IR 05000387/2017004

From kanterella
Jump to navigation Jump to search
Revised Integrated Inspection Report 05000387/2017004 and 05000388/2017004
ML18071A194
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 03/12/2018
From: James Krafty
Reactor Projects Region 1 Branch 4
To: Rausch T
Susquehanna
Krafty J
References
IR 2017004
Download: ML18071A194 (34)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BOULEVARD, SUITE 100 KING OF PRUSSIA, PA 19406-2713 March 12, 2018 Mr. Timothy President and Chief Nuclear Officer Susquehanna Nuclear, LLC 769 Salem Blvd., NUCSB3 Berwick, PA 18603 SUBJECT: SUSQUEHANNA STEAM ELECTRIC STATION - REVISED INTEGRATED INSPECTION REPORT 05000387/2017004 AND 05000388/2017004

Dear Mr. Rausch:

The enclosed, revised report replaces Integrated Inspection Report 05000387/2017004 and 05000388/2017004 issued on February 1, 2018, ADAMS Accession Number ML18033A012.

The report is being reissued to correct documentation errors in the 2RS1, Radiological Hazard Assessment and Exposure Controls, section of the Report. The revised report documents the completion of the Risk-Significant High Radiation Area and Very High Radiation Area Controls sample and removes the Radiation Worker Performance and Radiation Protection Proficiency sample.

This letter, its enclosure, and your response, (if any), will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRCs Public Document Room in accordance with 10 Code of Federal Regulations (CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

James A. Krafty, Acting Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos. 50-387 and 50-388 License Nos. NPF-14 and NPF-22

Enclosure:

Revised Inspection Report 05000387/2017004 and 05000388/2017004 w/Attachment:

Supplementary Information

REGION I==

Docket Nos. 50-387 and 50-388 License Nos. NPF-14 and NPF-22 Report No. 05000387/2017004 and 05000388/2017004 Licensee: Susquehanna Nuclear, LLC (Susquehanna)

Facility: Susquehanna Steam Electric Station, Units 1 and 2 Location: Berwick, Pennsylvania Dates: October 1, 2017 through December 31, 2017 Inspectors: L. Micewski, Senior Resident Inspector T. Daun, Resident Inspector S. Barber, Senior Project Engineer J. Ambrosini, Senior Emergency Preparedness Inspector A. Turilin, Project Engineer M. Fannon, Resident Inspector J. Furia, Senior Health Physicist E. DiPaolo, Senior Reactor Inspector T. Fish, Operations Engineer T. Hedigan, Operations Engineer Approved By: James A. Krafty, Acting Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure

SUMMARY

IR 05000387/2017004 and 05000388/2017004; October 1, 2017 through December 31, 2017;

Susquehanna Steam Electric Station Units 1 and 2; Integrated Inspection Report.

This report covered a three-month period of inspection by resident inspectors and announced baseline inspections performed by regional inspectors. The Nuclear Regulatory Commissions (NRC) program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.

No findings were identified.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent power. On October 26, 2017, operators reduced power to approximately 64 percent for a rod sequence exchange. Operators returned the unit to 100 percent on October 29, 2017. On November 26, 2017, operators reduced power to approximately 77 percent to perform a rod pattern adjustment and returned the unit to 100 percent the next day. On December 17, 2017, operators reduced power to approximately 77 percent to perform a rod pattern adjustment and returned the unit to 100 percent the next day. On December 24, 2017, operators reduced power to approximately 80 percent to perform a rod pattern adjustment and returned the unit to 100 percent power the same day. On December 26, 2017, operators reduced power to approximately 65 percent to remove a reactor feed pump from service to repair a hydraulic fluid leak on the pressure control unit. Operators returned the unit to 100 percent power the same day. The unit remained at or near 100 percent power for the remainder of the inspection period.

Unit 2 began the inspection period at 100 percent power. On October 27, 2017, operators reduced power to approximately 60 percent by inserting a runback in response to rapidly degrading main condenser vacuum caused by a spurious trip of the hydrogen recombiner.

Following restoration of a hydrogen recombiner, main condenser vacuum was restored and operators returned the unit to 100 percent on the same day. On December 8, 2017, operators reduced power to approximately 65 percent to perform a leak repair on the moisture separator.

