IR 05000373/1985033

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Insp Repts 50-373/85-33 & 50-374/85-34 on 851001-1112. Violations Noted:Failure to Follow Tech Spec Limiting Condition for Operations Concerning Inoperable LPCI Pump & Failure to Review & Approve Plant Mods
ML20141G785
Person / Time
Site: LaSalle, 05003748  Constellation icon.png
Issue date: 12/27/1985
From: Wright G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20141G761 List:
References
50-373-85-33, 50-374-85-34, NUDOCS 8601100410
Download: ML20141G785 (14)


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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports N /85033(DRP); 50-374/85034(DRP)

Docket No ; 50-374 Licenses No. NPF-11; NPF-18 Licensee: Commonwealth Edison Company Post Office Box 767 Chicago, IL 60690 Facility Name: LaSalle County Station, Units 1 and 2 Inspection At: LaSalle Site, Marseilles, IL Inspection Conducted: October 1 through November 12, 1985 Inspectors: M. J. Jordan J. Bjorgen R. Kopriva N. Choules

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k. C. Wright, ' Chief Approved By: /8!/7 f5d" Reactor Projects Section 2C Date Inspection Summary Inspection on October 1 through November 12, 1985 (Reports No. 50-373/85033(DRP);

50-374/85034(DRP))

Areas Inspected: Routine, unannounced inspection conducted by resident inspectors and one regional inspector of licensee actions on previous inspection findings; operational safety; surveillance; maintenance; preparation for refueling; Licensee Event Reports; emergency preparedness training; region requests; unit trips and followup on events. The inspection invol.ved a' total of 369 inspector-hours onsite by four NRC inspectors including 61 hours7.060185e-4 days <br />0.0169 hours <br />1.008598e-4 weeks <br />2.32105e-5 months <br /> onsite during off-shift Results: Of the 10 areas inspected, no violations or deviations were identified in 8 areas; two violations were identified in the remaining two areas (failure to follow Technical Specification Limiting Condition for Operations - Paragraph 3; and failure to review and approve plant modifications - Paragraph 5). The licensee's effort to schedule and plan work was having some effect on jobs being accomplished in a reasonable tim "

8601100410 851231 PDR ADDCK 05000373 G PDR

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Unit 2 restart _has been delayed after the scram (see Paragraph 10) due to an extended inspection and replacement of non Environmentally Qualified wiring on limitorque operators. Approximately 160 valves required reinspection for proper wiring. Improper wiring appears to have been installed by the manufacture The licensee is also completing the remaining Environmentally Qualified equipment replacement prior to returning Unit 2 to power. The licensee continued to have difficulty in identifying operability of safety ~related systems while changing component positions (see paragraph 3) resulting in: safety systems not bein operable. Also maintenance / modification was a problem in the failure to control unauthorized work during the inspection perio = }

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DETAILS 1. Persons Contacted ; Routine Inspection

  • J. Diederich, Manager, LaSalle Station
  • D. Bishop, Services Superintendent
  • E. Sargent, Production Superintendent D. Berkman, Assistant Superintendent, Technical Services
  • W.' Huntington, Assistant Superintendent, Operations
  • M. Jeisy, Quality Assurance P. Manning, Tech Staff Supervisor T. Hammerich, Assistant Tech Staff Supervisor

- *W. Shelton, Assistant Superintendent, Maintenance

~The inspectors also talked with and interviewed members of the

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, operations, maintenance, health physics, and instrument and control

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  • Denotes personnel attending the exit interview held on-November 12, 198 ' Persons Attending Enforcement Conference on' December 4, 1985 Commonwealth-Edison B. L. Thomas, Executive Vice President-C. Reed, Vice President of Nuclear Operations-D.-P. Galle, Assistant Vice President and General Manager for Nuclear Station Division L. O. De1 George, Assistant Vice President of Licensing and Engineering D. Farrar, Director of Nuclear Licensing K. L..Graesser, Division Vice President, Nuclear Stations M..S. Turbak, Operations Plant Licensing Director

. P. Wagner, Operations Manager

. Bitel, Operations QA Manager L. F. Gerner, Superintendent - Regulatory Assurance S..L.--Trubatch, Staff Attorney G..J. Diederich, Station Manager, LaSalle Station W. R.- Huntington, Assistant Superintendent - Operations, LaSalle Station

, C. E. Sargent, Production Superintendent, LaSalle Station T.'A. Hammerich, Assistant Technical Staf" Supervisor, LaSalle Station NRC Representatives

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A. B. Davis ~, Deputy Regional Administrator .

