IR 05000336/2018004
ML19037A138 | |
Person / Time | |
---|---|
Site: | Millstone |
Issue date: | 02/05/2019 |
From: | Daniel Schroeder Reactor Projects Branch 2 |
To: | Stoddard D Dominion Energy |
Schroeder D | |
References | |
EA-16-090 IR 2018004 | |
Download: ML19037A138 (25) | |
Text
D.
UNITED STATES NUCLEAR REGULATORY COMMISSION ary 5, 2019
SUBJECT:
MILLSTONE POWER STATION - INTEGRATED INSPECTION REPORT 05000336/2018004 AND 05000423/2018004
Dear Mr. Stoddard:
On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Millstone Power Station (Millstone), Units 2 and 3. On January 17, 2019, the NRC inspectors discussed the results of this inspection with Mr. John Daugherty, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC inspectors did not identify any findings or violations of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Daniel L. Schroeder, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos. 50-336 and 50-423 License Nos. DPR-65 and NPF-49
Enclosure:
Inspection Report 05000336/2018004 and 05000423/2018004
Inspection Report
Docket Numbers: 50-336 and 50-423 License Numbers: DPR-65 and NPF-49 Report Numbers: 05000336/2018004 and 05000423/2018004 Enterprise Identifier: I-2018-004-0061 Licensee: Dominion Energy Nuclear Connecticut, Inc. (Dominion)
Facility: Millstone Power Station, Units 2 and 3 Location: P.O. Box 128 Waterford, CT 06385 Inspection Dates: October 1 to December 31, 2018 Inspectors: J. Fuller, Senior Resident Inspector L. McKown, Resident Inspector C. Highley, Resident Inspector H. Anagnostopoulos, Senior Health Physicist J. Kulp, Senior Reactor Inspector D. Silk, Senior Operations Engineer J. Brand, Reactor Inspector A. Turilin, Reactor Inspector J. DeBoer, Emergency Preparedness Physicist K. Mangan, Senior Reactor Inspector Approved By: Daniel L. Schroeder, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Dominions performance at Millstone, Units 2 and 3 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC-identified and self-revealing findings, violations, and additional items are summarized in the table below.
No findings or more-than-minor violations were identified.
Additional Tracking Items Type Issue number Title Inspection Status Results Section NOV 05000423/2016-001-01 Repetitive Failures to 71152 Closed Correct Unit 3 Turbine Driven Auxiliary Feedwater Pump Performance (Enforcement Action (EA)-16-090)
TABLE OF CONTENTS
PLANT STATUS
...........................................................................................................................
INSPECTION SCOPES
................................................................................................................
REACTOR SAFETY
..................................................................................................................
RADIATION SAFETY
..............................................................................................................
OTHER ACTIVITIES - BASELINE
..........................................................................................
INSPECTION RESULTS
............................................................................................................
EXIT MEETINGS AND DEBRIEFS
............................................................................................ 15 THIRD PARTY REVIEWS .......................................................................................................... 15
DOCUMENTS REVIEWED
......................................................................................................... 16
PLANT STATUS
Unit 2 began the inspection period in a scheduled refueling outage and raised power to
approximately 19 percent power on November 3 and then shut down on November 4 for an
unplanned outage due to equipment issues. On December 2, during the Unit 2 power
ascension, a Heater Drain Tank Normal Level Control Valve was operating erratically and
reactor power was lowered to approximately 75 percent to complete repairs. Unit 2 then
returned to rated thermal power on December 4.
Unit 3 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors performed plant status activities described in
IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem
Identification and Resolution. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess Dominion Energys performance and
compliance with Commission rules and regulations, license conditions, site procedures, and
standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather (2 Samples)
The inspectors evaluated readiness for seasonal extreme weather conditions prior to the
seasonal cold temperatures at Unit 2 on December 12, 2018, and Unit 3 on
November 15, 2018.
External Flooding (1 Sample)
The inspectors evaluated readiness to cope with external flooding on October 15, 2018.
71111.04 - Equipment Alignment
Partial Walkdown (2 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
Unit 2
(1) Partial equipment alignment of shutdown cooling system during containment spray
isolation valve maintenance on October 1, 2018.
Unit 3
(2) Partial equipment alignment of the service water system to reactor plant closed cooling
water heat exchangers during isolation valve maintenance on November 29, 2018.
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the Unit 2
pressurizer pressure relief system on November 20, 2018.
71111.05A/Q - Fire Protection Annual/Quarterly
Quarterly Inspection (6 Samples)
The inspectors evaluated fire protection program implementation in the following selected
areas:
Unit 2
(1) Containment (Fire Area C-1 elevations 146, -36, and -22) during routine refueling
outage activities on October 5, 2018
(2) Containment (Fire Area C-1 elevation 386) during welding and grinding activities
associated with flow accelerated corrosion repairs on October 9, 2018
(3) Control room, operator breakroom, and new computer room (Fire Areas A-25, A-26, and
A-27) on November 26, 2018
(4) Auxiliary building general area and safeguard rooms at the -45'6" elevation on
December 9, 2018 (Fire Zones A-1A,A-8A, and Fire Areas A-3, A4)
Unit 3
(5) Cable spreading area spurious fire alarm (Fire Area CB-8) on October 16, 2018
(6) Main steam valve building (Fire Area MSV-1) on October 24, 2018
71111.07 - Heat Sink Performance
Heat Sink (1 Sample)
The inspectors evaluated Dominions monitoring and maintenance of the Unit 2 increased
heat load on service water due to a planned invertor modification on October 12, 2018.
