cutting Aspects

The inspectors concluded that the performance characteristic of this finding, that is the

most significant contributor to the performance deficiency, was in the cross-cutting area

of human performance. Specifically, the licensee did not use conservative decision

making before proceeding. The inspectors noted that the licensee was aware of

potential concerns regarding the new procedure prior to completing the initial

10 CFR 50.59 evaluation and again prior to revising the evaluation in response to

concerns raised by the inspectors; however, the incorrect conclusion, that the new

procedure was not a change to the TS and that a license amendment was not

necessary, was reached in both revisions of the evaluation. (IMC 0310 H.1(b))

Enforcement

Title 10 CFR 50.59, Changes, Tests and Experiments, establishes conditions under

which licensees may make changes to their facilities and procedures as described in

the safety analysis report without prior NRC approval. Title10 CFR 50.59 (c)(1)(i) stated,

in part, that a licensee may make changes in the facility as described in the final safety

analysis report without obtaining a license amendment pursuant to 10 CFR 50.90 only if

a change to the TS incorporated in the license is not required.

Contrary to the above, on June 15, 2009, the licensee implemented procedure

CPS 3711.01, CPS Operations with the Potential to Drain the Reactor Vessel,

Revision 0, without obtaining prior NRC approval. Implementing this new procedure,

in effect, constituted a change to the TS incorporated into the licensing basis by altering

the plain language definition of an OPDRV in the TS and resulted in a significant change

in process for when the licensee enters a number of TS LCO action statements.

This Severity Level IV Violation is associated with a Green SDP finding and will be

20 Enclosure

treated as a NCV consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000461/2010003-02, Failure to Perform an Adequate 10 CFR 50.59

Evaluation for CPS Procedure 3711.01). This violation was entered into the licensees

corrective action program as AR 01063405.

Unresolved Item 05000461/2010002-06 is closed.

1R15 Operability Evaluations (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

AR 01017464, "1B21F028A: LLRT [Local Leak Rate Test] on Main Steam

Line A, B, and C Test Failure";

AR 01065232, "0AP03E: ERAT: Core Ground Test Results Lower Than

Expected";

AR 01059174, "The ERDS [Emergency Response Data System] System

Did Not Connect to the NRC";

AR 01063878, "NRC TIA [Task Interface Agreement] Applicability of

TSSR [Technical Specification Surveillance Requirement] 3.0.3 for IST

[Inservice Testing] of Excess Flow Check Valves."

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors verified that the conditions

did not render the associated equipment inoperable or result in an unrecognized

increase in plant risk. When applicable, the inspectors verified that the licensee

appropriately applied TS limitations, appropriately returned the affected equipment to an

operable status, and reviewed the licensees evaluation of the issue with respect to the

regulatory reporting requirements. Where compensatory measures were required to

maintain operability, the inspectors determined whether the measures in place would

function as intended and were properly controlled. The inspectors determined, where

appropriate, compliance with bounding limitations associated with the evaluation.

In addition, the inspectors verified that problems related to the operability of

safety-related plant equipment were entered into the licensees corrective action

program with the appropriate characterization and significance. Selected action

requests were reviewed to verify that corrective actions were appropriate and

implemented as scheduled.

This inspection constituted four operability evaluation inspection samples as defined in

IP 71111.15.

.2 Findings

(1) Operability Assessment of Inservice Testing Surveillance Discrepancies for Excess Flow

Check Valves

(Closed) URI 05000461/2009003-04, Review of Applicability of TSSR 3.0.3 to Multiple

Missed Surveillance Intervals for Excess Flow Check Valves

21 Enclosure

Introduction

The inspectors identified a finding of very low safety significance (Green) associated with

the licensees failure to evaluate the functionality of multiple excess flow check valves

that had not been tested in accordance with the American Society of Mechanical

Engineers / American National Standards Institute (ASME/ANSI) Code Inservice Testing

(IST) requirements to establish whether the nonconforming condition warranted starting

the TS action time for the suppression pool makeup (SPMU) system. No violation of

regulatory requirements was identified because subsequent testing by the licensee

determined that the valves were functional.

Discussion

On November 18, 2008, the licensee identified that nine excess flow check valves

(1CM002A, 1CM002B, 1CM003A, 1E22-F330, 1E22-F332, 1E51-F377A, 1E51-F377B,

1SM008 and 1SM009) were incorrectly removed from its IST Program in 2002.

The valves have a safety function to re-open following a design basis accident to provide

instrumentation assumed to be available post-accident. The ASME/ANSI Operations

and Maintenance Code (OMa 1988, Part 10) would require a position verification test for

these valves once every two years and an opening test once every three months, with

exceptions allowed for refueling cycle frequency. The valves had not been tested since

2000.

Upon discovery of the excess flow check valve testing issue, the licensee utilized the

relief afforded by TSSR 3.0.3 for a missed surveillance to allow up to the limit of the

specified frequency to perform missed surveillances. During review of the issue in

April 2009, the inspectors questioned the licensee whether it was appropriate to utilize

the relief allowed by TSSR 3.0.3 because these did not appear to be cases of a single

missed surveillance.

The NRC staff had concluded in TIA 2008-004, Evaluation of Application of TS 4.0.3,

Surveillance Requirement Applicability, at Pilgrim, that a missed surveillance

(i.e., inadvertently exceeded surveillance) is not equivalent to a never-performed

surveillance for which TSSR 3.0.3 would not apply. The basis for the relief allowed by

TSSR 3.0.3 is that the past surveillance testing history provides a level of confidence

that the component or system is most likely operable. A surveillance that has never

been performed does not have this basis for a presumption of operability.

Consistent with the "level of confidence" argument that was provided in TIA 2008-004,

the inspectors questioned whether it would be correct for the licensee to apply

TSSR 3.0.3 for the excess flow check valves. After all, the licensee removed the valves

from its IST Program and discontinued testing, exceeding four previously defined test

frequency periods without testing the valves. Therefore, the basis for a presumption of

operability may not exist because the licensee was not demonstrating operability by

performing the required testing of the excess flow check valves all along. The inspectors

open URI 05000461/2009003-04 to track the NRC staffs review of this question to

determine if additional NRC guidance was necessary to specify whether TSSR 3.0.3

applies in the case where more than one surveillance interval is exceeded.

The inspectors used the "level of confidence" argument discussed in TIA 2008-004 as

the basis to question the functionality of the valves. Up to this point, the licensee had

taken for granted that utilizing the relief allowed by TSSR 3.0.3 and performing a risk

22 Enclosure

evaluation obviated the need to address operability of the instrumentation supported by

the excess flow check valves for the ASME/ANSI Code noncompliance. Subsequently,

on June 20, 2009, the licensee revised the calculation defining the design basis function

for the excess flow check valves to remove the active support safety function of five of

the check valves. Of the remaining four check valves that have an active safety function

(1CM002B, 1E22-F332, 1E51-F377B, and 1SM008), one check valve (1E22-F332) was

tested satisfactorily with the unit in Mode 1 on March 6, 2009, and again on June 5,

2009. In response to the inspectors questions, on June 24, 2009, the licensee

completed an evaluation for the remaining three check valves. The inspectors

subsequently reviewed the evaluation and discussed it with the licensees staff.

The inspectors review of the operability evaluation was documented in NRC

Inspection Report 05000461/2009-004. The inspectors did not believe that the

licensees supporting basis provided a high degree of confidence that the valves would

function as required; however, without actually testing the valves, the inspectors were

unable to prove that the valves would not function. The licensee maintained that it was

satisfied with its determination in the evaluation. The licensee subsequently tested the

three excess flow check valves satisfactorily during an unplanned forced outage that

began on September 29, 2009. A licensee-identified NCV of 10 CFR 50.55a(f) was

documented in NRC Inspection Report 05000461/2009-004 for the licensees failure to

perform inservice testing of the excess flow check valves.

The NRC staff reviewed the question of applicability of TSSR 3.0.3 to missed inservice

testing of the excess flow check valves at Clinton Power Station in TIA 2010-001,

Evaluation of Application of Technical Specification Surveillance Requirement 3.0.3,

Surveillance Requirement Applicability, at Clinton Power Station. In short, the

NRC staff concluded that TSSR 3.0.3 was not applicable to the missed inservice testing

of the excess flow check valves discussed above because the valves were not tested in

accordance with TS required surveillances. The statement of applicability of TSSR 3.0.3

in TS 5.5.6, Inservice Test Program, is only to maintain the allowances for surveillance

frequency extensions for TS required surveillances.

The requirement to declare the LCO not met referred to in TSSR 3.0.3 is contained in

TSSR 3.0.1 and the allowance to delay compliance with that requirement is available

for TSSRs that have frequencies governed by the Inservice Testing Program

(e.g., TSSR 3.4.4.1). Invoking TSSR 3.0.3 merely allows delaying the declaration that

an LCO is not met and does not modify the separate requirement of the LCO that the

associated systems be operable. Failure to perform a surveillance of this nature is also

a noncompliance and should be resolved as discussed in Regulatory Issue Summary

(RIS) 2005-20, Revision to NRC Inspection Manual Part 9900 Technical Guidance,

Operability Determinations & Functionality Assessments for Resolution of Degraded or

Nonconforming Conditions Adverse to Quality or Safety, Revision 1.

Invoking TSSR 3.0.3 for an inservice test that is not a TSSR would be inappropriate

because there has been no surveillance that was not performed within its specified

frequency, which is necessary to invoke TSSR 3.0.3, and there is no associated

requirement from TSSR 3.0.1 to declare an LCO not met. The noncompliance with the

inservice testing requirements in 10 CFR 50.55a(f) should also be resolved as discussed

in RIS 2005-20, Revision 1.

The TS definition of OPERABLE does not allow a grace period before a component that

is not capable of performing its specified function is declared inoperable. Thus, an

23 Enclosure

assessment of the functionality of the excess flow check valves was required to establish

whether the degraded/nonconforming condition warranted starting the TS action time for

the supported system. This is consistent with NRC staffs Operability Determination

Process guidance in RIS 2005-20 for addressing degraded and nonconforming

conditions because these valves perform specified functions described in the UFSAR or

other elements of the current licensing basis. As stated in this guidance:

There is no explicit time limit for completing a prompt determination. Nevertheless,

timeliness is important and should depend on the safety significance of the issue.

For example, it may be appropriate to make a prompt operability determination within

a few hours for situations involving highly safety significant SSCs [structures,

systems, or components]. Prompt determinations can often be done within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

of discovery even if complete information is not available. If more time is needed to

gather additional information (such as a vendor analyses or calculations), the

licensee can evaluate the risk importance of the additional information to decide

whether to prolong the operability determination. TS completion time is one factor

that can be used in determining an appropriate time frame within which a prompt

determination should be completed.

In the current instance, inoperability of the affected SPMU instrumentation would require

declaring the SPMU subsystem inoperable within one hour (LCO 3.3.6.4). Inoperability

of one SPMU subsystem would require restoring it to operable status within 7 days or

changing to Modes 3 and 4 in 12 and 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />, respectively. In this context, the delay in

conducting an operability determination from November 18, 2008, until June 24, 2009,

would be considered excessive.

The inspectors original question about applying TSSR 3.0.3 when there are multiple

missed surveillance intervals was not addressed in TIA 2010-001.

Analysis

The inspectors determined that the licensees failure to evaluate the functionality of the

excess flow check valves to establish whether the nonconforming condition warranted

starting the TS action time for the SPMU system was a licensee performance deficiency

warranting a significance evaluation. The inspectors assessed this finding using the

SDP. The inspectors reviewed the examples of minor issues in IMC 0612,

Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues, and

found no examples related to this issue. Consistent with the guidance in IMC 0612,

Appendix B, Issue Screening, the inspectors determined that the failure to correctly

evaluate a degraded/nonconforming condition potentially affecting the operability of

SSCs required to be operable by TS would become a more significant safety concern,

if left uncorrected, and was, therefore, more than a minor concern, because it could

reasonably result in an unrecognized condition of an SSC failing to fulfill a safety-related

function. Because the SPMU system was primarily associated with long term decay

heat removal following certain design basis accidents, the inspectors concluded that

this issue was associated with the Mitigating Systems Cornerstone. The inspectors

performed a Phase 1 SDP review of this finding using the guidance provided in

IMC 0609, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of

Findings. In accordance with Table 4a, Characterization Worksheet for IE

[Initiating Events], MS [Mitigating Systems], and BI [Barrier Integrity] Cornerstones,

the inspectors determined that that this finding was a licensee performance deficiency

24 Enclosure

of very low safety significance (Green) because the finding: (1) was not a design or

qualification deficiency; (2) did not represent an actual loss of safety function of a

system; (3) did not represent an actual loss of safety function of a single train for greater

than its TS allowed outage time; (4) did not represent an actual loss of safety function of

one or more non-TS trains of equipment designated as risk significant; and (5) did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event.

Cross-Cutting Aspects

The inspectors concluded that this finding affected the cross-cutting area of human

performance. Specifically, the licensee did not have a formal process in place with

adequate guidance and training to enable licensed senior reactor operators to properly

and promptly evaluate operability in this instance. As a result, senior reactor operators

took it for granted that utilizing the relief allowed by TSSR 3.0.3 and performing a risk

evaluation obviated the need to address operability of the instrumentation supported by

the excess flow check valves for the ASME/ANSI Code noncompliance.

(IMC 0310 H.1(a))

Enforcement

No violation of regulatory requirements was identified. This issue is considered to be a

finding. (FIN 05000461/2010003-03, Operability Assessment of Inservice Testing

Surveillance Discrepancies for Excess Flow Check Valves). The licensee entered

this finding into its corrective action program as AR 01063878.

Unresolved Item 05000461/2009003-04 is closed.

1R19 Post-Maintenance Testing (71111.19)

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance testing for the following activities to verify

that procedures and test activities were adequate to ensure system operability and

functional capability:

WO 00488712-05, "CPS 9053.04 - RHR A B C Valve OP";

WO 01028895-04, RHR Pump 'A' Seal Cooler SX Inlet Valve;

WO 01082152-02, Division 2 DG Verify Sync-Check Relay 225-DG1KB;

WO 01307425-08, 1GC01PA: High Vibration on GC [Stator Cooling Water]

Pump A; and

WO 01321254-03, "Leak Check 1C85D002MG, 1C85D002 Back Up Filter."

The inspectors reviewed the scope of the work performed and evaluated the adequacy

of the specified post-maintenance testing. The inspectors verified that the

post-maintenance testing was performed in accordance with approved procedures; that

the procedures contained clear acceptance criteria, which demonstrated operational

readiness and that the acceptance criteria was met; that appropriate test instrumentation

was used; that the equipment was returned to its operational status following testing;

and, that the test documentation was properly evaluated.

25 Enclosure

In addition, the inspectors reviewed corrective action program documents associated

with post-maintenance testing to verify that identified problems were entered into the

licensee's corrective action program with the appropriate characterization. Selected

action requests were reviewed to verify that the corrective actions were appropriate and

implemented as scheduled.