Operators returned the unit to 100 percent the next day. On December 15, 2017, operators reduced power to approximately 69 percent to perform a rod pattern adjustment. Operators returned the unit to 100 percent power the next day, and remained at or near 100 percent power for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors reviewed Susquehannas readiness for the onset of seasonal low temperatures. The review focused on the engineered safeguard service water pump house and the emergency service water (ESW) system. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), technical specifications (TS), control room logs, and the corrective action program (CAP) to determine what temperatures or other seasonal weather could challenge these systems, and to ensure Susquehanna personnel had adequately prepared for these challenges. The inspectors reviewed station procedures, including Susquehannas seasonal weather preparation procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during cold weather conditions. Documents reviewed for each section of this inspection report are listed in the Attachment.

b. Findings

No findings were identified.

.2 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

The inspectors reviewed Susquehannas preparations for a high wind and snow advisory on December 12, 2017. The inspectors reviewed the implementation of adverse weather preparation procedures before the onset of and during this adverse weather condition. The inspectors walked down the emergency diesel generators and ESW to ensure system availability. The inspectors verified that operator actions defined in Susquehannas adverse weather procedure maintained the readiness of essential systems. The inspectors discussed readiness and staff availability for adverse weather response with operations and work control personnel.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

  • Unit 1, division 1 residual heat removal (RHR) during division 2 SOW on October 30, 2017 The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, TSs, work orders, condition reports (CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted the systems performance of its intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether Susquehanna staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Resident Inspector Quarterly Walkdowns

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that Susquehanna controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

  • Unit 2, core spray A pump room (fire zone 2-1B) on November 2, 2017
  • Unit 1, remote shutdown panel room (fire zones 1-2B, 1-2D) on November 9, 2017
  • Unit Common, diesel generator bay B (fire zone 0-41B) on November 22, 2017
  • Unit 2, equipment and battery rooms east side (fire zones 0-28A-I, 0-28G, 0-28E, 0-28C) on December 11, 2017
  • Unit 1, lower relay room (fire zone 0-24D) on December 11, 2017

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

a. Inspection Scope

The inspectors observed licensed operator simulator training on October 23, 2017, which included a feedwater heater leak resulting in a manual reactor scram, a loss of coolant accident, and the failure of select components to automatically start as required.

The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the technical specification action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

a. Inspection Scope

The inspectors observed and reviewed reactivity manipulations associated with a rod pattern adjustment conducted on Unit 1 November 26, 2017. The inspectors observed the reactivity control briefing to verify that it met the criteria specified in Susquehannas Operations Section Expectations Handbook. Additionally, the inspectors observed licensed operator performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.

b. Findings

No findings were identified.

.3 Licensed Operator Requalification

a. Inspection Scope

The following inspection activities were performed using NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision 11, and Inspection Procedure Attachment 71111.11, Licensed Operator Requalification Program.

Examination Results The operating tests for the week of November 27, 2017, were reviewed for quality and performance.

On December 22, 2017, the results of the annual operating tests were reviewed to determine if pass/fail rates were consistent with the guidance of NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision 11, and NRC IMC 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process. The review verified that the failure rate (individual or crew) did not exceed 20 percent.

  • 1 of 70 operators failed at least one section of the Annual Exam. The overall individual failure rate was 1.4 percent.
  • 0 of 13 crews failed the simulator test. The crew failure rate was 0 percent.

Written Examination Quality The inspectors reviewed three written examinations previously administered during the October/November 2016 examination cycle for qualitative and quantitative attributes as specified in Appendix B of Attachment 71111.11, Licensed Operator Requalification.

Operating Test Quality Ten job performance measures (JPMs) and five scenarios were reviewed for qualitative and quantitative attributes as specified in Appendix C of 71111.11, Licensed Operator Requalification Program.

Licensee Administration of Operating Tests Observations were made of the dynamic simulator exams and JPMs administered during the week of November 27, 2017. These observations included facility evaluations of crew and individual performance during the dynamic simulator exams and individual performance of JPMs.

Examination Security The inspectors assessed whether facility staff properly safeguarded exam material.

JPMs, scenarios, and written examinations were checked for excessive overlap of test items.

Remedial Training and Re-Examinations The remediation plans and retake exams for operators who failed either the 2016 operating test or 2016 biennial written exam were reviewed to assess the effectiveness of the remedial training. Remediation for the individuals was processed in accordance with site procedures.

Conformance with Operator License Conditions Medical records for three senior reactor operator (SRO) licenses and three reactor operator (RO) licenses were reviewed to assess conformance with license conditions.

All records reviewed were satisfactory.