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C. E. Norelius, Director,. Division of Reactor Projects J. A. Hind,-Director, Division of Radiological and Material-Safety Programs

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G. C. Wright, Chief, Reactor Projects Section 2C W. H. Schultz, Enforcement Coordinator B. Stapleton, Enforcement Coordinator

- B. Berson, Regional Counsel M. Jordan, Senior. Resident Inspector, LaSalle

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J. Bjorgen, Resident Inspector, LaSalle R. Kopriva, Resident Inspector, LaSalle R. B. Landsman, Project Manager, Projects Section 2C

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T. C. Poindexter, HQ Enforcement Staff Licensee Action on Previous Inspection Findings (92702)

(Closed) Open Item'(374/85018-03(DRP)): The licensee was to provide-

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additional guidance to contractor Quality Control groups in the areas-

- of drawing updates, QC holdpoints, and operability tests. The inspector has reviewed the implementation. documentation and the revised licensee procedures for Quality Control and has no further concern in this area at this' tim ,

, (Closed) Open Item (374/85018-04(DRP)): The licensee'was to upgrade

- contractor Quality Control programs by August 1,1985. The inspector.

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has reviewed the documentation and revised licensee and contractor procedures and has no further concern in this area at this time.

i '(Close'd) Open Item (374/85018-02(DRP)): .The licensee was-to provide test

-results, conclusions, and a summary of corrective. actions taken in response

- to the' June 17, 1985 Confirmatory Action Letter. The-inspector reviewed'

o the information provided via memorandum from G. Diederich to M. Jordan

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dated July 10,-1985-and, based on discussions with the. licensee staff, -

considers that this item may be closed. The licensee has implemented '

plans for increased involvement of the engineering staff, conducted 4 training, improved the. methods of identifying post modification testing

and declaring systemr. operabl (Closed) Open Item (373/85012-02(DRP); 374/85012-02(DRP))
The licensee was to evaluate procedure LOS-VG-M1 to assure that heater performance of l the Standby Gas Treatment System was adequately monitored. The licensee has revised the procedure to require checking the local system

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. thermometers as well as-the' remote temperature indicators in the control P roo (Closed) Open Item (374/8100-51D): The licensee was to upgrade the

. emergency response procedures and have them in place by September 30, 1985. The inspector verified that the new LGA procedures are in place

and that operator training for the new procedures has been complete . Operational Safety Verification (71707)

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The inspector obse.7ed control room operations, reviewed applicable logs and conducted discussions with control room operators during the

- inspection. period. The inspector verified the operability of selected emergency systems, reviewed tagout records, and verified proper return to service-of affected components. Tours of Units 1 and 2 reactor buildings

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~and turbine buildings were conducted to observe plant equipment conditions,

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. including potential fire hazards, fluid leaks, and excessive vibrations

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and to' verify that maintenance requests had been initiated.for equipment in need.of maintenance. The inspector by observatian.and direct interview

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-verified that the physical security plan was being implemented in accordance L .

with the s'.ation security pla The inspector observed plant housekeeping / cleanliness conditions and

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verified implementation of_ radiation protection control ,'

During the month of October 1985, the inspector walked down the accessible portions of the following systems to verify operability:

Unit 1 Standby Liquid Control System

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Unit 1 Standby Gas Treatment System Unit 1 and 2 Emergency Diesel Generators

~ Unit 1 and 2 Division I & II 125 and 250 Volt

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Batteries and Switchgear Unit 2 Reactor Core Isolation Cooling System

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-Unit 2 Low Pressure Core Spray System Unit 1 Residual Heat Removal System Service Water Pump Rooms and Related Piping Unit 1 Division'III Battery and Switchgear While reviewing the Shift Engineer's log on September 30, 1985, the inspector'noted that the:2B Diesel Generator cooling water pump breaker had' tripped when an attempt was made to start the diesel. The inspector realized that this was the second time in a week that the pump breaker had tripped. On 0ctober l', 1985, this concern was relayed to a region-

-based inspector for investigation. The results of this investigation was documented in the maintenance portion (paragraph.5) of this inspection-report.

