IR 05000397/2018001
ML18116A407 | |
Person / Time | |
---|---|
Site: | Columbia |
Issue date: | 04/25/2018 |
From: | Mark Haire NRC/RGN-IV/DRP |
To: | Sawatzke B Energy Northwest |
Mark Haire | |
References | |
IR 2018001 | |
Download: ML18116A407 (21) | |
Text
ril 25, 2018
SUBJECT:
COLUMBIA GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000397/2018001
Dear Mr. Sawatzke:
On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Columbia Generating Station. On April 19, 2018, the NRC inspectors discussed the results of this inspection with Mr. G. Hettel, Vice President for Operations, and other members of your staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented one finding of very low safety significance (Green) in this report.
This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violation or significance of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Columbia Generating Station.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the Columbia Generating Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Mark Haire, Chief Project Branch A Division of Reactor Projects Docket No. 50-397 License No. NPF-21 Enclosure:
Inspection Report 05000397/2018001 w/ Attachment: Documents Reviewed
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Columbia Generating Station in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.
List of Findings and Violations Failure to Follow Procedure Leads to Loss of Secondary Containment Cornerstone Significance Cross-cutting Report Aspect Section Barrier Integrity Green H.5 - Work 71153 -
NCV 05000397/2018001-01 Management Follow-up of Closed Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, Green, non-cited violation of Technical Specification 5.4.1.a for the licensees failure to perform maintenance in accordance with documented instructions appropriate to the circumstances. Specifically, on September 12, 2017, the failure to verify power sources per Work Order 02072924 caused an electrical transient that caused the reactor building exhaust valve and supply valve to lose power and close, resulting in a loss of secondary containment.
Additional Tracking Items Type Issue Number Title Report Status Section LER 05000397/2017003-00 Momentary Loss of 71153 Closed Secondary Containment Due to Weather LER 05000397/2017005-00 Valve Closure Results in 71153 Closed Momentary Increase in Secondary Containment Pressure LER 05000397/2017006-00 Condition Prohibited by 71153 Closed Technical Specifications Due to Incomplete Action Statement
PLANT STATUS
The plant began the inspection period at 100 percent rated thermal power. On January 6, 2018, the unit was down-powered to 72 percent for turbine valve testing and a control rod sequence exchange. The unit was returned to 100 percent rated thermal power on January 6, 2018. On March 31, 2018, the unit was down-powered to 70 percent for turbine valve testing and a control rod sequence exchange. The unit was returned to 100 percent rated thermal power on March 31,
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection period unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.
Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection Impending Severe Weather
The inspectors evaluated readiness for impending adverse weather conditions associated with high winds on February 17, 2018.
External Flooding (1 Sample)
The inspectors evaluated readiness to cope with external flooding on January 12, 2018.
71111.04 - Equipment Alignment Partial Walkdown
The inspectors evaluated system configurations during partial systems/trains walkdowns:
- (1) diesel generator 1 starting air on February 6, 2018
- (2) diesel generator 2 starting air on February 22, 2018
- (3) diesel generator 3 starting air on February 26, 2018
- (4) diesel generator 3 governor on March 12, 2018
- (5) diesel generator 2 governor on March 29, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated standby service water loop A system configurations during a complete walkdown on January 12, 2018
71111.05AQ - Fire Protection Annual/Quarterly Quarterly Inspection
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Fire Area R-6/2: RCIC Pump Room on January 8, 2018
- (2) Fire Area R-7/1: RHR-C Pump Room on January 9, 2018
- (3) Fire Area R-8/1: LPCS Pump Room on January 10, 2018
- (4) Fire Area RC-13/2: Chiller, Communications, I & C Area on January 26, 2018
- (5) Fire Area RC-11/1: HVAC Equipment Room A Division 1 on January 26, 2018
- (6) Fire Area RC-12/2: HVAC Equipment Room B Division 2 on January 26, 2018
71111.06 - Flood Protection Measures Internal Flooding
The inspectors evaluated internal flooding mitigation protections:
- (1) Reactor Building 422 level on February 14, 2018
Cables (1 Sample)
The inspectors evaluated cable submergence protection:
- (1) Manhole E-MH-E8 on February 22, 2018
- (2) Manhole E-MH-01B, 10, 11, 13, 15 on February 28, 2018
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification
The inspectors observed and evaluated a crew during a simulator evaluated scenario for licensed operator requalification training on January 22, 2018.
