IR 05000454/2019001

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NRC Integrated Inspection Report 05000454/2019001 and 05000455/2019001
ML19121A595
Person / Time
Site: Byron  Constellation icon.png
Issue date: 05/01/2019
From: Hironori Peterson
NRC/RGN-III
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2019001
Download: ML19121A595 (12)


Text

SUBJECT:

BYRON STATION, UNITS 1 AND 2NRC INTEGRATED INSPECTION REPORT 05000454/2019001 AND 05000455/2019001

Dear Mr. Hanson:

On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Byron Station, Units 1 and 2. On April 3, 2019, the NRC inspectors discussed the results of this inspection with Mr. M. Kanavos and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspectors did not identify any finding or violation of more than minor significance.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos.: 05000454; 05000455 License Nos.: NPF-37; NPF-66

Enclosure:

IR 05000454/2019001; 05000455/2019001

Inspection Report

Docket Numbers: 05000454 and 05000455 License Numbers: NPF-37 and NPF-66 Report Numbers: 05000454/2019001 and 05000455/2019001 Enterprise Identifier: I-2019-001-0058 Licensee: Exelon Generation Co., LLC Facility: Byron Station, Units 1 and 2 Location: Byron, IL Inspection Dates: January 01, 2019 to March 31, 2019 Inspectors: D. Betancourt-Roldan, Senior Resident Inspector C. Hunt, Resident Inspector J. McGhee, Senior Resident Inspector C. Thompson, Illinois Emergency Management Agency Approved By: Hironori Peterson, Chief Branch 3 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a quarterly inspection at Byron Station, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations No findings or violations were identified.

Additional Tracking Items None.

PLANT STATUS

Unit 1 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities or small load changes requested by the transmission dispatcher, the unit remained at or near full power for the entire inspection period.

Unit 2 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities or small load changes requested by the transmission dispatcher, the unit remained at or near full power for the majority of the inspection period. At the conclusion of the inspection period, the unit was in coast down operations for a planned refueling outage.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection Impending Severe Weather Sample (IP Section 03.03)

The inspectors evaluated readiness for impending adverse weather conditions for extreme/extended cold temperatures for the period of January 20-30, 2019.

71111.04 - Equipment Alignment Partial Walkdown (IP Section 02.01)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) The Unit 1B Emergency Diesel Generator (EDG) and auxiliaries after surveillance and before expected snow, high wind and subzero temps on January 17, 2019
(2) The 1B EDG during a scheduled 1A EDG work window on March 4, 2019
(3) The 2A Essential Service Water (SX) train during the 2B SX pump maintenance work window on March 18, 2019

71111.05Q - Fire Protection Quarterly Inspection (IP Section 03.01)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire Zone (FZ) 3.3A (B,C,D)-2, U-2 Upper Cable Spreading Room on January 8, 2019
(2) FZ 18.5-2, Security Control Center on February 28, 2019
(3) FZ 5.6-1, Division 11, Miscellaneous Electrical Equipment and Battery Room, 451' elevation on March 5, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

The inspectors observed and evaluated activities in the station's main control room, which included response to degrading Main Condenser Vacuum on January 8, 2019.

Additionally, the inspectors observed a first time evolution on Unit 2 relating to a new system line up in the component cooling system with an emphasis on configuration control on February 11, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated a crew of licensed operators during comprehensive crew simulator training on March 5, 2019.

71111.12 - Maintenance Effectiveness Quality Control (IP Section 02.02)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

10 CFR Part 21 for AMTEC A voltage sensing boards on January 4, 2019 Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

Unit 1 and 2 Radiation Monitoring System

71111.13 - Maintenance Risk Assessments and Emergent Work Control Risk Assessment and Management Sample (IP Section 03.01)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) The 1A EDG maintenance work window and 2-year inspections as documented in multiple work orders (WOs) on March 4, 2019
(2) Activities involving the installation of station auxiliary transformer (SAT) 242-2 during the weeks ending in March 16 through March 23, 2019
(3) Troubleshooting and repairs of a leak on line 0SX03A-30 during the week ending on March 23, 2019