Proficiency watch standing records from January 2016 through November 2017 were reviewed. All active licensed operators met the watch standing requirements to maintain an active license.

No operators were reactivated from inactive status since the last inspection. Therefore, this area was not inspected.

Records for the participation of licensed operators in the requalification program from January 2016 through November 2017 were reviewed. Records for the performance of licensed operators on annual requalification operating tests and biennial requalification written exams were reviewed.

Simulator Performance Simulator performance and fidelity were reviewed for conformance to the reference plant control room. A sample of simulator deficiency reports was also reviewed to ensure facility staff addressed identified modeling problems. Simulator test documentation was also reviewed.

Problem Identification and Resolution A review was conducted of recent operating history documentation found in inspection reports, the licensees corrective action program, and the most recent NRC plant issues matrix. The inspectors also reviewed specific events from the licensees corrective action program which indicated possible training deficiencies, to verify that they had been appropriately addressed. The senior resident inspector was also consulted for insights regarding licensed operators performance. These reviews did not detect any operational events that were indicative of possible training deficiencies.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system, and component performance and reliability.

The inspectors reviewed system health reports, CAP documents, maintenance work orders, and maintenance rule basis documents to ensure that Susquehanna was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the structure, system, or component was properly scoped into the maintenance rule in accordance with 10 Code of Federal Regulations (CFR) 50.65 and verified that the (a)(2)performance criteria established by Susquehanna staff was reasonable. As applicable, for structures, systems, and components classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these structures, systems, and components to (a)(2). Additionally, the inspectors ensured that Susquehanna staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.

  • Unit Common, sticking contacts on 480 volts-alternating current (VAC) motor control center breakers on November 7, 2017
  • Unit 1 and 2, electro-hydraulic control system degradations System 193/293 on November 14, 2017
  • Unit Common, commercial-grade dedication of capacitors on December 22, 2017 (quality control)

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that Susquehanna performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that Susquehanna personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When Susquehanna performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the stations probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

  • Unit 1, protected equipment and risk management during the RCIC SOW on October 25, 2017
  • Unit 1, elevated risk during RHR division 2 SOW on October 30, 2017
  • Unit 1, protected equipment during HPCI SOW on November 28, 2017 and November 29, 2017
  • Unit 1, protected equipment during division 2 ESW piping replacement on December 13, 2017

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-conforming conditions based on the risk significance of the associated components and systems:

  • Unit 1, RCIC with a 53VDC short on October 25, 2017
  • Unit Common, ESW/residual heat removal service water (RHRSW) piping corrosion found during in-service inspection on December 15, 2017
  • Unit Common, containment boundary valve limit switches not environmentally qualified for safety function on December 20, 2017
  • Unit Common, fuel oil leak on diesel fuel oil pump on December 22, 2017
  • Unit 1, standby liquid control accumulator tank pressure low on December 26, 2017 The inspectors evaluated the technical adequacy of the operability determinations to assess whether technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to Susquehannas evaluations to determine whether the components or systems were operable. The inspectors confirmed, where appropriate, compliance with bounding limitations associated with the evaluations.

b. Findings

No findings were identified.

1R18 Plant Modifications

.1 Permanent Modifications

a. Inspection Scope

The inspectors evaluated a modification to the containment hydrogen and oxygen analyzers, Install Delphi Control System 11901 Temperature Control Board and

===11901-MK Modification Kit. The inspectors verified that the design bases, licensing bases, and performance capability of the affected systems were not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design change, including design specifications, system drawings, installation and testing procedures, and the consequence risk factors screening.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with the information in the applicable licensing basis and/or design basis documents, and that the test results were properly reviewed and accepted and problems were appropriately documented. The inspectors also walked down the affected job site, observed the pre-job brief and post-job critique where possible, confirmed work site cleanliness was maintained, and witnessed the test or reviewed test data to verify quality control hold point were performed and checked, and that results adequately demonstrated restoration of the affected safety functions.

  • Unit 1, RCIC following SOW on October 26, 2017
  • Unit 1, RHR division 2 following SOW on October 31, 2017
  • Unit 1, HPCI following SOW on December 1, 2017
  • Unit 1, RHRSW following SOW on December 20, 2017

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems, and components to assess whether test results satisfied TSs, the UFSAR, and Susquehanna procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied.

Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:

  • Unit 1, RHR division 1 quarterly flow surveillance on November 9, 2017
  • Unit 2, drywell leakage on November 28, 2017 and November 29, 2017 (RCS leak detection)
  • Unit 1, RHRSW pump A automatic transfer logic test on December 18, 2017
  • Unit 2, RHRSW division 1 quarterly flow verification testing on December 19, 2017

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Evaluation

a. Inspection Scope

The inspectors conducted an onsite review to assess the maintenance and testing of the Susquehanna alert and notification system (ANS). During this inspection, the inspectors reviewed the Susquehanna siren system and backup route alerting, and the associated ANS procedures and the Federal Emergency Management Agency ANS Design Report to ensure compliance with design report commitments for system maintenance and testing.

b. Findings

No findings were identified.

1EP3 Emergency Response Organization Staffing and Augmentation System

a. Inspection Scope

The inspectors conducted a review of the Susquehanna Emergency Response Organization (ERO) augmentation staffing requirements and the process for notifying and augmenting the ERO to verify the readiness of key staff to respond to an emergency event and to verify their ability to activate their emergency response facilities (ERFs) in a timely manner. The inspectors reviewed: the Susquehanna Emergency Plan for ERF activation and ERO staffing requirements, the ERO duty roster, applicable station procedures, augmentation test reports, call-in drill reports, and corrective action reports related to this inspection area. The inspectors also reviewed a sample of ERO responder training records to verify training and qualifications were up to date.

b. Findings

No findings were identified.

1EP5 Maintaining Emergency Preparedness

a. Inspection Scope

The inspectors evaluated the efficacy of efforts to maintain the Susquehanna emergency preparedness (EP) program. The inspectors reviewed: memorandums of agreement with offsite agencies; procedures for the 10 CFR 50.54(q) Emergency Plan change process; Susquehannas maintenance of equipment important to EP; records of evacuation time estimate population evaluation; and provisions for, and implementation of, primary, backup, and alternative ERF maintenance. The inspectors also verified compliance with NRC EP regulations regarding: emergency action levels for hostile action events, protective actions for on-site personnel during events, emergency declaration timeliness, ERO augmentation and alternate facility capability, evacuation time estimate updates, on-shift ERO staffing analysis, and ANS back-up means.

The inspectors further evaluated the ability to maintain Susquehannas EP program through their identification and correction of EP weaknesses, by reviewing a sample of drill reports, self-assessments, EP-related CRs, and 10 CFR 50.54(t) reviews since the last NRC EP program inspection in November 2015.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Occupational/Public Radiation Safety (PS)

2RS1 Radiological Hazard Assessment and Exposure Controls

a. Inspection Scope

The inspectors reviewed Susquehannas performance in assessing and controlling radiological hazards in the workplace. The inspectors used the requirements contained in 10 CFR 20, TSs, Regulatory Guide 8.38, and the procedures required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors reviewed the performance indicators (PIs) for the occupational exposure cornerstone, radiation protection program audits, and reports of operational occurrences in occupational radiation safety since the last inspection.

Radiological Hazard Assessment ===

The inspectors conducted independent radiation measurements during walkdowns of the facility and reviewed the radiological survey program, air sampling and analysis, continuous air monitor use, recent plant radiation surveys for radiological work activities, and any changes to plant operations since the last inspection to verify survey adequacy of any new radiological hazards for onsite workers or members of the public.

Instructions to Workers (1 sample)

The inspectors reviewed high radiation area work permit controls and use, observed containers of radioactive materials and assessed whether the containers were labeled and controlled in accordance with requirements.

The inspectors reviewed several occurrences where a workers electronic personal dosimeter (EPD) alarmed. The inspectors reviewed Susquehannas evaluation of the incidents, documentation in the CAP, and whether compensatory dose evaluations were conducted when appropriate. The inspectors verified follow-up investigations of actual radiological conditions for unexpected radiological hazards were performed.

Contamination and Radioactive Material Control (1 sample)

The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material. The inspectors selected several sealed sources from inventory records and assessed whether the sources were accounted for and were tested for loose surface contamination. The inspectors evaluated whether any recent transactions involving nationally tracked sources were reported in accordance with requirements.

Risk-Significant High Radiation Area (HRA) and Very High Radiation Area (VHRA)

Controls (1 sample)

The inspectors reviewed the procedures and controls for HRAs, VHRAs, and radiological transient areas in the plant.

Problem Identification and Resolution (1 sample)

The inspectors evaluated whether problems associated with radiation monitoring and exposure control (including operating experience) were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings

No findings were identified.