71111.08 - Inservice Inspection Activities (1 Sample)
The inspectors evaluated pressurized water reactor non-destructive examination and
welding activities by reviewing the following examinations from October 8 to 18, 2018:
(1) Volumetric Examinations
a) Manual ultrasonic and phase array ultrasonic testing of feedwater welds FWA-C-G-
06-A, FWA-C-G-05-A, and FWA-C-G-04-C.
b) Manual encoded phased array ultrasonic testing of safety injection weld overlays
BSI-C-1001, BSI-C-1003, BSI-C-2001, BSI-C-2003, BSI-C-3000, BSI-C-3002, BSI-
C-4000, and BSI-C-4002.
c) Manual ultrasonic testing of Loop 2 hot leg shutdown cooling line weld BSD-C-2005.
d) Manual ultrasonic testing of safety injection to loop 2A cold leg weld BSI-C-2005 and
loop 2B cold leg weld BSI-C-4006.
e) Manual ultrasonic and phase array ultrasonic testing of welds W11 BPV-C-5039B,
W12 BPV-C-5049B, W1 BPV-C-5029B, and W2 BPV-C-5051B associated with the
PORV 2-RC-402 and 2-RC-404 replacement.
(2) Visual Examinations
a) General visual examination of containment liner.
b) System leakage test (VT2) of reactor head penetration #26, 38, 42, and 72 area
performed in accordance with American Society of Mechanical Engineers (ASME)
Section XI Code Case N-729-4.
c) System leakage test (VT2) of Loop 2B Cold Leg instrument Tap 3 performed in
accordance with ASME Section XI Code Case N-722-1.
d) Remote visual examination (VT-3) of eight shroud assembly tie rods located at
2°/18°, 72°/108°, 162°/198°, and 252°/288° performed in response to industry
operating experience OE #434420.
(3) Surface Examination (PT/MT)
a) Magnetic particle tests of feedwater system welds FWA-C-G-06-A, FWA-C-G-05-A,
and FWA-C-G-04-
- C.
b) Liquid penetrant tests of welds W11 BPV-C-5039B, W12 BPV-C-5049B, W1 BPV-C-
29B, and W2 BPV-C-5051B associated with the pressurizer PORV 2-RC-402 and
2-RC-404 replacement. This review involved welding activities associated with a
pressure boundary risk significant system.
(4) The inspectors reviewed the welding activities associated with the replacement of a
portion of line of 18-EBB-6 in accordance with MP2-17-00177 (welds W201 FWA-C-G-
06-A, W202 FWA-C-G-05-A, and W203 FWA-C-G-04-C).
(5) The inspectors reviewed the welding activities associated with the replacement of the
pressurizer PORV 2-RC-402 and 2-RC-404 and associated piping (welds W11 BPV-C-
5039B, W12 BPV-C-5049B, W1 BPV-C-5029B, and W2 BPV-C-5051B).
(6) The inspectors evaluated Dominions boric acid corrosion control program performance.
(7) The inspectors performed an independent walkdown of accessible portions of the
containment liner and moisture barrier.
(8) The inspectors did not review steam generator tube or reactor vessel head examination
activities because none were performed during this refueling outage.
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance
Operator Requalification (2 Samples)
The inspectors observed and evaluated operators in the plant simulators during just in time
training for the Unit 2 startup on October 13, 2018, and Unit 3 licensed operator
requalification training on November 27, 2018.
Operator Performance (2 Samples)
The inspectors observed Unit 2 operator performance in the control room during reactor
startup and low power physics testing on November 2, 2018, and Unit 3 operator
performance in the control room during a downpower for turbine valve testing on
November 9, 2018.
71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance
(Annual)
Operator Requalification Exam Results (Annual) (2 Samples)
The inspectors reviewed and evaluated requalification examination results for Unit 2 (written
and operating test) and Unit 3 (written and operating test) on December 20, 2018.
71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance
(Biennial)
Operator Requalification Program and Operator Performance (Biennial) (1 Sample)
The inspectors reviewed and evaluated operator performance, evaluator performance, and
simulator performance during the Unit 2 requalification examinations completed on
December 6, 2018.
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness (1 Sample)
The inspectors evaluated the effectiveness of routine maintenance activities associated
with the following equipment and/or safety significant functions:
(1) Review of the licensees 10 CFR 50.65 (a)(3) Periodic Evaluation for the period of
July 1, 2015 to December 31, 2016
71111.13 - Maintenance Risk Assessments and Emergent Work Control (3 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent
work activities:
Unit 2
(1) Elevated shutdown risk due to performance of A and B train containment spray header
isolation valve invasive maintenance during high decay heat load and decreased reactor
vessel inventory on October 1, 2018
(2) Contingency risk plan for temporary bonnet on 2-CS-16.1A/B during invasive valve
maintenance on October 5, 2018
Unit 3
(3) Emergent high risk when the 15G-14T-2, southern disconnect to Unit 3 normal station
supply transformer breaker, was opened online, which resulted in a single output
breaker in service on October 10, 2018
71111.15 - Operability Determinations and Functionality Assessments (3 Samples)
The inspectors evaluated the following operability determinations and functionality
assessments:
Unit 2
(1) CR1106817 - Non-Conservatisms in Main Steam Line Break Departure from Nucleate
Boiling Ratio Analysis Methodology on October 11, 2018
(2) Immediate operability determination for A and B pressurizer block valves being closed
due to leakage past pressurizer power operated relief valves on December 3, 2018
Unit 3
(3) CR1107892 - Potential Impact to UFSAR 15.1.5.4 Dose Consequence for Main Steam
Line Break due to Delayed Natural Circulation Cooldown on November 2, 2018
71111.18 - Plant Modifications (4 Samples)
The inspectors evaluated the following temporary or permanent modifications:
Unit 2
(1) Replacement of A and B trains containment spray header isolation valve Anchor
Darling motor operated valve stem on October 1, 2018
(2) C reactor protection system bistable and auxiliary bistable trip units design change
number MP2-15-01097 on October 9, 2018
(3) Cutout and weld repair of access hole in the containment airlock on October 29, 2018
(4) Pressurizer power operated relief valve replacement during the refueling outage
(October - November 2018)
71111.19 - Post Maintenance Testing (3 Samples)
The inspectors evaluated post maintenance testing for the following maintenance/repair
activities:
Unit 2
(1) A emergency diesel generator jacket water and aftercooler heat exchanger
replacement on October 15, 2018
(2) 2-SI-468, Shutdown cooling pump suction relief valve replacement with flange leak
check on October 17, 2018
(3) Local leak rate testing and nondestructive examination associated with modification to
containment airlock penetration on October 29 and 30, 2018
71111.20 - Refueling and Other Outage Activities (2 Samples)
The inspectors evaluated Unit 2 scheduled refueling outage (2R25) activities from October 1
through November 3, 2018, and unplanned forced outage activities from November 4
through November 30, 2018.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Containment Isolation Valve (1 Sample)
(1) SP 2605D-013, Containment Leak Test Type C, Penetration 5(O), 2-CS-4.1B, as
performed on October 6, 2018
Routine (2 Samples)
(1) Unit 2, MOV 1220, Motor Operated Valve Testing as performed under joint owners
group commitments for A containment sump outlet header isolation valve as performed
on October 11, 2018
(2) Unit 2, Train B solid state protection system operational test on December 12, 2018
71114.04 - Emergency Action Level and Emergency Plan Changes (1 Sample)
The inspectors verified that the changes made to the emergency plan were done in
accordance with 10 CFR 50.54(q)(3), and any change made to the Emergency Action
Levels, Emergency Plan, and its lower-tier implementing procedures, had not resulted in any
reduction in effectiveness of the plan. This evaluation does not constitute NRC approval.