This inspection constituted five post-maintenance testing inspection samples as defined

in IP 71111.19.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following surveillance testing activity to

determine whether risk-significant systems and equipment were capable of performing

their intended safety function and to verify that the testing was conducted in accordance

with applicable procedural and TS requirements:

CPS 9015.01, Standby Liquid Control System Operability. (IST)

The inspectors observed selected portions of the test activity to verify that the testing

was accomplished in accordance with plant procedures. The inspectors reviewed the

test methodology and documentation to verify that equipment performance was

consistent with safety analysis and design basis assumptions, and that testing

acceptance criteria were satisfied.

In addition, the inspectors verified that surveillance testing problems were entered into

the licensees corrective action program with the appropriate characterization and

significance. Selected action requests were reviewed to verify that corrective actions

were appropriate and implemented as scheduled.

This inspection constituted one in-service test inspection sample as defined in

IP 71111.22.

b. Findings

No findings of significance were identified.

26 Enclosure

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Evaluation (71114.02)

.1 Alert and Notification System Evaluation

a. Inspection Scope

The inspectors held discussions with Emergency Preparedness (EP) staff regarding

the operation, maintenance, and periodic testing of the Alert and Notification System

(ANS) in the Clinton Power Stations plume pathway Emergency Planning Zone.

The inspectors reviewed monthly trend reports and siren test failure records from

March 2008 through March 2010. Information gathered during document reviews

and interviews was used to determine whether the ANS equipment was maintained

and tested in accordance with Emergency Plan commitments and procedures.

This alert and notification system inspection constituted one inspection sample as

defined in IP 71114.02.

b. Findings

No findings of significance were identified.

1EP3 Emergency Response Organization Augmentation Testing (71114.03)

.1 Emergency Response Organization Augmentation Testing

a. Inspection Scope

The inspectors reviewed and discussed with plant EP staff the Emergency Plan

commitments and procedures that addressed the primary and alternate methods of

initiating an Emergency Response Organization (ERO) activation to augment the on-shift

ERO as well as the provisions for maintaining the ERO emergency telephone book.

The inspectors also reviewed reports and a sample of corrective action program records

of unannounced off-hour augmentation tests, which were conducted from March 2008

through April 2010, to determine the adequacy of post-drill critiques and associated

corrective actions. The inspectors reviewed the EP training records of approximately

63 ERO personnel assigned to key and support positions to determine the status of

their ERO training.

This emergency response organization augmentation testing inspection constituted one

inspection sample as defined in IP 71114.03.

27 Enclosure

b. Findings

Introduction

The inspectors identified a finding of very low safety significance (Green) with an

associated NCV of 10 CFR 50.54(q) for the licensees failure to follow and maintain the

Emergency Plan, which meets the standards in 10 CFR 50.47(b) and the requirements

in Appendix E to 10 CFR 50. Specifically, the licensees Emergency Plan calls for the

performance of periodic drills to evaluate the ability to augment its ERO. However, the

Emergency Plan implementing procedure used for the conduct of these augmentation

drills exempts certain ERO members from participation in these drills, a situation which

prevents the licensee from fully demonstrating its ability to augment all the ERO

positions in a timely manner. The licensees approved Emergency Plan does not

provide for such an exemption.

Description

The Clinton Station Emergency Plan consists of the Exelon Standardized Radiological

Emergency Plan and the Clinton Station Annex. The Emergency Plan is supported by a

series of Emergency Plan implementing procedures and associated program

administrative documents, the intent of which is to provide instructions for the

implementation of the program elements identified in the plan. The standardized

Emergency Plan states that augmentation drills are used to demonstrate the capability

to augment the on-shift staff with a Technical Support Center (TSC), Operations Support

Center (OSC), and Emergency Operating Facility (EOF) in a short period after

declaration of an emergency. Two methods are described in the Emergency Plan:

(1) quarterly unannounced off-hours ERO augmentation drills where no actual travel is

required (call-in), and (2) at least once per drill cycle (every 6 years), an off-hours

unannounced activation of the ERO with actual response to the emergency facilities

(drive-in). The licensees Emergency Plan specifies a minimum ERO staffing that

includes management personnel and skilled/technical personnel. The standardized

Emergency Plan implementing procedure for conducting drills and exercises,

EP-AA-122-1001, Drill and Exercise Scheduling, Development and Conduct,

Attachment 2, states the call-in augmentation drills are intended to demonstrate the

ability to contact selected ERO personnel. Mechanical, electrical, and instrument

maintenance, radiation protection and chemistry are not required to be contacted for the

quarterly call-in augmentation drills. As a result, the call-in quarterly drills do not test all

the positions for the 60-minute response augmentation required staffing. Since

skilled/technical positions are assigned to the Emergency Plans minimum staffing

requirements for the ERO, an augmentation exercise that exempts selected ERO

positions is not an adequate demonstration of the licensees ability to augment the

on-shift staff and activate the emergency response facilities as required by the

Emergency Plan and by planning standards 10 CFR 50.47(b)(2) and

10 CFR 50.47(b)(8). Although the skilled/technical personnel would be required to

participate in the 6-year drive in drill, the licensee has had difficulty in the past with

augmentation during an actual emergency.

28 Enclosure

Analysis

The use of an implementing procedure that causes the conduct of an activity to be

inconsistent with the associated requirements in the licensees Emergency Plan results

in a failure to follow and maintain the Emergency Plan and is a performance deficiency.

As a result of the limitations in the procedure, the licensee failed to conduct call-in drills

to demonstrate timely augmentation of ERO positions filled by skilled/technical

personnel. The deficiency did not impact the NRCs regulatory process or contribute to

actual safety consequences; therefore, the performance deficiency was screened using

the Emergency Preparedness SDP, as a failure to comply.

The deficiency was determined to be of more than minor significance because it

adversely affected the EP cornerstone objective to ensure the licensee is capable of

implementing adequate measures to protect the health and safety of the public in a

radiological emergency. The failure to conduct the augmentation call-in drills in

accordance with the Emergency Plan had the attribute associated with ERO readiness

and in the area of ERO augmentation testing. The inspector evaluated the finding using

the IMC 0609, Appendix B, Sheet I, Failure to Comply Flowchart. The licensees

conduct of augmentation drills failed to comply with an Emergency Plan requirement and

was associated with two planning standard requirements for timely augmentation.

Title 10 CFR 50.47(b)(2) required, in part, that timely augmentation of response

capabilities be available. NUREG-0654, Criteria for Preparation and Evaluation of

Radiological Emergency Response Plans and Preparedness in Support of Nuclear

Power Plants, is used by the NRC to evaluate licensee compliance with the regulations

in the absence of an approved alternative. Evaluation criterion II.B.5 required, in part,

the licensee be able to augment on-shift capabilities within a short period after

declaration of an emergency. Title 10 CFR 50.47(b)(8) required that adequate

emergency facilities and equipment are provided and maintained. NUREG-0654

evaluation criterion II.H.4 required that each organization shall provide for timely

activation and staffing of the facilities and centers described in the Plan. These

requirements are applicable to any individual that the licensee assigns to the ERO and

who performs emergency response functions identified in the Emergency Plan.

The inspector evaluated the failure to comply with regulatory requirements and the

standards for ERO augmentation as a degraded planning standard function since the

licensees conduct of the augmentation exercises did not include all ERO positions.

The finding was determined to be of very low safety significance (Green).

Cross-Cutting Aspects

The inspector determined the finding had a cross-cutting aspect in the problem

identification and resolution area with a component in self and independent

assessments. The licensees augmentation call-in drills were not comprehensive to

include all ERO augmentation staffing positions. (IMC 0310 P.3(a))

29 Enclosure

Enforcement

Title 10 CFR 50.54(q) required, in part, the licensee to follow and maintain in effect

Emergency Plans which meet the standards in section 50.47(b).

Title 10 CFR 50.47(b)(2), required, in part, timely augmentation of response capabilities

is available in key functional areas. The Exelon Standardized Radiological Emergency

Plan required, in part, augmentation drills to demonstrate the capability of the process to

augment the on-shift staff with a TSC, OSC, and EOF through quarterly unannounced

off-hours ERO augmentation call-in drills.

Contrary to the above, the licensee failed to follow and maintain in effect Emergency

Plans which meet the standards in § 50.47(b) and the requirements in Appendix E to

10 CFR 50, in that the conduct of augmentation drills did not meet the requirement in the

licensees Emergency Plan because the licensee exempted certain members of the

ERO from participation. Because the violation was of very low safety significance and

was entered into the licensees corrective action program as AR 01057263, the violation

is being treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement

Policy (NCV 05000461/2010003-04, Inadequate Emergency Plan Augmentation

Call-In Drills).

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

.1 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The inspectors conducted a review of all the emergency action level changes and

sampled the revisions to the Emergency Plan to evaluate whether the changes

identified in the revisions may have decreased the effectiveness of the Emergency Plan.

The inspection included a review of the 10 CFR 50.54(q) change process

documentation. Since the last NRC Emergency Plan change inspection and in

accordance with 10 CFR 50.54(q), the Radiological Emergency Plan Annex for Clinton

Station, Revision 15, was implemented based on the licensees determination that the

changes resulted in no decrease in effectiveness of the Emergency Plan and the revised

Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to

10 CFR 50. The NRC review of the revisions does not constitute formal approval of the

changes; therefore, the emergency action level and Emergency Plan changes remain

subject to future NRC inspection in their entirety.

This emergency action level and Emergency Plan changes inspection constituted one

inspection sample as defined in IP 71114.04.

b. Findings

No findings of significance were identified.

30 Enclosure

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

.1 Correction of Emergency Preparedness Weaknesses and Deficiencies

a. Inspection Scope

The inspectors reviewed a sample of the Nuclear Oversight staffs 2008 and 2009 audits

of the Clinton Power Station Emergency Preparedness Program to determine if the

independent assessments met the requirements of 10 CFR 50.54(t). The inspectors

also reviewed critique reports and samples of corrective action program records

associated with the 2009 biennial exercise, as well as various EP drills conducted in

2008 and 2009, in order to determine that the licensee fulfilled the drill commitments and

to evaluate the licensees efforts to identify, track, and resolve concerns. Additionally,

the inspectors reviewed a sample of corrective actions related to the EP Program and

activities to determine whether corrective actions were completed in accordance with the

sites corrective action program.

This correction of emergency preparedness weaknesses and deficiencies inspection

constituted one inspection sample as defined in IP 71114.05.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a full scale emergency preparedness exercise

on May 19, 2010, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities. This drill was

planned to be evaluated and was included in performance indicator data regarding drill

and exercise performance. The inspectors observed emergency response operations in

the Operations Simulator and Technical Support Center to determine whether the event

classification, notifications, and protective action recommendations were performed in

accordance with procedures. The inspectors also attended the licensees drill critique to

compare any inspector-observed weaknesses with those identified by the licensees staff

in order to evaluate the critique and to verify whether the licensees staff was properly

identifying weaknesses and entering them into the corrective action program.

This inspection constituted one emergency preparedness drill evaluation inspection

sample as defined in IP 71114.06.

b. Findings

No findings of significance were identified.

31 Enclosure

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

This inspection constituted one radiological hazard assessment and exposure control

inspection sample as defined in IP 71124.01.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed all licensee performance indicators for the Occupational

Exposure Cornerstone for follow-up. The inspectors reviewed the results of Radiation

Protection Program audits (e.g., licensees quality assurance audits or other

independent audits). The inspectors reviewed any reports of operational occurrences

related to occupational radiation safety since the last inspection. The inspectors

reviewed the results of the audit and operational report reviews to gain insights into

overall licensee performance.

b. Findings

No findings of significance were identified.

.2 Radiological Hazard Assessment (02.02)

a. Inspection Scope

The inspectors determined if there have been changes to plant operations since the last

inspection that may result in a significant new radiological hazard for onsite workers or

members of the public. The inspectors determined whether the licensee assessed the

potential impact of these changes and has implemented periodic monitoring, as

appropriate, to detect and quantify the radiological hazard.

The inspectors reviewed the last two radiological surveys from three selected plant

areas. The inspectors evaluated whether the thoroughness and frequency of the

surveys were appropriate for the given radiological hazard.

The inspectors selected three air sample survey records and determined whether

the samples were collected and counted in accordance with license procedures.

The inspectors observed work in potential airborne areas and evaluated whether the air

samples were representative of the breathing air zone. The inspectors evaluated

whether continuous air monitors were located in areas with low background to minimize

false alarms and were representative of actual work areas. The inspectors determined

whether the licensee had a program for monitoring levels of loose surface contamination

in areas of the plant with the potential for the contamination to become airborne.

b. Findings

No findings of significance were identified.

32 Enclosure

.3 Instructions to Workers (02.03)

a. Inspection Scope

The inspectors selected five containers holding nonexempt licensed radioactive

materials that may cause unplanned or inadvertent exposure of workers, and assessed

whether the containers were labeled and controlled in accordance with 10 CFR 20.1904,

Labeling Containers, or met the requirements of 10 CFR 20.1905(g).

The inspectors reviewed selected occurrences where a workers electronic personal

dosimeter noticeably malfunctioned or alarmed. The inspectors evaluated whether

workers responded appropriately to the off-normal condition. The inspectors assessed

whether the issue was included in the corrective action program and dose evaluations

were conducted as appropriate.

The inspectors determined whether, for selected work activities, the licensee had

established a means to inform workers of changes in work area conditions that could

significantly impact their occupational dose.

b. Findings

No findings of significance were identified.

.4 Contamination and Radioactive Material Control (02.04)

a. Inspection Scope

The inspectors observed locations where the licensee monitors potentially contaminated

material leaving the radiologically controlled area (RCA), and inspected the methods

used for control, survey, and release from these areas. The inspectors observed the

performance of personnel surveying and releasing material for unrestricted use and

evaluated whether the work was performed in accordance with plant procedures. The

inspectors also reviewed whether the procedures were sufficient to control the spread of

contamination and prevent unintended release of radioactive materials from the site.

The inspectors assessed whether the radiation monitoring instrumentation had

appropriate sensitivity for the type(s) of radiation present.

The inspectors reviewed the licensees criteria for the survey and release of potentially

contaminated material. The inspectors evaluated whether there was guidance on how to

respond to an alarm that indicates the presence of licensed radioactive material.

The inspectors reviewed the licensees procedures and records to determine whether

the radiation detection instrumentation was used at its typical sensitivity level based on

appropriate counting parameters. The inspectors assessed whether or not the licensee

has established a de facto release limit by altering the instruments typical sensitivity

through such methods as raising the energy discriminator level or locating the instrument

in a high-radiation background area.

The inspectors selected three sealed sources from the licensees inventory records and

assessed whether the sources were accounted for and verified to be intact (i.e., they

were not leaking their radioactive content).

33 Enclosure

The inspectors determined whether any transactions, since the last inspection,

involving nationally tracked sources, required reporting or were reported in accordance

with 10 CFR 20.2207.

b. Findings

No findings of significance were identified.

.5 Radiological Hazards Control and Work Coverage (02.05)

a. Inspection Scope

The inspectors examined the licensees physical and programmatic controls for highly

activated or contaminated materials (nonfuel) stored within spent fuel and other storage

pools. The inspectors assessed whether appropriate controls (i.e., administrative and

physical controls) were in place to preclude inadvertent removal of these materials from

the pool.

The inspectors inspected the posting and physical controls for selected high radiation

areas (HRAs) and very high radiation areas (VHRAs), to verify conformance with the

Occupational Exposure Control Effectiveness Performance Indicator.

b. Findings

No findings of significance were identified.