71111.15 - Operability Determinations and Functionality Assessments Operability Determinations and Functionality Assessments (IP Section 02.01)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) The impact of a leak on the 2A auxiliary feedwater pump identified during surveillance run as documented in IR 4179107 on January 2, 2019
(2) The slow stroke time of valve 1SD002B, 2B steam generator blowdown isolation valve, during a surveillance as documented in IR 4206230 on January 4, 2019
(3) The low differential pressure during a scheduled 2A containment spray pump surveillance as documented in IR 4210938 on January 14, 2019
(4) The Unit 1 source range and intermediate range nuclear Instrumentation loss of function as documented in IR 4665957 on January 28, 2019
(5) The impact of a through wall leak on valve 0SX007, Unit 0 component cooling water heat exchanger outlet valve, as documented in IR 4665957 on March 9, 2019

71111.18 - Plant Modifications Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

The inspectors evaluated the following temporary or permanent modifications:

Elimination of Rod Worth Testing (PR-19-006)

71111.19 - Post Maintenance Testing Post Maintenance Test Sample (IP Section 03.01)

The inspectors evaluated the following post maintenance tests:

(1) Unit 1 steam generator blowdown isolation valve, 1SD002B, stroke test and local position verification tests after rebuild as documented in work order (WO) 04833739 on January 4, 2019
(2) Functional and operational testing of 0A SX make-up pump following a work window as documented in WO 4872076 on February 11, 2019
(3) Functional and operational test on the 2B SX pump following truncated work on March 19, 1019

71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: In Service Testing (IST) (IP Section 03.01)

Unit 1 residual heat removal pump group A IST test as documented in 1BOSR 5.5.8.RH.5-1A on February 5, 2019 Reactor Coolant System (RCS) Leak Detection (IP Section 03.01) (1 Sample)

Unit 2 reactor coolant system unidentified leakage surveillance as documented in WO

124386 on February 22, 2019 Surveillance Testing (IP Section 03.01)

(1) Performance of the Anticipated Transient Without SCRAM Mitigation System (AMS)at power semiannual surveillance as documented on 1BOSR FW-SA1 on January 10, 2019
(2) Use of the Surveillance Frequency Program Change Program for change in diesel generator 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> endurance run and hot restart surveillance as documented on BY-18-003 on January 11, 2019
(3) Semi-annual operability surveillance of the 2B diesel generator as documented on 2BOSR 8.1.2-2 on February 20, 2019

71114.06 - Drill Evaluation Emergency Preparedness (EP) Drill (IP Section 02.01)

(1) The inspectors evaluated a full-scale Emergency Planning Drill conducted on March 7, 2019
(2) The inspectors evaluated a full-scale Emergency Planning Drill conducted on March 14,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) ===

(1) Unit 1 Unplanned Scrams per 7000 Critical Hours (January 1, 2018 -

December 31, 2018)

(2) Unit 2 Unplanned Scrams per 7000 Critical Hours (January 1, 2018 -

December 31, 2018)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1) Unit 1 Unplanned Power Changes per 7000 Critical Hours (January 1, 2018 -

December 31, 2018)

(2) Unit 2 Unplanned Power Changes per 7000 Critical Hours (January 1, 2018 -

December 31, 2018)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03)

(2 Samples)

(1) Unit 1 Unplanned Scrams with Complications (January 1, 2018 -

December 31, 2018)

(2) Unit 2 Unplanned Scrams with Complications (January 1, 2018 -

December 31, 2018)

71152 - Problem Identification and Resolution Annual Follow-Up of Selected Issues (IP Section 02.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Review of actions taken to address a condition that caused the open phase relay for SAT 242-2 to not be able to detect all postulated open phase conditions.

INSPECTION RESULTS

Observation 71152 The inspectors performed a review of plant issues, particularly those entered into the licensees corrective action program, associated with the upcoming replacement of the failed Unit 2 SAT 242-2 transformer. During their review, the inspectors noted that IR 4218559 documented that the open phase relay for the new transformer would not be able to detect an open phase condition for all postulated cases once the work window to replace the transformer was completed. In particular, the calculations showed that for the B phase the open phase logic would be unable to detect the grounded open phase. The condition was described to be the result of the new transformer having a Shell-Type design instead of the current Core-Form of the original transformer.