71114.06 - Drill Evaluation
Emergency Planning Drill (1 Sample)
The inspectors evaluated the conduct of a routine emergency planning drill for Unit 2 on
December 13, 2018.
Drill/Training Evolution (1 Sample)
The inspectors evaluated and observed the Unit 2 licensed operator requalification
program simulator annual operating examination with two event classifications on
November 14, 2018.
RADIATION SAFETY
71124.01 - Radiological Hazard Assessment and Exposure Controls
Radiological Hazard Assessment (1 Sample)
The inspectors evaluated radiological hazards assessments and controls.
Instructions to Workers (1 Sample)
The inspectors evaluated worker instructions.
Contamination and Radioactive Material Control (1 Sample)
The inspectors evaluated contamination and radioactive material controls.
Radiological Hazards Control and Work Coverage (1 Sample)
The inspectors evaluated radiological hazards control and work coverage.
High Radiation Area and Very High Radiation Area Controls (1 Sample)
The inspectors evaluated risk-significant high radiation area and very high radiation area
controls.
Radiation Worker Performance and Radiation Protection Technician Proficiency (1 Sample)
The inspectors evaluated radiation worker performance and radiation protection technician
proficiency.
71124.02 - Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls
Implementation of ALARA and Radiological Work Controls (1 Sample)
The inspectors reviewed ALARA practices and radiological work controls by reviewing the
following activities:
(1) ALARA Plan AP-2-18-01
(2) ALARA Plan AP-2-18-11
(3) ALARA Plan AP-2-18-13
(4) ALARA Plan AP-2-18-26
Radiation Worker Performance (1 Sample)
The inspectors evaluated radiation worker and radiation protection technician performance.
71124.03 - In-Plant Airborne Radioactivity Control and Mitigation
Use of Respiratory Protection Devices (1 Sample)
The inspectors evaluated respiratory protection.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified Dominions performance indicators submittals listed below for the
period from October 2017 through October 2018. (2 Samples)
(1) OR01: Occupational Exposure Control Effectiveness
(2) PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual
Radiological Effluent Occurrences
The inspectors verified Dominions performance indicators submittals listed below for the
period from October 2017 through October 2018. (12 Samples)
Unit 2
(1) MS05: Safety System Functional Failures
(2) MS06: Emergency AC Power System Mitigating System
(3) MS07: High Pressure Injection System Mitigating System
(4) MS08: Heat Removal System
(5) MS09: Residual Heat Removal System
(6) MS10: Cooling Water Support System
Unit 3
(7) MS05: Safety System Functional Failures
(8) MS06: Emergency AC Power System Mitigating System
(9) MS07: High Pressure Injection System Mitigating System
(10) MS08: Heat Removal System
(11) MS09: Residual Heat Removal System
(12) MS10: Cooling Water Support System
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (5 Samples)
The inspectors reviewed Dominions implementation of its corrective action program related to
the following issue:
(1) NRC Notice Of Violation (NOV)05000423/2016001-01, Repetitive Failures to Correct
Unit 3 Turbine Driven Auxiliary Feedwater Pump Performance Issues (EA-16-090)
(2) Corrective action (CA3066486), associated with the repair and replacement activities
associated with the through wall leak on the Unit 2 containment spray recirculation test
(3) Condition report CR1098865, Part 21 Notification Westinghouse control rod drive
mechanism (CRDM) Unit 3 Thermal Sleeve Wear
(4) Condition report CR1103594, High Differential Temperature Across RCP Seal
Package, and CR 1039762, A Reactor Coolant Pump Return Controlled Bleed-off
Flow at 0.8 Gallons per Minute
(5) Repetitive degraded performance of Millstone Unit 2 service water train A flow
instrumentation
INSPECTION RESULTS
Observation 71152
Follow-up of selected
issues
NRC Notice Of Violation (NOV)05000423/2016001-01, Repetitive Failures to Correct Unit 3
Turbine Driven Auxiliary Feedwater Pump Performance Issues (EA-16-090)
NRC issued NOV 05000423/2016001-01 (EA-16-090) for Dominions repetitive failure to take
effective corrective actions for a significant condition adverse to quality involving the degradation
of the Unit 3 turbine driven auxiliary feedwater (TDAFW) pump turbine control valve linkage.
