IR 05000305/2009002

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IR 05000305-09-002, on 01/01/2009 - 03/31/2009; Kewaunee Power Station, Flooding, Maintenance Risk Assessments and Emergent Work Control, and Follow Up of Events and Notices of Enforcement Discretion
ML091280300
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 05/08/2009
From: Michael Kunowski
NRC/RGN-III/DRP/B5
To: Christian D
Dominion Energy Kewaunee
References
FOIA/PA-2010-0209 IR-09-002
Download: ML091280300 (57)


Text

May 8, 2009

SUBJECT:

KEWAUNEE POWER STATION INTEGRATED INSPECTION REPORT 05000305/2009002

Dear Mr. Christian:

On March 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Kewaunee Power Station. The enclosed report documents four of the five inspection findings, which were discussed on April 8, 2009, with Mr. S. Scace and other members of your staff. The remaining inspection finding is related to physical security and is documented in Inspection Report 05000305/2009008.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

The report documents three NRC-identified findings and one self-revealed finding of very low safety significance (Green). The findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as Non-Cited Violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy.

If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, Region III; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Kewaunee.

In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at Kewaunee. The information you provide will be considered in accordance with Inspection Manual Chapter 0305. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Michael A. Kunowski, Chief Branch 5 Division of Reactor Projects Docket No. 50-305 License No. DPR-43 Enclosure: Inspection Report 05000305/2009002 w/Attachment: Supplemental Information cc w/encl: S. Scace, Site Vice President M. Wilson, Director, Nuclear Safety and Licensing C. Funderburk, Director, Nuclear Licensing and Operations Support T. Breene, Manager, Nuclear Licensing L. Cuoco, Senior Counsel D. Zellner, Chairman, Town of Carlton J. Kitsembel, Public Service Commission of Wisconsin P. Schmidt, State Liaison Officer

SUMMARY OF FINDINGS

IR 05000305/2009002; 01/01/2009 - 03/31/2009; Kewaunee Power Station; Flooding;

Maintenance Risk Assessments and Emergent Work Control; and Follow-Up of Events and Notices of Enforcement Discretion.

This report covers a three-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. Four Green findings were identified by the inspectors. The findings were considered Non-Cited Violations (NCVs) of NRC regulations.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified

and Self-Revealed Findings

Cornerstone: Initiating Events

Green.

A finding of very low safety significance (Green) and associated Non-Cited Violation of 10 CFR 50.65(a)(4) was identified by the inspectors for the failure to properly assess risk that resulted from risk significant maintenance being performed on the component cooling water (CCW) system, when the licensee inappropriately applied criteria for the use of a dedicated operator to meet availability requirements. As part of its corrective actions, the licensee stopped work that required the use of a dedicated operator pending further evaluation.

The issue was more than minor because the licensees risk assessment for March 11, 2009, failed to consider the CCW unavailable during maintenance.

Specifically, the failure to account for the unavailability of CCW resulted in an inadequate daily risk assessment and could affect the unavailability time of this system in related performance and maintenance rule indicators. The inspectors evaluated the finding using the Significance Determination Process in accordance with Inspection Manual Chapter 0609, Significance Determination Process, Attachment K, Maintenance Risk Assessment and Risk Management Significance Determination Process, dated May 19, 2005, and determined the issue screened as having very low safety significance (Green), because the incremental conditional core damage probability was less than 1E-6 due to the test condition lasting only four hours. The inspectors determined that the finding had a cross-cutting aspect in the corrective action program component of problem identification and resolution, because the licensee failed to thoroughly evaluate a prior problem such that the resolution addressed the causes and extent of conditions necessary to preclude this event. (P.1(c)) (Section 1R13)

Cornerstone: Mitigating Systems

Green.

A finding of very low safety significance and associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified by the inspectors for the failure to translate the flooding design basis into specifications, procedures, and instructions. Specifically, the licensee failed to control the storage of material in the steam generator blowdown tank room that could potentially clog a floor drain, in an adjoining room, that was credited in a flood analysis. As part of its corrective actions, the licensee removed or secured the material of concern.

The finding was determined to be more than minor because it was associated with the Mitigating Systems Cornerstone attribute of Protection Against External Events and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the licensee did not put adequate controls in place to ensure that the drain would performed its credited function to be open and free flowing during an internal flood scenario involving a break in a 4-inch condensate line. The inspectors evaluated the finding using the Significance Determination Process in accordance with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of Findings, Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008.

