IR 05000458/2018004

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NRC Integrated Inspection Report 05000458/2018004 and Independent Spent Fuel Storage Installation Inspection Report 07200049/2018001
ML19031C939
Person / Time
Site: River Bend  Entergy icon.png
Issue date: 01/29/2019
From: Jason Kozal
NRC/RGN-IV/DRP/RPB-C
To: Vercelli S
Entergy Operations
References
IR 2018001, IR 2018004
Download: ML19031C939 (39)


Text

ary 29, 2019

SUBJECT:

RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2018004 AND INDEPENDENT SPENT FUEL STORAGE INSTALLATION INSPECTION REPORT 07200049/2018001

Dear Mr. Vercelli:

On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station, Unit 1. On January 14, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented five findings of very low safety significance (Green) in this report.

Four of these findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violations or significance of these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the River Bend Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the River Bend Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Jason W. Kozal, Chief Project Branch C Division of Reactor Projects Docket Nos. 50-458 and 72-049 License No. NPF-47

Enclosures:

Inspection Report 05000458/2018004 and 07200049/2018001 w/Attachments:

1. Documents Reviewed 2. O

Inspection Report

Docket Numbers: 05000458 and 07200049 License Number: NPF-47 Report Numbers: 05000458/2018004 and 07200049/2018001 Enterprise Identifier: I-2018-004-0009 and I-2018-001-0109 Licensee: Entergy Operations, Inc.

Facility: River Bend Station and Independent Spent Fuel Storage Installation Location: Saint Francisville, Louisiana Inspection Dates: October 1, 2018 to December 31, 2018 Inspectors: C. Speer, Acting Senior Resident Inspector B. Parks, Resident Inspector/Acting Senior Resident Inspector T. DeBey, Acting Resident Inspector L. Carson II, Senior Health Physicist N. Greene, PhD, Senior Health Physicist M. Learn, Reactor Engineer, MCID, RIII L. Brookhart, Senior Spent Fuel Storage Inspector, FCDB R. Rodriquez, Structural Engineer, DSFM, HQ D. Tang, Senior Structural Engineer, DSFM, HQ Approved By: J. Kozal Chief, Project Branch C Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at River Bend Station, Unit 1, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC-identified and self-revealed findings, violations, and additional items are summarized in the table below.

Licensee-identified non-cited violations are documented in the Inspection Results at the end of this report.

List of Findings and Violations Failure to Disposition Adverse Conditions Associated with the Offgas System as Required by Procedures Cornerstone Significance Cross-cutting Inspection Aspect Procedure Public Green H.4 - 71111.15 -

Radiation FIN 05000458/2018004-01 Teamwork Operability Safety Closed Determinations and Functionality Assessments The inspectors identified a finding for the licensees failure to disposition adverse conditions as required by Procedure EN-LI-102, Corrective Action Program, Revision 35. Specifically, the licensee did not categorize conditions associated with the offgas system as adverse as required by the procedure.

Failure to Control Entrance Into a High Radiation Area Cornerstone Significance Cross-cutting Inspection Aspect Procedure Occupational Green H.11 - 71124.01 -

Radiation NCV 05000458/2018004-02 Challenge the Radiological Safety Closed Unknown Hazard Assessment and Exposure Controls The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.7.1,

High Radiation Area, for the licensees failure to control activities in a high radiation area.

Specifically, a worker entered into the lower area of the reactor building steam tunnel via a ladder, conservatively posted and controlled as a locked high radiation area (i.e., an area with dose rates greater than 100 millirem per hour and below 1,000 millirem per hour at 30 cm),

without knowledge of current radiological conditions and without continuous Radiation Protection oversight, as required. The worker received an unexpected dose alarm.

Inadequate Risk Mitigation Actions in Work Procedure Leads to Inadvertent High Pressure Core Spray Initiation Cornerstone Significance Cross-cutting Inspection Aspect Procedure Mitigating Green H.12 - Avoid 71153 -

Systems NCV 05000458/2018004-03 Complacency Follow-up of Closed Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for the licensees failure to implement a procedure required by Regulatory Guide 1.33,

Revision 2, Appendix A, dated February 1978. Specifically, the licensee failed to pre-plan and perform maintenance on level transmitter B21-LTN081C in accordance with a procedure appropriate to the circumstances. The failure led to a perturbation in the C instrument reference leg that caused an invalid actuation of the high pressure core spray system at power.

Control Room Fresh Air Surveillance Procedures Inappropriate to the Circumstances Cornerstone Significance Cross-cutting Inspection Aspect Procedure Barrier Green H.14 - 71153 -

Integrity NCV 05000458/2018004-04 Conservative Follow-up of Closed Bias Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, which occurred because the licensee did not prescribe procedures for performing surveillance tests on the main control room fresh air subsystem that were appropriate to the circumstances. Specifically, the licensee allowed up to 31 days to receive and review the results of charcoal filtration bed samples. As a result, the Division II control room fresh air subsystem was inoperable from April 17, 2018, to May 3, 2018, exceeding Technical Specification 3.7.2 allowed outage time of 7 days.

Inappropriate Maintenance Procedure Leads to Water Intrusion into Division II Emergency Diesel Generator Lube Oil System Cornerstone Significance Cross-cutting Inspection Aspect Procedure Mitigating Green H.12 - Avoid 71153 -

Systems NCV 05000458/2018004-05 Complacency Follow-up of Closed Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for the licensees failure to implement a procedure required by Regulatory Guide 1.33,

Revision 2, Appendix A, dated February 1978. Specifically, the licensee failed to pre-plan and perform maintenance on the Division II emergency diesel generator in accordance with a procedure appropriate to the circumstances. As a result, the emergency diesel generator was rendered incapable of performing its specified safety function.

Additional Tracking Items Type Issue number Title Inspection Status Procedure LER 05000458/2018-002-00 Inadvertent High Pressure 71153 Closed Core Spray Initiation and Loss of Safety Function Due to Inadequate Work Instruction Mitigation Actions LER 05000458/2018-003-00 Condition Prohibited by 71153 Closed Technical Specifications Due to Untimely Recognition of Failed Laboratory Analysis of Ventilation Charcoal Sample LER 05000458/2018-006-00 Potential Loss of Safety 71153 Closed Function and Condition Prohibited by Technical Specifications Due to Emergency Diesel Generator Lube Oil Chiller Leak Caused by Design Deficiency

PLANT STATUS

River Bend Station began the inspection period at rated thermal power. On October 27, 2018, the unit was down powered to 63 percent for a control rod sequence exchange and to suppress a suspected nuclear fuel leak. The unit was returned to rated thermal power on November 5, 2018. On November 10, 2018, the unit experienced a scram due to a failure of the number three turbine control valve. The unit was returned to rated thermal power on November 23, 2018. On December 14, 2018, the unit was down powered to 72 percent for a control rod sequence exchange. The unit was returned to rated thermal power on December 16, 2018, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01Adverse Weather Protection Seasonal Extreme Weather

The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures on October 19, 2018.

71111.04Equipment Alignment Partial Walkdown

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Division I standby diesel generator on October 15, 2018
(2) High pressure core spray on October 25, 2018
(3) Division II emergency diesel generator on November 23, 2018

71111.05AQFire Protection Annual/Quarterly Quarterly Inspection

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Diesel generator B room, fire area DG-4/Z-1, on October 10, 2018
(2) Standby switchgear 1C room, fire area C-22, on October 24, 2018
(3) Diesel generator C room, fire area DG-5/Z-1, on October 24, 2018
(4) Diesel generator A room, fire area DG-6/Z-1, on November 23, 2018

71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification

The inspectors observed and evaluated licensed operator requalification training on

===October 25, 2018.

Operator Performance (1 Sample)===

The inspectors observed and evaluated the operators performance as the plant was returning to steady state full power after a rod sequence adjustment on November 2, 2018.