Specifically, Dominions corrective actions to correct the TDAFW control system had not fully
considered all potential failure modes such that continued unreliable operation due to linkage and
control systems problems resulted in another overspeed trip in February 2016. Inspectors
previously documented this condition in 2014 under NCV 05000423/2014013-02, a Green NCV
of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, and in violation (VIO)05000423/2014008-02, a White VIO, also of 10 CFR Part 50, Appendix B Criterion XVI,
Corrective Action. Dominions root cause evaluation (RCE-CA3024960) determined the
February 22, 2016, TDAFW overspeed trip was due to a seized cam follower bearing caused by
corrosion due to control valve packing leakage as a result on an oversized stuffing box allowing
excessive play and bypass of the carbon rings and spacers that accelerated packing wear and
resulted in steam/water impingement on the cam follower bearing and linkage.
By letter dated June 3, 2016, Dominion responded to NOV EA-16-090. Dominion committed to
perform a comprehensive evaluation of additional methods to improve design and operating
margins within the TDAFW pump linkage and control system, and to notify the NRC of the results
of the comprehensive evaluation and planned corrective actions. These results were presented
to the NRC via letter 16-204A, dated September 29, 2016. Applicable corrective actions
included: commissioning an independent third party failure modes and effect analysis, and
consulting with industry and vendor representatives to develop appropriate corrective actions;
replacement of the cam follower bearing with a lubricated bearing; replacement of the governor
control valve bonnet with a new stem packing assembly designed, developed, and recommended
by the vendor; changing the governor as-left (starting) rack setting to increase available stem
force at turbine start-up; creating an activity to inspect and lubricate linkage joints, cam follower
bearing, and packing assembly every refueling outage; lowering the turbine speed; replacement
of steam traps with continuous restriction orifices and added daily operators temperature checks
to verify proper operation of the orifices or to initiate blowdown as necessary; and implementing a
design change to install a metal shield to reduce the amount of steam and condensate impact on
the cam follower bearing. The inspectors reviewed the comprehensive evaluation and completed
corrective actions to verify they have been properly implemented.
The inspectors reviewed applicable modifications of the cam follower and metal shield, performed
field walkdowns to verify installation of these components and restriction orifices, verified
procedures and drawings have been revised, and reviewed quarterly surveillance tests and the
full flow tests performed on the TDAFW pump since February 2016. The inspectors noted that no
related overspeed trips have occurred since the implementation of these corrective actions. The
inspectors determined the causes of the problems were reasonably identified and that corrective
actions were completed focused on addressing the problems and intended to prevent recurrence.
No issues of concern were identified.
Observation 71152
Follow-up of selected
issues
Corrective action (CA3066486), associated with the repair and replacement activities associated
with the through wall leak on the unit 2 containment spray recirculation test header
On September 21, 2017, Dominion identified a very small through-wall leak on an ASME Class 2
pressure boundary pipe associated with the emergency core cooling system. The inspectors
reviewed Dominions corrective actions associated with this nonconforming condition including
the ASME Section XI repair and replacement activities during the Unit 2 refueling outage. The
inspectors determined that Dominions corrective action to replace the leaking pipe was
appropriate; however, the inspectors noted that Dominion had several opportunities to identify the
leak prior to September 21, 2017.
The inspectors noted that Dominion initiated condition report CR1067106 on May 3, 2017, in
response to the identification of white residue on the piping insulation during an ASME Section XI
VT-2 leakage inspection. Dominions chemistry department incorrectly stated that the white
residue was not boric acid, but they recommended that the piping insulation be removed for a
closer inspection of the pressure boundary piping. This was not performed and all work orders
were canceled. Dominion documented a relevant indication on the VT-2 inspection report, but
failed to take further corrective actions to identify the source of the leakage. A work order had
been created, but was canceled with no actions taken.
The inspectors noted that Dominion initiated a second condition report related to this through-wall
leak on September 5, 2017, which stated that this was a repeat indication of leakage from
CR1067106; however, Dominion referred back to the previous, incorrect evaluation from
chemistry stating that the white residue was not boric acid. Therefore, Dominion took no further
corrective action at that time to remove the insulation and investigate the leak. The inspectors
noted that the ASME Section XI VT-2 inspection report remained open without an evaluation of
the relevant indication. This was identified by the NRC inspectors as a second missed
opportunity to identify and correct the leak.
Based on questions asked by the NRC resident inspectors and engagement of Dominion senior
management, the insulation was removed and the piping inspected on September 21, 2017.
CR1078830 was then written to document a through-wall leak on the ASME Class 2 pressure
boundary piping and an immediate operability determination was performed followed by
supplemental ultrasonic inspections and leak rate monitoring until the piping was replaced in the
Fall 2018 refueling outage.
The inspectors noted that CR1078830 provided an adequate operability determination but failed
to acknowledge the untimely identification of the condition. The inspectors noted that the
management review screening of CR1078830 called for a lost opportunity evaluation, which if
performed, would have likely identified similar concerns to those described above. However, the
inspectors noted that this lost opportunity evaluation was not performed.
This issue was determined to be of minor significance because the emergency core cooling
system remained operable after Dominion determined that the flaw was within the limits
established by a structural integrity evaluation in accordance with Code Case N-513-3,
Evaluation Criteria for Temporary Acceptance of Flaws in Moderate Energy Class 2 or 3 Piping,
Section XI, Division 1.
Dominion entered the inspector's observations into their corrective action program as condition
report CR1113486.
Observation 71152
Follow-up of selected
issues
Condition report CR1098865, Part 21 Notification Westinghouse control rod drive mechanism
(CRDM) Unit 3 Thermal Sleeve Wear.
The inspectors assessed Dominions corrective actions associated with CR1098865 to address
the recommendations of NSAL 18-1, Thermal Sleeve Flange Wear Leads to Stuck Control Rod.
This condition was identified at a foreign nuclear power plant and is described in NRC Information Notice 2018-10 (ADAMS Accession No. ML18214A710). The inspectors reviewed Dominions
measurement results completed for Millstone Unit 3 during the 3R18 refueling outage in October
2017 and their technical evaluation of measurement results. The inspectors determined
Dominions response implemented the recommendations, was timely and commensurate with the
safety significance of the issue, and included appropriate corrective actions involving planned
actions to monitor via periodic measurement.