2RS2 Occupational ALARA Planning and Controls

a. Inspection Scope

The inspectors assessed Susquehannas performance with respect to maintaining occupational individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors used the requirements contained in 10 CFR 20, Regulatory Guides 8.8 and 8.10, TSs, and procedures required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors conducted a review of Susquehannas collective dose history and trends; ongoing and planned radiological work activities; previous post-outage ALARA reviews; radiological source term history and trends; and ALARA dose estimating and tracking procedures.

Radiological Work Planning (1 sample)

The inspectors selected the following radiological work activities based on exposure significance for review:

  • RWP 2-17-2320, Drywell Scaffold
  • RWP 2-17-2315, Drywell Temporary Shielding
  • RWP 2017-2370, Nozzle and Vessel ISI For each of these activities, the inspectors reviewed: ALARA work activity evaluations, exposure estimates, exposure reduction requirements, results achieved (dose rate reductions, actual dose), person-hour estimates and results achieved, and post-job reviews that were conducted to identify lessons learned.

Implementation of ALARA and Radiological Work Control (1 sample)

The inspectors reviewed radiological work controls and ALARA practices during the observation of in-plant work activities. The inspectors verified use of shielding, contamination controls, airborne controls, RWP controls, and other work controls were consistent with ALARA plans. The inspectors ensured that work-in-progress reviews were performed in a timely manner and adjustments made to the ALARA estimates when appropriate. The inspectors reviewed the results achieved against the intended ALARA estimates to confirm adequate implementation and oversight of radiological work controls. The inspectors also verified that the ALARA staff was involved with emergent work activities and were revising both dose estimates and ALARA controls in the associated RWPs/ALARA Plans, as appropriate.

Problem Identification and Resolution (1 sample)

The inspectors evaluated whether problems associated with ALARA planning and controls were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment

a. Inspection Scope

The inspectors reviewed the monitoring, assessment, and reporting of occupational dose. The inspectors used the requirements in 10 CFR 20, Regulatory Guides 8.9 and 8.34, TSs, and procedures required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors reviewed radiation protection program audits, National Voluntary Laboratory Accreditation Program (NVLAP) dosimetry testing reports and procedures associated with dosimetry operations.

Source Term Characterization (1 sample)

The inspectors reviewed the plant radiation characterization (including gamma, beta, alpha, and neutron) being monitored. The inspector verified the use of scaling factors to account for hard-to-detect radionuclides in internal dose assessments.

External Dosimetry (1 sample)

The inspectors reviewed dosimetry NVLAP accreditation, onsite storage of dosimeters, the use of correction factors to align electronic personal dosimeter results with NVLAP dosimetry results, dosimetry occurrence reports, and CAP documents for adverse trends related to external dosimetry.

Internal Dosimetry (1 sample)

The inspectors reviewed internal dosimetry procedures, whole body counter measurement sensitivity and use, adequacy of the program for whole body count monitoring of plant radionuclides or other bioassay technique, adequacy of the program for dose assessments based on air sample monitoring and the use of respiratory protection, and internal dose assessments for any actual internal exposure.

Special Dosimetric Situations (1 sample)

The inspectors reviewed Susquehannas worker notification of the risks of radiation exposure to the embryo/fetus, the dosimetry monitoring program for declared pregnant workers, external dose monitoring of workers in large dose rate gradient environments, and dose assessments performed since the last inspection that used multi-badging, skin dose or neutron dose assessments.

Problem Identification and Resolution (1 sample)

The inspectors evaluated whether problems associated with occupational dose assessment were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Emergency Preparedness Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed data for the following three EP PIs:

(1) drill and exercise performance,
(2) ERO drill participation, and,
(3) ANS reliability. The last NRC EP inspection at Susquehanna was conducted in the fourth calendar quarter of 2016.

Therefore, the inspectors reviewed supporting documentation from EP drills and equipment tests from the fourth calendar quarter of 2016 through the second calendar quarter of 2017 to verify the accuracy of the reported PI data. The review of the PIs was conducted in accordance with NRC Inspection Procedure 71151. The acceptance criteria documented in NEI 99-02, Regulatory Assessment PI Guidelines, Revision 7, was used as reference criteria.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index

a. Inspection Scope

The inspectors reviewed Susquehannas submittal of the Mitigating Systems Performance Index for the following systems for the period of October 1, 2016 through September 30, 2017:

  • Unit 1 RHR System
  • Unit 2 RHR System
  • Unit 1 RHRSW/ESW
  • Unit 2 RHRSW/ESW To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment PI Guideline, Revision 7. The inspectors also reviewed Susquehannas operator narrative logs, CRs, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.

b. Findings

No findings were identified.