The significance of the finding was determined to be of very low safety significance (Green) because the inspectors answered no to the questions in the Mitigation Systems Cornerstone column. The inspectors did not identify a cross-cutting aspect associated with this finding because the controls over material that could plug the drain should have been implemented when calculation 2005-05708 was completed and incorporated in the flooding design basis in 2005; therefore, this issue was not reflective of current performance. (Section 1R06)

Green.

A finding of very low safety significance (Green) and associated Severity Level IV, Non-Cited Violation of 10 CFR 50.59 was identified by the inspectors while reviewing Unresolved Item 05000305/2008003-03, Siphon Line Which Interconnected Two Diesel Generator Emergency Fuel Oil Storage Tanks Was Not Functioning as Designed. Specifically, while performing Updated Safety Analysis Report change request, UCR 93-031, the licensee inappropriately screened the removal of the Updated Safety Analysis Report reference to the siphon line when plant staff incorrectly answered no to all of the 10 CFR 50.59 evaluation questions. The licensee entered this issue into its corrective action program for evaluation and development of corrective actions, as appropriate.

Because violations of 10 CFR 50.59 are considered to be violations that potentially impede or impact the regulatory process, they are dispositioned using the traditional enforcement process. As described in Supplement I of the Enforcement Policy, to determine the severity of a 10 CFR 50.59 violation, the underlying technical issue was evaluated under the Significance Determination Process. The inspectors evaluated the finding using the SDP in accordance with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of Findings, Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008.

The inspectors answered yes to Question 2 in the Mitigation System Cornerstone column which required the issue to be evaluated in accordance with Appendix A, of Inspection Manual Chapter 0609. Using Appendix A, the inspectors screened the issue as very low safety significance (Green) because the quantity of fuel to the diesel generators that was historically available always exceeded that needed for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of operation, thereby, resulting in the probabilistic risk assessment function for the diesels being met. The inspectors determined that the issue had a cross-cutting aspect in problem identification and resolution, corrective action program, because the licensee had identified similar deficiencies with accurately applying or interpreting the current licensing basis, and failed to take timely action to complete corrective actions, or establish barriers to prevent recurrence of this deficiency (P.1(d)). Section 4OA3.2)

Cornerstone: Barrier Integrity

Green.

A finding of very low safety significance (Green) and associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the licensees failure to follow the corrective action program procedure to implement corrective actions that could have prevented a December 30, 2008, door seal failure, which rendered both trains of control room ventilation inoperable. The licensee entered this issue into its corrective action program and, as partially corrective action, has increased its monitoring of doors for potential failure mechanisms.

The finding was determined to be more than minor because it was associated with the Barrier Integrity Cornerstone attribute of Configuration Control and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. The inspectors evaluated the finding using the Significance Determination Process (SDP) in accordance with Inspection Manual Chapter (IMC) 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of Findings, dated January 10, 2008, and determined the finding represented a degradation of the barrier function to protect against radiological hazards, toxic gas, and smoke that required a Phase 3 analysis. A Region III Senior Reactor Analyst completed a qualitative Phase 3 analysis and determined that because the duration of the event was small, 44 minutes, the issue screened as having very low safety significance (Green). The inspectors determined that the finding had a cross-cutting aspect in the corrective action program component element of problem identification and resolution because the licensee failed to take appropriate corrective actions to address safety issues and adverse trends in a timely manner. (P.1(d)) (Section 4OA3.)

Licensee-Identified Violations

No violations of significance were identified.

REPORT DETAILS

Summary of Plant Status

Kewaunee operated at full power for the entire inspection period except for brief downpowers to conduct planned maintenance and surveillance activities, and with the following exception:

  • On March 26, 2009, Kewaunee experienced an unplanned power change when they reduced power below 1673 megawatts thermal as required by Technical Specifications (TS) 3.4.b.3. Specifically, at 12:26 p.m. a high energy line break (HELB) door was declared non-functional, and as a result all three auxiliary feedwater (AFW) pumps were declared inoperable. Technical Specification 3.4.b.3 states that if two of the three AFW trains are inoperable, then within two hours, reduce reactor power to less than or equal to 1673 megawatts thermal. The HELB door was returned to a functional status at 5:40 p.m. and the licensee exited the action statements and returned to full power.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with the design basis probable maximum flood. The evaluation included a review to check for deviations from the descriptions provided in the Updated Safety Analysis Report (USAR) for features intended to mitigate the potential for flooding from external factors.