.6 Risk-Significant High Radiation Area and Very High Radiation Area (VHRA) Controls

(02.06)

a. Inspection Scope

The inspectors evaluated licensee controls for VHRAs and areas with the potential to

become a VHRA, and ensured that an individual was not able to gain unauthorized

access to VHRAs.

b. Findings

No findings of significance were identified.

.7 Radiation Worker Performance (02.07)

a. Inspection Scope

The inspectors reviewed 10 radiological problem reports since the last inspection that

found the cause of the event to be human performance errors. The inspectors evaluated

whether there was an observable pattern traceable to a similar cause. The inspectors

assessed whether this perspective matched the corrective action approach taken by the

licensee to resolve the reported problems. The inspectors discussed with the Radiation

Protection Manager any problems with the corrective actions planned or taken.

34 Enclosure

b. Findings

No findings of significance were identified.

.8 Radiation Protection Technician Proficiency (02.08)

a. Inspection Scope

The inspectors reviewed 10 radiological problem reports since the last inspection that

found the cause of the event to be radiation protection technician error. The inspectors

evaluated whether there was an observable pattern traceable to a similar cause. The

inspectors assessed whether this perspective matched the corrective action approach

taken by the licensee to resolve the reported problems.

b. Findings

No findings of significance were identified.

.9 Problem Identification and Resolution (02.09)

a. Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensees corrective action program. The

inspectors assessed the appropriateness of the corrective actions for a selected sample

of problems documented by the licensee that involve radiation monitoring and exposure

controls. The inspectors assessed the licensees process for applying operating

experience to its plant.

b. Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

2RS7 Radiological Environmental Monitoring Program and Radioactive Material Control

Program (71124.07)

This inspection constituted one Radiological Environmental Monitoring Program and

Radioactive Material Control Program inspection sample as defined in IP 71124.07.

.1 Inspection Planning (02.01)

a. Inspection Scope

The inspectors reviewed the annual radiological environmental operating reports and the

results of any licensee assessments since the last inspection, to assess whether the

Radiological Environmental Monitoring Program (REMP) was implemented in

accordance with the TS and the Offsite Dose Calculation Manual (ODCM). This review

included report changes to the ODCM with respect to environmental monitoring,

35 Enclosure

commitments in terms of sampling locations, monitoring and measurement frequencies,

land use census, inter-laboratory comparison program, and analysis of data.

The inspectors reviewed the ODCM to identify locations of environmental monitoring

stations and the UFSAR for information regarding the environmental monitoring program

and meteorological monitoring instrumentation.

The inspectors reviewed quality assurance audit results of the program to assist in

choosing inspection smart samples and audits and technical evaluations performed on

the vendor laboratory program.

The inspectors reviewed the annual effluent release report and the 10 CFR Part 61,

Licensing Requirements for Land Disposal of Radioactive Waste, report, to determine if

the licensee was sampling, as appropriate, for the predominant and dose-causing

radionuclides likely to be released in effluents.

b. Findings

No findings of significance were identified.

.2 Site Inspection (02.02)

a. Inspection Scope

The inspectors walked down five of the air sampling stations and five of the

thermoluminescent dosimeter (TLD) monitoring stations to determine whether they were

located as described in the ODCM and to determine the equipment material condition.

The air sampling stations were selected based on operability history and included those

located in areas of highest effluent deposition based on historical meteorological

conditions (X/Q, D/Q wind sectors). Dosimeter monitoring stations were selected based

on the most risk-significant locations (e.g., those that have the highest potential for

public dose impact). The inspectors reviewed the calibration and maintenance records

of several environmental air samplers including those observed during the walkdowns.

The records were reviewed to determine whether the equipment was adequately

maintained consistent with the licensees procedures. The inspectors determined

whether the licensee initiated sampling of other appropriate media upon loss of a

required sampling station, if applicable.

The inspectors observed the collection and preparation of two environmental samples

from different environmental media (e.g., ground and surface water, milk, vegetation,

sediment, and soil) as available to assess whether the environmental sampling was

representative of the release pathways as specified in the ODCM and that sampling

techniques were in accordance with procedures.

Based on direct observation and review of records, the inspectors evaluated whether

the meteorological instruments were operable, calibrated, and maintained in

accordance with guidance contained in the UFSAR, NRC Regulatory Guide 1.23,

Meteorological Monitoring Programs for Nuclear Power Plants, and licensee

procedures. The inspectors also evaluated whether the meteorological data readout and

recording instruments in the control room and, if applicable, at the tower were operable.

36 Enclosure

The inspectors assessed whether missed and/or anomalous environmental

samples were identified and reported in the annual environmental monitoring report.

The inspectors selected four events that involved a missed sample, inoperable sampler,

lost TLD, or anomalous measurement to evaluate whether the licensee identified the

cause and implemented corrective actions. The inspectors reviewed the licensees

assessment of any positive sample results (i.e., licensed radioactive material detected

above the lower limits of detection (LLDs) and reviewed the associated radioactive

effluent release data that was the source of the released material.

Inspectors selected three SSCs that involve or could reasonably involve licensed

material for which there is a credible mechanism for licensed material to reach ground

water, and assessed whether the licensee implemented a sampling and monitoring

program sufficient to detect leakage of these SSCs to ground water.

The inspectors reviewed historical records required by 10 CFR 50.75(g) of leaks, spills,

and remediation to assess the adequacy of the informational content and its

retrievability.

The inspectors reviewed significant changes made by the licensee to the ODCM as the

result of changes to the land census, revised deposition calculations and/or changes in

assessed meteorological conditions or sampler stations since the last inspection.

The inspectors reviewed technical justifications for any changed sampling locations to

determine whether the licensee performed the required reviews to ensure that the

changes did not affect the licensees ability to monitor the impacts of radioactive effluent

releases on the environment.

The inspectors determined if ODCM required detection sensitivities were met for various

sample media (i.e., the samples meet required LLDs). The inspectors reviewed the

results of the vendor analytical laboratory quality control program, including the

inter-laboratory comparison program, to determine the adequacy of the environmental

sample analyses provided by the vendor.

b. Findings

No findings of significance were identified.

.3 Identification and Resolution of Problems (02.03)

a. Inspection Scope

The inspectors reviewed various corrective action program documents to determine

whether problems associated with the REMP were being identified by the licensee at an

appropriate threshold. Additionally, the inspectors determined whether the corrective

actions for a selected sample of REMP related problems documented by the licensee

were adequately evaluated and resolved.

b. Findings

No findings of significance were identified.

37 Enclosure

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Review of Submitted Quarterly Data

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the First

Quarter 2010 Performance Indicators for any obvious inconsistencies prior to its public

release in accordance with IMC 0608, "Performance Indicator Program."

This inspection was not considered to be an inspection sample as defined in IP 71151.

b. Findings

No findings of significance were identified.

.2 Safety System Functional Failures

a. Inspection Scope

The inspectors reviewed a previously identified issue with respect to the identification

and reporting of an event under the Safety System Functional Failure Performance

Indicator.

This inspection was not considered to be an inspection sample as defined in IP 71151.

b. Findings

In September 2009, the inspectors identified that floor drains in the RHR A Pump Room

and the Radwaste Pipe Tunnel were interconnected, which resulted in the plant being in

an unanalyzed condition that could have prevented fulfillment of the safety function of

the ECCS. The inspectors opened URI 05000461/2009004-01 to review the licensees

evaluation of the condition. This issue is further discussed in Section 1R06.1 of this

inspection report.

In its evaluation of the unanalyzed condition, the licensee concluded that it was not

reportable to the NRC under the requirement of 10 CFR 50.73(a)(2)(v) as a condition

that could have prevented the fulfillment of the safety function of structures or systems

that are needed to mitigate the consequences of an accident and, therefore, did not

count it as an occurrence under the performance indicator. During this inspection

period, the inspectors reviewed the licensees evaluation and determined that the

unanalyzed condition met the 10 CFR 50.73(a)(2)(v)(D) reporting criterion and

documented a Severity Level IV non-cited violation of 10 CFR 50.73(a)(1),

Licensee Event Report System, because the licensee had failed to submit a required

LER within 60 days after discovery of the condition. Therefore, the licensee should also

have counted the event as an occurrence under the Safety System Functional Failure

Performance Indicator.

38 Enclosure

The inspectors noted that the performance indicator was at two occurrences during the

Fourth Quarter 2009 and First Quarter 2010, with the Green-to-White threshold at six

occurrences. One additional occurrence would not cause the performance indicator to

change color. Therefore, the inspectors concluded that the licensees failure report this

additional occurrence under the Safety System Functional Failure Performance Indicator

constituted a violation of 10 CFR 50.9, Completeness and Accuracy of Information,

of minor significance and is not subject to enforcement action in accordance with the

NRCs Enforcement Policy. The licensee entered this violation into its corrective action

program as AR 01080117.

.3 Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Specific Activity Performance

Indicator from the Third Quarter 2009 through the Second Quarter 2010. To determine

the accuracy of the performance indicator data reported during those periods,

performance indicator definitions and guidance contained in Nuclear Energy Institute

(NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,

dated October 2009, were used. The inspectors reviewed the licensees RCS chemistry

samples, TS requirements, action requests, event reports, and NRC Integrated

Inspection Reports for the period of August 2009 through May 2010, to validate the

accuracy of the submittals. The inspectors also reviewed the licensees corrective action

program database to determine if any problems had been identified with the data

collected or transmitted for this performance indicator. In addition to record reviews, the

inspectors observed a chemistry technician obtain and analyze a RCS sample.

This inspection constituted one RCS Specific Activity Performance Indicator inspection

sample as defined in IP 71151.

b. Findings

No findings of significance were identified.

.4 Drill/Exercise Performance

a. Inspection Scope

The inspectors sampled the licensee submittals for the Drill/Exercise Performance

Indicator for the Fourth Quarter 2009. To determine the accuracy of the performance

indicator data reported during those periods, performance indicator definitions and

guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, dated October 2009, were used. The inspectors verified the

accuracy of the number of reported drill and exercise opportunities and the licensees

critiques and assessments for timeliness and accuracy of the opportunities. The

inspectors reviewed the licensees documentation for control room simulator training

sessions, the 2009 biennial exercise, and other designated drills to validate the accuracy

of the submittals.

This inspection constituted one Drill/Exercise Performance Indicator inspection sample

as defined in IP 71151.

39 Enclosure

b. Findings

No findings of significance were identified.

.5 Emergency Response Organization Drill Participation

a. Inspection Scope

The inspectors sampled the licensee submittals for the ERO Drill Participation

Performance Indicator for the Fourth Quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors

reviewed the licensees records and ERO roster to validate the accuracy of the

submittals for the number of ERO members assigned to fill key positions and the

percentage of ERO members who had participated in a performance enhancing drill or

exercise.

This inspection constituted one ERO Drill Participation Performance Indicator inspection

sample as defined in IP 71151.

b. Findings

No findings of significance were identified.

.6 Alert and Notification System

a. Inspection Scope

The inspectors sampled the licensee submittals for the Alert and Notification System

Performance Indicator for the Fourth Quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6, dated October 2009, were used. The inspectors

reviewed the records of the licensees reported number of successful siren operability

tests as compared to the number of siren tests conducted during the reporting period to

validate the accuracy of the submittals.

This inspection constituted one Alert and Notification System inspection sample as

defined in IP 71151.

b. Findings

No findings of significance were identified.

40 Enclosure

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify that they were

being entered into the licensees corrective action program at an appropriate threshold,

that adequate attention was being given to timely corrective actions, and that adverse

trends were identified and addressed. Some minor issues were entered into the

licensees corrective action program as a result of the inspectors observations; however,

they are not discussed in this report.

This inspection was not considered to be an inspection sample as defined in IP 71152.

b. Findings

No findings of significance were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors reviewed repetitive or closely-related issues documented in the

licensees corrective action program to look for trends not previously identified. The

inspectors also reviewed action requests regarding licensee-identified potential trends to

verify that corrective actions were effective in addressing the trends and implemented in

a timely manner commensurate with the significance.

This inspection constituted one semi-annual trend review inspection sample as defined

in IP 71152.

b. Assessment and Observations

(1) Overall Effectiveness of Trending Program

The inspectors determined that the licensees trending program was generally effective

at identifying, monitoring, and correcting adverse performance trends. The inspectors

reviewed several common cause evaluations performed by the licensee to evaluate

potential adverse performance trends. In general, these common cause evaluations

were performed well and identified appropriate corrective actions to address adverse

trends that were identified. The inspectors did not identify any adverse trends that were

not already identified by the licensee and entered into its corrective action program.

(2) Adverse Trend in Human Performance

From the most recent refueling outage, C1R12, the inspectors noted that there were a

high number of human performance related prompt investigations initiated by the

licensee.

41 Enclosure

The licensee performed a common cause evaluation, AR 01066830-02, on the subject of

human performance/technical human performance for C1R12. In this evaluation, the

licensee reviewed 24 different corrective action program products, which contained

human performance related issues. In the evaluation, the licensee concluded that the

common cause of C1R12 human performance events was inaccurate risk perception by

the supplemental workforce and a willingness to proceed in the face of uncertainty.

During review of this evaluation, inspectors noted that half of the 24 issues were

attributed to supplemental workers and the other half to station personnel. As a

corrective action to this issue, the licensee implemented a Return to Excellence Plan,

focused upon improvements in plant staff performance. This plan has three

components: technical human performance, online dose, and work management.

The licensee is also taking corrective action to implement technical human performance

training in operations and maintenance due to an Exelon fleet-wide initiative to address

gaps. Sufficient time has not elapsed for the inspectors to evaluate the effectiveness of

these particular corrective actions.

A review of inspection results from the past year revealed five findings documented in

quarterly NRC resident inspection reports with human performance cross-cutting

aspects. This inspection report documents four. Because there are current corrective

actions being implemented and specific human performance issues have been

adequately addressed individually to date, this adverse trend in human performance is

considered to be an observation at this time. The inspectors have noted that since the

refueling outage has completed, there has been a reduction in the number of human

performance related incidents.

.3 Annual In-Depth Review Sample

a. Inspection Scope

The inspectors selected the following action request for in-depth review:

AR 01023530, "Gate Seals Lost During CRVCS [Containment and Reactor

Vessel Control System] System Functional Test."

The inspectors verified the following attributes during their review of the licensee's

corrective actions for the above action request and other related action requests:

Complete and accurate identification of the problem in a timely manner,

commensurate with its safety significance and ease of discovery;

Consideration of the extent of condition, generic implications, common cause and

previous occurrences;

Evaluation and disposition of operability/reportability issues;

Classification and prioritization of the resolution of the problem, commensurate

with safety significance;

Identification of the root and contributing causes of the problem; and

Identification of corrective actions, which were appropriately focused to correct

the problem.

The inspectors discussed the corrective actions and associated action request

evaluations with licensee personnel.

42 Enclosure

This inspection constituted one annual in-depth review inspection sample as defined in

IP 71152.

b. Findings and Observations

(1) Failure to Follow Procedure Resulting in 46,500 Gallons of Leakage Into Reactor Cavity

Introduction

A finding of very low safety significance (Green) with an associated NCV of 10 CFR 50,

Appendix B, Criteria V, Instructions, Procedures, and Drawings, was self-revealed on

January 29, 2010, when the dryer cavity gate seal depressurized during the performance

of the containment and reactor vessel isolation functional surveillance procedure. When

the seal lost pressure, approximately 46,500 gallons of water leaked from the dryer

cavity pool into the reactor cavity.