The inspectors reviewed the planned corrective actions and compensatory actions that the licensee planned to undertake to restore to open phase protection for the transformer. Upon installation of the new 242-2 transformer, the licensee established compensatory actions consistent to their response to NRC Bulletin 2012-01, Design Vulnerability in Electrical Power System. The inspectors reviewed the standing order, revised procedures, and talked with operations personnel to assess the actions. No concerns were identified.

At the end of this inspection period, the licensee was proposing a two phase approach to address the issue described above. The first involved updating the pertinent calculations, which would be followed by a physical modification to the transformer so that the ratio of negative to positive voltages can be used for open phase detection.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 3, 2019, the inspector presented the quarterly integrated inspection results to Mr. M. Kanavos and other members of the licensee staff.

DOCUMENTS REVIEWED

71111.01Adverse Weather Protection

- AR 04216408, Protection of the Plant During a Cold Weather Unit Trip, 02/01/2019

- AR 04217573, Security - Check Suspended due to Inclement Weather, 02/05/2019

- AR 04215528, 2B DG Lube Oil Temp Degrading, 01/30/2019

- AR 04215466, RSH Local Area Heater Tripping Breaker, 01/30/2019

- AR 04215365, Sensing Line Froze, 01/30/2019

71111.04Equipment Alignment

- BOP DG-M2A, Train A Diesel Generator System Valve Lineup, Revision 10

- BOP DG-E1A, Diesel Generator Train A Electrical Line up, Revision 3

- BOP DG-M1B, Train B Diesel Generator System Valve Lineup, Revision 14

71111.05AQFire Protection Annual/Quarterly

- Pre-Fire Plan #30, FZ 3.3A-2 Auxiliary Building 463-0 Upper Cable Spreading Room,

Revision 3

- Pre-Fire Plan #32, FZ 3.3B-2 Auxiliary Building 463-0 Upper Cable Spreading Room,

Revision 3

- Pre-Fire Plan #34, FZ 3.3C-2 Auxiliary Building 463-0 Upper Cable Spreading Room,

Revision 3

- Pre-Fire Plan #36, FZ 3.3D-2 Auxiliary Building 463-0 Upper Cable Spreading Room,

Revision 4

- Pre-Fire Plan #2431, FZ 18.5-2 Security Control Center, Revision 2

71111.11Licensed Operator Requalification Program and Licensed Operator Performance

- AR 04179107, Leak on 2A AF Pump During Surveillance Run When Pressurized, 10/01/2018

- AR 04209128, Unexpected Main Control Room Alarms due to Degraded Main Condenser

Vacuum, 01/08/2019

- 1BOA SEC-3, Loss of Condenser Vacuum Unit 1, Revision 107;

- AR 04209528, 4.0 Critique for Unit 1 Main Condenser Vacuum Degrading, 01/09/2019

71111.12Maintenance Effectiveness

- EN 53816, AMTEC Solid State Controls, Part 21 -Components Provided as Safety-related

Spare Parts Without Being Dedicated; 01/08/2019

- AR 04162360, Part 21 53529 AMTEC A Voltage Sense Board; 08/07/2018

- ER-AA-310, Implementation of the Maintenance Rule, Revision 11

- ER-AA-310-1001, Maintenance Rule - Scoping, Revision 4

- ER-AA-310-1002, Maintenance Rule Functions - Safety Significant Classification, Revision 3

- ER-AA-310-1003, Maintenance Rule - Performance Criteria Selection, Revision 5

- ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 14

- AR 04221808; Unexpected Alarm 0PR05J Loss of Sample Flow, 02/20/2019

- AR 04221681; 2PR28J Vent Stack HI Gas Channel in High Alarm/Interlock, 02/19/2019

- AR 04215048; Trend on Check Sources Failure, 01/29/2019

- AR 04221410; IST Program Health Report, 02/19/2019

- AR 04218721; 2PR027J Loss of Sample Flow, 02/09/2019

- AR 04216838; OPS Focus - Radiological Monitor Issues, 02/03/2019

71111.13Maintenance Risk Assessments and Emergent Work Control

- 1BOL8.1, LCOAR AC Sources - Operating Tech Spec LCO #3.8.1; Revision 22

- OP-BY-108-117-1000, Byron Protected Equipment Worksheet, Revision 11

- BOP SX-21, Initiating And Terminating Alternate Cooling Flow to SX Pumps Oil Coolers and