Observation 71152
Follow-up of Selected
Issues
Condition report CR1103594, High Differential Temperature Across RCP Seal Package, and CR
1039762, A Reactor Coolant Pump Return Controlled Bleed-off Flow at 0.8 Gallons per Minute.
The inspectors reviewed Dominions corrective actions that were planned or performed following
the identification of degradation of the seal faces installed in the Unit 3 reactor coolant pumps
(RCPs) documented in CR1103594 and CR1039762. Dominion first identified the degradation
following the failure of the A RCP 3-stage seal in June 2016. New RCP 3-stage seal packages
were installed in the A and D RCP in October 2014, and the B and C RCP in April 2016. The
seals were expected to be in service for up to 10 years before replacement. Following the failure of
the seal, Dominion entered the issue into the corrective action program, replaced the A RCP seal,
and developed actions to troubleshoot and evaluate the cause of the failure. Dominion staff
identified an increasing temperature trend across the other RCP seals and was informed that two
similar seal packages installed at another U.S. nuclear power plant experienced similar problems.
Dominion staff in consultation with the seal manufacturer determined the seal face degradation was
caused by electrical charges passing between the seal plates. Corrective actions included the
installation of RCP motor shaft grounding straps to eliminate shaft induced voltage concerns.
Dominion staff later identified similar temperature trends during the operating cycle following the
completion of the corrective actions. Dominion staff evaluated the temperature rise in the corrective
action program and developed actions to minimize the degradation. Dominions corrective actions
included optimizing seal cooling parameters in order to minimize the degradation mechanism and
monitoring RCP seal temperatures to identify degradation in the seal. Based on the results of this
monitoring program, Dominion staff intend to replace several seals during the next Unit 3 refueling
outage. The inspectors noted that Dominion staff are working with the industry on the seal
degradation to develop the appropriate final corrective actions. The inspectors were informed that
Flowserve personnel have performed additional testing on the seal and concluded that the most
likely cause of the degradation was due to electro-corrosion and is working on a solution within their
corrective action program. Dominions final corrective action to address the RCP seal degradation
is to install a new seal design when the design is complete and tested. The inspectors concluded
that the corrective actions to monitor seal performance and optimize seal cooling parameters while
planning for seal replacement with an improved design in the future was reasonable and
commensurate with the safety significance of the issue.
Observation 71152
Follow-up of selected
issues
Repetitive degraded performance of Millstone Unit 2 service water train A flow instrumentation
The inspectors assessed Dominions corrective actions associated with repetitive degraded
performance of Millstone Unit 2 service water train A flow instrumentation. Dominion began to
observe the instrument intermittently failing low as documented in 2015 in CR579486, in 2016 in
CR1042477 and CR1042902, in 2017 in CR1072632, and in 2018 in CR1107186. The
inspectors reviewed Dominions corrective actions in each case and the establishment of a plant
modification to perform long term restoration.
Based upon the conditions reviewed and corrective actions taken, the inspectors have identified
no more than minor concerns associated with this issue. Dominion appears to have identified
adverse conditions upon inappropriate instrument performance and established corrective actions
in accordance with their safety significance.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On January 17, 2019, the inspectors presented the quarterly resident inspector inspection
results to Mr. John Daugherty, Site Vice President, and other members of the Millstone staff.
THIRD PARTY REVIEWS
Inspectors reviewed the Institute of Nuclear Power Operations report that was issued during the
inspection period.
DOCUMENTS REVIEWED
71111.01 - Adverse Weather Protection
Procedures
C OP 200.13, Seasonal Weather Operations, Revision 11
C OP 200.13-003, Unit 3 Cold Weather Preparation Checklist, Revision 001-01
SP 2665, Building Flood Gate Inspections, Revision 005
MP 2701E, Unit 2 Flood Gates Installation and Removal, Revision 000
Miscellaneous
U2 cold weather status of corrective actions check list, dated December 7, 2018
U3 cold weather status of corrective actions check list, dated November 15, 2018
MP2 FSAR Chapter 2, Section 2.5.4.2.3, Intake Flood Protection
71111.04 - Equipment Alignment
Miscellaneous
P&ID 25203-260014 SH 2, Reactor Coolant System, Revision 49
203-26015, PID Low Pressure Safety Injection System, Sheet 1, Revision 50
212-26933, PID Service Water System, Sheet 2, Revision 91
71111.05 - Fire Protection
Procedures
U2-24-FFS-BAP01-CONT, Fire Fighting Strategies for Containment, Revision 003
C SP 600.22, U2 Containment Fire Hose Station Flow Test, Revision 005
Condition Reports
1112858* 1106814 1112508 1112533
1112538 1112541 1112544 1112866