71111.12Maintenance Effectiveness Routine Maintenance Effectiveness

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety-significant functions:

(1) Functional failure and maintenance review of the standby emergency diesel generators on October 15, 2018

71111.13Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Yellow risk during surveillance testing on Division II containment unit cooler on October 17, 2018
(2) Yellow risk during surveillance testing of Division I containment unit cooler with Division I emergency diesel generator in extended outage on November 1, 2018
(3) Green risk during inoperability of Division III emergency diesel generator due to failure of turbocharger lube oil pumps on November 28, 2018

71111.15Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Division I residual heat removal pump after flow through mechanical seal cooler was discovered to be below minimum specification on October 11, 2018
(2) Repeated offgas system degraded conditions on November 7, 2018

71111.19Post Maintenance Testing

The inspectors evaluated the following post maintenance tests:

(1) WO 00510064, HVC-ACU1B Failed to Auto Start During Divisional Swap/TBS Fin PMT, following replacement of a relay in the control circuitry for the Division II control room air handling unit on October 5, 2018
(2) WO 52734869, OPS Perform Operability Testing, following maintenance overhaul of Division I emergency diesel generator on November 7, 2018
(3) WO 00513628, Troubleshoot E22-S001DCP (HPCS Diesel DC Soakback Pump Motor), and WO 00513629, Troubleshoot E22-S001ACP (HPCS Diesel AC Soakback Pump Motor), following repair of the soakback oil pumps (AC and DC) for the high pressure core spray (Division III) diesel engine on December 18, 2018

71111.20Refueling and Other Outage Activities

The inspectors evaluated forced outage activities from November 10, 2018, to November 23, 2018. The forced outage occurred as a result of inadvertent closure of the number three turbine control valve. Station personnel conducted a forced outage and replaced a failed component in the number three turbine control valve.

71111.22Surveillance Testing The inspectors evaluated the following surveillance test: Routine

(1) STP-302-1605, Revision 26, HPCS Degraded Voltage Channel Calibration and Logic System Functional Test, on October 25,

RADIATION SAFETY

71124.01Radiological Hazard Assessment and Exposure Controls Radiological Hazard Assessment

The inspectors evaluated radiological hazards assessments and controls.

Instructions to Workers (1 Sample)

The inspectors evaluated worker instructions.

Contamination and Radioactive Material Control (1 Sample)

The inspectors evaluated contamination and radioactive material controls.

Radiological Hazards Control and Work Coverage (1 Sample)

The inspectors evaluated radiological hazards control and work coverage.

High Radiation Area and Very High Radiation Area Controls (1 Sample)

The inspectors evaluated risk-significant high radiation area and very high radiation area controls.

Radiation Worker Performance and Radiation Protection Technician Proficiency (1 Sample)

The inspectors evaluated radiation worker performance and radiation protection technician proficiency.

71124.03In-Plant Airborne Radioactivity Control and Mitigation Engineering Controls

The inspectors evaluated airborne controls and monitoring.

Use of Respiratory Protection Devices (1 Sample)

The inspectors evaluated respiratory protection.

Self-Contained Breathing Apparatus for Emergency Use (1 Sample)

The inspectors evaluated the licensees self-contained breathing apparatus program.

OTHER ACTIVITIES - BASELINE

71151Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

(1) BI01: Reactor Coolant System Specific Activity Sample (10/01/2017 - 09/30/2018)
(2) BI02: Reactor Coolant System Leak Rate Sample (10/01/2017 - 09/30/2018)
(3) OR01: Occupational Exposure Control Effectiveness Sample (01/01/2018-09/30/2018)
(4) PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (01/01/2018-09/30/2018)

71152Problem Identification and Resolution Semiannual Trend Review

The inspectors reviewed the licensees corrective action program for trends that might be indicative of a more significant safety issue. The inspectors noted that the station continues to exhibit an adverse trend in the area of equipment reliability.

Observation During the first half of the year, the licensee documented an adverse trend in the area of equipment reliability. This trend continued into the second half of the year, with the station experiencing three additional fuel failures, inoperability of the Division II emergency diesel generator after a failure of packing in the lube oil cooler, inoperability of the Division III emergency diesel generator after a failure of turbo charger lube oil pumps, and a reactor scram driven by a spontaneous failure of a turbine control valve. These failures have been documented in the corrective action program, and the adverse trend remains open in the licensees trending and performance review process. The station is planning to implement plant modifications in the upcoming refueling outage to reduce the likelihood and frequency of subsequent fuel failures.

71153Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports

The inspectors evaluated the following licensee event reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000458/2018-002-00, Inadvertent High Pressure Core Spray Initiation and Loss of Safety Function Due to Inadequate Work Instruction Mitigation Actions on April 26, 2018 On April 26, 2018, an invalid initiation of the high pressure core spray system occurred.

The inspectors reviewed the LER associated with the event and determined that the report adequately documented the summary of the event, including the cause of the event and potential safety consequences. The inspectors issued a finding for the licensees failure to properly pre-plan and perform maintenance on safety-related components in accordance with documented instructions appropriate to the circumstances. This LER is closed.

(2) LER 05000458/2018-003-00, Condition Prohibited by Technical Specifications due to Untimely Recognition of Failed Laboratory Analysis of Ventilation Charcoal Sample on April 30, 2018 The inspectors reviewed the LER submittal and documented a self-revealed, Green non-cited violation. This LER is closed.
(3) LER 05000458/2018-006-00, Potential Loss of Safety Function and Condition Prohibited by Technical Specifications due to Emergency Diesel Generator Lube Oil Chiller Leak Caused by Design Deficiency on July 5, 2018 On July 5, 2018, the licensee discovered water intrusion into the Division II emergency diesel generator lube oil system, rendering the system inoperable. The inspectors reviewed the LER associated with the event and determined that the report adequately documented the summary of the event, including the cause of the event and potential safety consequences. The inspectors issued a finding for the licensees failure to properly pre-plan and perform maintenance on safety-related components in accordance with documented instructions appropriate to the circumstances. This LER is closed.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 60855Operation of an Independent Spent Fuel Storage Installation and 60857Review of 10 CFR 72.48 Evaluations The inspectors evaluated the licensees operation of the independent spent fuel storage installation (ISFSI) from November 5 through November 8, 2018, on-site at the River Bend Station.

The River Bend Station ISFSI is licensed as a general 10 CFR Part 72 license and utilizes the Holtec HI-STORM 100 System, approved under Certificate of Compliance 1014, License Amendments 2 and 5, and Final Safety Analysis Report (FSAR), Revisions 3 and 7. The River Bend Station had been loading HI-STORM 100S Version B overpacks containing the Multi-Purpose Canister, MPC-68. The River Bend Stations ISFSI contained a total of 29 HI-STORM overpacks at the time of the routine inspection. The licensee was in the middle of its loading 2018 campaign. An inspector was onsite to observe loading activities associated with cask Number 30. The River Bend Station planned to complete an additional canister by the end of the campaign, increasing the total number of casks to 31 at the ISFSI.