Operator Performance (1 Sample)
The inspectors observed and evaluated operator performance during the following activities:
- (1) maintenance on main generator seal oil pressure regulator on January 9, 2018
- (2) diesel generator 3 testing on January 24, 2018
71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) fire pump 110 starting issue on January 10, 2018
- (2) standby service water loop B planned maintenance, week of January 15, 2018
- (3) diesel generator 3 annual preventive maintenance, week of January 22, 2018
- (4) SM4 relay testing on February 27, 2018
- (5) diesel generator 2 12-year maintenance, March 19-30, 2018
Quality Control (1 Sample)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:
- (1) main control room emergency chiller B maintenance, week of February 19, 2018
71111.13 - Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) yellow risk due to standby service water system A maintenance, week of January 1, 2018
- (2) yellow risk due to maintenance on main generator seal oil pressure regulator on January 9, 2018
- (3) yellow risk for diesel generator 3 maintenance on January 22, 2018
- (4) yellow risk for circuit breaker S/2 maintenance on January 24, 2018
- (5) yellow risk for maintenance on backup transformer, February 16-17, 2018
- (6) yellow risk for standby gas treatment B and SM4 relay testing, February 26-28, 2018
- (7) yellow risk for diesel generator 3 24-hour load test and loss of coolant accident test, March 1-3, 2018
- (8) yellow risk for diesel generator 2 12-year maintenance, March 19-30, 2018
71111.15 - Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) diesel generator 3 diesel oil valve DO-V-14 on January 22, 2018
- (2) diesel generator 3 exhaust thermocouple on January 24, 2018
- (3) diesel generator 3 temperature test switch on January 25, 2018
- (4) main control room emergency chiller B unexpected start during tagout on February 18, 2018
- (5) high pressure core spray motor oil on March 8, 2018
- (6) diesel generator 2 engine governor on March 28, 2018
- (7) diesel generator 2 fuel oil pump on March 29, 2018
71111.18 - Plant Modifications
The inspectors evaluated the following temporary or permanent modifications:
- (1) Engineering Change (EC) 14954, CCH Bypass Line, Emergency Chilled Water, on January 24, 2018
- (2) Temporary Modification (TM) 16326, adjust setpoint of containment instrument air pressure control valve on February 2, 2018
- (4) TM 16170 main control room chiller B bearing high temp switch on February 16, 2018
- (5) EC 16066 vital island fire protection installation on March 31, 2018
71111.19 - Post Maintenance Testing
The inspectors evaluated the following post maintenance tests:
- (1) fire pump 110 maintenance on January 10, 2018
- (2) standby service water loop B maintenance on January 16, 2018
- (3) diesel generator 3 maintenance on January 25, 2018
- (4) TR-B backup transformer maintenance on February 17, 2018
- (5) tower make-up pump C maintenance on February 21, 2018
- (6) fuel pool cooling pump B maintenance on February 23, 2018
- (7) RHR-V-68B standby service water supply isolation to residual heat removal heat exchanger 1B maintenance on February 26, 2018
- (8) RHR-V-116 cross tie connection from standby service water maintenance on March 1, 2018
- (9) diesel generator 2 12-year outage on March 29, 2018
71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: Routine
- (1) service water spray pond quarterly surveillance test per OSP-SW-Q101, on January 4, 2018
- (2) main steam isolation valve SCRAM closure test per OSP-RPS-S402, on January 7, 2018
- (3) diesel generator 3 load testing per TSP-DG3-B502, on March 2, 2018
- (4) diesel generator 3 loss of coolant accident test per TSP-DG3/LOCA-B501, on March 3, 2018
- (5) main turbine bypass valve testing per OSP-MS-Q702, on March 31, 2018
In-service (1 Sample)
- (1) residual heat removal loop A operability test per OSP-RHR/IST-Q702, on February 7, 2018
71114.01 - Exercise Evaluation
The inspectors evaluated the licensees biennial emergency plan exercise and subsequent identification of performance weaknesses. The exercise scenario simulated the following on March 27, 2018:
- (1) a loss of feedwater heating causing a power excursion which required the reactor be shut down
- (2) a problem with the reactor protection system which failed to shut down the reactor
- (3) a failure of some control rods to insert into the reactor
- (4) an unisolable pipe break on the reactor water clean-up system outside of containment
- (5) an unfiltered and monitored radioactive release from the radioactive waste building through the plant vent which increased in activity over time
- (6) emergency depressurization of the reactor
71114.04 - Emergency Action Level and Emergency Plan Changes
The inspectors evaluated submitted Emergency Action Level changes in-office on January 30, 2018. This evaluation does not constitute NRC approval.