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At 6:35 p.m. on October 4, 1985, the licensee declared the Unit 28 Diesel

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Generator cooling water pump and the High Pressure Core Spray System (HPCS) inoperable due to continued problems with the cooling water pump breaker tripping. The licensee then commenced troubleshooting the i problem'with the breaker. At 10:40 a.m. on October 7, 1985,-while e ' reviewing the Shift Engineer's log, the inspector noted that the Division

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1 "2A" Low Pressure Coolant Injection (LPCI) minimum flow valve 2E12F064A Y .had been removed from service at 2:30 a.m. on October 7, 1985. The unit was at 100% power.

The inspector requested the Shift Engineer to explain why Emergency Core Cooling System (ECCS) Division 1 was still considered operable. The

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Shift. Engineer referred to Technical Specification 3.3.3 which allows the LPCI pump "A" discharge flow-low (bypass) switch, which opens the minimum flow valve on low flow, to be tripped for up to seven days. Accordingly, the licensee considered that the valve should be capable of being out of service for up to seven days. What the licensee failed to recognize, was i that the switch actuated on decreasing flow and as such tripping the switch:(required action statement for T.S. 3.3.3. for inoperable switch)

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OPENS not closes the valv i

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' Subsequent-discussion with Region III management and NRR confirmed the-NRC position that with the minimum flow valve out of service the LPCI pump was inoperable. Section 6.3.2.8 of the Updated Final Safety Analysis Report assumes no operator action for ten minutes during postulated accidents. Accordingly, with the minimum flow valve closed and upon initiation, the assumption was that the "A" LPCI pump would operate dead headed for a .ninimum of ten minutes. A significant concern exists that the pump may overheat and fail prior to the operator taking action to provide a flow pat Based on this evaluation, the inspector requested the licensee to reevaluate the operability status of the "A" LPCI subsystem. The licensee subsequently declared the "A" LPCI system inoperable at 3:45 p.m. on October 7, 1985. The minimum flow valve was returned to service and the "A" LPCI system was declared operable at 4:44 p.m.'on October 7, 198 Technical Specification 3.5.1 requires three divisions of Emergency Core Cooling Systems to be operable in Operating Condition 1 with: ECCS Division 1 consisting of: The OPERABLE Low Pressure Core Spray (LPCS) Syste . The OPERABLE Low Pressure Coolant Injection (LPCI) Subsystem

"A" of the RHR syste . At least 6 OPERABLE ADS valve 'ECCS Division 2 consisting of: The OPERABLE Low Pressure Coolant Injection (LPCI) Subsystems

"B" and "C" of the RHR syste . At least 6 OPERABLE ADS valve ECCS Division 3 consisting of the OPERABLE High Pressure Core Spray (HPCS) Syste When the "A" LPCI pump minimum flow valve was closed the licensee should have declared the system inoperable and followed the requirements of TS 3.0.3 as the HPCS system was already inoperable. The licensee did not declare the LPCI system inoperable until thirteen hours and fifteen minutes after the minimum flow valve was removed from service. The licensee returned the minimum flow valve to service and declared the

"A" LPCI pump operable within the one hour time limit of Section 3. Once the LPCI pump had been declared inoperable. Notwithstanding the actions taken once the LPCI pump was declared inoperable this event is considered a violation of Technical Specification, Section 3.0.3 which requires that action be taken within one hour when an LC0 is not met to place the unit in an operational condition where the LC0 is not applicable. (374/85034-01(DRP)).

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Refer to Paragraph 5 of.this report for additional evaluation of the HPCI diesel-cooling water pump breaker proble '

The licensee declared an Unusual _ Event at 6:30 a.m. CDT on October 16,

1985~due to a Unit 2 shutdown required by Technical. Specifications. The Primary Containment Atmosphere Particulate and Gaseous Monitoring System-spuriously tripped and could.not be immediately restarted and the Primary

. Containment Air Coolers Condensate Flow Monitoring-System was isolate This left the Containment Sump Flow Monitoring System as the only operable Coolant Leakage Detection System and thus, required a unit shutdown per Technical Specification 3.4.3.1. The Containment Atmosphere Monitoring System was repaired and the Unusual Event terminated at 7:40 a.m. on October 16, 1985. The licensee is. investigating the cause of the tri It appears that the 2PL15J monitor tripped due to a flow setting