Miscellaneous
U3-24-FFS, Millstone Unit 3 Fire Fighting Strategies, Revision 0
Millstone Unit 3 Fire Protection Evaluation Report, Revision 21.3
71111.07 - Heat Sink Performance
Procedures
SPROC ENG18-2-005, S-SW-181A Summer Valve Position Determination, Revision 1
Miscellaneous
Calculation PA-090-070-01223EE, MS U2 Electrical Heat Release Calculation in the Z1, 480V
West Switchgear Room at Elevation 36 6, Turbine Building, Revision 1
Calculation 12-280, PROTO-HX Model Development of MP2 Room Coolers X-181 A/B and X-
183 and Elevation of 80 F Service Water with Addendum Heat Exchanger Heat Load
Updates for 1, 3, 5 Inverter Replacement, Revision 00
Calculation 92-FFP-00934ES, MPS2 West 480 Volt AC Load Center Heat Gains, Revision 04
Calculation 12-001, MP2 SW Model and Design Bases Analysis with Addendum Heat Load
Changes Due to Inverter Replacement in the East DC Vital Switchgear Room and the
West 480V Switchgear Room, Revision 02
71111.08 - Inservice Inspection Activities
Procedures
ER-AA-CII-102, ASME Section XI Containment Inservice Inspection (Metal/IWE) Program Fleet
Implementation Requirements, Revision 3
ER-AP-BAC-101, Boric Acid Corrosion Control Program (BACCP) Inspections, Revision 12
ER-AA-NDE-UT-706, Ultrasonic Examination for the Detection of Laminar Indications,
Revision 1
ER-AA-NDE-UT-801, Ultrasonic Examination of Ferretic Piping Welds in Accordance with ASME
Section XI, Appendix VIII, Revision 7
ER-AA-NDE-MT-200, ASME Section XI Magnetic Particle Examination Procedure, Revision 5
ER-AA-NDE-UT-742, Encoded Phased Array Ultrasonic Examination of Ferretic and Austenitic
Welds, Revision 3
ER-MP-NDE-UT-816, Manual Phased Array Procedure for Weld Overlaid Similar and Dissimilar
Metal Welds, Revision 1
ER-AA-NDE-VT-604, Visual Examination (VE) for Leakage of PWR Reactor Head Penetrations,
Revision 3
ER-AA-NDE-VT-607, VE Examination of Pressure Retaining welds in Class 1 Components
Fabricated with Alloy 600/82/182 Materials, Revision 2
ER-AA-NDE-VT-608, VT-3 Visual Examination Procedure for Examination Category B-N-1,
Interior of Reactor Vessel, Revision 0
ER-AA-NDE-UT-802, Ultrasonic Examination of Austenitic Piping Welds in Accordance with
ASME Section XI, Appendix VIII, Revision 5
Condition Reports (*initiated in response to inspection)
1012448 1064672 1065914 1099890
1105795 1106136 1106137 1106140
1106237 1106290 1106297 1106308
1106389 1106402 1106471
Maintenance Order/Work Order
53102884929 53103117773 53103120600 53103147770
NDE Reports
M2-UT-18-003, UT Examination Report for FWA-C-G-05-A, dated September 25, 2018
M2-UT-18-004, UT Examination Report for FWA-C-G-05-A, dated September 25, 2018
M2-UT-18-028, UT Examination Report for FWA-C-G-04-C, dated October 13, 2018
M2-UT-18-029, UT Examination Report for FWA-C-G-06-A, dated October 13, 2018
M2-MT-18-001, MT Examination Report for FWA-C-G-05-A, dated September 25, 2018
M2-MT-18-004, MT Examination Report for FWA-C-G-04-C, dated October 13, 2018
M2-MT-18-005, MT Examination Report for FWA-C-G-06-A, dated October 13, 2018
FAC2-Weld-203, UT Examination Report for 18-EBB-6, dated October 13, 2018
FAC2-Weld-201, UT Examination Report for 18-EBB-6, dated October 13, 2018
M2-UTU-18-009, UT Examination Report for BSI-C-1001, dated October 4, 2018
M2-UTU-18-011, UT Examination Report for BSI-C-1003, dated October 4, 2018
M2-UTU-18-006, UT Examination Report for BSI-C-2001, dated October 4, 2018
M2-UTU-18-012, UT Examination Report for BSI-C-2003, dated October 4, 2018
M2-UTU-18-005, UT Examination Report for BSI-C-3000, dated October 4, 2018
M2-UTU-18-008, UT Examination Report for BSI-C-3002, dated October 4, 2018
M2-UTU-18-013, UT Examination Report for BSI-C-4000, dated October 6, 2018
M2-UTU-18-014, UT Examination Report for BSI-C-4002, dated October 6, 2018
BOP-VT-18-041, VT Examination Report for RPV Head Penetrations 26, 38, 42 and 72, dated
October 5, 2018
M2-VT-18-108, VT Examination Report for Loop 2B CL Instrument Tap 3, dated October 2, 2018
BOP-VT-18-042, VT Examination Report for M2H1-CSB - Examined per OE Condition Report
CR1099890, dated October 7, 2018
M2-UT-18-011, UT Examination Report for BSD-C-2005, dated October 6, 2018
M2-UT-18-012, UT Examination Report for BSD-C-2005, dated October 6, 2018
M2-UT-18-007, UT Examination Report for BSI-C-2005, dated October 5, 2018
M2-UT-18-008, UT Examination Report for BSI-C-2005, dated October 5, 2018
M2-UT-18-013, UT Examination Report for BSI-C-4006, dated October 7, 2018
M2-PT-18-006, PT Examination Report for BPV-C-5029B, dated October 8, 2018
M2-PT-18-007, PT Examination Report for BPV-C-5039B, dated October 8, 2018
M2-PT-18-008, PT Examination Report for BPV-C-5049B, dated October 8, 2018
M2-PT-18-009, PT Examination Report for BPV-C-5051B, dated October 8, 2018
M2-UT-18-017, UT Examination Report for BPV-C-5029B, dated October 8, 2018
M2-UT-18-021, UT Examination Report for BPV-C-5029B, dated October 9, 2018
M2-UT-18-019, UT Examination Report for BPV-C-5039B, dated October 8, 2018
M2-UT-18-022, UT Examination Report for BPV-C-5039B, dated October 9, 2018
M2-UT-18-020, UT Examination Report for BPV-C-5049B, dated October 8, 2018
M2-UT-18-023, UT Examination Report for BPV-C-5049B, dated October 9, 2018
M2-UT-18-018, UT Examination Report for BPV-C-5051B, dated October 8, 2018