Cubicle Coolers; Revision 4

- AR 04230553, Potential Inactive Leak on 2SX03B Line, 03/18/2019

- AR 04228530, 2A DG Tripped During the Cooldown Cycle, 03/11/2019

- AR 04231438, Unexpected Alarm, 03/21/2019

71111.15Operability Determinations and Functionality Assessments

- AR 04179107, Leak on 2A AF Pump During Surveillance Run When Pressurized on

October 01, 2018, dated 01/02/2019

- AR 04210938, 2A CS Pump DP Not Within Range for DG Frequency Uncertainties,

01/15/2019

- WO 4807795, 2CS01PA Comprehensive IST Requirements for Containment Spray,

10/11/2018

- EC 624019, Determine Interim IST Testing Admin Limits Considering Lower Frequency Admin

Limits, Revision 1

- Calculation BYR06-029, SI/RHR/CS/CV System Hydraulic Analysis in Support of GSI-191,

Revision 5b

- AR 04206230, 1SD002B Stroke Slow During Surveillance, 12/27/2018

- AR 04228044, SX Leak By 0SX007, 03/09/2019

- AR 04228044, Pinhole Leak on a Weld on 0SX03A-30, 03/20/2019

71111.18Plant Modifications

- NF-BY-510, Low Power Physics Test Program, Revision 15

- PR-19-006, Rod Worth Testing Optimization, Revision 0

- NF-AP-100-7080, Rod Worth Testing - Scope Selection Process, Revision 0

71111.19Post Maintenance Testing

- AR 04209032, Gaps in Documentation of STT Of 1SD002B During B1R22, 01/08/2019

- WO 04833739, Rebuild Actuator, Replace Elastomers Set Stroke, 09/23/2018

- WO 04801879, STT for 1SD002A-H and SD005A-D, 09/19/2018

- M-42, Diagram of Essential Service Water, Sheet 6

- WO 04872076, 2BOST 5.5.8.SX.5-2C 2B SX Comprehensive, 03/18/2019

- AR 04231041, Failed PMT 2B SX Pump Minor Oil Leak, 03/19/2019

- AR 04230570, 2SX01AB HX Failed GL 89-13 Acceptance Criteria, 03/18/2019

71111.20Refueling and Other Outage Activities

- 2 Month Readiness Report, 01/29/2019

71111.22Surveillance Testing

- BY-18-003, Surveillance Test Interval Evaluation: Revise the Diesel Generator 24 Hour

Endurance Run and Hot Restart Surveillance from Once per 18 Months to Once per 36

Months, Revision 000

- BB-STI-029, Risk Evaluation of Surveillance Interval Extension for EDG Endurance Test,

Revision 0

- AR 04217336, 1A RH ASME Surveillance Issues, 02/05/2019

- WO 00124386-01, 2BOSR 4.13.1-1 Unit 2 Reactor Coolant System Water Inventory Balance

Surveillance Computer Calculation, 03/03/2019

71114.06Drill Evaluation

- Drill Scenario Information, 03/07/2019

- Drill Scenario Information, 03/14/2019

71151Performance Indicator Verification

- Unit 1 and Unit 2 Unplanned Scrams per 7000 Critical Hours (01/01/2018-12/31/2018)

- Unit 1 and Unit 2 Unplanned Power Changes per 7000 Critical Hours (01/01/2018-12/31/2018)

- Unit 1 and Unit 2 Unplanned Scrams with Complications per 7000 Critical Hours (01/01/2018-

2/31/2018)

71152Problem Identification and Resolution

- AR 04226197, Corrective Action Out of Process with PI-AA-125, 03/04/2019

- AR 04217533, Calculation Error in DGDO9301, 02/05/2019

- AR 04217336; 1A RH ASME Surveillance Issues, 02/05/2019

- AR 04216459, Cold Weather Lessons Learned, 02/01/2019

- AR 04220197, Oil Temperature Elevated, 02/14/2019

- 2BOl AP1, Unit 2 SAT Low Load or Trouble Condition Loss of Phase Monitoring, Revision 3

10