As part of this evaluation, the inspectors checked for obstructions that could prevent draining, and determined that barriers required to mitigate the flood were in place and operable. Additionally, the inspectors performed a walkdown of the protected area to identify any modification to the site which would inhibit site drainage during a probable maximum precipitation event or allow water ingress past a barrier. The inspectors also reviewed the abnormal operating procedure for mitigating the design basis flood to ensure it could be implemented as written. Documents reviewed are listed in the to this report.

This inspection constituted one external flooding sample as defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • component cooling water system - train B; and

The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, USAR, TS requirements, condition reports (CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions.

The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program (`)

with the appropriate significance characterization. Documents reviewed are listed in the to this report.

These activities constituted two partial system walkdown samples as defined in IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Routine Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:

  • fire zone TU-95B, 480-volt switchgear, bus 1-61 and 1-62 room;
  • fire zone TU-70A, screen house;
  • fire zone TU-70B, screen house; and
  • fire zone TU-90, 1A diesel generator room.

The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded, or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP. Documents reviewed are listed in the Attachment to this report.

These activities constituted four quarterly fire protection inspection samples as defined in IP 71111.05-05.

b. Findings

No findings of significance were identified.

1R06 Flooding

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors reviewed flood analyses and design documents, including the USAR, engineering calculations, and abnormal operating procedures to identify licensee commitments. The specific documents reviewed are listed in the to this report. In addition, the inspectors reviewed licensee drawings to identify areas and equipment that may be affected by internal flooding caused by the failure or misalignment of nearby sources of water, such as the fire suppression or the circulating water systems. The inspectors also reviewed the licensees corrective action documents with respect to past flood-related items identified in the CAP to verify the adequacy of the corrective actions. The inspectors performed a walkdown of the following plant area to assess the adequacy of watertight doors and verify drains and sumps were clear of debris and were operable, and that the licensee complied with its commitments:

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b. Findings

Potential Debris Sources Could Clog a Drain Credited During Internal Floods

Introduction:

A finding of very low safety significance and associated NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified by the inspectors for the failure to translate the flooding design basis into specifications, procedures, and instructions. Specifically, the licensee failed to control the storage of material that could potentially clog a floor drain credited in the flood analysis and located in the Bus 1 and 2 switchgear room.

Description:

The inspectors reviewed the licensees flooding analysis and its design features to prevent and mitigate the consequences of internal flooding during the first quarter of 2009. After the review, the inspectors walked down the steam generator blowdown tank (SGBT) room on March 7, 2009, to look for any possible deficiencies.

The inspectors identified multiple sources of debris including an unsecured storage drum of new filters and a clear poly bag containing rope, multiple pieces of anti-contamination clothing, and rubber gloves. The inspectors had noted, during their flooding basis review, that the floor drain in the adjacent Bus 1 and 2 switchgear room was credited for removing water during a flood scenario that originated in the SGBT room, and concluded that the debris could clog the drain during a flooding event. The inspector informed the control room of their concern, and the licensee removed or secured the items of concern.

The inspectors reviewed calculation 2005-05708, Internal Flood Levels Due to Postulated Ruptures in General Lines in the Auxiliary Building. The calculation credited the Bus 1 and 2 switchgear room floor drain and contained a discussion that emphasized the need for the floor drain to be open and free flowing. The calculation further stated that if the drain becomes blocked the results for that case were no longer valid. The inspectors also found that this calculation was referenced in the USAR to evaluate flooding sources that originated in the auxiliary building, from which, worst case scenarios were used to develop flood protection strategies and indicated the maximum flood height for the auxiliary building basement was 6 inches. The inspectors asked the licensee what the new auxiliary building flood heights would be without crediting the Bus 1 and 2 floor drain. The licensee performed an analysis where the floor drain was not credited and determined that the new flood height was 7.3 inches instead of the original 6 inches. The licensee verified that no additional components in the auxiliary building were affected that were not already analyzed in the original calculation.

The inspectors reviewed the new analysis and identified that the licensee had failed to assess the impact on equipment in safeguards alley where the barrier protecting safeguards alley from the floor was only 7 inches high. The safeguards alley flood zone (5B) contains all three of the licensees AFW pumps and both trains of the safety-related 480-volt switchgears. The licensee subsequently performed an additional analysis and found that the water added from removing the credited floor drain from the flooding scenario filled the trench in safeguards alley and covered the floor to a depth of approximately a tenth of an inch, however, no equipment was affected.