The ISFSI activities specifically reviewed during the on-site inspection and the subsequent in-office review included:

(1) Evaluated and observed fuel selection and fuel loading operations associated with the 7th canister of the campaign (the 30th cask placed at the ISFSI).
(2) Evaluated and observed welding of the canister, non-destructive testing of the welds, bulk water removal, and forced helium drying.
(3) Reviewed the licensee's loading, processing, and heavy load procedures associated with its current dry fuel storage campaign.
(4) Reviewed licensees corrective action program implementation for ISFSI operations since the last routine ISFSI inspection which was completed in May 2016.
(5) Reviewed quality assurance program implementation, including recent quality assurance audits, surveillances, receipt inspection, and quality control activities.
(6) Reviewed documentation related to technical specification required operational surveillance activities and FSAR-required annual maintenance activities.
(7) Reviewed the licensees radiological monitoring data for calendar years 2016 and 2017 to verify compliance with 10 CFR 72.104 requirements.
(8) Reviewed spent fuel documentation for the canisters loaded since the last routine ISFSI inspection (Canisters 24-30) to confirm the fuel met all technical specification requirements for storage at the ISFSI.
(9) Reviewed annual maintenance activities for heavy lifting components which included special lifting devices, the vertical cask transporter, and the sites single-failure proof cask handling crane.
(10) Reviewed all 10 CFR 72.48 safety evaluations/screenings for changes made to the licensees ISFSI operations in accordance with Inspection Procedure 60857, since the last routine ISFSI inspection.
(11) Reviewed all changes made to the licensees 10 CFR 72.212 Report from Revision 2 to Revision 3 under the licensees 10 CFR 72.48 program in accordance with Inspection Procedure 60857.
(12) The Region IV Fuel Cycle and Decommissioning Branch submitted a technical assistance request to the NRC Division of Spent Fuel Management to evaluate the adequacy of the licensee's revised seismic stability analysis for the stack-up operations associated with the use of the Holtec HI-STORM 100 system. The revised analysis showed acceptable seismic response characteristics during a safe shutdown earthquake event at River Bend Station. The site specific responses calculated in the seismic stack-up analysis were below the maximum criteria established using guidance from the NRC Regulatory Issue Summary 2015-13, Seismic Stability Analysis Methodologies for Spent Fuel Dry Cask Loading Stack-up Configuration.

The inspectors did not identify any issues or concerns requiring documentation.

INSPECTION RESULTS

Failure to Disposition Adverse Conditions Associated with the Offgas System as Required by Procedures Cornerstone Significance Cross-cutting Inspection Aspect Procedure Public Radiation Green H.4 -

==71111.15 - Safety FIN 05000458/2018004-01 Teamwork Operability

==

Closed Determinations and Functionality Assessments The inspectors identified a finding for the licensees failure to disposition adverse conditions as required by Procedure EN-LI-102, Corrective Action Program, Revision 35. Specifically, the licensee did not categorize conditions associated with the offgas system as adverse as required by the procedure.

Description:

In a review of a sample of condition reports (CRs) associated with the offgas system, the inspectors identified six conditions that were not categorized as adverse conditions as required by Procedure EN-LI-102, Corrective Action Program, Revision 35, for conditions that resulted in a failure, malfunction, deficiency, deviation, or nonconformance of a structure, system, or component described in the current license basis. In each instance, the licensee generated a CR documenting the deficient condition associated with the system, but inappropriately concluded that the condition was non-adverse and so the requirements of EN-LI-102 to address adverse conditions within the corrective action program did not apply.

  • CR-RBS-2018-03866 documented alarms associated with high temperature in the adsorber vessel and abnormally high vault temperatures.
  • CR-RBS-2018-03939 documented bubbles found in refrigeration machine A contrary to procedural guidance.
  • CR-RBS-2018-04625 documented the failure of a valve associated with dryer bed A to fully open.
  • CR-RBS-2018-05273 documented an abnormal condition for the refrigeration machine A oil receiver tank identified on operator rounds.

After questioning from the inspectors, the station determined that personnel responsible for categorizing CRs based their assessment on the functionality determination section of Procedure EN-OP-104, Operability Determination Process, Revision 16. If plant equipment was determined not to be within the scope of the functionality assessment process, licensee personnel assumed that equipment was also outside of the scope of the corrective action program. Because most of the offgas system falls outside the scope of EN-OP-104, the licensee categorized most CRs associated with the offgas system as non-adverse.

Licensee personnel did not recognize that the scope of EN-OP-104 functionality assessment differs from the scope of EN-LI-102 adverse conditions for installed plant equipment.

Step 6.3 of EN-OP-104 limits the scope of functionality assessments to particular license basis documents such as the Technical Requirements Manual. Most of the offgas system does not fall within the scope of EN-OP-104. However, EN-LI-102, Attachment 9.1 includes any condition which results in a failure, malfunction, deficiency, deviation, or nonconformance of structures, systems, or components described in the current license basis. The updated safety analysis report is a current license basis document. Chapter 11 of the updated safety analysis report includes an extensive description of the offgas system, resulting in more conditions with the offgas system falling within the scope of EN-LI-102 adverse conditions and requiring resolution through the corrective action program than recognized by the licensee.

Corrective Actions: The licensees corrective actions included reviewing CRs related to the offgas system to revise them as adverse as required by EN-LI-102. The licensee is also planning to review extent of condition to address other systems potentially inappropriately treated as falling outside the scope of the EN-LI-102 adverse conditions.

Corrective Action Reference: CR-RBS-2018-05816

Performance Assessment:

Performance Deficiency: The failure to consistently disposition adverse conditions as required by Procedure EN-LI-102, Corrective Action Program, Revision 35, was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because, if left uncorrected, it would have the potential to lead to a more significant safety concern. Specifically, programmatic failure to categorize conditions associated with the offgas system as adverse and address them in the corrective action program could affect the availability and reliability of the offgas system to maintain the doses associated with releases to the environment as low as reasonably achievable.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix D, Public Radiation Safety Significance Determination Process. The finding was determined to be of very low safety significance (Green) because it involved the Effluent Release Program and it did not impair the ability to assess dose and did not exceed the 10 CFR Part 50, Appendix 1, or 10 CFR 20.1301(d) limits.

Cross-cutting Aspect: The finding had a cross-cutting aspect in the area of human performance, teamwork, because individuals and work groups did not communicate and coordinate their activities within and across organizational boundaries to ensure nuclear safety was maintained. Specifically, individuals and groups responsible for categorizing CRs did not communicate and coordinate their activities to ensure conditions were categorized correctly as required by procedures [H.4].

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

Failure to Control Entrance Into a High Radiation Area Cornerstone Significance Cross-cutting Inspection Aspect Procedure Occupational Green H.11 - 71124.01 Radiation NCV 05000458/2018004-02 Challenge the Radiological Safety Closed Unknown Hazard Assessment and Exposure Controls The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.7.1, High Radiation Area, for the licensees failure to control activities in a high radiation area.

Specifically, a worker entered into the lower area of the reactor building steam tunnel via a ladder, conservatively posted and controlled as a locked high radiation area (i.e., an area with dose rates greater than 100 millirem per hour and below 1,000 millirem per hour at 30 cm),without knowledge of current radiological conditions and without continuous radiation protection (RP) oversight, as required. The worker received an unexpected dose alarm.

Description:

On February 15, 2017, the worker (a contract carpenter) was briefed on radiological conditions by a supplemental RP technician using historical radiation survey data.

The two-year old survey showed a maximum dose rate of 20 to 30 millirem per hour for the work area. However, after the worker entered the work area, the maximum dose rate was found to be 560 millirem per hour. This was more than 18 times higher than what had been briefed by RP. As a result, the worker accumulated additional dose and received a dose alarm based on his radiological work permit (RWP) dose alarm setpoint of 52 millirem. Once the alarm was received, the worker stopped and left the area. The worker was logged onto RWP 20171709, Task 5, which only allowed entry into the area with knowledge of the work area dose rates and continuous RP coverage. In addition, the RP technician failed to take timely, current, and thorough radiation surveys because the RP technician placed too much reliance on two-year old survey data. Overall, the RP technician did not have a full understanding of radiological changes within the work area.

Corrective Actions: The licensee took immediate corrective actions, including coaching the job coverage RP technician and appropriately surveying the work area. Survey RBS-1702-0953 was updated accordingly.

Corrective Action Reference: CR-RBS-2017-01511

Performance Assessment:

Performance Deficiency: The failure to control work activities in a high radiation area, including providing incorrect information about radiological conditions to a worker, is a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the human performance attribute of the Occupational Radiation Safety Cornerstone and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Appendix C, Occupational Radiation Safety Significance Determination Process, and determined the violation was of very low safety significance (Green) because it:

(1) was not related to as low as reasonably achievable planning,
(2) did not involve an overexposure or substantial potential for overexposure, and
(3) did not compromise the ability to assess dose.

Cross-cutting Aspect: This finding involved the cross-cutting aspect of human performance, challenge the unknown, because the event was a direct result of not stopping when faced with uncertain conditions. The RP technician providing oversight failed to question the need to survey all areas, ensure the correct work location within the work area, and provide continuous oversight to ensure the individuals working in the area were not entering spaces not briefed for entry [H.11].