. drift. The 2PL75J monitor was found to have a leaking connection-in the

"0" ring seal area of the iodine caniste The Technical Staff is evaluating the reliability of these monitors for possible maintenance procedure improvements. Completion of this action will be followed as an open-item (374/85034-02DRP)). Monthly Surveillance Observation (61726)

On October 2, 1985, the licensee found an instrument isolation valve for

'an' alarm function.2C11F361, out of pasition while performing surveillance LOS-RD-W1, Scram Discharge Volume Water Test. All remaining valves in the area were checked and found satisfactory. The investigation of this

. event determined that the second verifier, to reduce radiation exposure, had stood back and observed.the first operator operate the valve and did not adequately verify that the valve was positioned properly. All personnel. involved were briefed on how to properly. verify valve positioning. No further action will be take .

The inspector observed the operation of the 2A Diesel Generator during performance of LOS-DG-M2. The inspector visually inspected the Diesel

. Generator for fluid leaks, abnormal noise or vibration, and satisfactory-indication of operating parameters, both locally and in the _ control roo .The Diesel Generator was considered to be operating satisfactorily in

.conformance to Technical Specification requirement The' inspector observed the closing time testing of the Primary Containment Isolation Valves, LOS-PC-Q1 and the scram functional testing of the Main

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-Steam Isolation Valves, LOS-RP-M The inspector verified the use of technically adequate procedures, appropriate preparation and adherence to required precautions and plant conditions, proper operation of equipment,

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and satisfactory return of equipment to operational status. The inspector and unit operator noted a typographical error on pages 14 and 15 of procedure LOS-PC-Q1. The licensee personnel took appropriate action to correct the procedure during the next routine revisio The inspector' observed weekly testing of the "A" Emergency Diesel Fire Pump, LOS-FP-W2 and the monthly operation of the "A" Standby Gas Treatment Train during the performance of LOS-VG-M1. The inspector verified the use 7 i

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of technically adequate procedures, conformance to Technical Specifications,

.that instruments used for test data had current calibrations, that equipment operated satisfactorily and was properly returned to standby statu The inspector observed troubleshooting and functional testing of the "B" Control Room Ventilation Ammonia and Chlorine Detectors using procedures LIS-VC-01, LIS-VC-053, and LIS-VC-03. The "B" train had tripped on September 29, 1985. The two chlorine detectors and the two ammonia detectors were functionally tested and were found to be satisfactor Due to an ongoing concern with the number of trips related to this equipment, the inspector reviewed the surveillance procedures, the vendor manuals, and the preventive maintenance procedures LIP-GM-939 (chlorine) and LIP-GM-940 (ammonia). This review failed to identify a reason for the continuing problems. As discussed in report No. 373/85030; Np. 374/85031, the licensee is continuing to evaluate corrective action plan . Monthly Maintenance Observation (62703)

The inspector monitored the licensee's activities during the first refuel outage preventive maintenance of the 1A Emergency Diesel Generator, procedure LMS-DG-0 The inspector verified the use of technically adequate procedures and observed portions of the post maintenance testing per procedures LOS-DG-M2 and LTS 800-5. The inspector observed the proper operation of the Diesel Generator during the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> ru The inspector also observed the electrical wiring inspection of the Main Steam Isolation Valve Leakage Control Valve 2E32F001J (Work Request 52489). The inspector verified the use of technically adequate procedures and appropriate radiological controls. This inspection was being performed as a followup to a 10 CFR 21 Report issued by the Zion Station. Zion had identified the use of incorrect wiring that invalidated the component's Environmental Qualifications. To date, the licensee has identified twenty seven wires which were known to be incorrect and replace On September 27, 1985, the NRC Resident Inspector noted that the Unit 2 shift turnover sheet listed under " Abnormal Technical Specification Condition", SDV vent valve. Review of the Degraded Equipment Log showed the following entry on August 27, 1985, " MMS replaced tension plate in valve actuator with non-safety related part Valve works: LOS-RD-MI done sat. Valve is only administratively inop." The inspector was told

" administratively inop" maans operable but lacking final paperwor The Resident Inspector expressed concern about the valv The licensee proceeded to replace the spring tension plate with a qualified part and tested the valve. This was completed on September 27, 1985. The spare part was received on September 24, receipt inspected on September 25, and maintenance noti fled on September 26. The subsequent followup inspection by a regional based inspector and the resident inspector determined the following information. On August 17, 1985 at 4:30 a.m., Unit 2 vent Valve 2C11-F380 on the Scram Discharge Volume (SDV) failed to completely close