71114.06 - Drill Evaluation Emergency Planning Drill
The inspectors evaluated:
- (1) a general emergency scenario drill on February 27, 2018
71114.08 - Exercise Evaluation - Scenario Review
The inspectors conducted an in-office review of the proposed biennial emergency plan exercise scenario between January 16 and February 22, 2018. The inspectors also discussed the proposed scenario with staff at FEMA Region X.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
- (1) IE01: Unplanned Scrams per 7000 Critical Hours (01/01/2017 - 12/31/2017)
- (2) IE03: Unplanned Power Changes per 7000 Critical Hours (01/01/2017 - 12/31/2017)
- (3) IE04: Unplanned Scrams with Complications (01/01/2017 - 12/31/2017)
- (4) EP01: Drill/Exercise Performance (01/01/2017 - 12/31/2017)
- (5) EP02: Emergency Response Organization Drill Participation (01/01/2017 - 12/31/2017)
- (6) EP03: Alert and Notification System Reliability (01/01/2017 - 12/31/2017)
71152 - Problem Identification and Resolution Annual Follow-up of Selected Issues
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) required test for Westinghouse 480v ac circuit breaker on February 20, 2018
- (2) licensees corrective action for abnormal procedure ABN-ASH on March 31, 2018
71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports
The inspectors evaluated the following Licensee Event Reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
- (1) LER 05000397/2017-003-00, Momentary Loss of Secondary Containment Due to Weather on June 26, 2017
- (2) LER 05000397/2017-005-00, Valve Closure Results in Momentary Increase in Secondary Containment Pressure on September 12, 2017
- (3) LER 05000397/2017-006-00, Condition Prohibited by Technical Specifications Due to Incomplete Action Statement on September 21,
INSPECTION RESULTS
Minor Performance Deficiency 71153 Minor Performance Deficiency: The inspectors reviewed LER 2017-006-00 and determined the failure to follow Procedure OSP-ELEC-W101, Offsite Station Power Alignment Check, Revision 30, was a performance deficiency.
Screening: The performance deficiency was minor because while it was associated with the configuration control attribute of the Mitigating Systems Cornerstone, it did not adversely affect the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, when operations personnel performed the offsite station power alignment check in its entirety, all breakers were correctly aligned, and power was available for each offsite circuit.
Failure to Follow Procedure Leads to Loss of Secondary Containment Cornerstone Significance Cross-cutting Aspect Report Section Barrier Integrity Green H.5 - Work 71153 - Follow-NCV 05000397/2018001-01 Management up of Events Closed and Notices of Enforcement Discretion During their inspection of LER 2017-005-00, the inspectors reviewed a self-revealed, Green, non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to perform maintenance in accordance with documented instructions appropriate to the circumstances.
Specifically, on September 12, 2017, the failure to verify power sources per Work Order 02072924 caused an electrical transient that caused the reactor building exhaust valve and supply valve to lose power and close, resulting in a loss of secondary containment.