Enforcement:

Violation: Technical Specification 5.7.1, High Radiation Areas, requires, in part, that any individual who enters a high radiation area shall be provided with or accompanied by one or more of the following:

(a) a radiation monitoring device that continuously integrates the radiation dose rate in the area and alarms when a preset integrated dose is received after the dose rate levels in the area have been established and personnel are aware of them and/or
(b) an individual qualified in RP procedures with a radiation dose rate monitoring device, who is responsible for providing positive control over the activities within the area and shall perform periodic radiation surveillance at the frequency specified by the health physics supervision in the RWP.

Contrary to the above, on February 15, 2017, an individual entered a high radiation area with a radiation monitoring device that continuously integrates the radiation dose rate in the area and alarms when a preset integrated dose is received, but the dose rate levels in the area had not been established and personnel were therefore not aware of them. Additionally, the individual qualified in RP procedures with a radiation dose rate monitoring device, who was responsible for providing positive control over the activities within the area, failed to perform periodic radiation surveillance at the frequency specified by the health physics supervision in the RWP.

Enforcement Action: This violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy.

Inadequate Risk Mitigation Actions in Work Procedure Leads to Inadvertent High Pressure Core Spray Initiation Cornerstone Significance Cross-cutting Inspection Aspect Procedure Mitigating Green H.12 - Avoid 71153 -

Systems NCV 05000458/2018004-03 Complacency Follow-up of Closed Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for the licensees failure to implement a procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, the licensee failed to pre-plan and perform maintenance on level transmitter B21-LTN081C in accordance with a procedure appropriate to the circumstances. The failure led to a perturbation in the C reactor water level instrument reference leg that caused an invalid actuation of the high pressure core spray (HPCS) system at power.

Description:

On April 26, 2018, with the plant operating at 100 percent power, the licensee attempted to replace channel C level instrument B21-LTN081C, which was reading lower than the other channels. When the newly installed instrument was returned to service after the replacement, air was released into the line. The air release caused a perturbation in the readings of two instruments that share a reference leg with B21-LTN081C. These instruments, B21-LTN073G and B21-LTN073C, provide inputs into the level 2 HPCS actuation logic and are together sufficient to cause a HPCS actuation. Upon the air release, a spurious level 2 condition was detected by both instruments, causing an actual initiation of HPCS to occur.

The inadvertent initiation of HPCS directed cold water into the shroud, high above the core.

The cold water condensed the steam in the area and led to a drop in pressure. The drop in pressure inserted negative reactivity, causing reactor power to fall from 100 percent to 94 percent. After verifying that a low level condition did not actually exist, operators secured HPCS. The securing of HPCS caused the system to be temporarily inoperable.

The cause of the inadvertent initiation was determined to be an inadequate procedure.

Specifically, the licensee restored the instrument to service using Procedure STP-051-4203, which did not contain actions to mitigate the possibility of an inadvertent HPCS actuation, even though such an actuation was a known risk.

Corrective Actions: The licensee restored the HPCS system to operable status after the event and modified STP-051-4203 to mitigate the risk of an inadvertent HPCS actuation.

Corrective Action Reference: CR-RBS-2018-02524

Performance Assessment:

Performance Deficiency: The failure to pre-plan and perform maintenance that can affect the performance of safety-related equipment using written procedures and documented instructions appropriate to the circumstances was a performance deficiency.

Screening: The inspectors determined that the performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, by conducting maintenance using a procedure inappropriate to the circumstances, the licensee caused a malfunction that led to an inadvertent safety system actuation and an associated power transient.

Significance: The inspectors assessed the significance of the finding using NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1 - Mitigating Systems Screening Questions. The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-cutting Aspect: The finding had a cross-cutting aspect in the area of human performance, avoid complacency, because individuals did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk even while expecting successful outcomes. Specifically, despite knowing that the maintenance had the potential to cause an inadvertent actuation of HPCS, the licensee failed to appropriately mitigate the risk [H.12].

Enforcement:

Violation: Technical Specification 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory Guide 1.33, Revision 2, Appendix A, Section 9.a specifies that maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to the above, on April 26, 2018, the licensee failed to pre-plan and perform maintenance that can affect the performance of safety-related equipment using written procedures and documented instructions appropriate to the circumstances. Specifically, the written procedures and documented instructions used to replace B21-LTN081C, a level instrument that can affect the performance of safety-related equipment, were not appropriate to mitigate the risk of an inadvertent actuation of the HPCS system.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

Control Room Fresh Air Surveillance Procedures Inappropriate to the Circumstances Cornerstone Significance Cross-cutting Inspection Aspect Procedure Barrier Integrity Green H.14 - 71153 -

NCV 05000458/2018004-04 Conservative Follow-up of Closed Bias Events and Notices of Enforcemen t Discretion The inspectors reviewed a self-revealed, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which occurred because the licensee did not prescribe procedures for performing surveillance tests on the main control room fresh air (CRFA) subsystem that were appropriate to the circumstances. Specifically, the licensee allowed up to 31 days to receive and review the results of charcoal filtration bed samples.

As a result, the Division II CRFA subsystem was inoperable from April 17, 2018, to May 3, 2018, exceeding Technical Specification 3.7.2 allowed outage time of 7 days.

Description:

On April 17, 2018, the licensee removed a sample canister of a carbon filter from the Division II CRFA air filter for laboratory testing in accordance with STP-004-002, Division II Main Control Room Fresh Air System Laboratory Carbon Filter, Revision 3, to fulfill technical specification surveillance requirements.

On April 30, 2018, the licensee reviewed the laboratory testing results and determined that they did not meet the acceptance criteria of STP-004-002 and declared the Division II CRFA subsystem inoperable. The licensee replaced the carbon filter media and restored the Division II CRFA subsystem to an operable status on May 3, 2018, 16 days after the test sample was removed.

Technical Specification 3.7.2 requires that two CRFA subsystems be operable during Modes 1, 2, and 3. It also requires that if one subsystem is inoperable, it be returned to service within 7 days or the unit be placed into Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The licensee did not meet this technical specification requirement from April 17, 2018, until May 3, 2018.

STP-004-002, Step 7.4.1, requires that the licensee obtain the results of laboratory testing of the CRFA carbon samples within 31 days of sample removal. This conflicts with Technical Specification 3.7.2 requirement. Because of this, the licensees procedure did not ensure that the licensee would return any inoperable subsystem to an operable status within 7 days or the unit be placed into Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> if laboratory testing results did not meet the acceptance criteria of STP-004-002.

Corrective Actions: The licensees immediate corrective action was to replace the Division II CRFA charcoal media to return the system to an operable status. Additional corrective actions included revising STP-402-8605 to obtain test results be reviewed within 3 days rather than 31 days or to take action to ensure the charcoal filters are in an operable status.

The licensee also reviewed the testing requirements for other charcoal filters related to technical specification requirements to ensure laboratory test results are reviewed within timeframes consistent with the technical specification requirements.

Corrective Action Reference: CR-RBS-2018-02592

Performance Assessment:

Performance Deficiency: The failure to provide procedures appropriate to the circumstances to ensure failed CRFA subsystem testing would be identified and addressed within Technical Specification 3.7.2 requirements was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the procedure quality attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents. Specifically, the licensees CRFA test procedures did not ensure that test failures would be identified and addressed within Technical Specification 3.7.2 requirements.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3, Barrier Integrity Screening Questions, dated June 19, 2012. The inspectors determined that the finding was of very low safety significance (Green) because it only represented a degradation of the radiological barrier function of the control room.

Cross-cutting Aspect: The finding had a cross-cutting aspect in the area of human performance, conservative bias, because the individuals did not use decision-making practices that emphasized prudent choices over those that were simply allowable.

Specifically, licensee personnel did not decide to take action to obtain test results within the 7-day technical specification allowed completion time rather than within the procedurally allowed 31 days [H.14].