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during surveillance test LOS-RD-M. An investigation determined that the valve was about 90% closed. A Work Request, L51278, was written to adjust the spring: tension on the valve. It was determined that the spring tension could not be adjusted at about 10:00 a.m.. The Work Request was-amended to disassemble and repair the. valve. Between L approximately 2:00 p.m. and 4:00 p.m., the valve was' disassembled. It was discovered that the spring tension button was broken. No replacement part was available on site. The vendor was contacted and indicated the

part was available in his storeroom and it would require about one week -

to get the part to the plant. ' Subsequently, the vendor determined they did not have the part and.it would have to be manufactured.

, Since a spring button was not available, the licensee decided to machine a button from steel bar stock. Plant personnel concl'ded u that since the

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button appeared to be a cast material, the steel bar stock would be as good or better than the original material. 'The button was machined and installed.in the valve. The part was tested by cycling the valve, which it did successfully. The installation and testing was completed by approximately 9:00 p.m. on August 17, 1985.

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At-the time the steel button was installed, no contact was made with

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Station Nuclear Engineering (SNED) nor was any kind of an evaluation of the-replacement part documente Commonwealth Edison Quality Requirements 3.0, requires that safety-related parts and equipment be reviewed for suitability of application and the evaluation documente ANSI N 18.7-1976, which the licensee is committed to, requires in

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5.2.13(1), sentence 3, 4, and 5 that:

% "In those cases where the QA requirements of the original item cannot be determined, an engineering evaluation shall be conducted by qualified

individuals to establish the requirements and controls. This evaluation shall assure that interfaces, interchangeability, safety, fit and j function are not adversely affected or contrary to applicable regulatory or code requirements. The results of this evaluation shall be documented."

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The failure to perform and document an engineering evaluation of the

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replacement of the spring button part for Valve 2C11-f380 with a button

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made by the licensee is considered to be an example of a violation of 10 CFR 50 Appendix B, Criterion III. (374/85034-03A).

SNED_was contacted on September 27, 1985 and an evaluation of the spring button'made by the licensee was performed. The evaluation concluded that the part was better than the original part.

F On August 19, 1985 breaker MCC 243-1, which controls power to the Unit 2 .

2B Diesel Generator (D/G) cooling water pump, failed. A Work Request, L51369, dated August 20, 1985, was initiated to repair the breaker. The

breaker was repaired. On August 23, 1985, surveillance test LOS-DG-M3 was performed and the breaker and cooling pump functioned properly and
was declared operable.

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. On September 23, 1985, surveillance test LOS-DG-M3 was again performed as required by the Technical Specifications by the operations departmen The.28 D/G cooling pump did not start because the MCC 243-1-breaker i tripped at 10:30 a.m.. At 10:40 a.m., LOS-DG-M3 was performed and the j breaker and pump functioned properly. Operations thought it was random failure and maintenance was not contacted. The pump was declared Joperabl ~ 0n September 27,.1985'due to other work on the 2B Diesel Generator, the

, cooling pump was started and the pump and breaker functioned properl n September 30, 1985 due to other work on the 2B Diesel Generator, surveillance LOS-DG-M3 was run. During this test, the cooling water pump breaker MCC 243-1 tripped and the pump did not start. Maintenance was contacted to investigate the failur ,

Work Request L52347 was written to investigate the problem: During this investigation it was determined that the screws holding the handle on the door of the breaker were too long and could interfere with operation of

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the breaker. The screws were replaced with screws of the proper length.

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The breaker was tested several times ad operated properly. At this time

it was thought that the long screws were the cause of the breaker trips.

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.However, during the initial. troubleshooting, the breaker tripped with the door open and the screws not contacting THE breaker switch mechanis This trip was observed by different personnel than those that determined the long screws were the apparent problem. The breaker trip with the door open apparently was not communicated to anyone els ' The installation of the long screws is another example of installing 4 different parts than-original replacement part without a documented evaluation as required by section 3.0 of Commonwealth Edison Quality Requirements and section 5.2.13(1) of ANSI N 18.7-1976. This is considered to be an example of a violation of 10 CFR 50 Appendix B, Criterion III (374/85034-03B(DRP)).