M2-UT-18-024, UT Examination Report for BPV-C-5051B, dated October 9, 2018
PORV-W1, UT Examination Report for PORV Weld W1, dated October 9, 2018
PORV-W2, UT Examination Report for PORV Weld W2, dated October 9, 2018
PORV-W11, UT Examination Report for PORV Weld W11, dated October 9, 2018
PORV-W12, UT Examination Report for PORV Weld W12, dated October 9, 2018
M2-UT-17-032, UT Examination Report for SI-CF-F-049, dated April 13, 2017
Miscellaneous
NRC Letter, Millstone Power Station, Units Nos. 2 and 3 - Alternative Request RR-04-27 and
IR-3-38, Revision 0, for the Use of Encoded Phased Array Ultrasonic Examination
Techniques in lieu of Radiography (EPID-L-2018-LLR-0011), (ML18252A003), dated
September 17, 2018
Millstone Power Station Unit 2 In-Service Inspection Program - Owner's Activity Report,
Refueling Outage 24, dated June 27, 2017
ETE-MP-2017-1015, Millstone Unit 2 Steam Generator Integrity Degradation Assessment
(2R24), Revision 0
ETE-MP-2017-1060, Millstone Unit 2 Steam Generator Integrity Condition Monitoring and
Operational Assessment Refueling Outage (2R24), Revision 0
ETE-MP-2018-1071, Degradation Assessment Technical Review for not Performing Primary or
Secondary Inspections of the Steam Generators During 2R25, Revision 0
71111.11 - Licensed Operator Requalification Program
Procedures
Unit 2 LORP 2C26 JITT, Reactor Start Up and Low Power Physics Testing Course # 75098,
Dated 12 October, 2018
Unit 2 LORP 2C26 Startup JITT, 2C26 Turbine Overspeed (ICCE), Main Turbine Synch to the
Grid and 2nd SGFP Startup Course # 75099, dated October 12, 2018
OP 2204, Load Changes, Revision 040
SP 3623.2, Turbine Overspeed Protection System Test, Revision 012
Miscellaneous
Reactivity Plan, M3C19 RXMANP03.3, Update 1
71111.12 - Maintenance Effectiveness
Miscellaneous
Periodic 10 CFR 50.65 (a)(3) self-assessment [July 1, 2015 to December 31, 2016];
PIR1059274
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Procedures
OU-AA-200, Shutdown Risk Management, Revision 10
WM-AA-301, Operational Risk Assessment, Revision 20
OU-M2-201, Shutdown Safety Assessment Checklist, Revision 23
MP 2702D1B, Anchor Darling 4 inch and Larger Double Disc Gate Valve Maintenance, Revision
NF-AA-PRA-370, Probable Risk Assessment Procedures and Methods: MRule (a)(4) Risk
Monitor Guidance, Revision 16
Condition Reports
1109048
Work Orders
53102909963 53203148327
Miscellaneous
203-26015, PID Low Pressure Safety Injection System, Sheet 1, Revision 50
2R25 Shutdown Risk Assessment
2R25 Shutdown Risk Schedule Review
Millstone Unit 2 Shutdown Safety Assessment Checklist dated October 1, 2018
Millstone Unit 2 Shutdown Safety Assessment Checklist dated October 5, 2018
EOOS Version 4.1 for Millstone Unit 3 on 10/5/2018
High Risk Plan for Sulfur Fluoride Gas addition to 15G-14T-2, Millstone Unit 3 South Bus Output
Breaker as Implemented on October 5, 2018
71111.15 - Operability Determinations and Functionality Assessments
Condition Reports
1106817 1107892 1107987 1111536
Miscellaneous
ETE-SU-2017-0069, SPS Emergency Diesel Generator Mission Time, Revision 0
71111.18 - Plant Modifications
Procedures
SP-M2-ME-1053, Procurement and Design Specification for MP2 Power Operated Valves 2-
RC-402 and 2-RC-404, Revision 6
SP 2401SE, PORV, Trip Inhibit, Trip Inhibit Annunciator and Matrix Circuit Ground Detection
Functional Test, Revision 002-00
SP 2401BB3, Channel C Wide Range Monitor Start-up Functional Test Data Sheet, Revision
003-00
SP 2401C, RPS Turbine Loss of Load Test with EHC system Initially Tripped Data Sheet,
Revision 009-04
SP 2401D, RPS Matrix Logic and Trip Path Relay Test Data Sheet, Revision 016-00
MP 2702D1B, Anchor Darling 4 Inch and Larger Double Disc Gate Valve Maintenance,
Revision 0
Condition Reports
1100125 1105171 1107996
Maintenance Orders/Work Orders
53102909963 53103042453 53103080132 53103081255
53103081259 53103147770 53203148327
Miscellaneous
Design Equivalent Change Package Number MP2-17-00178, Millstone 2 PORV Replacement,
Revision 0 and Revision 1
ETE-MP-2018-1085, Transmittal of PORV Stroke Time for use in Thermal-Hydraulic Analysis,
Revision 0
Calculation Number 32-5072658-005, Millstone Unit 2 PORV/PSV Relief Piping Transient Loads
Calculation, Revision 5
203-26015, PID Low Pressure Safety Injection System, Sheet 1, Revision 50
DC-18-00131, Containment Spray Header Isolation Valve Stem Replacement, Revision 0
71111.19 - Post-Maintenance Testing
Procedures
ER-AA-NDE-RT-400, Radiographic Examination Procedure, Revision 1
SP 2613A, Periodic DG Operability Test, Facility 1 (Fast Start, Loaded Run), Revision 023
SP 2670, A RBCCW HX D/P Determination, Revision 011-01
Condition Reports
1108817 1110413 1110584
Maintenance Orders/Work Orders
53102842362 53102842741 53103106290 53103118384
203150809
Miscellaneous
Post Maintenance Test Plan for U2 Containment Airlock dated 10/29/18
ETE-MP-2018-1092, MP2 Containment Personnel Air Lock Access Window, Revision 0
71111.22 - Surveillance Testing
Procedures
SP 3446B12, Train B Solid State Protection System Operational Test, Revision 017
Work Orders
53102573331 53102909963 53102909966 53203148327
203148330
Condition Reports
1107290
71114.04: Emergency Action Level and Emergency Plan Changes
Miscellaneous