Description:
On September 12, 2017, electricians performed planned maintenance per Work Order 02072924 to replace the reactor core isolation cooling (RCIC) system direct current (DC) motor control center (MCC) buckets. As part of the work, electricians conducted live-dead-live checks of wiring in the cubicle to check for DC voltage. The workers found DC voltage as expected and lifted the terminals, per instructions. Another live-dead-live test for DC power was conducted which showed no voltage. While lifting a control wire, a maintenance worker believed they saw faint evidence of arcing. Another live-dead-live test was conducted which showed no evidence of DC voltage. However, when electricians lifted the wire, it shorted out against the bucket chassis and caused a reactor building exhaust inboard isolation valve to lose power and close, resulting in a loss of secondary containment.
The wire shorted because alternating current (AC) voltage was present on the control wire and the DC voltage checks were not adequate to identify the presence of AC voltage.
Operations personnel responded to the incident and restored secondary containment to operable status within approximately 1 minute.
The inspectors noted Work Order 02072924 Precaution and Limitations Step 2.5 states that electrical energy may be present, follow the requirements of ISPM-7 & ISPM-20. Step 2.6 states, in part, to as needed, check all control wiring terminals in the cubicle for voltage prior to working in the cubicle.
ISPM-20, Electrical Arc Protection Work Practices and PPE Requirements, Revision 14, Step 3.1.2 states that electrical equipment and lines shall be considered energized until verified de-energized by a live-dead-live check. ISPM-7, Electrical Safety, Revision 17, Step 3.1.10 states that all circuits shall be tested utilizing a live-dead-live method to verify that it is de-energized prior to commencing work, unless the circuit is planned to be worked live.
In both procedures, two notes precede these steps. The first note states, NOTE: Live-Dead-Live Check - Ensure test equipment is rated for and set to the correct voltage source (AC/DC) range prior to use. Test the meter on a known live source, perform necessary checks, then test the meter on a known live source. The live source must be the same voltage type as the circuit to be worked. (AC/DC)
The second note states, NOTE: Pre and post voltage verification is required when performing determinations/re-terminations on a known live circuit. A Live Dead Live does not apply in this situation. When working on known live voltage sources per approved work documents, voltage verification is not required. (e.g. Battery surveillances)
Work Order 02072924 Step 4.6 states, in part, Disconnect all external wiring at the bucket, using the attached de-term/re-term data sheet, [Motor Control Center] as-found diagram and/or cable termination instruction (CTI) as appropriate.
A warning note immediately prior to this step states, Control circuits will be energized. Refer to drawing EWD-6E-007. Ensure all wire terminals are checked for voltage, prior to disconnecting. Note any discrepancies.
Maintenance personnel only performed a live-dead-live check for DC voltage because the workers erroneously believed only DC voltage was present in the cubicle. The inspectors noted that drawing EWD-6E-007, Reactor Core Isolation Cooling System Pump RCIC-P-2 (E51-C002) Revision 13, clearly shows AC voltage sources also located in the same cubicle.
The inspectors determined the maintenance personnel failed to conduct a proper live-dead-live check because the workers did not follow the warning note in Work Order 02072924 and refer to drawing EWD-6E-007.
Corrective Actions: The licensees corrective actions included immediately restoring secondary containment to operable status and conducting a work stand down with all electricians to review requirements of Procedures ISPM-20 and ISPM-7 and reinforce the expectation that drawings will be posted at the job site at all times.
Corrective Action Reference: Action Request 371264
Performance Assessment:
Performance Deficiency: The failure to perform maintenance in accordance with documented instructions appropriate to the circumstances was a performance deficiency.
Screening: The performance deficiency was more than minor, and therefore a finding, because it was associated with the configuration control attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding, reactor coolant system, and containment) protect the public from radionuclide releases caused by accidents or events.
Specifically, the failure to verify power sources per Work Order 02072924 caused an electrical transient that caused the reactor building exhaust valve and supply valve to lose power and close, resulting in a loss of secondary containment.
Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3, Barrier Integrity Screening Questions, dated June 19, 2012. The inspectors determined the finding was of very low safety significance (Green) because the finding only represented a degradation of the radiological barrier function provided for the control room, auxiliary building, spent fuel pool, or standby gas treatment system.
Cross-cutting Aspect: This finding had a cross-cutting aspect in the area of human performance, work management, in that the licensee failed to plan and execute the work activity adequately. Specifically, electricians performed an inadequate live-dead-live check for the presence of only DC voltage when 120V AC voltage was present as reflected in the drawing [H.5].
Enforcement:
Violation: Technical Specification 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.a of Appendix A of Regulatory Guide 1.33, Revision 2, requires, in part, that maintenance that can affect the performance of safety-related equipment should be performed in accordance with documented instructions appropriate to the circumstances. The licensee established Work Order 02072924 to meet the Regulatory Guide 1.33 requirement. The warning note preceding Step 4.6 of Work Order 02072924 requires the electricians Refer to drawing EWD-6E-007. Ensure all wire terminals are checked for voltage, prior to disconnecting.
Contrary to the above, on September 12, 2017, the licensee did not refer to drawing EWD-6E-007 and ensure all wire terminals are checked for voltage, prior to disconnecting.
Specifically, the licensee should have identified there was live AC voltage present in the cubicle per drawing EWD-6E-007 and properly checked for AC voltage prior to disconnecting the wires. As a result, on September 12, 2017, the failure to verify power sources per Work Order 02072924 caused an electrical transient that caused the reactor building exhaust valve and supply valve to lose power and close, resulting in a loss of secondary containment.
Disposition: This violation is being treated as a Non-Cited Violation consistent with Section 2.3.2.a of the NRC Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
Unless otherwise noted, the inspectors verified no proprietary information was retained or documented in this report.
- On February 20, 2018, the inspectors discussed the proposed exercise scenario with Mr. W. Webb, Branch Chief, Technological Hazards, FEMA Region X.
- On February 22, 2018, the inspectors discussed the results of the in-office review of the licensees preliminary exercise scenario with Mr. S. Clizbe, Manager, Emergency Preparedness, and other members of the licensee staff.
- On March 30, 2018, the inspectors presented the results of the on-site inspection of the licensees biennial emergency preparedness exercise and subsequent determination of performance weaknesses to Mr. R. Schuetz, Plant General Manager, Acting Vice President, Operations, and other members of the licensee staff. The inspectors also discussed exercise performance with Mr. W. Webb, Branch Chief, Technological Hazards, FEMA Region X.
- On April 19, 2018, the inspectors presented the integrated inspection results for the quarter to Mr. G. Hettel, Vice President for Operations, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision/
Procedure Date
71111.01 Procedures ABN- Flooding 019
FLOODING
1.3.76 Integrated Risk Management 049
ABN-WIND Tornado/High Winds 029
71111.04 Procedures 3.1.6J Instrument Rack Valve Line up 004
PPHSE, CWPH, & TMU
PPHSE
SOP-DG1-LU Emergency Diesel Generator 005
(Div 1) Valve and Power
Supply Lineup