Enforcement:

Violation: As required by Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances.

Contrary to the above, prior to April 30, 2018, surveillance testing activities on the Division II CRFA subsystem, which are activities affecting quality, were not prescribed by documented procedures appropriate to the circumstances. Specifically, the procedure for conducting surveillance testing on the Division II CRFA subsystem allowed up to 31 days to receive and review the results of charcoal filtration bed samples. As a result, the Division II CRFA subsystem was inoperable from April 17, 2018, to May 3, 2018, exceeding Technical Specification 3.7.2 allowed outage time of 7 days.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

Inappropriate Maintenance Procedure Leads to Water Intrusion into Division II Emergency Diesel Generator Lube Oil System Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Green H.5 - Work 71153 -

Systems NCV 05000458/2018004-05 Management Follow-up of Closed Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a for the licensees failure to implement a procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, the licensee failed to pre-plan and perform maintenance on the Division II emergency diesel generator in accordance with a procedure appropriate to the circumstances. As a result, the emergency diesel generator was rendered incapable of performing its specified safety function.

Description:

On July 6, 2018, the Division II emergency diesel generator at River Bend Station was declared inoperable due to confirmed water intrusion into the lube oil system.

The cause of the water intrusion was a failure of the packing material that separates the water side of the lube oil heat exchanger tube sheet from the oil side.

The emergency diesel generator lube oil heat exchanger is designed with a floating tube sheet on one end to allow for thermal expansion and contraction during operation. The floating end contains two rings of rubber packing and an internal lantern ring, with weep holes that direct packing leakage outside of the heat exchanger onto the floor.

When exposed to repeated thermal stresses over time, the packing material has the potential to deform over time. The system is designed so that water leakage caused by this deformation will pass through the weep holes in the lantern ring onto the floor, where the station will be detect and respond to it.

The lantern ring that the licensee used in the seal was incorrectly sized relative to the tube sheet itself. The tube sheet was machined to a smaller, non-standard size by the original vendor, but the size of the installed lantern ring was never adjusted accordingly. The structure therefore exhibited excessive clearance that allowed the packing, as it deformed and degraded, to extrude and block the lantern ring drain holes when heated from ambient to standby temperatures. This condition had the potential to send water leakage into the lube oil side of the heat exchanger rather than onto the floor as designed.

The licensee was aware of this non-conforming condition since the year 2000 and experienced several water leaks in the lube oil system as a result of it, with the most recent leak occurring in 2008. The leaks occurred in conjunction with extended maintenance outages in which the lube oil system was cooled down to ambient temperature and then heated up to standby conditions.

On June 24, 2018, the licensee entered into an extended maintenance outage on the Division II emergency diesel generator. During this outage, the licensee allowed the emergency diesel generator lube oil system to cool down to ambient temperatures. On July 1, 2018, the licensee completed the outage and heated the lube oil system back up to standby conditions. The licensee ran the emergency diesel generator for post maintenance tests, accumulating 187 minutes of run time with normal parameters. During the post maintenance testing, the licensee identified an issue associated with relays that control the emergency start circuit. To correct this issue, the licensee tagged out the engine and auxiliaries, allowing temperatures in the lube oil system to return back to ambient levels. On July 3, 2018, after resolving the relay issue, the licensee removed tags and heated the lube oil system back up to standby conditions. On July 4, 2018, the licensee completed post maintenance testing on the emergency diesel generator and declared it operable. On the evening of July 5, 2018, a watchstander noted a large increase in the differential pressure across the filter for the lube oil strainer. After sampling the lube oil system, the licensee found evidence of water intrusion and declared the emergency diesel generator inoperable.

After investigation, the licensee determined that the cooldown of the system on July 1, 2018, induced contractions in the packing that caused a leak. On July 3, 2018, when the packing subsequently expanded on startup of the system, it extruded and covered the lantern ring drain holes. Because the leaking water was unable to travel through the lantern ring, it intruded into the lube oil side of the heat exchanger where it spread throughout the system, causing the high differential pressure reading on the strainer and rendering the emergency diesel generator inoperable.

The improperly-sized lantern ring represented a non-conforming condition that made the lube oil system vulnerable to water intrusion in response to thermal cycling. Despite knowing about this non-conforming condition and having experienced water intrusion related to it in multiple prior maintenance outages, the licensee exposed the system to the failure mechanism associated with the condition without utilizing any precautions, steps, or references in any procedures or work instructions to verify that the system remained intact and functioning properly prior to returning it to service.

Corrective Action(s): The licensee replaced the deformed packing and the lantern ring in the Division II emergency diesel generator and declared the emergency diesel generator operable on July 9, 2018. The licensee installed a correctly-sized lantern ring on the Division I emergency diesel generator in the most recent outage and has issued a work order to install a correctly-sized lantern ring in the next Division II emergency diesel generator outage.

Corrective Action Reference: CR-RBS-2018-3804

Performance Assessment:

Performance Deficiency: The failure to pre-plan and perform maintenance that can affect the performance of safety-related equipment using written procedures and documented instructions appropriate to the circumstances was a performance deficiency.

Screening: The inspectors determined that the performance deficiency was more than minor, and therefore a finding, because it was associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the procedures used in the maintenance outage failed to contain precautions, steps, or instructions to ensure that the lube oil system was intact and functioning properly after being repeatedly exposed to a known historical failure mechanism. As a consequence, the licensee incorrectly designated the Division II emergency diesel generator as operable and placed the Division I emergency diesel generator in maintenance mode for a test run, creating a condition in which the Division I and Division II emergency diesel generators were simultaneously inoperable.

Significance: The inspectors assessed the significance of the finding using NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 2 - Mitigating Systems Screening Questions. The inspectors determined that the finding was of very low safety significance (Green) because the water intrusion, which began on or after July 1, 2018, did not represent

(1) an actual loss of function of at least a single train for greater than its technical specification allowed outage time,
(2) two separate safety systems out-of-service for greater than its technical specification allowed outage time, or
(3) an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Cross-cutting Aspect: The finding had a cross-cutting aspect in the area of human performance, work management, because the station failed to implement a work process that included the identification and management of risk commensurate to the work.

Specifically, the licensee failed to recognize and plan for the risk, confirmed in prior station operating experience, that the packing and lantern ring in the emergency diesel generator heat exchanger might fail in response to repeated cooldowns and heatups of the system during an outage [H.5].

Enforcement:

Violation: Technical Specification 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978.

Regulatory Guide 1.33, Revision 2, Appendix A, Section 9.a specifies that maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to the above, from June 24, 2018, until July 9, 2018, the licensee failed to pre-plan and perform maintenance that can affect the performance of safety-related equipment using written procedures and documented instructions appropriate to the circumstances.

Specifically, the written procedures and documented instructions used in the maintenance were not appropriate to the circumstances in that they repeatedly exposed the system to a known historical failure mechanism without directing operators to take appropriate action to verify that the system was intact and functioning properly prior to returning it to service.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

On November 8, 2018, the inspectors presented the baseline radiation safety inspection results to Mr. W. Maguire, Site Vice President, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.

On December 13, 2018, the lead inspector presented the results from the routine ISFSI inspection to Mr. Kent Scott, General Manager Plant Operations, and other members of the licensee staff. Licensee personnel acknowledged the information presented. The inspectors confirmed that proprietary information was controlled to protect from public disclosure.

On January 14, the inspector presented the quarterly resident inspector inspection results to Mr. S. Vercelli, Site Vice President, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.