On October 4, 1985 at the request of the-Senior Resident Inspector, the surveillance was again performed and the pump and' breaker performed properly. Also on this date, the licemee's management became concerned and it was determined that the long screws could not have caused the failure. The Senior Resident Inspector concluded that if this was the case, the original. problem had not been solved. The licensee performed extensive testing and troubleshooting including cycling the breaker, meggering the pump and other wiring, and checking breaker trip currents.

L The breaker tripped several times. No problems were found with the pump and wirin Inspection and testing of the breaker and spare breaker showed they were tripping at approximately 1000 amp vs 1650 nominal breaker setting. A new breaker was obtained and the trip points checked at 1650 amps. The

, new breaker was installed and tested and no trip occurred.

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The root cause of the breaker trips is that the breaker tripped at a *

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lower amperage than the nominal setpoint amperage for the breake Review of- the breaker specifications .showed the setpoint to be +40-25%

, . accurate. , Based on this accuracy, any breaker of this type needs to be

tested prior to installatio >

Review of;this~ event indicates that there was a lack of proper communications during the period from September 23 to October 4, 1985.

t On September 23, operations never contacted maintenance regarding the-breaker trip. On September 30 the root cause of the problem may have i

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been determined had all the available information been available in one place. -_It was not until October 4 after the NRC got involved, that an

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] .indepth review of the problem was performed by plant managemen . -Preparations-For Refueling (60705)

On October 18, 1985 at 12:01.a.m. (CDT),. Unit 1 commenced a scheduled shutdown as they began a twenty (20) week first refueling /maintenanca outage. The inspector observed the shutdown including power reduction, shutdown of the turbine generator, shutdown surveillances, and reactor

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shutdown. Also observed were control room work practices and certain

]f valve. operations when the unit was taken to Cold Shutdown. Major items to take place during the outage are'as follows: refueling, Environmental ,

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Qualification (EQ) modifications, Induction Heat Stress Improvement i'

1 (IHSI),_and electrical and mechanical maintenance work item The inspector reviewed the licensee's preparations for refueling b procedure; review, attendance in meetings, and discussion with licensee- l r

personnel. The inspector verified completion of training of operations and maintenance personnel. The inspector also reviewed administrative, maintenance, surveillance, and accidert procedures to assure that all

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. Technical. Specification and industry standard requirements were being implemented. Since this is the licensee's first refueling, the-inspectors intend to closely monitor the licenree's activities.

' Licensee Event Reports (92700)

, Through direct observations, discussions with-licensee personnel, and review of records, the following Licensee Event Reports (LERs) were

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reviewed to determine that reportability requirements were fulfilled, immediate corrective action was accomplished, and corrective action to prevent recurrence had been accomplished-in accordance with Technical i Specification /85040-00 - Standby Liquid Control (SBLC) Tank Concentration Hig This event report identified several regulatory concerns as follows:

. The. event date stated in the report is wrong. The date should be August 22, 1985 not August 23, 1985.

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! Licensee did not declare the Standby Liquid Control System inoperable in a timely fashion. Per the surveillance procedure, LGP 110-9, revision 4, the Chemistry Supervisor and the Shift Engineer are to be notified immediately if the concentration is not within the Technical Specification limits. These persons were notified and the SBLC system was not declared inoperable for two-(2) hours. This is poor operating practic By delaying the declaration of inoperability of the SBLC system, the

. licensee delayed the start of their time clock as stated in the Technical Specification By having delayed the declaration of the SBLC system inoperable, therefore, initiating the time clock per Technical Specifications, the initiation of the nuclear plant shutdown required by the plant's

" Technical Specifications was delaye Having delayed the plant shutdown, also delayed the notification of the NRC by the licensee of the non-emergency even There are discrepancies in SBLC tank volume used to calculate the concentration and for deciding if the SBLC tank volume is within specification The licensee has recognized that there are several inconsistencies within this LER and will be issuing a revision to this LER to more accurately reflect the facts of the occurrence. The licensee also has identified several items which they are going to resolve: Change procedure for more accurate determination of results and for reporting of those results, Increase communications between Chemistry and the Shift Engineers, Discuss with management a declaration of equipment inoperabilit ' Adequacy of SBLC tank level indicatio e.- Revising the LE These will be tracked as open item (373/85033-01 (DRSS)) and has been transferred to regional based inspectors for closur '8. Emergency Preparedness Training (82206)