Discussion

During the refueling outage on January 29, 2010, the licensee performed surveillance

procedure CPS 9601.04, Containment Drywell Isolation Auto Actuation. During this

procedure an isolation signal is generated, which causes the isolation of some primary

containment penetrations, including the service air, to containment. When this occurred,

the dryer cavity gate seal should have transferred to the backup air supply bottles, but

instead, began to leak water when service air was lost. The total amount of leakage due

to this event was approximately 46,500 gallons from the dryer cavity pool into the reactor

cavity. In addition, a large amount of this water subsequently leaked past the drywell

head, down into the drywell, and onto the drywell floor at the bottom of containment.

The licensee performed Root Cause Report #01023530-16 to determine the cause of

the failure of the dryer cavity gate seal to transfer to the backup air supply bottles.

During the licensees evaluation of the event, it was discovered that the proper valve

operation sequence had not been followed when the gate seal inflation procedure was

performed. Specifically, while performing CPS 8117.11, Installation and Removal of

Upper Containment and Fuel Building Gates, both the inflate position valve levers

were positioned before the regulator pressures were adjusted, which was contrary to the

sequence specified by procedure CPS 8117.11. The Reactor Services maintenance

craftsman performing the procedure noted that he was not able to lower the regulator

setting below 48 pounds-per-square-inch gage (psig). At that time, he also noted that

this value of 48 psig was within the accuracy of the gage for 45 psig, and he, therefore,

concluded that it was acceptable. However, because the procedure steps had been

performed out of sequence, backpressure from the normal service air header was

actually indicated on the backup air bottle pressure regulator gage, and not the air

pressure supplied from the backup air bottles. The craftsman stated that he attempted

to adjust the regulator pressure, but that he was unable to lower the indicated pressure

below 48 psig. The craftsman was interviewed and asked why the inflation valves were

opened before the regulators were both set. The answer provided was that the inflation

valves were opened first because they were in the cabinet and he would not have to

come back to the cabinet after setting the backup supply bottle pressure.

This event resulted in a loss of inventory from the dryer cavity pool and partial flooding of

the lower reactor cavity. In addition, due to excess water leakage into the drywell, the

drywell drains backed up onto the drywell floor. Increased dose was received by outage

43 Enclosure

personnel to allow time to drain the water and attempt to re-perform cavity

decontamination. Additional dose was received for work added for the reassembly of

the reactor vessel and removal of the reactor head from the flange to clean and

re-inspect the O-rings due to potential wetting from the leakage. An additional concern

during this event was the potential to create airborne contamination in containment due

to the dryer cavity pool walls being highly contaminated and their potential drying out

due to lower pool levels.

The inspectors thoroughly examined the licensees root cause evaluation and concluded

that the licensee had not neglected any significant issues. The licensee concluded that

the root cause was the failure of the Reactor Services maintenance craftsman to follow

the correct sequence of procedural steps to properly align the backup air supply bottles

for the dryer cavity gate seal. The inspectors concluded that the corrective actions taken

by the licensee in response to the documented causes appeared to be appropriate.

Analysis

The inspectors determined that the licensees failure to correctly install the upper

containment dryer cavity gate in accordance with the licensees prescribed procedures

was a performance deficiency warranting a significance evaluation. The inspectors

assessed this finding using the SDP. The inspectors reviewed the examples of minor

issues in IMC 0612, Power Reactor Inspection Reports, Appendix E, Examples of

Minor Issues, and determined that Example 4c was related to this issue in that data

recorded during installation of the dryer cavity gate seal was incorrect and resulted in

backup air bottle supply pressure left outside the acceptable range. In addition,

consistent with the guidance in IMC 0612, Appendix B, Issue Screening, the inspectors

determined that the licensees failure to correctly install the upper containment dryer

cavity gate could be reasonably viewed as a precursor to a significant event and, if left

uncorrected, would potentially lead to a more significant safety concern (i.e., increased

dose or personnel contamination). Therefore, the inspectors concluded that this finding

was of more than minor safety significance. Because the dryer cavity gate seal is

intended to contain highly radioactive fluids within containment, which supports the

radiological barrier functions to protect plant workers and the public following serious

transients or accidents, the inspectors concluded that this issue was associated with the

Barrier Integrity Cornerstone. The inspectors performed a Phase 1 SDP review of this

finding using the guidance provided in IMC 0609 Appendix G, Shutdown Operations

Significance Determination Process, Attachment 1, Significance Determination Process

Phase 1 Operational Checklists for Both PWRs and BWRs, Checklist 6, BWR Cold

Shutdown or Refueling Operation - Time to Boil < 2 Hours: RCS Level < 23 Above Top

of Flange, and determined that Item II.B.(1), Inventory Control Guidelines, Procedures,

was not being met due to the performance deficiency. However, because there was no

increase in the likelihood of a loss of RCS inventory and the issue could not result in the

loss of RCS level instrumentation, the finding did not require a quantitative Phase 2 or

Phase 3 analysis and could, therefore, be screened as very low safety significance

(Green).

Cross-Cutting Aspects

The inspectors concluded that this finding affected the cross-cutting area of human

performance. Specifically, licensee personnel work practices did not support successful

human performance. The licensee's Root Cause Report described the root cause as the

44 Enclosure

maintenance craftsman performed steps out of sequence and failed to comply with the

procedure. Therefore, as concluded by the Root Cause Report, in this instance, the

licensee did not effectively communicate expectations regarding procedural compliance

and, as a result, the Reactor Services maintenance craftsman did not correctly follow the

procedure by performing steps out of sequence and restoring a system to service that

was incorrectly aligned. (IMC 0310 H.4(b))

Enforcement

Title 10 CFR 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings

required, in part, that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances and

shall be accomplished in accordance with these instructions, procedures, or drawings.

Contrary to the above, on January 29, 2010, the licensee failed to accomplish

CPS 8117.11, Installation and Removal of Upper Containment and Fuel Building Pool

Gates, Revision 8, in accordance with the procedure. Specifically, the licensee failed to

adhere to the correct sequence of procedural steps to properly align the backup air

supply bottles for the dryer cavity gate seal. Because of the very low safety significance,

this violation is being treated as a NCV consistent with Section VI.A of the NRC

Enforcement Policy (NCV 05000461/2010003-05, Failure to Follow Procedure

Resulting in Gate Seal Leakage). The licensee entered this violation into its corrective

action program as AR 00969157.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) LER 05000461/2008-003-00, Excessive Leakage Through Feedwater Isolation

Valve 1B21F032A

On January 28, 2008, a local leak rate test (LLRT) performed on feedwater primary

containment isolation check valve 1B21F032A failed the acceptance criterion in

TSSR 3.6.1.3.11. The licensee performed maintenance on the valve and retested it

satisfactorily. During the root cause evaluation of an LLRT failure for the opposite train

feedwater primary containment isolation check valve (1B21F032B) during the Cycle 12

refueling outage in January 2010, the licensee recognized that an LER was never

submitted to report the 1B21F032A test failure two years before. The licensee

subsequently reported the 1B21F032A test failure as a condition that resulted in the

nuclear power plant being in an unanalyzed condition that significantly degraded plant

safety in accordance with 10 CFR50.73(b)(3)(ii), and as a condition that could have

prevented the fulfillment of the safety function of structures or systems needed to

control the release of radioactive material and mitigate the consequences of an accident

in accordance with 10 CFR 50.73(a)(2)(v). A licensee-identified NCV of

10 CFR 50.73(a)(1) for the licensees failure to submit a required LER within 60 days

after discovery of the 1B21F032A LLRT failure is discussed Section 4OA7.1 of this

inspection report.

During review of the LER, the inspectors identified that the licensee did not report this

event as an operation or condition prohibited by the plants TSs in accordance with

10 CFR 50.73(a)(2)(i)(B). The inspectors reviewed the reporting guidance in

NUREG-1022, Event Reporting Guidelines - 10 CFR 50.72 and 50.73, Revision 2, and

noted that an operation or condition prohibited by the TSs existed and is reportable if

45 Enclosure

surveillance testing indicates that equipment was not capable of performing its specified

safety function (and was thus inoperable) for a period of time longer than allowed by

TSs. NUREG-022 further states that for testing conducted within the required

surveillance interval, it should be assumed that the discrepancy occurred at the time of

its discovery unless there is firm evidence, based on a review of relevant information

such as the equipment history and the cause of failure, to indicate that the discrepancy

existed previously. The licensee entered this minor reporting issue into its corrective

action program as AR 01076505.

The licensee performed a root cause evaluation following the 1B21F032B valve test

failure and determined the cause of the failure of both check valves to satisfy the

minimum leakage acceptance criterion was age-related degradation of lubrication on the

valve actuator, causing increased friction. Based on the cause determination, the

inspectors concluded that this valve had not been capable of performing its specified

safety function (and thus was inoperable) for a period of time before its discovery longer

than allowed by TS 3.6.1.3. A licensee-identified NCV of TS 3.6.1.3 for operating with

1B21F032A inoperable as a result of the licensees failure to implement appropriate

preventive maintenance is discussed in Section 4OA7.2 of this inspection report. As a

corrective action, the licensee implemented a preventive maintenance task to clean and

re-lubricate the valve actuator during refueling outages.

Licensee Event Report 05000461/2008-003-00 is closed.

This inspection constituted one event follow-up inspection sample as defined in

IP 71153.

.2 (Closed) LER 05000461/2010-002-00, Excessive Leakage Through Feedwater Isolation

Valve 1B21F032B

On February 3, 2010, after Unit 1 had entered Mode 2 during plant startup from the

C1R12 refueling outage, the licensee identified that the LLRT performed on feedwater

containment isolation check valve 1B21F032B had failed the acceptance criterion in

TSSR 3.6.1.3.11. This was discovered by a plant engineer during review of the LLRT

test package. Technical Specification Surveillance Requirement 3.6.1.3.11 required that

the combined leakage rate for both primary containment feedwater penetrations be less

than or equal to 2.0 gpm. The measured leakage rate for the penetration with

1B21F032B was 2.5 gpm. Operators performing the test on January 19, 2010, and the

senior reactor operator reviewing the completed test package upon completion did not

recognize that the TSSR acceptance criterion was not met because the acceptance

criterion was not stated in the surveillance test procedure. The licensee returned the

unit to Mode 4 to perform maintenance on 1B21F032B and to re-test it. The

motor-operated feedwater primary containment isolation valve (1B21F065B) in the

affected flow path was closed prior to plant startup and had remained closed; therefore,

the containment penetration flow path was isolated and no actual leakage path existed.

The licensee reported this valve test failure as a condition that resulted in the nuclear

power plant being in an unanalyzed condition that significantly degraded plant safety in

accordance with 10 CFR50.73(b)(3)(ii), and as a condition that could have prevented the

fulfillment of the safety function of structures or systems needed to control the release of

radioactive material and mitigate the consequences of an accident in accordance with

10 CFR 50.73(a)(2)(v).

46 Enclosure

The inspectors identified during review of the LER that the licensee did not report this

event as an operation or condition prohibited by the plants TSs in accordance with

10 CFR 50.73(a)(2)(i)(B). The inspectors reviewed the reporting guidance in

NUREG-022, Event Reporting Guidelines - 10 CFR 50.72 and 50.73, Revision 2, and

noted that an operation or condition prohibited by the TSs existed and is reportable if

surveillance testing indicates that equipment was not capable of performing its specified

safety function (and was thus inoperable) for a period of time longer than allowed by the

TSs. NUREG-022 further states that for testing conducted within the required

surveillance interval, it should be assumed that the discrepancy occurred at the time of

its discovery unless there is firm evidence, based on a review of relevant information

such as the equipment history and the cause of failure, to indicate that the discrepancy

existed previously. The licensee entered this minor reporting issue into its corrective

action program as AR 01076505.

The licensee performed a root cause evaluation and determined the cause for the failure

was age-related degradation of lubrication on the valve actuator, causing increased

friction. No preventive maintenance had been performed on the valve actuator. It was

discovered that the lubrication had dried or hardened, causing the valve actuator to bind

and not allow the check valve to fully seat. Based on the cause determination, the

inspectors concluded that this valve had not been capable of performing its specified

safety function (and thus was inoperable) for a period of time before its discovery longer

than allowed by TS 3.6.1.3. A licensee-identified NCV of TS 3.6.1.3 for operating with

1B21F032B inoperable as a result of the licensees failure to implement appropriate

preventive maintenance is discussed in Section 4OA7.3 of this inspection report. As a

corrective action, the licensee implemented a preventive maintenance task to clean and

re-lubricate the valve actuator during refueling outages.

A licensee-identified NCV of 10 CFR 50, Appendix B, Criteria V, Instructions,

Procedures, and Drawings for the licensees failure to provide appropriate quantitative

or qualitative acceptance criteria in CPS 9861.05D014, LLRT Data Sheet for 1MC010,

Revision 2, is discussed in Section 4OA7.4 of this inspection report.

LER 05000461/2010-002-00 is closed.

This inspection constituted one event follow-up inspection sample as defined in

IP 71153.

.3 (Closed) LER 05000461/2010-001-00, Unanalyzed Leakage Pathway Affecting

Residual Heat Removal A Pump Room Flooding Analysis

During review of plant drawings for floor drain system piping in the ECCS and RCIC

Pump Rooms on the 7070 elevation of the Auxiliary Building, the inspectors identified

that floor drains in the RHR A Pump Room appeared to be connected via permanent

4-inch pipe embedded in the floor to floor drains in the Radwaste Pipe Tunnel. The

inspectors noted that each of the separate pump rooms was supposedly designed to be

isolated from other areas of the plant and not susceptible to flooding from sources

external to the pump rooms.

In its evaluation of the unanalyzed condition, the licensee concluded that the condition

was not reportable to the NRC under the requirements of 10 CFR 50.73(a)(2)(ii)(B) as a

condition that resulted in the nuclear power plant being in an unanalyzed condition that

significantly degraded plant safety, and 10 CFR 50.73(a)(2)(v)(D) as a condition that

47 Enclosure

could have prevented the fulfillment of the safety function of structures or systems

needed to mitigate the consequences of an accident. The inspectors questioned this

conclusion and maintained an Unresolved Item open to review the reporting

requirements. The licensee wrote AR 01031977 to address the open questions and

subsequently submitted this voluntary LER.

The inspectors reviewed LER 05000461/2010-001-00 and did not concur with the

licensees conclusion that the reporting criteria were not met. As discussed in

Section 1R06.1.b.(1) of this inspection report, the inspectors determined that the

unanalyzed condition met the 10 CFR 50.73(a)(2)(ii)(B) and 50.73(a)(2)(v)(D) reporting

criteria and documented a Severity Level IV non-cted violation of 10 CFR 50.73(a)(1),

Licensee Event Report System, because the licensee failed to submit a required LER

within 60 days after discovery of a condition that met the above reporting criteria.

No immediate corrective actions were taken to address this finding; however, the

licensee entered this issue into its corrective action program for evaluation.