MP-18-07S, MP-26-EPI-EPMP, Millstone Power Station Emergency Plan, Revision 56
MP-18-08S, MP-26-EPA-REF03, Millstone Unit 3 Emergency Action Level Scheme (I-7 of 8),
Revision 23
71151 - Performance Indicator Verification
Procedures
4Q2017 Derivation and Margin Reports for Millstone Unit 2 Mitigating System Performance
Index Performance Indicator Emergency AC, High Pressure Injection, Heat Removal,
Residual Heat Removal, and Cooling Water System Inputs
1Q2018 Derivation and Margin Reports for Millstone Unit 2 Mitigating System Performance
Index Performance Indicator Emergency AC, High Pressure Injection, Heat Removal,
Residual Heat Removal, and Cooling Water System Inputs
2Q2018 Derivation and Margin Reports for Millstone Unit 2 Mitigating System Performance
Index Performance Indicator Emergency AC, High Pressure Injection, Heat Removal,
Residual Heat Removal, and Cooling Water System Inputs
3Q2018 Derivation and Margin Reports for Millstone Unit 2 Mitigating System Performance
Index Performance Indicator Emergency AC, High Pressure Injection, Heat Removal,
Residual Heat Removal, and Cooling Water System Inputs
4Q2017 - 3Q2018, Safety System Functional Failure Performance Indicator Submittal, Millstone
Unit 2
3Q2018 Derivation and Margin Reports for Millstone Unit 3 Mitigating System Performance
Index Performance Indicator Emergency AC, High Pressure Injection, Heat Removal,
Residual Heat Removal, and Cooling Water System Inputs
2Q2018 Derivation and Margin Reports for Millstone Unit 3 Mitigating System Performance
Index Performance Indicator Emergency AC, High Pressure Injection, Heat Removal,
Residual Heat Removal, and Cooling Water System Inputs
4Q2017 - 3Q2018, Safety System Functional Failure Performance Indicator Submittal, Millstone
Unit 3
Nuclear Energy Institute Documents 99-02, Regulatory Assessment Performance Indicator
Guideline, Revision 7
71152 - Problem Identification and Resolution
Condition Reports (*initiated in response to inspection)
CA3066486 1112355 * 1112359 * 535411
537933 538353 538743 579486
27923 1034887 1039762 1042477
1042902 1072632 1078830 1082517
1083296 1098865 1103594 1105524
1107186 1109579
Procedures
OP 3304A, Revision 40
OP 3337, Revision 19
OP 3301D, Reactor Coolant Pump Operation, Revision 21
Instruction Manual TM-0400, Three Stage NX Seal Cartridge, Revision G
Engineering Evaluations
ETE-MP-2017-1172, Evaluation of Wear of MPS3 Closure Head Penetration Thermal Sleeves
Upper Flanges, Revision 1
Drawings
212-29001, SH-6010, RPV General Arrangement Elevation, Revision 0C
212-29001, SH-6024, Sh 7 of 9, RPV As Built Closure Head Penet, Revision 0A
Miscellaneous
MRP 2018-027, NEI 03-08 Needed Inspection Guidance for PWR CRDM Thermal Sleeve Wear,
dated August 31, 2018
LTR-NRC-18-34, Westinghouse Letter: Notification of the Potential Existence of Defects
Pursuant to 10CFR Part 21, dated May 23, 2018
NSAL-18-1, Thermal Sleeve Flange Wear Leads to Stuck Control Rod, dated July 9, 2018
PWROG-16003-P, Evaluation of Potential Thermal Sleeve Flange Wear, Revision 1
TB-07-2, Reactor Vessel Head Adapter Thermal Sleeve Wear, Revision 3
2-927824-000, Millstone Unit 3 CRDM Thermal Sleeve As-Found Dimensional Report, dated
October 27, 2017
MP2-18-01079, Replacement of FIT-6471 with Flexim Flowmeter, Revision 0
Reactor Coolant Pump Seal Injection Temperature data, dated 13/12/18
Reactor Coolant Pumps A, B, C and D Vibration data, 5/27/02 to 3/31/18
Operational Decision Making Checklist for CR 1103594
The Evolution of Successful Elimination of Electro-Corrosion In Mechanical Seals for Reactor-
and Boiling Feed Water Pumps Handling Ultra-Pure Water, Proceedings of the Twenty-
ninth International Pump Users, Symposium, September 30 - October 3, 2013
Letter from Flowserve to NextEra FPL, Subject: Updated to NX Seal Root Cause Evaluation,
dated 6/11/18
3033992, Root Cause Evaluation, Revision 1
3069444, Root Cause Evaluation, Revision 0
212-26945, Piping & Instrumentation Diagram, Turbine Plant Miscellaneous Drains, Rev. 44
212-29736, Governor Lever and Valve Section, Rev. E
DCN MP3-16-01145, MP3 TDAFW Pump Control Valve 3MSS*MCV5 Reliability Enhancement,
dated 7/11/17
ETE-MP-2016-1023, Engineering Technical evaluation- TDAFW Pump Cam Follower Bearing
Greasing and Steam Spray Shield, Rev. 0
RCE CA3024960, Root cause Evaluation MP3 TDAFW Pump Tripped While Starting for
Operational Test, Rev. 0
Q3-2018 U-3, 3322 Auxiliary Feedwater & DWST System Health Report, dated 12/4/18
SP 3622.3, Auxiliary Feedwater Pump 3FWA*P2, Operational Readiness Test, Rev. 25
3FWA*P2 (3M) IST Pump Reference Value Evaluation, dated 10/7/18
SP 3622.3-001, TDAFW Pump Operational Readiness and Quarterly IST Group B Pump Test,
completed 10/25/18
SP 3622.3-005, TDAFW Pump IST Comprehensive Pump and Check Valve Test, completed
9/28/16
SP 3622.3-005, TDAFW Pump IST Comprehensive Pump and Check Valve Test, completed
3/5/18
SP 3622.3-006, TDAFW Pump Overspeed Test (Using Compressed Air), completed 11/1/17
SP 3636C.1-001, Main Steam Drain Valve Stroke Time Test, completed 9/25/18
SP 3670.1-011, Plant Equipment Rounds-Radwaste, Rev. 16
U-3, M33FWA*P2, Lubricating Oil Analysis History
U-3, M33FWA*P2, Vibration Data History
U-3, Steam Traps A, B, D Line temperatures-History
Work Orders
53102961658
53103031305
53103120906