Analysis:

The inspectors determined that the failure to properly control the storage of material that could potentially clog the credited floor drain in the Bus 1 and 2 switchgear room was a performance deficiency. The inspectors determined that the performance deficiency was more than minor in accordance with IMC 0612, Appendix B, Issue Disposition Screening, dated December 4, 2008, because it was associated with the Mitigating Systems Cornerstone attribute of Protection Against External Events and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the licensee did not put adequate controls in place to ensure that the drain would perform its credited function to be open and free flowing during a flooding scenario involving a break of a 4-inch condensate line.

The inspectors determined the finding could be evaluated using the SDP in accordance with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of findings, Table 4a for the Mitigating Systems Cornerstone, dated January 10, 2008. The significance of the finding was determined to be of very low safety significance (Green) because the inspectors answered no to all of the questions in the Mitigation Systems Cornerstone column.

The inspectors did not identify a cross-cutting aspect associated with this finding because the controls should have been implemented when calculation 2005-05708 was completed and incorporated in the flooding design basis in 2005, therefore this issue was not reflective of current performance.

Enforcement:

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that measures be established to assure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, procedures, and instructions.

Contrary to the above, when the licensee incorporated calculation 2005-05708 into its flooding design basis and implemented flooding mitigation strategies, the licensee failed to translate the flooding design basis into specifications, procedures, and instructions to control the storage of material that could potentially clog the credited floor drain in the Bus 1 and 2 switchgear room. The licensee immediately removed or secured the items of concern and has planned long-term corrective actions to update the controls in their station housekeeping procedure. Because this violation was of very low safety significance, and it was entered into the licensees CAP as CR 325836 and CR 327802, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000305/20090002-01).

1R07 Annual Heat Sink Performance

.1 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed the licensees testing of turbine building fan coil unit heat exchangers to verify that potential deficiencies did not mask the licensees ability to detect degraded performance, to identify any common cause issues that had the potential to increase risk, and to ensure that the licensee was adequately addressing problems that could result in initiating events that would cause an increase in risk. The inspectors reviewed the licensees observations against acceptance criteria, the correlation of scheduled testing and the frequency of testing, and the impact of instrument inaccuracies on test results. Inspectors also verified that test acceptance criteria considered differences between test conditions, design conditions, and testing conditions. Documents reviewed are listed in the Attachment to this report.

This annual heat sink performance inspection constituted one sample as defined in IP 71111.07-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On February 3 and February 10, 2009, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.

The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk significant system:

The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structure, system, and component (SSC)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly maintenance effectiveness sample as defined in IP 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • emergent equipment deficiencies during the week of January 4-8, 2009;
  • feedwater pump seal water controller maintenance;
  • notice of enforcement discussion for emergency diesel fuel volume;
  • component cooling water pump and valve test - train A.

These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Documents reviewed are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted five samples as defined in IP 71111.13-05.

b. Findings

Inappropriate Application of a Dedicated Operator During a CCW Surveillance

Introduction:

A finding of very low safety significance (Green) and associated NCV of 10 CFR 50.65(a)(4) was identified by the inspectors for the failure to properly assess risk that resulted from risk significant maintenance being performed on the CCW system, when the licensee inappropriately applied criteria for the use of a dedicated operator to meet availability requirements.

Description:

While assessing daily risk and maintenance activities for March 11, 2009, the inspectors noted that procedure SP-31-168A, Train A Component Cooling Pump and Valve Test - IST, Revision 15, was performed, yet did not contribute to the daily risk. The inspectors inquired about the basis for not including the test in the daily risk and were informed that the procedure contained steps for a dedicated operator to be stationed locally to accomplish tasks necessary to assure availability of the system.

The inspectors reviewed procedure SP-31-168A to assess the controls that allowed the system to be considered available for risk management purposes. Procedure SP-31-168A required the operator to be stationed locally, for the control room operator and the dedicated local operator to establish communications, for the local operator to be in possession of directions necessary to accomplish system restoration in the event of a need, and for the unit supervisor to provide the restoration order.