The inspectors participated in ar. assembly drill involving all site personnel. This drill was done to assess the licensee's ability to account for all onsite personnel during an accident that night require site evacuation. The inspectors also wanted to assess the time required for essential personnel to arrive at designated emergency response locations. For example, it took 10 minutes for the inspector to reach the control room from the service building. The inspector noted that the

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assembly drill was executed in a reasonably timely manner and that all

. but two onsite personnel were readily accounted for. The licensee considers these two individuals experienced a problem with the assembly area card reader. The individuals apparently did not verify that the reader responded to their badges, i

9 '. Region' Requests (92705)

Regi.on III management requested the inspector to investigate the

. licensee's evaluation and corrective action plans for an excessive number 4 Lof failures of the Residual Heat Removal System Service Water Pump Motor The licensee considers that the majority of electrical short failures was

. . caused from a buildup of concrete dust during construction combined with-the moist pump room environment. This situation caused eventual

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insulation wear and shorting of the motor windings. The licensee has not done a generic evaluation of all ~ Reliance motors based on the failure I mode. .The inspector also discussed the continuing problems'with-the Standby Gas Treatment (SBGT) System radiation monitors with the licensee.

The monitor has a digital readout and a pen recorder-to monitor the

, activity in the train. The pen recorder has experienced spurious spiking that the licensee-has been unable to resolve. This included'several

! visits from the equipment vendor's representative. This will be tracked as an open' item (373/85033-02(DRP); 374/85034-04(DRP)).

-1 Unit Trips (93702)

4 Unit 2 received a Group I isolation and scrammed from 100% power at 12:48

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p.m. CDT on October 21, 1985 while performing surveillance testing on the

"B" Main Steam Line Low Pressure isolation logic. Concurrently, the licensee was troubleshooting the Reactor Water Cleanup High Flow

- isolation which apparently caused a spurious spike in the "A" Main Steam line High Area Temperature isolation logic. This completed the Group I

. ' isolation signal. -All' systems functioned as expected. The licensee

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elected to enter. Cold Shutdown to complete some Environmental r Qualification wor The cause of-the spurious isalation signal was

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determined to be a voltage dip from the Reactor Water Cleanup System isolation timer. When the timer completed its cycle, the resultant

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voltage'. dip caused a perturbation in the Group I power supply. The-licensee has initiated a system change to dampen the voltage di [ 1 Followup on Events (93702)

The licensee reported to the resident inspector an event where three (3)

-contract individuals were working in the offgas building and a security

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guard passing through detected the smell of marijuana smok The three individuals were escorted off site for testin They were prevented access to the site until the results of the testing was determined. Two of the individuals passed the testing and one failed. The individuals who passed were allowed access back to the site and sent back to work and the one who failed was not allowed back on site.

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- 12. Open Items Open items are matters which have been discussed with the licensee, which will be reviewed further.by the inspector, and which involve some action on the part of the NRC or licensee or both. Open items disclosed during the~ inspection are discussed in Paragraphs 7 and . Exit Interview (30703)

~ The inspector met with licensee representatives (denoted in Paragraph 1)

throughout the month and at the conclusion of the inspection period and summarized the scope and findings of the inspection activities. Tha licensee acknowledged these findings. The inspector also discussed the likely informational contents of the inspection report with regard to documents or processes reviewed by the inspector during the inspectio The. licensee did not identify any such documents or processes as

- proprietar Enforcement Conferenc An Enforcement Conference was held in the Region IIILoffice on' December 4, 1985 as a result of a routine safety inspection which identified an apparent violation of NRC requirements. The purpose of the conference was ~to (1) _ discuss the-apparent violation, its significance and causes, and the. licensee's corrective actions, (2) determine whether there were any aggravating or mitigating circumstances, and (3) obtain other

information which would help determine the appropriate enforcement actio Mr. A. Bert Davis, Deputy Regional Administrator, Region III, opened the meeting by describing the purpose and scope of the meeting as well'as the NRC enforcement policy and concerns raised as a result of the October 1 through November 12, 1985 inspectio In addressing the apparent violation the licensee acknowledged the facts and presented corrective actions to prevent recurrence. The licensee

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. felt that the violation resulted from a lack of complete understanding concerning the function of the switch. .The licensee's representatives did not believe the event resulted from a breakdown in management control .

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