Licensee Event Report 05000461/2010-001-00 is closed.

This inspection constituted one event follow-up inspection sample as defined in

IP 71153.

.4 Licensee Event Notification 45901, Invalid Actuation of Division 2 Drywell Ventilation

and Drywell Cooling Primary Containment Isolation Valves

On May 5, 2010, the licensee notified the NRC via telephone that the Division 2 Drywell

Ventilation and Drywell Cooling Primary Containment Isolation Valves closed for

isolation Groups 11 and 17. The event occurred on March 15, 2010, at 0136 during full

power operations. The telephone notification was made in accordance with

10 CFR 50.73(a)(1) within the 60-day reporting requirement.

The inspectors reviewed the event notification, prompt investigation, equipment apparent

cause evaluation, and the action request (AR 01042588) documented for the event.

The inspectors also reviewed the associated operability evaluation as an inspection

sample during the first quarter of 2010. The inspectors concluded that the event was

correctly reported in accordance with the requirements. During review of the equipment

apparent cause evaluation, the inspectors noted that although the licensee has

experienced card failures in the past, the corrective actions for the load driver card

failure that caused this event were appropriate and commensurate with the significance

of the equipment failure. There was no performance deficiency of significance identified

with this issue.

This inspection constituted one event follow-up inspection sample as defined in

IP 71153.

4OA5 Other Activities

.1 (Closed) URI 05000461/20100002-07, Main Turbine Trip During On-Line Testing

During the performance of turbine on-line testing following the C1R12 refueling outage

on February 5, 2010, with Unit 1 at about 17 percent power and the main generator

synchronized to the grid, the turbine unexpectedly tripped due to mechanical overspeed.

The turbine mechanical trip device was mis-adjusted during the refueling outage,

48 Enclosure

which caused the turbine trip logic to activate prematurely during plant start-up testing.

The reactor remained on line while troubleshooting the cause for the turbine trip.

The licensee completed repairs and synchronized the unit to the grid on February 8th.

The inspectors opened URI 0500461/2010002-07, pending review of the licensees

cause evaluation of the event, to determine whether there was a performance issue of

more than minor significance.

During this inspection period, the inspectors thoroughly reviewed the licensees root

cause evaluation for the turbine trip event and concluded that the licensee had not

neglected any likely factors. The root cause was determined to be that Turbine Services

personnel had failed to ensure the preferred method of resetting the turbine mechanical

trip finger was used prior to measuring the running gap due to less than adequate work

instructions. This produced an inaccurate gap check when measured and ultimately

resulted in improper gap adjustment.

With the unit at 17 percent power, there was no significant transient on the plant due to

the turbine trip. Therefore, the inspectors concluded that the performance issue was of

minor significance.

Unresolved Item 0500461/2010002-07 is closed.

.2 (Closed) URI 05000461/2009005-02, Standby Gas Treatment System Flow/Heater

Operability Surveillance Test

The inspectors determined that the licensees failure to establish an adequate

surveillance test procedure with appropriate quantitative or qualitative acceptance

criteria to satisfy the monthly standby gas treatment system surveillance testing

requirement in TSSR 3.6.4.3.1 was a finding of very low safety significance (Green).

The inspectors documented a finding with an associated NCV of 10 CFR 50,

Appendix B, Criteria V, Instructions, Procedures, and Drawings, in NRC Inspection

Report 05000461/2010002 (NCV 05000461/2010002-08, Inadequate Test Criteria in

Standby Gas Treatment System Flow/Heater Operability Surveillance Test).

Unresolved Item 0500461/2009005-02 is closed.

.3 (Closed) NRC Temporary Instruction 2515/173 Review of the Industry Ground Water

Protection Voluntary Initiative

a. Inspection Scope

A NRC assessment was performed of the licensees implementation of the Nuclear

Energy Institute - Ground Water Protection Initiative (NEI-GPI) (dated August 2007

(ML072610036)) at Clinton Power Station (CPS). Under the voluntary initiative, each

site was to have developed an effective, technically sound groundwater protection

program that aligned with the NEI initiative by August 2008.

The inspectors assessed whether the licensee evaluated work practices that could

lead to leaks and spills and performed an evaluation of systems, structures, and

components that contain licensed radioactive material to determine potential leak or

spill mechanisms.

49 Enclosure

The inspectors determined if the licensee completed a site characterization of geology

and hydrology to identify the predominant ground water gradients and potential

pathways for ground water migration from onsite to offsite locations. The inspectors also

determined if an onsite ground water monitoring program had been implemented to

monitor for potential licensed radioactive leakage into groundwater and that the licensee

had provisions for the reporting of its ground water monitoring results.

(See http://www.nrc.gov/reactors/operating/ops-experience/tritium/plant-info.html)

The inspectors reviewed the licensees procedures for the decision making process for

potential remediation of leaks and spills, including consideration of the long-term

decommissioning impacts. The inspectors reviewed records of leaks and spills that

were recorded in the licensees decommissioning files to determine if the information

was in accordance with 10 CFR 50.75(g).

The inspectors reviewed the licensees notification protocols to determine whether they

were consistent with the Groundwater Protection Initiative and/or State of Illinois

statutes. The inspectors assessed whether the licensee identified the appropriate local

and state officials and conducted briefings with these officials on its ground water

protection initiative. The inspectors also determined whether protocols were established

for notification of the applicable local and state officials regarding detection of leaks and

spills.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

.1 Resident Inspectors Exit Meeting

The inspectors presented the inspection results to Mr. M. Kanavos and other members

of the licensees staff at the conclusion of the inspection on July 8, 2010. The licensee

acknowledged the findings presented. Proprietary information was examined during this

inspection, but is not specifically discussed in this report.

.2 Interim Exit Meetings

Interim exit meetings were conducted for:

The results of the Radiological Hazards Assessment and Exposure Control

Inspection with Mr. T. Chalmers and other members of the licensees staff on

May 14, 2010. The inspectors confirmed that none of the potential report input

discussed was considered proprietary. Proprietary material received during the

inspection was returned to the licensee.

The results of the Groundwater Protection Initiative and Radiological

Environmental Monitoring Program Inspection with Mr. M. Kanavos and other

members of the licensees staff on June 11, 2010. The inspectors confirmed that

none of the potential report input discussed was considered proprietary.

The results of the Emergency Preparedness Inspection with Mr. M. Kanavos and

other members of the licensees staff on April 16, 2010. The inspectors

50 Enclosure

confirmed that none of the potential report input discussed was considered

proprietary. A subsequent exit meeting with Mr. D. Kemper and other members

of the licensees staff by telephone was held on June 30, 2010.

.3 Regulatory Performance Meeting

On June 2, 2010, the NRC held a meeting with the licensee at the Clinton Power Station

to discuss the Clinton Power Station annual plant performance assessment.

.4 Public Meeting

On June 2, 2010, the NRC held a public open house meeting at the Clinton Elks Lodge

to engage interested members of the public on the performance of the Clinton Power

Station and the role of the NRC in ensuring safe plant operations upon completion of the

Clinton Power Station annual plant performance assessment in accordance with

Section 09.01 of IMC 0305, Operating Reactor Assessment Program.

4OA7 Licensee-Identified Violations

The following violations of very low significance (Green and Severity Level IV) were

identified by the licensee. The violations met the criteria of Section VI of the NRC

Enforcement Policy, for dispositioning as non-cited violations.

.1 Failure to Submit a Required LER

Title 10 CFR 50.73(a)(1) required, in part, that the licensee submit an LER for any event

of the type described in this paragraph within 60 days after the discovery of the event.

Title 10 CFR 50.73(a)(2)(ii) required, in part, that the licensee report any event or

condition that resulted in the nuclear power plant being seriously degraded or in an

unanalyzed condition that significantly degraded plant safety.

Title 10 CFR 50.73(a)(2)(v) required, in part, that the licensee report any event or

condition that could have prevented the fulfillment of the safety function of structures or

systems needed to control the release of radioactive material and mitigate the

consequences of an accident. In addition, 10 CFR 50.73(a)(2)(i)(B) required, in part,

that the licensee report any operation or condition prohibited by the plants TSs.

Contrary to the above, the licensee failed to submit a required LER within 60 days after

discovery of an event on January 28, 2008. The event involved the failure of a primary

containment local leak rate test performed on feedwater system check valve

1B21-F032A. The inspectors determined that this finding was of more than minor

significance because the NRC relies on licensees to identify and report conditions or

events meeting the criteria specified in the TS and the regulations in order to perform its

regulatory function. This is a Severity Level IV violation consistent with Supplement I,

Paragraph D.4, of the NRC Enforcement Policy and is being treated as a NCV

consistent with Section VI.A of the NRC Enforcement Policy. The licensee entered this

violation into its corrective action program as AR 01047133. The licensee subsequently

submitted LER 05000461/2008-003-00 on May 17, 2010. Refer to Section 4OA3.1 of

this inspection report for the review and closure of the LER.

51 Enclosure

.2 Failure to Meet TS 3.6.1.3 for Primary Containment Isolation Valve 1B21F032A

(Train A Feedwater Primary Containment Isolation Check Valve)

Technical Specification 3.6.1.3 required, in part, that each primary containment isolation

valve be operable in Modes 1, 2, and 3. TS 3.6.1.3, Condition C.1 stated that with one

or more penetration flow paths with the leakage rate not within the limit restore the

leakage rate to within the limit within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. Technical Specification 3.6.1.3,

Condition E stated that if the required action and associated completion time of

Condition C is not met, be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Contrary to the above, primary containment isolation valve 1B21F032A was found

with leakage in excess of the limit during testing on January 28, 2008. The licensee

determined the cause for the failure was age-related degradation of lubrication on the

valve actuator, causing increased friction. Based on the cause determination, the

inspectors concluded that this valve had not been capable of performing its specified

safety function (and thus was inoperable) for a period of time before its discovery

longer than allowed by TS 3.6.1.3. The inspectors determined that this violation was

associated with a licensee-identified finding of very low safety significance (i.e., Green)

during a Phase 2 SDP review using the guidance in IMC 0609, Appendix H,

Containment Integrity Significance Determination Process, because the as-found

leakage from the penetration was significantly less than the 1,000% containment volume

per day criterion in Table 6.2, Phase 2 Risk Significance - Type B Findings at Full

Power. The inspectors also noted that multiple barriers exist to a large release through

the feedwater system lines. This violation of TS 3.6.1.3 is being treated as a NCV

consistent with Section VI.A of the NRC Enforcement Policy. The licensee entered this

violation into its corrective action program as AR 01047133. The licensee submitted

LER 05000461/2008-003-00 on May 17, 2010, but did not characterize the event as a

condition prohibited by the plants TSs. The licensee entered this minor reporting issue

into its corrective action program as AR 01076505. Refer to Section 4OA3.1 of this

inspection report for the review and closure of the LER.

.3 Failure to Meet TS 3.6.1.3 for Primary Containment Isolation Valve 1B21F032B

(Train B Feedwater Primary Containment Isolation Check Valve)

Technical Specification 3.6.1.3 required, in part, that each primary containment isolation

valve be operable in Modes 1, 2, and 3. TS 3.6.1.3, Condition C.1 stated that with one

or more penetration flow paths with the leakage rate not within the limit restore the

leakage rate to within the limit within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. Technical Specification 3.6.1.3,

Condition E stated that if the required action and associated completion time of

Condition C is not met, be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Contrary to the above, primary containment isolation valve 1B21F032B was found with

leakage in excess of the limit during testing on January 18, 2010. The licensee

determined the cause for the failure was age-related degradation of lubrication on the

valve actuator, causing increased friction. Based on the cause determination, the

inspectors concluded that this valve had not been capable of performing its specified

safety function (and thus was inoperable) for a period of time before its discovery longer

than allowed by TS 3.6.1.3. The inspectors determined that this violation was

associated with a licensee-identified finding of very low safety significance (i.e., Green)

during a Phase 2 SDP review using the guidance in IMC 0609, Appendix H,

Containment Integrity Significance Determination Process, because the as-found

52 Enclosure

leakage from the penetration was significantly less than the 1,000% containment volume

per day criterion in Table 6.2, Phase 2 Risk Significance - Type B Findings at Full

Power. The inspectors also noted that multiple barriers exist to a large release through

the feedwater system lines. This violation of TS 3.6.1.3 is being treated as a NCV

consistent with Section VI.A of the NRC Enforcement Policy. The licensee entered this

violation into its corrective action program as AR 01025446. The licensee submitted

LER 05000461/2010-002-00 on April 1, 2010, but did not characterize the event as a

condition prohibited by the plants TSs. The licensee entered this minor reporting issue

into its corrective action program as AR 01076505. Refer to Section 4OA3.2 of this

inspection report for the review and closure of the LER.

.4 Inadequate Acceptance Criteria in Surveillance Test Procedure for LLRT of Feedwater

Isolation Check Valves

Title 10 CFR 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings

required that activities affecting quality shall be prescribed by documented instructions,

procedures, or drawings, of a type appropriate to the circumstances and shall be

accomplished in accordance with these instructions, procedures, or drawings.

Instructions, procedures, or drawings shall include appropriate quantitative or qualitative

acceptance criteria for determining that important activities have been satisfactorily

accomplished.

Contrary to the above, on or about January 18, 2010, the licensee failed to provide

appropriate quantitative or qualitative acceptance criteria in surveillance test procedure

CPS 9861.05D014, LLRT Data Sheet for 1MC010, Revision 2, to enable operators

performing testing and evaluating the results of testing for compliance with the limits in

TSSR 3.6.1.3.11, an activity affecting quality, to identify when the testing results

exceeded the limits. Specifically, the procedure did not contain the relevant

acceptance criteria. The inspectors determined that this violation was associated with a

licensee-identified finding of very low safety significance (i.e., Green) during a Phase 2

SDP review using the guidance in IMC 0609, Appendix H, Containment Integrity

Significance Determination Process, because the as-found leakage from the

penetration was significantly less than the 1,000% containment volume per day

criterion in Table 6.2, Phase 2 Risk Significance - Type B Findings at Full Power.

The inspectors also noted that multiple barriers exist to a large release through the

feedwater system lines. This violation is being treated as a NCV consistent with

Section VI.A of the NRC Enforcement Policy. The licensee entered this violation into its

corrective action program as AR 01025446. Refer to Section 4OA3.2 of this inspection

report for the review and closure of the LER.

.5 Failure to Complete an Independent Review of All Program Elements of the Emergency

Preparedness Program

The licensee identified a finding of very low safety significance with an associated

NCV of 10 CFR 50.54(t), Conditions of Licenses, for the failure to complete an

independent review of all program elements of the EP Program. The independent

assessment did not evaluate and document the adequacy of the interfaces with state

and local governments at an interval not to exceed 12 months for all groups. The

Nuclear Oversight Emergency Preparedness Program Audit procedure allowed sampling

and did not require all state and local governments to be evaluated for adequacy of

interfaces. Specifically, Nuclear Oversights assessment failed to evaluate the adequacy

53 Enclosure

of interface with Macon and Piatt Counties in 2008. All required audits were conducted

in 2009 (Dewitt, Macon, McLean, Piatt and the State of Illinois).