The inspectors reviewed the guidance contained in NRC-endorsed industry guidance NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the definition of Unavailability, SSC. This definition states that SSCs out-of-service for testing are considered unavailable, unless the test configuration is automatically overridden by a valid starting signal, or the function can be promptly restored either by an operator in the control room or by a dedicated operator stationed locally for that purpose. Restoration actions must be contained in a written procedure, must be uncomplicated (a single action or a few simple actions), and must not require diagnosis or repair. Credit for a dedicated local operator can be taken only if (s)he is positioned at the proper location throughout the duration of the test for the purpose of restoration for the train should a valid demand occur. The intent of this paragraph is to allow licensees to take credit for restoration actions that are virtually certain to be successful (i.e., probability nearly equal to 1) during accident conditions.

The inspectors concluded that the criteria requiring that the system be promptly restored either by an operator in the control room or by a dedicated operation stationed locally for that purpose was not met because the procedure used the unit supervisor to recognize the condition and provide the order for restoration, a control room operator to communicate the order to the local dedicated operator, and the local dedicated operator to restore the condition. The inspectors noted that the licensee considered the fact that the procedure established communications between the control room operator and the dedicated operator would be sufficient to afford a high degree of certainty that system restoration would be completed if necessary. The inspectors disagreed because the control room operator was not dedicated and could be called to other tasks during an emergency, the procedure did not establish a requirement that the unit supervisor remain at the controls during the performance of the test, and the procedure did not establish requirements to ensure the reliability of the communications equipment.

Additionally, the procedure was deficient because in the event on an emergency where the control room operator or unit supervisor may be needed to perform other tasks, it did not institute a requirement to restore the system alignment prior to performing those tasks.

The inspectors also concluded that the criterion requiring that restoration actions . . .

must not require diagnosis or repair was also not met because the procedure did not provide guidance specifying which indication or alarm would require the initiation of restoration actions. The inspectors interviewed operations department management to ascertain their understanding of expectations and the indications that the unit supervisor would use to make a decision for restoration. Operations management indicated that there could be multiple conditions that may require a restoration decision and that the unit supervisor would know when to make a restoration order. The inspectors concluded that without a singular alarm or indication that keyed the restoration decision, diagnosis of the systems actual performance would be required.

Regarding the single operator requirement, the inspectors concluded that, if a remote operator were utilized to recognize and communicate restoration criteria for an operator stationed at the restoration site locally in the field, the remote operator must be equally as dedicated. That is to say, the remote operator should be dedicated and have procedural guidance defining restoration criteria; that the procedurally defined criteria do not require diagnosis or repair, that guidance existed (training, procedural, pre-job brief, etc.) which defined the elements necessary for communications activities; and that reliable and redundant communications methods had been verified to be functional (either by routine surveillance or through a pre-job test), all prior to the performance of the task. Additionally, if the remote or performing operators were the control room operator and was not dedicated, then the control room operator must have restoration criteria that need to be performed prior to the performing/assuming alternate duties. The inspector found that the licensee did not identify any restoration criteria for the control room operator as part of the procedure, training, or as part of the pre-job briefing for the activity.

The inspectors asked the licensee to provide the risk information necessary to understand the significance of the activity if a dedicated operator were not credited for immediate restoration. Using the approved risk model in effect during the performance of the surveillance the licensee indicated that the risk, which was modeled as green at 4.30E-5, would have been at 1.15E-4, yellow.

The inspectors noted that this issue will require a historic review by the licensee and may impact out-of-service times for systems that input into both the maintenance rule and performance indicators. Additionally, the licensees misunderstanding of the requirements necessary to credit availability for a dedicated operator may extend into other procedures. Therefore, the inspectors concluded that the impact of the misapplication of maintenance rule guidance relative to out-of-service times for systems on both performance indicators and maintenance rule availability will be considered an unresolved item (URI) pending a review of the licensee corrective actions and extent-of-condition reviews for this issue (URI 05000305/2009002-02).

Analysis:

The inspectors concluded that the incorrect designation of an operator as dedicated to credit availability was a performance deficiency warranting further review.

The issue was more than minor in accordance with IMC 0612, Appendix B, Issue Disposition Screening, dated December 4, 2008, because the licensees risk assessment for March 11, 2009, failed to consider the CCW unavailable during maintenance. Specifically, the failure to account for the unavailability of CCW resulted in an inadequate daily risk assessment and could affect unavailability time of this system in related performance and maintenance rule indicators.