SOP-DG2-LU Emergency Diesel Generator 005
(Div 2) ) Valve and Power
Supply Lineup
SOP-DG3-LU High Pressure Core Spray 007
Diesel Generator Valve and
Power Supply Lineup
SOP-DG-DSA Diesel Starting Air Operations 014
OSP-SW- Standby Service Water Loop A 037
M101 Valve Position Verification
71111.05 Procedures 1.3.10B Active Fire System Operability 015
and Impairment Control
1.3.10C Control of Transient 020
Combustibles
SOP-FP- Fire Protection System Drain 001
DRAIN
SOP-FP-FILL Fire Protection System Fill 003
SOP-FP-LU Fire Protection System Valve 009
and Breaker Lineup
MWP-1 Maintenance Welding 020
Operating Procedure
PFP-RW-525 Radwaste 525 005
10.2.222 Seismic Storage 001
Requirements for Transient
Equipment
Miscellaneous ISP 17-0124 Ignition Source Permit: 01/02/2018
CCH-CR-1A, Control Room
Emergency Chiller
Action 375440 376161 377528 378082
Requests 377895 377052
Attachment
Inspection Type Designation Description or Title Revision/
Procedure Date
71111.06 Procedures 1.3.57 Barrier Impairment 036
ME-02-02-02 Calculation for Reactor Building 002
Flooding Analysis
Work Orders 02100891 02116122
71111.11 Procedures OI-09 Operations Standards and 068
Expectation
13.1.1A Classify the Emergency - 033
Technical Bases
13.1.1 Classifying the Emergency 049
Miscellaneous Energy Northwest 4.0 Critique 01/22/2018
Summary for Crew F Evaluated
Scenario Cycle 18-1
71111.12 Procedure 1.5.11 Maintenance Rule Program 015
Work Orders 02046756 02061863 02080115 02100745
2110118 02113431 02123160
Action 373929 373936 375680 375996
Requests 376135 376155
71111.13 Procedures 1.3.76 Integrated Risk Management 049
26871 High Risk Work Plan 013
1.3.83 Protected Equipment Program 026
Miscellaneous High Risk Work Plan for MCR 12/20/2017
Chiller A Outlet Line
71111.15 Procedure 1.3.66 Operability and Functionality 034
Evaluation
Action 375995 375997 375998 376135
Requests 376155 377143 377670 378475
378407 378408
71111.18 Procedure EC 14954 CCH Bypass Line 000 - 004
Action 376012
Request
71111.19 Procedures OSP-ELEC- HPCS Diesel Generator 060
S703 Semi-Annual Operability Test
TSP-DG2- Standby Diesel Generator DG2 024
B502 Load Testing
OSP-ELEC- Diesel Generator 2 - Monthly 062
M702 Operability Test
OSP-ELEC- Offsite Station Power Alignment 031
W101 Check
15.1.4 FP-P-110 Operability Test 038
SOP-TMU- Tower Makeup Water System 013
START Start
SOP-TMU- Tower Makeup Water 011
OPS Operation
Inspection Type Designation Description or Title Revision/
Procedure Date
71111.19 Procedures OSP- Fuel Pool Cooling System 037
FPC/IST- Operability Surveillance
Q701
OSP- Standby service Water Loop B 032
SW/IST- Operability
Q702
8.3.447 Testing RHR-V-89, RHR-V-115, 001
and RHR-V-116
OSP-SW- Standby Service Water Loop B 038
M102 Valve Position Verification
Work Orders 02096335 02120536 02123160 02090131
Action 373929 373936 375680
Requests
71111.22 Procedures SYS-2-27 Sonar Inspection - Service 000
Water Spray Pond Sediment
Measurements
Calculations ME-02-83-21 Calculation for Spray Pond 002
Water Level Change
ME-02-92-41 Calculation for Ultimate Heat 007
Sink Analysis
Work Orders 02090434 02092445 02097247
71114.01 Procedures EPIP 13.1.1 Classifying the Emergency
and EPIP Classifying the Emergency, 033
Documents 13.1.1A Technical Bases,
January 17, 2018
EPIP 13.2.1 Emergency Exposure 022
Levels/Protective Action
Guides, December 21, 2017
EPIP 13.2.2 Determining Protective Action 020
Recommendations,
December 21, 2017
EPIP 13.4.1 Emergency Notifications, 043
August 29, 2017
EPIP 13.5.1 Local, Protected Area or Site 029
Evacuation, March 8, 2017
EPIP 13.8.1 Emergency Dose Projection 038
System Operations