The deficiency was screened using the Emergency Preparedness SDP and determined

to be of more than minor significance because the finding was associated with the offsite

attribute of the EP Cornerstone and affected the objective to ensure the licensee is

capable of implementing adequate measures to protect the health and safety of the

public in a radiological emergency. The licensee failed to evaluate the working

relationship and interfaces between the offsite and onsite emergency response

organizations and as a result, failed to conduct an assessment of the overall conduct

and effectiveness of the EP Program. The inspector evaluated the finding using the

IMC 0609, Appendix B, Sheet I, Failure to Comply Flowchart. The audit program was

noncompliant with a regulatory requirement not involving an EP planning standard or a

risk significant planning standard; therefore, the finding was determined to be of very low

safety significance (Green). The licensee entered this violation into its corrective action

program as AR 00889346.

ATTACHMENT: SUPPLEMENTAL INFORMATION

54 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Baker, Design Engineering Senior Manager

R. Campbell, RP Technical Specialist

T. Chalmers, Operations Director

J. Cunningham, Security Manager

A. Darelius, EP Manager

J. Domitrovich, Work Management Director

C. Dunn, Shift Operations Superintendent

S. Fatora, Maintenance Director

R. Frantz, Regulatory Assurance

S. Gackstetter, Training Director

G. Hall, Performance Improvement Program Manager

M. Heger, Mechanical/Structural Design Engineering Manager

N. Hightower, Radiological Engineering Manager

M. Kanavos, Plant Manager

F. Kearney, Site Vice President

D. Kemper, Regulatory Assurance Manager

S. Lakebrink, Mechanical Design Engineering

K. Leffel, Operations Support Manager

S. OReley, EP Coordinator

J. Peterson, Regulatory Assurance

F. Pournia, Engineering Director

J. Rappeport, Chemistry Manager

S. Soliman, Senior Chemist

J. Stovall, Radiation Protection Manager

J. Ufert, Fire Marshall

C. VanDenburgh, Nuclear Oversight Manager

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000461/2010003-01 NCV Failure to Satisfy 10 CFR 50.72 and 50.73 Reporting

Requirements (Section 1R06.b.(1))05000461/2010003-02 NCV Failure to Perform an Adequate 10 CFR 50.59 Evaluation for

CPS Procedure 3711.01 (Section 1R13.b.(1))05000461/2010003-03 FIN Operability Assessment of Inservice Testing Surveillance

Discrepancies for Excess Flow Check Valves

(Section 1R15.b.(1))05000461/2010003-04 NCV Inadequate Emergency Preparedness Augmentation Call-In

Drills (Section 1EP3.1)05000461/2010003-05 NCV Failure to Follow Procedure Resulting in Gate Seal Leakage

(Section 4OA2.3.b.(1))

1 Attachment

Closed

05000461/2009004-01 URI Interconnecting Floor Drains Between the Residual Heat

Removal A Pump Room and Radwaste Pipe Tunnel

(Section 1R06.b.(1))05000461/2010003-01 NCV Failure to Satisfy 10 CFR 50.72 and 50.73 Reporting

Requirements (Section 1R06.b.(1))05000461/2010002-06 URI Questions Regarding 10 CFR 50.59 Evaluation for CPS

Procedure 3711.01 Involving Operations with the Potential to

Drain the Reactor Vessel (Section 1R13.b.(1))05000461/2010003-02 NCV Failure to Perform an Adequate 10 CFR 50.59 Evaluation for

CPS Procedure 3711.01 (Section 1R13.b.(1))05000461/2009003-04 URI Review of Applicability of TSSR 3.0.3 to Multiple Missed

Surveillance Intervals for Excess Flow Check Valves

(Section 1R15.b.(1))05000461/2010003-03 FIN Operability Assessment of Inservice Testing Surveillance

Discrepancies for Excess Flow Check Valves

(Section 1R15.b.(1))05000461/2010003-04 NCV Inadequate Emergency Preparedness Augmentation Call-In

Drills (Section 1EP3.1)05000461/2010003-05 NCV Failure to Follow Procedure Resulting in Gate Seal Leakage

(Section 4OA2.3.b.(1))

05000461/2008-003-00 LER Excessive Leakage Through Feedwater Isolation Valve

1B21F032A (Section 4OA3.1)

05000461/2010-002-00 LER Excessive Leakage Through Feedwater Isolation Valve

1B21F032B (Section 4OA3.2)

05000461/2010-001-00 LER Unanalyzed Leakage Pathway Affecting Residual Heat

Removal A Pump Room Flooding Analysis (Section 4OA3.3)05000461/2010002-07 URI Main Turbine Trip During On-line Testing (Section 4OA5.1)05000461/2009005-02 URI Standby Gas Treatment System Flow/Heater Operability

Surveillance Test (Section 4OA5.2)

2515/173 TI NRC Temporary Instruction 2515/173 Review of the Industry

Ground Water Protection Voluntary Initiative

(Section 4OA5.3)

Discussed

05000461/2010002 03 NCV Unanalyzed Condition of Interconnecting Floor Drains

Between the RHR A Pump Room and Radwaste Pipe

Tunnel (Section 1R06.1.(b))05000461/2010002-08 NCV Inadequate Test Criteria in Standby Gas Treatment System

Flow/Heater Operability Surveillance Test (Section 4OA5.2)

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

- AR 00100707, Leakage from VT Cooling Coils Following Restoration

- AR 01052661, Improperly Secured Items South of Plant

- AR 01053631, Severe Weather Off-Normal Entry

- CPS 1860.02, Summer Readiness Operation, Revision 0a

- CPS 1860.01C002, Cold Weather Restoration Checklist, Revision 5b

- CPS 1860.01C003, Cold Weather Heater and Heat Trace Operability Checklist, Revision 1

- CPS 4302.01, Tornado/High Winds, Revision 19

- WC-AA-107, Seasonal Readiness Re-Write, Revision 6

- Plant System Readiness Reviews

- CPS Summer Readiness March Conference Call notes

- Work Order 01225359-01, Initiate Cold Weather Restorations IAW 1860.01, March 22, 2010

- Work Order 01232603-01, Return the 0VA03A Cooling Coil to Service, April 19, 2010

- OP-CL-108-107-1001, Interface between AmerenIP and Clinton Power Station for Switchyard

Operations, Maintenance, and Engineering, Revision 8

- AR 00959044, SY [Switchyard] Issues Discovered During System Manager Walkdown

- AR 00934821, Relay System #1 Test Breaker Found in the Off Position

- AR 01071939, Utility Pole Leaning Toward 12 KV Bus Work

- AR 01036598, 1AP02EA: Tasks Required for New RATs for Summer Readiness

- AR 01034028, Voltage Transient on 345 KV South Bus at 362.1 KV

- AR 00467624, Numerous Control Cables Not Properly Trained in the Panels

- AR 00469667, Breaker 4510 Relay (Boulzer 52) 50 PU, LED Illuminated

- AR 00467634, Potential for GE CCVTs, GE-CD31 to Fail Prematurely

- AR 00480385, CCVTs in the CPS Switchyard Are Prone to Failure

- AR 00552451, 345 KV Lights in Main Control Room Deenergized

- AR 00832377, MPT C Cooling Fan Hi Vibrations

- AR 01027314, 1AP08EJ Failed to Close During 4160 V Bus 1B Source Shifting

- AR 00956663, South Bus Voltage Momentarily Above 362.2 KV

- AR 00715427, South Bus Voltage Exceeded 362.2 KV Due to Low Grid Load

- AR 01038986, Excessive Fuzzing in Power Lines to New RATs

- OP-CL-108-107-1002, Degraded Grid Actions, Revision 2

- CPS 9082.01, Offsite Source Power Verification, Revision 39b

- Nuclear Plant Operating Agreement for Clinton Power Station

- Second Revised Interconnection Agreement, dated 11/4/03

1R04 Equipment Alignment

- CPS 3312.01, "Residual Heat Removal," Revision 38a

- CPS 3312.01V001, "Residual Heat Removal Valve Lineup," Revision 17

- CPS 3312.01V002, "Residual Heat Removal Instrument Valve Lineup," Revision 9

- AR 01061692, "1TVY006: RHR 'B' Pump Room Fan Did Not Autostart on Temp"

- AR 01061693, "1TVY005: RHR 'B' Pump Room Fan Did Not Autostart on Temp"

3 Attachment

- CPS 3506.01, Diesel Generator and Support Systems, Revision 34a

- CPS 3506.01V001, Diesel Generator and Support Systems Valve Lineup, Revision 13a

- CPS 3506.01V002, Diesel Generator and Support Systems Instrument Valve Lineup,

Revision 11b

- CPS 3506.01E001, Diesel Generator and Support Systems Electrical Lineup, Revision 18a

- CPS 3310.01, Reactor Core Isolation Cooling (RI), Revision 27b

- CPS 3310.01V002, RCIC Instrument Valve Lineup, Revision 9e

- CPS 3310.01V001, Reactor Core Isolation Cooling Valve Lineup, Revision 12e

- CPS 3310.01E001, Reactor Core Isolation Cooling Electrical Lineup, Revision 14b

- M05-1079, P&ID Reactor Core Isolation Cooling (RCIC) (RI), Sheet 001, Revision AH

- M05-1079, P&ID Reactor Core Isolation Cooling (RCIC) (RI), Sheet 002, Revision AJ

1R05 Fire Protection

- Fire Loading Calculation IP-M-0177, Revision 6

- CPS 3822.17, "Emergency Lighting Battery Pack Verification and Testing," Revision 13d

- AR 01060560, "LL System Classified as Maintenance Rule (A)(2) At Risk

- AR 01040525, "EMER Safe S/D Light at Remote S/D PNL Failed 1LL59BP02E

- AR 01079601, NRC Observations in FC Heat Exchanger Room

- Clinton Power Station Updated Final Safety Analysis Report, Appendix E, Fire Protection

Evaluation Report - Clinton Power Station Unit 1, Revision 11

- Clinton Power Station Updated Final Safety Analysis Report, Appendix F, Fire Protection Safe

Shutdown Analysis - Clinton Power Station Unit 1, Revision 11

- OP-AA-201-009, Control of Transient Combustible Material, Revision 9

- OP-CL-201-009, Control of Transient Combustible Material, Revision 1

- Clinton Power Station Updated Final Safety Analysis Report, Appendix E, Fire Protection

Evaluation Report - Clinton Power Station Unit 1, Revision 11

- Clinton Power Station Updated Final Safety Analysis Report, Appendix F, Fire Protection Safe

Shutdown Analysis - Clinton Power Station Unit 1, Revision 11

- OP-AA-201-009, Control of Transient Combustible Material, Revision 9

- OP-CL-201-009, Control of Transient Combustible Material, Revisions 0 and 1

- CPS 1893.04M400, 712 Fuel: Basement Prefire Plan, Revision 5

- CPS 1893.04M131, 781 Auxiliary (West): Div 2 Containment Electrical Penetrations Prefire

Plan, Revision 5

- AR 01077996, NRC Identified Combustibles During Inspection

- AR 01077973, NRC Identified Deficiencies

1R06 Flood Protection Measures

- CPS 4304.01, Flooding, Revision 4e

- CPS 4411.03, Injection/Flooding Sources, Revision 7

- CPS 3208.01, Cycled/Makeup Condensate, Revision 12a

- Clinton Power Station Updated Safety Analysis Report, Revision 13

- NRC Information Notice 2009-006, Construction-Related Experiences with Flood Protection

Features, July 21, 2009

- SL-4576, Internal Flooding - Safe Shutdown Analysis and INPO SOER No. 85-5 Comparison

Evaluation Report (Sargent & Lundy), January 31, 1990

- A26-1000-01A, Auxiliary Building Basement Plan Area 1, Revision AC

- A26-1000-02A, Auxiliary Building Basement Plan Area 2, Revision V

- A26-1000-03A, Auxiliary Building Basement Plan Area 3, Revision V

- A26-1000-04A, Auxiliary Building Basement Plan Area 4, Revision M

4 Attachment

- A26-1000-05A, Auxiliary Building Basement Plan Area 5, Revision L

- A30-1000-01C, Control Building Intermediate Floor Plan - Area 1, Revision F

- AR 00976295, ECCS Room Floor Drain Piping Connected to the Radwaste Pipe Tunnel

- AR 01031977, Questions Regarding IR 976295 Conclusions

- AR 01039042, Suppression Pool to ECCS Room Flood Equalization Levels

- Apparent Cause Evaluation AR 00976295, ECCS Room Floor Drain Piping Connected to the

Radwaste Pipe Tunnel

- LER 05000461/2010-001-00, Unanalyzed Leakage Pathway Affecting Residual Heat

Removal A Pump Room Flooding Analysis, March 25, 2010

- EC 380335, Issue Calculation IP-M-0782, Suppression Pool Equalization Levels, Revision 0

- Calculation IP-M-0782, Suppression Pool Equalization Levels, Revision 0

1R07 Heat Sink Performance

- NRC Generic Letter 89-13, Service Water System Problems Affecting Safety-Related

Equipment

- ER-AA-340-1002, Service Water Heat Exchanger and Component Inspection Guide,

Revision 4

- ER-AA-340, GL 89-13 Program Implementing Procedure, Revision 6

- ER-AA-340-1001, GL 89-13 Program Implementation Instructional Guide, Revision 7

- CPS 1003.10, Clinton Power Station (CPS) Program for NRC Generic Letter 89-13,

Revision 6a

- CPS 8130.01, Heat Exchanger Maintenance/Repairs, Revision 2

- CPS 9843.02, Operational Pressure Testing of Class 1, 2, and 3 Systems, Revision 41a

- AR 01062474, 1VY02C - Anemometer Does Not Meet Requirements

- AR 01062536, Change To Chemical Cleaning Impacted Dose Estimate

- Work Order 01133424-10, 89-13 Cooling Coil Inspection and Cleaning of Cooling Coil

1VY02AB, April 29, 2010

- Work Order 01133425-10, 89-13 Cooling Coil Inspection and Cleaning of Cooling Coil

1VY02AA, April 29, 2010

- Work Order 01133424-12, EP/MM VT2 Maintenance PMT - 9843.02 for 1VY02AB,

March 10, 2010

1R11 Licensed Operator Requalification Program

- AR 01068322, TQ-JA-150-08 Increases Admin Burden for NARS Form Completion

- AR 01073222, NOS ID: Required ANSI Parameters Missed During Transient Test

- TQ-AA-150, Operator Training Program, Revision 4

- TQ-AA-224, Exelon Nuclear Training - Implementation Phase, Revision 4

- TQ-AA-306, Simulator Management, Revision 1

- OP-AA-102-104, Pertinent Information Program, Revision 1

1R12 Maintenance Effectiveness

- ER-AA-310, "Implementation of the Maintenance Rule," Revision 8

- ER-AA-310-1001, "Maintenance Rule - Scoping," Revision 4

- MA-AA-716-210, "Performance Centered Maintenance (PCM) Process," Revision 9

- NUMARC 93-01, "Industry Guideline for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants," Revision 2

- AR 01025101, 1H13P634 Troubleshooting Results on A2 Subloop for 1B33F060A

- AR 01024342, "A - RR FCV Troubleshooting is Delaying Reactor Startup"

5 Attachment

- AR 01039243, "1B33D003A1: RR Subloop A1 Pressurized Light Did Not Come On"