Although CCW affected both Mitigating Systems and Initiating Events Cornerstones the inspectors evaluated this system against the initiating events indicator because a loss of the redundant train of this system at 100 percent power, the plant condition when the performance deficiency was identified, could cause a plant transient and potentially lead to a reactor coolant pump seal failure. The inspectors evaluated the finding using the SDP in accordance with IMC 0609, Significance Determination Process, Attachment K, Maintenance Risk Assessment and Risk Management Significance Determination Process, dated May 19, 2005, and determined the issue screened as having very low safety significance (Green), because the incremental conditional core damage probability was less than 1E-6 due to the test condition lasting only four hours.

The inspectors determined that the finding had a cross-cutting aspect in the CAP component of problem identification and resolution, because the licensee failed to thoroughly evaluate a prior problem such that the resolution addressed the causes and extent of conditions necessary to preclude this event. Specifically, in September 2008, CR108628 identified that emergency core cooling system unavailability may not be properly counted during surveillance testing because of the licensees misinterpretation of the requirements for crediting availability through the use of dedicated operators. As a result of this issue, the licensee submitted a frequently asked question (FAQ) related to crediting availability through the use of dedicated operators for the mitigating systems performance indicator. The licensee subsequently recognized in a corrective action related to this condition report, CA 129337, issued February 20, 2009, that prior use of the dedicated operator and not counting the unavailability in the performance indicator data submittal was inappropriate and acknowledged that the prior occurrences where the use of a dedicated operator was credited was unacceptable. Therefore, the licensee withdrew the FAQ from review and indicated that the performance indicator data would be corrected to accurately reflect the unavailability. However, the licensee limited their immediate corrective actions to the issue associated with the performance indicator reporting requirements and failed to institute corrective actions to assess the extent of condition of the problem or institute barriers to prevent similar occurrences (P.1(c)).

Enforcement:

10 CFR 50.65(a)(4) states, in part, that before performing maintenance activities the licensee shall assess and manage the increase in risk that may result form the proposed maintenance activity. Contrary to this requirement, on March 11, 2009, the licensee failed to properly assess and manage risk when availability credit was taken for a dedicated operator who did not meet the allowance criteria for being considered dedicated; this resulted in the licensee not accounting for risk significant maintenance being performed on the CCW system in the daily risk management profile.

The licensee entered this issue into its corrective action program as CR 326625. The licensee immediately issued a shift order to curtail the use of dedicated operators until an evaluation of their use was completed. Corrective actions planned include a review of all procedures crediting the use of a dedicated operator against the endorsed NUMARC guidance. Because this violation was of very low safety significance and it was entered into the licensees corrective action program, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000305/2009002-03).

1R15 Operability Evaluations

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • crack identified in reactor coolant pump shaft;
  • safeguards light causes short;
  • safety injection pump control room pressure indicator malfunction; and
  • component cooling water - HELB.

The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and USAR to the licensees evaluations, to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the to this report.

This operability inspection constituted five samples as defined in IP 71111.15-05

b. Findings

Multiple CCW Pipes in Close Proximity to High Energy Feedwater Lines

Introduction:

The inspectors identified a unresolved item relating to the identification of multiple CCW pipes in close proximity to a high energy feedwater line.

Description:

During a CCW system alignment walkdown, the inspectors identified a location where the steam supply pipe to the turbine-driven AFW pump and multiple CCW pipes, including the CCW line to the surge tank, were routed in close proximity to a 16 inch feedwater line. The inspectors noted that the USAR, under Chapter 10A, Postulated Pipe Failure Analysis, stated where high-energy pipes were routed in the vicinity of structures and systems necessary for safe shutdown of the nuclear plant, a small break in the piping system would be postulated.

However, the licensee informed the inspectors that the HELB basis was being updated and that there would no longer be a need to postulate cracks in that area of feedwater piping, based on vendor calculations that had been performed. The licensee provided the inspectors a 2005 extent-of-condition documentation sheet that described the concern of the CCW lines being in close proximately to the feedwater line. The document also restated, that under vendor calculation KNPP-205614-P01, Kewaunee would no longer be required to postulate a break or a crack in that area of piping.

The inspectors reviewed the licensing basis for HELB and found that Kewaunee did not fall under the requirements of the NRCs Standard Review Plan, which allowed for analyzing potential stresses in high energy pipes that if found low enough would preclude the licensee from postulating cracks near safe shutdown equipment. The licensee did fall under the requirements of a letter sent to the licensee in 1972 by the Atomic Energy Commission, (the Giambusso letter - signed by NRC staff member, Mr. A. Giambusso). The letter stated that where high-energy pipes were routed in the vicinity of structures and systems necessary for safe shutdown of the nuclear plant, a crack in the piping system would be postulated.