DOCUMENTS REVIEWED

71111.01 - Adverse Weather Protection

Condition Reports (CR-RBS-)

2018-05172 2018-05174 2018-05449 2018-05473

Miscellaneous Documents

WT-WTRBS-2018-00075

Procedures

Number Title Revision

EN-FAP-WM-016 Seasonal Reliability 1

OSP-0043 Freeze Protection and Temperature Maintenance 39

Work Orders

2714395 52717534 52768742 52833091

71111.04 - Equipment Alignment

Condition Reports (CR-RBS-)

2018-00526 2018-01850 2018-02670 2018-03262 2018-03476

2018-03780 2018-04225 2018-04490 2018-04550 2018-04807

2018-04826 2018-05094 2018-05556 2018-05563

Procedures

Number Title Revision

PEP-0026 Diesel Generator Operating Logs 015

SOP-0030 High Pressure Core Spray 33

SOP-0053 Standby Diesel Generator and Auxiliaries (SYS 309) 339

SOP-0061 Diesel Generator Building Ventilation 016

71111.05AQ - Fire Protection Annual/Quarterly

Calculation

Number Title Revision

G13.18.12.2-022 River Bend Station - Combustible Loading 5

Condition Reports (CR-RBS-)

2017-05946 2018-00331 2018-01736 2018-02863 2018-03079

2018-04613

Procedures

Number Title Revision

CB-116-131- Standby Switchgear 1C Room, Fire Area C-22 3

DG-98-050 Diesel Generator B Room Fire Area DG-4/Z-1 3

DG-98-051 Diesel Generator B Control Room Fire Area DG-4/Z-1 4

DG-98-052 Diesel Generator C Room Fire Area DG-5/Z-1 4

DG-98-053 Diesel Generator C Control Room Fire Area DG-5/Z-1 4

DG-98-054 Diesel Generator A Room Fire Area DG-6/Z-1 4

SEP-FPP-RBS-001 River Bend Station Fire Protection Program 4

SEP-FPP-RBS-004 Guidelines for Preparation of Pre-Fire Strategies and 2

Pre-Fire Plans

SOP-0053 Standby Diesel Generator and Auxiliaries (SYS 309) 339

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Procedures

Number Title Revision

EN-OP-115 Conduct of Operations 025

GOP-0002 Power Decrease / Plant Shutdown 082

71111.12 - Maintenance Effectiveness

Condition Reports (CR-RBS-)

2007-03766 2017-03638 2017-07080 2017-07111 2017-07532

2018-00505

Miscellaneous Document

Number Title Revision

SDC-309 System Design Criteria Standby Diesel Generator 3

System

Procedures

Number Title Revision

EN-DC-203 Maintenance Rule Program 4

EN-DC-205 Maintenance Rule Monitoring 6

EN-DC-206 Maintenance Rule (A)(1) Process 3

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Condition Reports (CR-RBS-)

2018-05603 2018-05824 2018-06363

Procedures

Number Title Revision

ADM-0096 Risk Management Program Implementation and On- 327

line Maintenance Risk Assessment

EN-WM-104 On Line Risk Assessment 018

STP-305-1604 ENGR-CHGR1B Load Test 302

STP-403-1200 HVR-UC1A System A Timer Channel Functional Test 012

STP-403-1201 HVR-UC1B System B Timer Channel Functional Test 006

STP-403-1300 HVR-UC1A System A Timer Channel Calibration 013

71111.15 - Operability Determinations and Functionality Assessments

Condition Reports (CR-RBS-)

2012-00160 2012-00178 2018-05468 2018-05479 2018-01190

2018-03866 2018-03939 2018-04134 2018-04531 2018-04625

2018-04864 2018-05264 2018-05273 2018-05816

Miscellaneous Documents

Number Title Revision

River Bend Station Emergency Plan 43

21.435-000-006 GE Design Specification, Residual Heat Removal 0

System

SDC-204 Residual Heat Removal System Design Criteria 4

System Number 204

Procedures

Number Title Revision

EN-LI-102 Corrective Action Program 35

EN-OP-104 Operability Determination Process 16

71111.19 - Post Maintenance Testing

Condition Reports (CR-RBS-)

2018-05378 2018-05866 2018-05874 2018-05875 2018-05876

2018-05880 2018-05909 2018-05915 2018-05937 2018-05944

2018-05981 2018-06011 2018-06063 2018-06363 2018-06375

Procedures

Number Title Revision

CMP-1026 MCC Circuit Breakers, Starters, and Thermal 21

Overloads (Testing Performed per Work Order

Instructions)

EN-MA-157 Configuration Control 2

Procedures

Number Title Revision

EN-WM-107 Post Maintenance Testing 1

MCP-1130 Testing and Calibration of Agastat Relays 11

SOP-0053 Standby Diesel Generator and Auxiliaries (Sys 309) 339

STP-309-0206 Division I Diesel Generator 184 Day Operability Test 030

Work Orders

00510064 00513628 00513629 52734869

71111.20 - Refueling and Other Outage Activities

Condition Reports (CR-RBS-)

2018-06018 2018-06256

Procedures

Number Title Revision

GOP-0001 Plant Startup 103

GOP-0003 Scram Recovery 032

71111.22 - Surveillance Testing

Condition Reports (CR-RBS-)

2018-01283 2018-01894 2018-01982 2018-01987 2018-03496

2018-05662 2018-05709

Work Order 276254

71124.01 - Radiological Hazard Assessment and Exposure Controls

Air Sample Surveys

Number Title Date

RBS-AS-2018-0082 Reactor Building Cavity 186 January 16, 2018

RBS-AS-2018-0085 Aux Platform 186 January 16, 2018

RBS-AS-2018-0107 RFF South 186 January 19, 2018

RBS-AS-2018-0285 Fuel Building 148 April 17, 2018

RBS-AS-2018-0559 Fuel Building Cask Pool 113 August 23, 2018

Audits and Self-Assessments

Number Title Date

LO-RLO-2017- RP Pre-NRC Focused Self-Assessment Radiation August 28, 2018

00071 Safety Inspection

Condition Reports (CR-RBS-)

2017-01233 2017-01262 2017-01323 2017-01343 2017-01372

2017-01410 2017-01511 2017-01534 2017-01648 2017-02099

2017-02910 2017-03011 2017-03424 2017-05519 2017-05787

2017-06922 2017-07100 2017-07664 2017-07929 2018-00523

2018-00596 2018-00725 2018-01764 2018-02221 2018-03241

2018-03534 2018-03845 2018-04681

Miscellaneous Documents

Number Title Date

EN-RP-101, Att. 6 LHRA/VHRA Key Log November 7, 2018

Pool Material Inventory Report Post RF-19 May 31, 2017

2018 Annual Inventory Reconciliation January 3, 2018

443615001 10 CFR Part 61 Waste Stream Sample Screening January 30, 2018

and Evaluation

2783772 Radioactive Source Leak Test April 11, 2018

Procedures

Number Title Revision

ADM-0071 Fuel Pools Material Control 008

ADM-0097 Hot spot/line Flushing Program 002

ADM-0103 Radiation Protection Standards and Expectations 006

EN-RP-100 Radiation Worker Expectations 011

EN-RP-101 Access Control for Radiologically Controlled Areas 012

EN-RP-102 Radiological Control 005

EN-RP-105 Radiological Work Permits 018

EN-RP-108 Radiation Protection Posting 018

EN-RP-109 Hot Spot Program 005

EN-RP-121 Radioactive Material Control 014

EN-RP-152 Conduct of Radiation Protection 001

EN-RP-201 Dosimetry Administration 005

EN-RP-202 Personnel Monitoring 012

EN-RP-311 Electronic Alarming Dosimeters 002

RSP-0229 Radiation Protection Response to Changing 019

Radiological Conditions

SOP-0112 Solid Radwaste Processing (SYS #604) 019

Radiation Surveys

Number Title Date

RBS-1702-0953 141 Reactor Building Follow Up Survey February 15, 2017

RBS-1804-0213 4300 Radwaste 136 April 23, 2018

Radiation Surveys

Number Title Date

RBS-1806-0149 4114 Special Nuclear Material Storage Room June 12, 2018

RBS-1808-0351 4024 Radwaste 90 Pipe Chase August 27, 2018

RBS-1809-0181 7500 Reactor Building 186 September 6, 2018

Radiation Work Permits

Number Title Revision

20171800 RF-19 Refuel Floor Outage Activities 06

20171953 RF-19 Bio-Shield Activities 00

20181001 Radiation Protection Activities 00

20181006 Decon, Radwaste & Radioactive Material Activities 00

20181071 Floor Drain Cleaning Project 00

20181214 Emergent Work Including All Support Activities 00

20181273 Reverse Osmosis (RO) Filter Move, Setup, & 00

Changeout

20181296 RWCU Pump A Seal Replacement 02

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Air Sample Surveys

Number Title Date

RBS-AS-2018-0321 Air Lapel Alpha Sample May 2, 2018

RBS-AS-2018-0327 Air Lapel Alpha Sample May 2, 2018

RBS-AS-2018-0328 Airborne Calculation Tri-Nuke Hose Cutup May 2, 2018

RBS-AS-2018-0336 Air Lapel Alpha Sample May 7, 2018

RBS-AS-2018-0341 Airborne Calculation Tri-Nuke Hose Cutup May 9, 2018

Audits and Self-Assessments

Number Title Date

LO-RLO-2017- RP Pre-NRC Focused Self-Assessment Radiation August 28, 2018

00071 Safety Inspection

Condition Reports (CR-RBS-)