.3 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors reviewed licensee submittals for the occupational radiological occurrences PI for the first through third quarter 2017. The inspectors used PI definitions and guidance contained in NEI 99-02, Revision 7, to determine the accuracy of the PI data reported. The inspectors reviewed electronic personal dosimetry accumulated dose alarms, dose reports, and dose assignments for any intakes that occurred during the time period reviewed to determine if there were potentially unrecognized PI occurrences. The inspectors conducted walkdowns of various Locked High and Very High Radiation Area entrances to determine the adequacy of the controls in place for these areas.

b. Findings

No findings were identified.

.4 Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a. Inspection Scope

The inspectors reviewed licensee submittals for the radiological effluent TS/Offsite Dose Calculation Manual radiological effluent occurrences PI for the first through third quarter of 2017. The inspectors used PI definitions and guidance contained in the NEI 99-02, Revision 7, to determine if the PI data was reported properly. The inspectors reviewed the public dose assessments for the PI for public radiation safety to determine if related data was accurately calculated and reported.

The inspectors reviewed the CAP database to identify any potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose. The inspectors reviewed gaseous and liquid effluent summary data and the results of associated offsite dose calculations to determine if indicator results were accurately reported.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, Problem Identification and Resolution, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify Susquehanna entered issues into the CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the corrective action program.

The inspectors also confirmed, on a sampling basis, that, as applicable, for identified defects and non-conformances, Susquehanna performed an evaluation in accordance with 10 CFR Part 21.

b. Findings

No findings were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a semi-annual review of site issues to identify trends that might indicate the existence of more significant safety concerns. As part of this review, the inspectors included repetitive or closely-related issues documented by Susquehanna in trend reports, site PIs, major equipment problem lists, system health reports, maintenance rule assessments, and maintenance or CAP backlogs. The inspectors also reviewed Susquehannas CAP database for the third and fourth quarters of 2017 to assess CRs written in various subject areas (equipment problems, human performance issues, etc.), as well as, individual issues identified during the NRCs daily CR review (Section 4OA2.1). The inspectors reviewed the most recent trend report for the period of May to August, 2017, conducted under LS-125-1009, Station Trending Manual, Revision 2, to verify that Susquehanna personnel were appropriately evaluating and trending adverse conditions in accordance with applicable procedures.

b. Findings and Observations

No findings were identified.

The inspectors noted a significant reduction in the number of CRs written in the past year. The licensee identified that there was a decrease in CR generation in the most recent trimester, but noted that taken on an annual basis, Susquehanna is still within 5 percent of the industry average for CR generation rate. The licensee documented an action in DI-2017-18445 for the Performance Improvement group to evaluate the decrease in CR generation. The inspectors will continue to monitor the trend, as well as review the results of the licensees evaluation.

The inspectors continued to focus on the licensees assessment and management of plant risk. Inspectors noted that the licensee has implemented a more formalized process for communicating risk management actions (RMAs) to the station during periods of elevated risk by including a written explanation of RMAs in the Plan of the Day. This has heightened awareness of the plant staff as a whole, and also specifies who is responsible for ensuring the completion of each RMA.

The inspectors continued to monitor the stations actions to address human performance errors and events. Susquehannas analysis of the adverse trend had determined that the common flawed defenses were questioning attitude, procedure use and adherence, and verification practices. Since these are already key elements of Susquehannas Focus on Five communication strategy, which is emphasized to the station on pamphlets, posters, and emails, the station intends to continue to communicate using the Focus on Five theme.

In the past two quarters, the inspectors have noted fewer examples of human performance errors, with no scrams. The inspectors will continue to monitor, as it is difficult to determine what is driving the statistical improvement, and whether or not it is sustainable and permanent. The licensee independently recognized this trend in the May - August 2017 Performance Assessment Report, which noted a 19 percent decrease in human performance error trend codes applied to CRs written for the 2nd trimester 2017, in comparison to the last 5 quarters, and that there were 10 percent fewer crew clock resets this trimester than the average for the last 5 trimesters.