- AR 00869875, "1B33D003A - RR Hydraulic Power Unit A

- AR 01022991, 1B33D003A1 - RR Hydraulic Power Unit 1A Subloop A1

- AR 01023016, 1B33D003A2 - RR Hydraulic Power Unit 1A Subloop A1

- Common Cause Analysis 00736646-02, C1R11 LRT Failures for Maint. Rule System 97 Need

Evaluated

- WO 01306068-01, RR A FCV Keeps Going to Lockout

- ER-AA-310-1001, Maintenance Rule - Scoping, Revision 4

- Maintenance Rule Failure Report for Reliability Monitoring of System 97 (Containment

Isolation/Integrity and Reactor Coolant Pressure Boundary), April 2007 through April 2010

- Maintenance Rule (a)(1) Determination for Reliability Performance Criteria 97-00-1 and

97-00-04 (Local Leak Rate Testing Program Valves), April 14, 2008

- Common Cause Evaluation (AR 00736646-02), C1R11 LLRT Failures for Maintenance Rule

System 97 Need Evaluated, March 12, 2008

- LER 2008-003-00, Excessive Leakage Through Feedwater Isolation Valve 1B21F032A,

May 17, 2010

- LER 2010-002-00, Excessive Leakage Through Feedwater Isolation Valve 1B21F032B,

April 1, 2010

- Root Cause Evaluation (AR 01025446-16), Late Identification of Feedwater 32B LLRT

Failure, March 29, 2010

- CPS 9861.05D014, LLRT Data Sheet for 1MC010, Revisions 2 and 2a

- AR 01059704, Evaluation of 1B21F032A Not Forwarded for System 97 Consideration

- AR 01025446, 1B21-F032B Fails LLRT Not Identified

- AR 01047133, Excessive Leakage From 1B21F032A Not Reported in C1R11

- AR 00736646-02, C1R11 LLRT Failures for Maintenance Rule System 97 Need Evaluated

- AR 01049694, Nuclear Oversight Identified Internal Inspection of Feedwater Checks Not

Implemented

1R13 Maintenance Risk Assessments and Emergent Work Control

- CPS 9051.05, "HPCS Discharge Header Filled and Flow Path Verification," Revision 27c

- Contingency Plan WC-CL-201, "9051.02 HPCS Valve Operability," Revision 0

- CPS 9051.02, "HPCS Valve Operability Test," Revision 39a

- AR 00720355, Possible Loss of Reactor Coolant Due to Work Package Inadequacy

- AR 01017904, Double Blade Guide Removed with Rod Inserted

- AR 01020181, NOS ID OPDRV Evaluation Per 3711.01 Not Performed for RR B

- AR 01029061, C1R12 LL - Critical Path Delay - DBG Removal w/Rod Inserted

- AR 01051306, NRC Concerns with the 50.59 for the new OPDRV Procedure

- AR 01052493, 1SX083A Check Valve Failed to Seat During 9831.09D004

- AR 01053125, NRC Question RE: RHR A HX Availability During 9861.09

- AR 01063405, NRC Review of 50.59 for OPDRV Procedure

- AR 01068302, Shut Down Cooling Procedure Needs Enhanced

- WC-AA-101, On-Line Work Control Process, Revision 16

- CPS 3211.01, Shutdown Service Water (SX), Revision 25a

- CPS 9861.09, Shutdown Service Water Boundary Valve Leak Testing, Revision 0F

- CPS 9861.09, Leakage Test on Valve 1SX082A, Revision1A

- Peach Bottom Technical Requirements Manual

- Drawing #S27-1004-03A, Containment Building Floor Framing Plan El. 803-3, Revision AG

- Drawing #S27-1200-00A, Containment Building Section 7-7 Lower, Revision 13

- Plant Operations Review Committee Meeting Minutes, Meeting Number 09-030, December 9,

2009

6 Attachment

- Plant Operations Review Committee Meeting Minutes, Meeting Number 10-002,

January 10, 2010

- Plant Operations Review Committee Meeting Minutes, Meeting Number 10-009, April 20, 2010

- Nuclear Energy Institute 96-07, Guidelines For 10CFR 50.59 Implementation, Revision 1

- NUMARC 91-06, Guidelines for Industry Actions to Assess Shutdown Management,

December 1991

- NUMARC 93-01, Industry Guideline For Monitoring The Effectiveness Of Maintenance at

Nuclear Power Plants, Revision 2

- 50.59 Evaluation Number CL-2010-E-001, CPS Procedure 3711.01, Revision 0

- 50.59 Evaluation Number CL-2010-E-001, CPS Procedure 3711.01, Revision 1

- EC 357294, Temporary Configuration Change for CPS 8117.04, Revision 0

- EC 376912, Evaluate Hole Size for OPDRV, Revision 1

- OP-AB-117-101, Operations with the Potential to Drain the Reactor Vessel (OPDRV),

Revision 0

- LaSalle Station LOP-NB-02, Operations with the Potential to Drain the Reactor Vessel,

Revision 10

- OU-CL-104, Shutdown Safety Management Program Clinton Power Station, Revision 4

- CPS 3711.01, CPS Operations With The Potential To Drain The Reactor Vessel (OPDRV),

Revision 0

- CPS 4006.01, Loss of Shutdown Cooling, Revision 4d

- CPS 4011.01, Reactor Cavity Leakage During Refueling, Revision 4e

- CPS 4011.02, Spent Fuel Pool Abnormal Water Level Decrease, Revision 5f

- CPS 8121.06, Control Rod Drive Removal and Installation (GE-SLDES III), Revision 0c

- CPS 8121.06C001, Control Rod Drive Removal and Installation Checklist (GE-SLDES III),

Revision 0b

- CPS 9093.01, Control Rod/Drive (CRD) Removal Requirements, Revision 25b

- CPS 9093.01C002, Multiple Control Rod/Drive (CRD) Removal Verification Checklist,

Revision 29b

- ER-AA-600, Risk Management, Revision 5

- ER-AA-600-1012, Risk Management Documentation, Revision 8

- ER-AA-310-1001, On-Line Risk Management, Revision 6

- WC-AA-101, On-Line Work Control Process, Revision 16

- WC-AA-104, Integrated Risk Management, Revision 15

1R15 Operability Evaluations

- AR 01065089, 0AP03E: Small Chips in Two Insulators for the ERAT

- AR 01065232, 0AP03E: ERAT Core Ground Test Results Lower Than Expected

- AR 01068918, Un-Attached Ground Cable in SE Corner of RAT SVC Yard

- AR 01070053, ERAT SOW Contingency Plans Not Fully Developed

- AR 01070098, Lessons Learned From ERAT SOW

- AR 01078890, System Manager Trending ID Potentially Increasing ERAT Core

- Operability Evaluation # 01065232-07, 0AP03E - Emergency Reserve Auxiliary Transformer

- Operational and Technical Decision Making #1065232-02, ERAT Core Ground Testing,

- May 4, 2010

- Adverse Condition Monitoring and Contingency Plan #1065232-08, ERAT Core Ground

Resistance, May 5, 2010

- Work Order 00934040, Doble Test ERAT, Megger ET4 Bus (Cable), May 26, 2010

- Work Order 01335439, ERAT Core Ground Test Results Lower Than Expected,

June 11, 2010

- Clinton Power Station Technical Specifications

7 Attachment

- Clinton Power Station Updated Final Safety Analysis Report, Revision 11

- NRC Regulatory Issue Summary 2005-20, Revision to NRC Inspection Manual Part 9900

Technical Guidance, Operability Determinations & Functionality Assessments for Resolution

of Degraded or Nonconforming Conditions Adverse to Quality or Safety, Revision 1

- Memorandum from G. Shear, (USNRC Region III, Division of Reactor Projects) to T. Blount,

(USNRC Office of Nuclear Reactor Regulation, Division of Policy and Rulemaking), Subject:

Task Interface Agreement - Evaluation of Application of Technical Specification Surveillance

Requirement 3.0.3, Surveillance Requirement Applicability, at Clinton Power Station

(TIA 2010-001), April 19, 2010

- Memorandum from J. Clifford, (USNRC Region I, Division of Reactor Projects) to T. Blount,

(USNRC Office of Nuclear Reactor Regulation, Division of Policy and Rulemaking), Subject:

Task Interface Agreement (TIA) - Evaluation of Application of Technical Specification (TS) 4.0.3, Surveillance Requirement Applicability, at Pilgrim (TIA 2008-004), December 31,

2008

- CL-SURV-03, Risk Analysis for Missed Surveillance, Failure to Test Various Excess Flow

Check Valves Used for Containment Isolation, Revision 0

- Operability Evaluation (AR 00846540-08), IST Surveillance Discrepancies for Excess Flow

Check Valves, Revision 0

- AR 01063878, NRC TIA on Applicability of TSSR 3.0.3 for IST of Excess Flow Check Valves

- AR 00846540, IST Surveillance Discrepancies for Excess Flow Check Valves

- AR 00943162, NRC Questions Operability Basis for Operability Evaluation 00846540-08

1R19 Post-Maintenance Testing

- WO 01028895-01, "IM Overhaul Actuator and Replace Accessories," 1SX029A

- WO 01028895-04, "OPS PMT Perform 9052.01, Verify 1SX029A Strokes Correctly"

- AR 01062042, "Maximum Friction Value Exceeds Acceptance Criteria"

- AR 01063858, Deficiencies Identified During Testing of 1E12-F037A

- CPS 9052.01, LPCS/RHR A Pumps & LPCS/RHR A Water Leg Pump Operability"

- WO 01321254-03, "OP PMT Leak Check 1C85D002MG, 1C85D002 Back Up Filter"

- CPS 3105.04, "Steam Bypass and Pressure Regulator (SB)," Revision 13

- WO 00488712-05, "OP CPS 9053.04 - Residual Heat Removal (RHR) A B C Valve OP"

- WO 00488712-01, "Perform Thrust Verification and Clean / Inspect 1E12F037A"

- CPS 9053.04C001, "RHR Loop A Valve Operability," Revision 1d

- CPS 9053.04D001, "RHR Loop A Valve Operability Data Sheet," Revision 43c

- CPS 3506.01, Diesel Generator and Support System (DG), Revision 34a

- CPS 9080.02, Diesel Generator 1B Operability Manual and Quick Start Operability,

Revision 49B

- Work Order 01082152-02, OP PMT Sync Div II DG to Verify Sync-Check Relay 225-DG1KB,

April 15, 2010

- Work Order 01320453, 9080.02B22 OP DG 1B Operability - Monthly Test, April 19, 2010

- AR 01069618, Locked Valve Throttling Per 3211.01V001

- AR 01070102, Bolts Were Over-torqued During ERAT [Emergency Reserve Auxiliary

Transformer] Restoration

- AR 01057592, 1GC01PA Is Running Hotter Than Normal

- WO 01307425, 1GC01PA: High Vibration on GC Pump A

1R22 Surveillance Testing

- AR 00919953, Configuration Error Traps in CPS 9915.01 - Enhancement

- AR 01064429, Evaluate LLRT on 1MC116 for Stop-It-Now

8 Attachment

- AR 01069981, IR 00919953 Closed Without Proper Actions/Changes - CCP

- CPS 9015.01, Standby Liquid Control System Operability, Revision 39e

- CPS 9015.01D001, Standby Liquid Control Pump and Valve Data Sheet, Revision 37

- Work Order 01308881-01, 9015.01E23 OP SLC Valve Operability (1C41-F001A & F001B),

May 10, 2010

- Work Order 01325404-01, OP SLC-SQUIB Valve Continuity and Flow Path Verification,

May 10, 2010

1EP2 Alert and Notification System Evaluation

- Clinton Nuclear Power Station Off-Site Emergency Plan Alert and Notification Addendum,

Prepared in Response to FEMA-REP-10 Documentation Criteria Requirements,

November 1985

- Clinton Off-Site Siren Test Plan, December 2007

- Siren Monthly Operability Reports, 2nd Quarter 2008 through 1st Quarter 2010

- Siren Daily Operability Reports, 2nd Quarter 2008 through 1st Quarter 2010

- Exelon Semi-Annual Siren Report, January 1, 2009 through June 30, 2009

- Exelon Semi-Annual Siren Report, July 1, 2009 through December 31, 2009

- AR 00823763, Clinton Alert and Notification System Reached an Outage of 25 Percent

- AR 00945792, 11 of 44 Offsite Emergency Sirens Lost Power

1EP3 Emergency Response Organization Augmentation Testing

- EP-AA-1000, Exelon Standardized Emergency Plan; Revision 20

- EP-AA-1003, Radiological Emergency Plan Annex for Clinton Station, Revision 16

- EP-AA-122-1001, Drill and Exercise Scheduling, Development, and Conduct, Revision 11

- TQ-AA-113, ERO Training and Qualification, Revision 16

- RP-AA-440, Respiratory Protection Program, Revision 9

- RP-CL-441, Evaluation and Selection Process for Radiological Respirator Use, Revision4

- CPS 7200.32, Drywell Entries, Revision 3c

- CPS 1021.01, Site Communications, Revision 7a

- CPS 3822.07, Gaitronics Verification, Revision 7

- OP-CL-101-102-1001, CPS Minimum On-Shift Staffing Functions, Revision 2

- ERO Augmentation Call-in Drill Reports and Detailed Records, March 2008 through April 2010

- Clinton Power Station Emergency Response Organization Duty Team Roster, April 5, 2010

- AR 00812026, NOS Identified Additional Review of Gaitronics Work Orders Needed

- AR 01042183, Degraded Gaitronics Speakers Not Definable in Passport

- AR 01016904, Contract Personnel Utilized to Fulfill ERO Positions

- AR 01046833, C1R12 LL Contract ERO Radiation Protection Technicians Need Respirator

Qualifications

- AR 01053501, Outage ERO Respirator Qualifications below Threshold

- AR 01057419, NRC Open Item: On-Shift Respirator Qualifications

- AR 01057263, NRC NCV Craft Participation in Augmentation Call-In Drills

- Clinton Station Selected Emergency Response Personnel Training Records

- Clinton Station Off-site Agencies Correspondence and Training Records

1EP4 Emergency Action Level and Emergency Plan Changes

- 10 CFR 50.54(q) Evaluation Package, Exelon Nuclear Radiological Emergency Plan Annex

for Clinton Station, Revision 15

9 Attachment

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

- LS-AA-126-1001, Attachment 2, FASA Self-Assessment Report Template, Clinton Station

2010 NRC Baseline Program Inspection Readiness Assessment, February 19, 2010

- NOSA-CPS-09-04 (AR 848185), Emergency Preparedness Audit for Clinton Station,

April 15, 2009

- NOSA-CPS-08-03 (AR 699076), Emergency Preparedness Audit for Clinton Power Station,

April 30, 2008

- NOSA-CPS-07-04 (AR 569195), Emergency Preparedness Audit for Clinton Station,

May 9, 2007

- NOSA-NCS-09-04, Emergency Preparedness Audit; NOS Objective Evidence Report,

March 30 through April 3, 2009

- NOSA-NCS-08-03; 2008 Emergency Preparedness Audit, NOS Objective Evidence Report,