2017-01217 2017-01422 2017-03366 2017-03880 2017-04151

2017-04156 2017-04941 2017-11262 2018-00177 2018-03534

HEPA and Charcoal Filter Test Records

Number Title Date

V-049 DOP HEPA Test Portable Ventilation September 20, 2017

VW-035 DOP HEPA Test Portable Ventilation May 24, 2017

35101639026068 DOP HEPA Test Portable Ventilation May 24, 2017

HEPA and Charcoal Filter Test Records

Number Title Date

35101639026069 DOP HEPA Test Portable Ventilation May 24, 2017

Miscellaneous Documents

Number Title Date

ODMI Failed Fuel Action Plan September 7, 2018

ODMI Failed Fuel Action Plan October 2, 2018

Procedures

Number Title Revision

EN-RP-402 DOP Challenge Testing of HEPA Vacuums and 004

Portable Ventilation Units

EN-RP-404 Operation and Maintenance of HEPA Vacuum 008

Cleaners and HEPA Ventilation Units

EN-RP-501 Respiratory Protection Program 005

EN-RP-502-01 FireHawk M7 SCBA 002

EN-RP-502-01 Inspection And Maintenance Of Respiratory 005

Protection Equipment

EN-RP-502-02 Flow Testing MSA Breathing Apparatus 000

EN-RP-502-03 AirHawk II SCBA 000

EN-RP-503 Selection, Issue and Use of Respiratory Protection 007

Equipment

EN-RP-504 Breathing Air 004

EN-RP-505 PortaCount Respirator Fit Testing 007

Respirator Testing, Inspection, and Inventory Records

Number Title Date

AMAG204076 SCBA October 3, 2017

AMAG203061 SCBA October 3, 2017

AMAG204076 SCBA February 14, 2018

AMAG199928 SCBA February 14, 2018

71151 - Performance Indicator Verification

Condition Reports (CR-RBS-)

2017-07277 2017-07777 2018-01613 2018-01756

Miscellaneous Documents

Number Title Date

RBG-47820 NRC Performance Indicator Submittal for 4th January 18, 2018

Quarter 2017

Miscellaneous Documents

Number Title Date

RBG-47856 NRC Performance Indicator Submittal for 1st April 18, 2018

Quarter 2018

RBG-47887 NRC Performance Indicator Submittal for 2nd July 23, 2018

Quarter 2018

RBS-47908 NRC Performance Indicator Submittal for 3rd October 29, 2018

Quarter 2018

Procedures

Number Title Revision

EN-LI-114 Regulatory Performance Indicator Process 11 & 12

NEI 99-02 Regulatory Assessment Performance Indicator 7

Guideline

71152 - Problem Identification and Resolution

Condition Reports (CR-RBS-)

2018-01277 2018-02656 2018-03001 2018-03182 2018-03804

2018-04253 2018-04921 2018-05564 2018-06018 2018-06363

Procedure

Number Title Revision

EN-LI-121 Trending and Performance Review Process 25

71153 - Follow-up of Events and Notices of Enforcement Discretion

Condition Report (CR-RBS-)

2018-02592

Procedure

Number Title Revision

STP-402-8605 Division II Main Control Room Fresh Air System 3&4

Laboratory Carbon Filter Analysis

4OA5.1 Other Activities (IP 60855) and (IP 60857)

CFR 72.48 Applicability Determinations and 10 CFR 72.48 Screens

Numerous, dated June 1, 2016, through October 21, 2018.

Condition Reports (CR-RBS-)

Numerous, dated June 1, 2016, through October 21, 2018.

Design Basis Documents

Number Title Revision

RBS-CS-17-0003 Methods and Criteria for Finite Element Analysis of 0

the Dry Cask Stack-Up Configuration

RBS-CS-17-0004 Report for the Seismic Stability Analysis of the 0

DFS Stack-up in the Cask Handling Area

N/A 10 CFR 72.212 Report; River Bend Station 3

Miscellaneous Documents

Number Title Revision

or Date

RQA-20-2016 2016 ISFSI Audit 1

RQA-20-2018 2018 ISFSI Audi 1

N/A RBS Cask 24-30 Fuel Selection Characteristic 0

Matrix

N/A 2017 Annual Radioactive Effluent Release Report May 1, 2018

1805-0323 Dry Fuel Cask Storage Area Radiological Survey May 29, 2018

STP-000-0001 Daily Operating Logs (numerous) Various

Procedures

Number Title Revision

DFS-0002 Dry Fuel Cask Loading 307

DFS-0003 MPC Transfer Operations and HI-STORM 4

Transport

DFS-0140 MPC Forced Helium Dehydration Operation 5

EN-DC-215 Fuel Selection for Holtec Dry Cask Storage 9

EN-LI-102 Corrective Action Program 35

Work Orders

00182838 00497642 52696446 52715421 52767513

The following items are requested for the

Occupational Radiation Safety Inspection

at River Bend Station

November 5-9, 2018

Integrated Report 2018004

Inspection areas are listed in the attachments below.

Please provide the requested information on or before October 26, 2018

Please submit this information using the same lettering system as below. For example, all

contacts and phone numbers for Inspection Procedure 71124.01 should be in a file/folder titled

1- A, applicable organization charts in file/folder 1- B, etc.

If information is placed on ims.certrec.com, please ensure the inspection exit date entered is at

least 30 days later than the onsite inspection dates, so the inspectors will have access to the

information while writing the report.

In addition to the corrective action document lists provided for each inspection procedure listed

below, please provide updated lists of corrective action documents at the entrance meeting.

The dates for these lists should range from the end dates of the original lists to the day of the

entrance meeting.

If more than one inspection procedure is to be conducted and the information requests appear

to be redundant, there is no need to provide duplicate copies. Enter a note explaining in which

file the information can be found.

If you have any questions or comments, please contact Louis Carson at (817)200-1221,

Louis.Carson@nrc.gov or Natasha Greene at (817)200-1154, Natasha.Greene@nrc.gov

PAPERWORK REDUCTION ACT STATEMENT

This letter does not contain new or amended information collection requirements subject

to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.). Existing information

collection requirements were approved by the Office of Management and Budget,

control number 3150-0011.

1. Radiological Hazard Assessment and Exposure Controls (71124.01) and

Performance Indicator Verification (71151)

Date of Last Inspection: February 10, 2017

A. List of contacts and telephone numbers for the Radiation Protection Organization Staff

and Technicians, as well as the Licensing/Regulatory Affairs staff. Please include area

code and prefix. If work cell numbers are appropriate, then please include them as well.

B. Applicable organization charts including position or job titles. Please include as

appropriate for your site, Site Management, RP, Chemistry, Maintenance (I&C),

Engineering, and Emergency Protection. (Recent pictures are appreciated.)

C. Copies of audits, self-assessments, LARs, and LERs written since the last inspection

date, related to this inspection area

D. Procedure indexes for the radiation protection procedures and other related disciplines.

E. Please provide procedures related to the following areas noted below. Additional

procedures may be requested by number after the inspector reviews the procedure

indexes.