.3 Annual Sample: Actions to Address an Adverse Trend in CR Initiation Timeliness

a. Inspection Scope

The inspectors performed an in-depth review of the licensees analysis and corrective actions associated with CR-2016-16254, Trend in CR initiation timeliness identified, written July 1, 2016. Specifically, a trend was identified in the timeliness of generating CRs, as well as processing CRs through the corrective action program.

The inspectors assessed Susquehannas apparent cause evaluation and the prioritization and timeliness of Susquehannas corrective actions were appropriate.

The inspectors review was predominantly focused on the results of daily CAP item screenings to gauge the timeliness of writing CRs for emerging issues.

The inspectors also reviewed specific materials such as documentation of work group discussions, email communications to the plant staff about expectations and standards for writing CRs, and special articles in weekly plant newsletters that addressed the adverse trend. This review constituted one follow-up inspection sample for in-depth review as defined in IP 71152.

b. Findings and Observations

No findings were identified.

The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were generally adequate to address the trend of untimely CR generation. The inspectors noted that occasionally, CR generation does not meet the station expectation of timeliness.

One recent example from September 2017 is CR-2017-16658 which was not written by plant staff until more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after plant staff were made aware of a deficiency, and only after the inspectors made station management aware of the condition. This deficiency concerned inadequate control of clear plastic on the refueling floor, with several noted examples of noncompliance with station procedure NDAP-QA-0507, Foreign Material Exclusion.

As another example, in July 2017, and again in November 2017, when engineering staff wrote CR-2017-13423 and CR-2017-19520 to document conditions adverse to quality concerning safety-related equipment, the descriptions had a level of detail beyond what is required for the initial reporting of a condition, including multi-page attachments, calculations, and analyses justifying operability. Station procedure NDAP-QA-0703, Operability Determinations and Functionality Assessments, states that a person discovering a potential or suspected degraded or nonconforming condition shall immediately notify the main control room and ensure the concern is documented in a CR. The procedure further states that entry into the CAP should not be delayed while waiting for completion of extensive evaluations.

The intent of the process laid out in the procedure is to inform the main control room as quickly as possible so a licensed operator can perform an Initial Operability Screening (IOS). The procedure does allow for an additional 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> of more in-depth information gathering and analysis through the prompt operability determination process, if this is considered appropriate following the initial operability screening. The inspectors determined that in both cases, CR generation was unnecessarily delayed while the engineer worked to first gather the information needed to support a potential prompt operability determination.

The inspectors independently evaluated the deficiencies noted above for significance in accordance with the guidance in Inspection Manual Chapter (IMC) 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues. The inspectors determined these conditions were deficiencies of minor significance and, therefore, are not subject to enforcement action in accordance with the NRCs Enforcement Policy.

.4 Annual Sample: Actions to Address Inadequate Self-Assessment of Fire Brigade

Deficiencies

a. Inspection Scope

The inspectors performed an in-depth review of the licensees analysis and CAP associated with CR-2017-10767, CR-2017-14358, and the associated NRC-identified violation documented in NRC Integrated Inspection Report 05000387; 388/2017002.

Specifically, the inspectors noted numerous discrepancies during a fire drill on May 1, 2017 that were not identified or documented by the drill controllers.

The inspectors assessed Susquehannas cause evaluation and the prioritization and timeliness of Susquehannas corrective actions to determine whether Susquehanna was appropriately identifying, characterizing, and correcting the problems identified during the May 1 drill. The inspectors also reviewed specific materials such as documentation of training and coaching provided to fire brigade members and drill controllers, and CRs generated following subsequent fire brigade drills. On December 20, 2017, the inspectors observed another fire drill to assess the performance of the fire brigade as well as the effectiveness of the drill monitors at identifying and critiquing deficiencies.

This review constituted one follow-up inspection sample for in-depth review as defined in IP 71152.

b. Findings and Observations

No findings were identified.

The inspectors assessed that the corrective actions taken by the licensee were adequate to address the issue. The inspectors noted very few weaknesses in fire brigade performance during the December 20, 2017 drill, and most of these were independently identified and critiqued by the licensee drill monitors. However, the inspectors observed that the control room once again did not sound the fire alarm until approximately nine minutes after drill initiation. This was also an observation made during the May 1, 2017 drill. The inspectors noted that the control room staff was waiting to sound the alarm because the step in the fire response procedure said to sound the alarm upon confirmation of actual fire, even after the drill simulation had presented two diverse indications that installed fire protection systems had actuated.

The licensee subsequently entered the issue into the CAP and intends to revise the fire response procedure to include an explicit definition of a confirmed actual fire.