EPIP 13.10.1 Control Room Operations and 035
Shift Manager Duties, February
14, 2017
EPIP 13.10.2 TSC Manager Duties, February 035
14, 2017
EPIP 13.10.9 Operations Support Center 049
Manager and Staff Duties,
January 24, 2017
EPIP 13.11.1 EOF Manager Duties, 044
October 4, 2017
Inspection Type Designation Description or Title Revision/
Procedure Date
71114.01 Procedures EPIP EP Equipment 013
and 13.14.11
Documents EPIP 13.14.8 Drill and Exercise Program, 018
June 29, 2016
EPI-13 Emergency Notification System, 008
August 29, 2017
EPI-17 After Action Report, 008
Improvement Plan, Formatting,
Distribution, and Retention,
December 9, 2013
EPI-21 Drill and Exercise Development 018
and Implementation, June 22,
2017
5.2.1 Primary Containment Control 027
5.8.1 Post-LOCA Hydrogen/Oxygen 002
Monitoring
2.5.33 Reactor Coolant Sampling 004.001
2.17.1 EOP Reactor Water Sampling 12/21/2017
DWG M528- Flow Diagram Control Rod 009
Drive System
RWP 2018 Emergency Drill 12/21/2017
30004172 Response Activities
Columbia Generating Station 02/11/2016
ERO Team B Drill Report,
January 12, 2016, After Action
Report/Improvement Plan
Columbia Generating Station 04/23/2016
ERO Team B Dress
Rehearsal Drill Report,
February 23, 2016, After Action
Report/Improvement Plan
Columbia Generating Station 04/29/2016
ERO Team B Exercise Drill
Report, March 29, 2016, After
Action Report/Improvement
Plan
Inspection Type Designation Description or Title Revision/
Procedure Date
71114.01 Documents Columbia Generating Station 04/29/2016
ERO Team B Exercise Drill
Report, March 29, 2016, After
Action Report/Improvement
Plan
Columbia Generating Station 06/03/2016
ERO Team D Drill, Drill
Report, May 3, 2016, After
Action Report/Improvement
Plan
Columbia Generating Station 09/22/2016
ERO Team A Drill, Drill
Report, August 30, 2016, After
Action Report/Improvement
Plan
Columbia Generating Station 11/22/2016
ERO Team C Drill, Drill
Report, October 25, 2016, After
Action Report/Improvement
Plan
Columbia Generating Station 02/07/2017
ERO Team B Drill, Drill
Report, January 10, 2017, After
Action Report/Improvement
Plan
Columbia Generating Station 04/24/2017
ERO Team D Drill, Drill
Report, March 14, 2017, After
Action Report/Improvement
Plan
Columbia Generating Station 08/15/2017
ERO Team A Drill, Drill
Report, July 18, 2017, After
Action Report/Improvement
Plan
Columbia Generating Station 11/31/2017
ERO Team C Drill, Drill
Report, October 31, 2017, After
Action Report/Improvement
Plan
Fire Brigade/First Responder 11/03/2016
Drill 2016,
Contaminated/Injured Man
Fire Brigade/First Responder 11/28/2017
Drill 2017,
Contaminated/Injured Man
Inspection Type Designation Description or Title Revision/
Procedure Date
71114.01 Documents Apparent Cause Evaluation, 04/11/2016
Violation of 10 CFR 50.54(q)(2)
for Failure to Conduct Medical
Emergency Drill in 2015
Action 347032 347050 347265 347490
Requests 348108 350241 353342 354107
356181 356227 356618 356826
357471 360335 360547 361134
361195 363014 366567 366884
366958 368177 368192 369531
369776 371856 373325 373732
374110 374115 374117 372561
375641 377563 378325 378339
378341 378394 378441 378471
378644
71114.04 Procedures Columbia Generating Station 065
and Emergency Plan
Documents EPIP Classifying the Emergency, 033
13.1.1A Technical Bases
EPI-16 50.54(Q) Change Evaluation, 015
July 19, 2017
71151 Procedures EPI-18 Emergency Preparedness 025
Performance Indicators,
May 31, 2017
Action 358298 360339 361467 366785
Requests 368711 369130 369725 372372
373237 373325
71152 Action 346054 376191 377044
Requests
71153 Action 371646 371777 376985
Requests
6