1. Radiation Protection Program

2. Radiation Protection Conduct of Operations, if not included in #1.

3. Personnel Dosimetry

4. Posting of Radiological Areas

5. High Radiation Area Controls

6. RCA Access Controls and Radiation Worker Instructions

7. Conduct of Radiological Surveys

8. Radioactive Source Inventory and Control

9. Fuel Pool Inventory Access and Control

F. Please provide a list of NRC Regulatory Guides and NUREGs that you are currently

committed to relative to this program. Please include the revision and/or date for the

commitment and where this may be located in your current licensing basis documents.

G. Please provide a summary list of corrective action documents (including corporate and

sub-tiered systems) since the last inspection date.

1. Initiated by the radiation protection organization

2. Assigned to the radiation protection organization

NOTE: These lists should include a description of the condition that provides sufficient

detail that the inspectors can ascertain the regulatory impact, the significance

level assigned to the condition, the status of the action (e.g., open, working,

closed, etc.) and the search criteria used. Please provide in document formats

which are sortable and searchable so that inspectors can quickly and

efficiently determine appropriate sampling and perform word searches, as

needed. (Excel spreadsheets are the preferred format.) If codes are used,

please provide a legend for each column where a code is used.

H. List of radiologically significant work activities scheduled to be conducted during the

inspection period. (If the inspection is scheduled during an outage, please also include a

list of work activities greater than 1 rem, scheduled during the outage with the dose

estimate for the work activity.) Please include the radiological risk assigned to each

activity.

I. Provide a summary of any changes to plant operation that have resulted or could result

in a significant new radiological hazard. For each change, please provide the

assessment conducted on the potential impact and any monitoring done to evaluate it.

J. List of active radiation work permits and those specifically planned for the on-site

inspection week.

K. Please provide a list of air samples taken to verify engineering controls and a separate

list for breathing air samples in airborne radiation areas or high contamination work

areas. Please include the RWP the breathing air sampling supports.

L. Please provide the current radioactive source inventory, listing all radioactive sources

that are required to be leak tested. Indicate which sources are deemed 10 CFR Part 20,

Appendix E, Category 1 or Category 2. Please indicate the radioisotope, initial and

current activity (w/assay date), and storage location for each applicable source.

M. The last two leak test results for all required/applicable radioactive sources that have

failed its leak test within the last two years. Provide any applicable condition reports.

N. A list of all non-fuel items stored in the spent fuel pools, and if available, their appropriate

dose rates (Contact / @ 30cm)

O. A list of radiological controlled area entries greater than 100 millirem, since the last

inspection date. The list should include the date of entry, some form of worker

identification, the radiation work permit used by the worker, dose accrued by the worker,

and the electronic dosimeter dose alarm set-point used during the entry (for

Occupational Radiation Safety Performance Indicator verification in accordance with IP 71151).

P. A list describing VHRAs and TS HRAs (> 1 rem/hour) that are current and historical.

Include their current status, locations, and control measures.

Q. Temporary effluent monitor locations and calibrations (AMS-4) used to monitor normally

closed doors or off-normal release points (e.g., equipment hatch or turbine heater bay

doors). Include any CRs associated with this monitoring or instrumentation.

3. In-Plant Airborne Radioactivity Control and Mitigation (71124.03)

Date of Last Inspection June 16, 2016

A. List of contacts and telephone numbers for the following areas. Please include area

code and prefix. If work cell numbers are appropriate, then please include them as well.

1. Respiratory Protection Program

2. Self-contained breathing apparatus

3. Ventilation Systems for breathing air (not effluents)

4. Licensing/Regulatory Affairs

B. Applicable organization charts including position or job titles. Please include as

appropriate for your site, Site Management, RP, Chemistry, Maintenance (I&C),

Engineering, and Emergency Protection. (Recent pictures are appreciated.)

C. Copies of audits, self-assessments, vendor or NUPIC audits for contractor support

(SCBA), LARs, and LERs, written since the date of last inspection related to:

1. Installed air filtration systems

2. Self-contained breathing apparatuses

D. Procedure index for Radiation Protection, Maintenance, I&C, and other related

disciplines.

1. Use, operation, and maintenance of installed and portable continuous air monitors

2. Use operation, and maintenance of installed air filtration units for breathing air (e.g.,

for airline respirators, emergency ventilation systems).

3. Use, operation, and maintenance of temporary air filtration units and vacuums

4. Respiratory protection and other related disciplines.

E. Please provide specific procedures related to the following areas noted below.

Additional Specific Procedures may be requested by number after the inspector reviews

the procedure indexes.

1. Respiratory protection program

2. Use and maintenance of self-contained breathing apparatuses

3. Air quality testing for SCBAs or other compressed or supplied air systems

4. Use and testing of installed plant air cleaning systems used for breathing air, such as

control room emergency ventilation, technical support center, operations support

center, and emergency operations facility (When containment purge is not used as

an effluent system, then it can be considered as a breathing air system used prior to

outages during RCS breach and flood up.)

F. Please provide a list of NRC Regulatory Guides and NUREGs that you are currently

committed to relative to this program. Please include the revision and/or date for the

commitment and where this may be located in your current licensing basis documents.

G. Please provide a summary list of corrective action documents (including corporate and

sub-tiered systems) written since the date of last inspection, related to the Airborne

Monitoring program including:

1. In-plant continuous air monitors (installed or portable), not effluent monitors

2. Self-contained breathing apparatus

3. Air Cleaning systems (not effluent)

4. Respiratory protection program

NOTE: These lists should include a description of the condition that provides sufficient

detail that the inspectors can ascertain the regulatory impact, the significance level

assigned to the condition, the status of the action (e.g., open, working, closed, etc.) and

the search criteria used. Please provide in document formats which are sortable and

searchable so that inspectors can quickly and efficiently determine appropriate

sampling and perform word searches, as needed. (Excel spreadsheets are the preferred

format.) If codes are used, please provide a legend for each column where a code is

used.

H. List of SCBA qualified personnel - reactor operators and emergency response

personnel. For the control room individuals, please indicate their normally scheduled

shift and specific mask size, as well as note if they are permitted/fitted for eyewear.

I. Inspection records for self-contained breathing apparatuses (SCBAs) staged in the plant

for use since the date of last inspection.

J. SCBA training and qualification records for control room operators, shift supervisors,

STAs, and OSC personnel for the last year.

A selection of personnel may be asked to demonstrate proficiency in donning, doffing,

and performance of functionality check for respiratory devices

K. List of respirators (available for use) by type (APR, SCBA, PAPR, etc.), manufacturer,

model, quantity by size, and location. Be prepared to demonstrate that these respirators

are NIOSH certified.

Include in the list the specific quantities and sizes staged for emergency use.

L. Provide one-line drawings of the supplied air and air cleaning systems identified in E.3

and E.4 above.

M. List work activities requiring respiratory protection and the type of respirator used

(include PAPRs)

N. Please have available, on-site, the records demonstrating the compressed air for SCBAs

or supplied air for a breathing air system is at least Grade D.

ML19031C939

SUNSI Review ADAMS: Non-Publicly Available Non-Sensitive Keyword:

By: JKozal Yes No Publicly Available Sensitive NRC-002

OFFICE ASRI:DRP/C ARI:DRP/C ASRI C:DRS/EB1 C:DRS/EB2 C:DRS/OB

NAME BParks TDeBey CSpeer VGaddy JDrake GWerner

SIGNATURE BDP TMD CAS vgg JD GEW

DATE 1/24/2019 1/25/2019 1/29/2019 1/17/19 1/16/2019 01/21/2019

OFFICE C:DRS/PSB2 TL:IPAT C:DNMS/FCDB BC:DRP/C

NAME HGepford RKellar JKatanic JKozal

SIGNATURE hjg RLK /RA/ JFK JWK

DATE 01/17/2019 01/16/2019 1/24/2019 1/29/2019