March 31 through April 4, 2008

- NOSA-NCS-07-04, Emergency Preparedness Audit, NOS Objective Evidence Report,

Cantera, May 18, 2007

- NOSA-NCS-07-04, Emergency Preparedness Audit; NOS Objective Evidence Report,

Clinton, May 2, 2007

- Clinton 2009 NRC Graded Exercise Evaluation Report, November 18, 2009

- EP Exercise Objective D.1 Failure; Root Cause Investigation Report Content and Format,

December 11, 2009

- AR 00889346, Local Counties Were Not Contacted during QDC NOS EP Audit

- AR 0083421, High Failure Rate on New Style Pagers

- AR 00897250, Training - Ineffective Change Management around EAL Revision

- AR 00995972, TSC Failed Facility Objective for I.2 Core Damage

- AR 00995985, Failed Demonstration Criteria in TSC and OSC Associated with K.5.4

(Habitability)

- AR 00778835, EP Exercise Evaluation for Objective J.6

- AR 00883223, Training - EP Performance in Annual License Exams

1EP6 Drill Evaluation

- AR 01078888, 2010 ERO Exercise OSC Performance Gaps

- AR 01078881, 2010 ERO Exercise OSC Demonstration Criteria Deficiencies

- AR 01078879, 2010 ERO Exercise TSC Demonstration Criteria Deficiencies

2RS1 Radiological Hazard Assessment and Exposure Controls

- AR 918784, Additional Qualifications Needed For Whole Body Counter, May 12, 2010

- AR 923634, Non-Exempt Source Not In Designated Source Locker,

- AR 924257, Enhancement to Survey Program, May 26, 2009

- AR 938734, Air Sample Not Counted in Accordance with Procedure, July 4, 2009

- AR 951729, Scaffold Access Ladder Not Posted Contamination Area, August 5, 2009

- AR 972937, Electronic Dosimeter Dose Rate Alarm, August 30, 2010

- AR 1012322, Worker Received Electronic Dosimeter Dose Alarm, January 5, 2010

- AR 1014236, Secured High Radiation Area Key Detached from Lanyard, January 8, 2010

- AR 1016247, TIP Area Accessed Without Proper Notification/Approval, January 11, 2010

- AR 1016378, Worker Received Electronic Dosimeter Dose Alarm, January 14, 2010

- AR 1016424, TIP Area Access Controls, January 14, 2010

- AR 1016902, Worker Received Electronic Dosimeter Dose Alarm, January 15, 2010

10 Attachment

- AR 1018482, Nuclear Oversight Identified Black Tape Used for Contaminated Boundary,

January 19, 2010

- AR 1018906, Nuclear Oversight Identified Radiation Area Brief Used Wrong Dose Estimates,

January 20, 2010

- AR 1020025, Source Closure Device Failed to Properly Retract, January 22, 2010

- AR 1020960, Nuclear Oversight Elevation of Inadequate Supervisory Radiation Protection

Oversight of Radiation Protection Technologists, January 25, 2010

- AR 1024118, Dry Well Entry Prior to Access Control Guard Checks Performed,

- AR 1024567. Nuclear Oversight Identification of Improper Posting of a Contamination Area,

February 1, 2010

- AR 1042235, Sur-Pak Locked High Radiation Area Not Locked, March 12, 2010

- AR 104309, Hand-Written Note on Radiation Protection Posting, March 16, 2010

- AR 1050562, Radioactive Sources Not Properly Controlled, March 30, 2010

- AR 1059639, Procedure Review Identifies Need for Source Report Tracking, April 21, 2010

- CR 865815, Senior Leadership Team Not Notified Prior to Exceeding the Dose Estimate for

Condensate Polisher Prefilters, January 12, 2009

- CR 888839, Higher than Expected Dose Rates on 0WX01TB Tank Top, March 4, 2009

- CR 876251, Temporary Shield Package 2009-052 Installed by Wrong Component,

February 4, 2009

- NF-AA-390, Spent Fuel Pool Material Control, Revision 4

- RP-AA-350-1001, Response to Gate House Alarms, Revision 0

- RP-AA-503, Unconditional Release Survey Method, Revision 2

- RP-AA-800, Control, Inventory and Leak Testing of Radioactive Sources, Revision 6

- RP-AA-800-001, Nationally Tracked Source Program, Revision 0

- ARP-CL-301-101, Clinton Power Station Radiological Air Sampling Program, Revision 3

- RP-CL-503-101, Clinton Power Station Unconditional Release Surveys, Revision 6

- Check-in Self-Assessment, Radworker Performance, July 31, 1009

- Check-in Self-Assessment, Infield Work Control, October 8, 2009

2RS7 Radiological Environmental Monitoring Program

- NOSA-CPS-08-04, Chemistry, Radwaste, Effluent and Environmental Monitoring Audit

Report,; AR 699063, April 16, 2008

- CY-AA-170-1000, Radiological Environmental Monitoring Program and Meteorological

Program Implementation, Revision 5

- Annual Report on the Meteorological Monitoring Program at the Clinton Power Station 2009,

Murray and Trettel Inc, March 2, 2010

- Monthly Report on the Meteorological Monitoring Program at the Clinton Power Station,

Murray and Trettel Inc, February 2010

- Monthly Report on the Meteorological Monitoring Program at the Clinton Power Station,

Murray and Trettel Inc, March 2010

- Sampling Procedures Manual, Environmental Incorporated Midwest Laboratory, Revision 13

- CPS No. 7200.06F00; 10 CFR 50.75(g)(1),Decommissioning Records of Radiological Spills

or Other Unusual Occurrences, February 3,1999

- RP-AA-228 Attachment 1, Record for 10 CFR 50.75(g), April 9, 2010

- NOVA-0980, Audit No. SR-2009-32, Exelon Audit of Murray and Trettel, Inc., October 20,

2009

- NOVA-09-43, Audit SR 2008-039; Exelon Audit of Environmental, Inc., June 22, 2009

- NUPIC Joint audit Number 20110; Teledyne Brown Engineering Enviro,Enviro Services,

December 1, 2008

11 Attachment

- Annual Report on the Meteorological Monitoring Program at the Clinton Power Station 2008,

Murray and Trettel Inc, September 1, 2009

- AR 01059978, High Spike in Gross Beta in September 2009, April 22, 2010

- AR 01059845, Surface Water CL-90 Had False Positive I-131 Result, April 22, 2010

- AR 01062303, No flow Through PDCM Water Compositor CL-14, April 28, 2010

- AR 01079023, Air Pump Calibration for ODCM Samples, June 9, 2010

4OA1 Performance Indicator Verification

- CPS 3222.10, Reactor Sample Station. Revision 11b

- CPS 6721.01, Reactor Water Radioisotopic Analysis, Revision 9

- CY-AA-130-3010, Dose Equivalent Iodine Determination, Revision 2

- Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6

- HU-AA-101, Human Performance Tools and Verification Practices, Revision 4

- Performance Indicator Summary, May 7, 2010

- LS-AA-2110, Monthly Data Elements for NRC Emergency Response Organization Drill

Participation Records; 4th Quarter 2009,

- LS-AA-2120, Attachment 1, Monthly Data Elements for NRC Drill/Exercise Performance

Reports, 4th Quarter 2009

- LS-AA-2130, Attachment 1, Monthly Data Elements for NRC Alert and Notification System

Reliability,4th Quarter 2009

4OA2 Identification and Resolution of Problems

- AR 01023530, Gate Seals Leakage During CRVCS System Functional Test

- AR 01029350, NOS ID Gate Seal Leaking Not Evaluated

- AR 01035399, Review SOER 85-1 On Gate Seals

- AR 01043002, RR Pump B #1 Seal Cavity Temp, T1, has Risen >4 F/day

- AR 01043146, Adverse Trend Identified in Main Control Room Deficiencies

- AR 01049383, Trend IR for Possible Declining Trend in Abnormal/Off Normal

- AR 01066830, Review of Human Performance Actions on Declining Performance

- AR 01067144, Step Change in RR Pump A Seal Pressure

- AR 01076457, Extent of Condition for IR 01023530

- Nuclear Network Operating Experience #1023530-39-01, Gate Seal Leakage During

Containment Isolation Valve System Functional Testing

- LS-AA-125, Corrective Action Program (CAP) Procedure, Revision 11

- Root Cause Investigation #1023530-17, Gate Seals Leakage During Containment Isolation

Valve System Functional Test

- Prompt Investigation #1023530-6, Gate Seals Leakage During CRVCS System Functional

Test

- Operations 1st Quarter 2010 Coding and Analysis Report

- Maintenance 1st Quarter 2010 Coding and Analysis Report

- Radiation Protection 1st Quarter 2010 Trending and Analysis Report

- Work Management 1st Quarter 2010 Trending and Analysis Report

- Common Cause Analysis #1066830-02, Human Performance/Technical Human Performance

Common Cause Analysis for C1R12

- NOL-10-002, Letter from Nuclear Oversight Manager to Radiation Protection Manager,

Elevation - Inadequate Supervisory Oversight to Correct Supplemental Radiation Protection

Technician Performance, January 25, 2010

- CPS 3007.01, Preparation and Recovery from Refueling Operations, Revision 14E

12 Attachment

- CPS 8117.11, Installation and Removal of Upper Containment and Fuel Building Pool Gates,

Revision 8C

- CPS 8117.11C001, Installation and Removal of Upper Containment and Fuel Building Pool

Gates Checklist, Revision 8A

- CPS 9061.04, Containment Drywell Isolation Auto Actuation, Revision 42A

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

- Licensee Event Notification 45901, Division 2 Drywell Ventilation and Drywell Cooling

Primary Containment Isolation Valves Closed, May 5, 2010

- Equipment Apparent Cause Evaluation (AR 01042588), Division 2 VP/WO Isolation

- PORC Meeting 10-010 Minutes, May 3, 2010

- PORC Meeting 10-011 Minutes, May 4, 2010

- LER 2008-003-00, Excessive Leakage Through Feedwater Isolation Valve 1B21F032A,

May 17, 2010

- LER 2010-002-00, Excessive Leakage Through Feedwater Isolation Valve 1B21F032B,

April 1, 2010

- LER 05000461/2010-001-00, Unanalyzed Leakage Pathway Affecting Residual Heat

Removal A Pump Room Flooding Analysis, March 25, 2010

- Root Cause Evaluation (AR 01025446-16), Late Identification of Feedwater 32B LLRT

Failure, March 29, 2010

- AR 01025446, 1B21-F032B Fails LLRT Not Identified

- AR 01042588, 1VP04CB: Div 2 VP/WO Isolation - Shunt Trip

- AR 01047133, Excessive Leakage From 1B21F032A Not Reported in C1R11

- AR 01076505, Reporting Criteria in LERS for FW 32 LLRT Failures

- CPS 9861.05D014, LLRT Data Sheet for 1MC010, Revisions 2 and 2a

4OA5 Other Activities

- Root Cause Investigation Report (AR 01026445), Turbine Trip During Turbine On Line

Testing, April 13, 2010

- Hydrogeologic Investigation Report, Fleetwide Assessment; Clinton Power Station,

De Witt County, Illinois; September 2006

- Annual Radioactive Effluent Release Report; Clinton Power Station - Docket Number 50-461,

January 1, 2009 - December 31, 2009

- Annual Radiological Environmental Operating Report, Clinton Power Station -

Docket Number 50-461, April 2010

- CY-CL-170-301, Offsite Dose Calculation Manual (ODCM), Clinton Power Station -

Docket Number 50-461, Revision 22

- CY-AA-170-400, Radiological Groundwater Protection Program, Revision 4

- CY-AA-170-4000, Radiological Groundwater Protection Program Implementation, Revision 4

- CY-CY-170-4160, Radioactive Groundwater Protective Program Scheduling and Notification,

Revision 5

- CY-AA-120-300, Tritium Management Program, Revision 1

- NEI Peer Assessment Report, NEI 07-07 NEI Groundwater Protection Initiative, February 29,

2010

- Groundwater Protection - Data Collection Questionnaire, July 27, 2006

- AR 00950069, Evaluate Enhancing RGPP Communications to Local Officials, August 5,

2009

- AR 01079446, Annual AREOR Report Does Not Have Complete RGPP Elements, June 11,

2010

13 Attachment

LIST OF ACRONYMS USED

AC Alternating Current

ADAMS Agencywide Documents and Management System

ANS Alert and Notification System

ANSI American National Standards Institute

AR Action Request

ASME American Society of Mechanical Engineers

BI Barrier Integrity

BWR Boiling Water Reactor

C1R12 Clinton Unit 1 Cycle 12 Refueling Outage

CFR Code of Federal Regulations

CNO Chief Nuclear Officer

CPS Clinton Power Station

CRDM Control Rod Drive Mechanism

CRVCS Containment and Reactor Vessel Cooling System

DG Diesel Generator

ECCS Emergency Core Cooling System

EOF Emergency Operations Facility

EOP Emergency Operating Procedure

EP Emergency Preparedness

ERAT Emergency Reserve Auxiliary Transformer

ERDS Emergency Response Data System

ERO Emergency Response Organization

FSAR Final Safety Analysis Report

FIN Finding

GDC General Design Criteria

GPM Gallons-Per-Minute

HRA High Radiation Area

IE Initiating Events

IEL Initiating Events Likelihood

IMC Inspection Manual Chapter

IP Inspection Procedure

IST Inservice Testing

LCO Limiting Condition for Operation

LER Licensee Event Report

LLDs Lower Limits of Detection

LLRT Local Leak Rate Test

LOI Loss of Inventory

LPCS Low Pressure Core Spray

MS Mitigating Systems

NCV Non-Cited Violation

NEI-GPI Nuclear Energy Institute - Ground Water Protection Initiative

NPSH Net Positive Suction Head

NRC U.S. Nuclear Regulatory Commission

NSPS Nuclear System Protection System

ODCM Offsite Dose Calculation Manual

OPDRV Operations with the Potential to Drain the Reactor Vessel

OSC Operations Support Center

PARS Publicly Available Records System

PSIG Pounds-Per-Square-Inch Gage

14 Attachment

POS Plant Operating State

RCA Radiologically Controlled Area

RCS Reactor Coolant System

RCIC Reactor Core Isolation Cooling

REMP Radiological Environmental Monitoring Program

RHR Residual Heat Removal

RIS Regulatory Issue Summary

SDP Significance Determination Process

SPMU Suppression Pool Makeup

SSCs Structures, Systems, and Components

SX Shutdown Service Water

TIA Task Interface Agreement

TLD Thermoluminescent Dosimeter

TS Technical Specification

TSC Technical Support Center

TSO Transmission System Operator

TSSR Technical Specification Surveillance Requirement

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

VHRA Very High Radiation Area

WO Work Order 15 Attachment

M. Pacilio -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website

at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket No. 50-461

License No. NPF-62

Enclosure: Inspection Report 05000461/2010-003

w/Attachment: Supplemental Information

cc: Distribution via ListServe

DISTRIBUTION:

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Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl

"E" = Copy with attach/encl "N" = No copy

OFFICE NRR/DORL ClintonRIO E RIII

Sect 1R13

NAME HChernoff BKemker by MR MRing:cs

for

DATE 08/03/10 by email 08/03/10 08/03/10

OFFICIAL RECORD COPY

Letter to M. Pacilio from M. Ring dated August 3, 2010

SUBJECT: CLINTON POWER STATION NRC INTEGRATED INSPECTION REPORT

05000461/2010-003

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