.5 Annual Sample: Repetitive Failures of Low Pressure Coolant Injection (LPCI) Swing

Bus Automatic Transfer Switches (ATS)

a. Inspection Scope

The inspectors performed an in-depth review of Susquehannas identification, evaluation, and resolution following repetitive failures of LPCI Swing Bus ATSs. This issue resulted in non-cited violation (NCV) 05000387, 388/2016004-02, Failure to Promptly Correct a Condition Adverse to Quality with LPCI Swing Bus ATS. Two redundant Class 1E 480 VAC swing buses provide power to their respective divisions LPCI valves. The LPCI swing bus is capable of receiving electrical power from either of two Class 1E 480 VAC sources, a preferred and an alternate source. An ATS is provided to automatically transfer the swing bus from the preferred to the alternate source upon a loss of power from the preferred source. The NCV was written as a result of two failures of ATSs to properly swap power supplies (one in March 2016 and one in September 2016) during surveillance testing. Both of these failures were determined to be the result of inadequate corrective actions. The issues were entered into the CAP as CR-2016-05589, CR-2016-21554, CR-2016-25715, and CR-2017-03953.

The inspectors assessed Susquehannas problem identification threshold, causal analysis, extent of condition reviews, compensatory actions, and the prioritization and timeliness of corrective actions to determine whether Susquehanna was appropriately identifying, characterizing, and correcting problems associated with these issues and whether the planned or completed corrective actions were appropriate. The inspectors compared the actions taken to the requirements of Susquehannas CAP, Title 10 of the CFR Part 50, Appendix B, and with the reportability requirements of 10 CFR 50.73. In addition, the inspectors reviewed documentation associated with this issue, and interviewed engineering and regulatory affairs personnel to assess the effectiveness of the implemented and planned corrective actions.

b. Findings and Observations

No findings were identified.

The inspectors determined that Susquehanna took appropriate actions to identify the apparent cause of the ATS failures and appropriately identified, prioritized, and implemented corrective actions. The March 2016 failure of 1ATS229 was determined to be due to a deformed upper linkage bolt caused by the upper linkage rod being out of proper adjustment. Prior corrective actions from an ATS failure in 2013 determined that linkage rods needed to be adjusted for proper operation of the ATSs. However, the preventive maintenance instructions were not adequate to ensure optimal linkage rod adjustment. The September 2016 failure of 2ATS219 was determined to be due to inadequate lubrication. During the prior performance of preventive maintenance on 2ATS219 the task of performing cleaning and lubrication of the main contactor hinge point was not performed. A CR was written to generate a work order and reschedule the task, however, the task was not rescheduled or performed.

Following the September 2016 failure of 2ATS219, Susquehanna consulted the ATS vendor manufacturer (Russelectric). The vendor provided technical input regarding proper linkage rod adjustment, ATS component lubrication practices, and well as other improved maintenance practices.

As a result, Susquehanna revised preventive maintenance instructions to incorporate the vendor recommended maintenance practices and reduced the preventive maintenance intervals for the ATSs. The inspectors verified that Susquehanna also incorporated these actions for the sites other Russelectric ATSs (i.e., the emergency diesel generator ATS). The inspectors concluded that the actions taken by Susquehanna to incorporate the vendor recommendations into maintenance instructions were appropriate and, had they been incorporated earlier, could have prevented subsequent failures.

4OA6 Meetings, Including Exit

On January 19, 2018, the inspectors presented the inspection results to Timothy S. Rausch, President and Chief Nuclear Officer, and other members of the Susquehanna staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Personnel

T. Rausch, President and Chief Nuclear Officer
B. Berryman, Site Vice President
D. Jones, Plant Manager
J. Barnhart, Radiological Operations Supervisor - Programs
B. Bridge, Radiation Protection Manager
R. Genovese, Nuclear Regulatory Affairs
J. Gorman, Emergency Preparedness Manager
B. Franssen, Support General Manager
J. Jennings, Nuclear Support General Manager
J. Jessick, Radiological Operations Supervisor - ALARA
T. Karc, Preventive Maintenance Program Owner
M. Krick, Nuclear Regulatory Affairs Supervisor
C. Manges, Regulatory Affairs Senior Engineer
C. Michaels, LOR Lead
N. Pagliano, Nuclear Regulatory Affairs
R. Williams, Components Maintenance Optimization Engineer

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

None.

LIST OF DOCUMENTS REVIEWED