The licensee performed an evaluation for the steam supply to the turbine-driven AFW pump and the CCW lines and found that they would not be affected by a feedwater pipe crack. The licensee, after further reviewing its HELB basis, stated that the CCW system may not be required for safe shutdown during a HELB. The inspectors reviewed the licensees list of systems required after a feedwater break and found that CCW was not listed as a required system. The inspector subsequently reviewed the licensees Appendix R Design Description for Safe Shutdown and found that CCW was listed as a required system for safe shutdown to hot shutdown. Specifically, CCW was required to perform reactivity and inventory control functions to support hot shutdown operations. The inspectors concluded that these functions were necessary for hot shutdown regardless of the initiating event. Therefore the inspectors could not validate the licensees assertion that CCW may not be required to support HELB.

The licensee is currently updating its HELB basis and this item will remain unresolved until the licensee completes this effort and can determine whether CCW should have been included in the systems required for safe shutdown after a HELB (URI 05000305/2009002-04).

1R19 Post-Maintenance Testing

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:

  • test of RHR pump B supply valve (RHR-400B); and

These activities were selected based upon the SSCs ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TSs, the USAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to verify that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted four post-maintenance testing samples as defined in IP 71111.19-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • reactor protection logic train B test;
  • motor-driven AFW pump A full flow test- Inservice Testing (IST);
  • seismic monitor surveillance test;
  • emergency diesel air system pressure prop test;
  • containment pressure instrument channel test.

The inspectors observed in-plant activities, reviewed procedures, and associated records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
  • were acceptance criteria clearly stated, did they demonstrate operational readiness, and were they consistent with the system design basis;
  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the USAR, procedures, and applicable commitments;
  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
  • test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers (ASME) code, and reference values were consistent with the system design basis;
  • where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
  • where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
  • where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
  • prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
  • equipment was returned to a position or status required to support the performance of its safety functions; and
  • all problems identified during the testing were appropriately documented and dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted three routine surveillance testing samples, one inservice testing sample, one reactor coolant system leak detection inspection sample, and one containment isolation valve sample as defined in IP 71111.22, Sections -02 and -05.

b. Findings

(i) Emergency Diesel Generator (EDG) Air System May Not Be Appropriately Qualified
Introduction:

The inspectors identified an unresolved item associated with the qualification of the EDG air start system. Specifically, the EDG starting air compressors were previously qualified Quality Assurance (QA) level 1 (QA-1) and may have been inappropriately downgraded to QA-2.

Description:

While reviewing of procedure OP-KW-OSP-DGE-006B, Diesel Generator B Start-up Air Leakage Test, the inspectors noted that the air receivers also supply controlling air to the ventilation dampers in the diesel rooms. Because the dampers and starting air were supplied from the system, the inspectors reviewed the calculations for the capacity of the air receivers and assessed the design basis of the associated air compressors.

The design of the system consisted of a normal and a spare bank of air receivers and an associated air compressor for each diesel generator. The air receivers for each diesel had the capability of be interconnected both to the designated diesel and to the alternate diesel. Additionally, procedures and equipment existed to interface the diesel air system with the station instrument air system through the use of hoses stationed locally for this purpose.

The inspectors reviewed the calculation for the diesel air receivers and found that the capacity of the receivers supported five start sequences of the diesel and had enough additional capacity to run the ventilation dampers for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors noted that with this capacity the safety-related air receivers, even if interconnected, could not support the diesel generator for the seven days needed to meet the TS fuel oil mission time. The inspectors also reviewed station documentation to ascertain the diesel generator mission time, but were unable to find any information to support a specific interval. Because the air receivers were only designed to support 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of operation without replenishment, the inspectors reviewed the qualifications of the supporting air compressors. The inspectors found that the air compressors, piping, and related power was, at one time, all classified as both seismic and QA-1; however, the compressors had been downgraded to QA-2 due to replacement part issues.

The inspectors asked the licensee to provide the design basis supporting the lower qualification of the air compressors and the acceptability of the design. The licensee entered this issue into its corrective action program as CR 326432, Missing Design and Licensing Basis for EDG Start Up Air System. This CR and associated operability determination supported the immediate operability assessment of the diesel generator; however, related prompt operability assessments were in-progress at the close of the inspection period. The inspectors considered this issue unresolved pending review of the licensees assessment and/or reconstitution of the related licensing basis and operability evaluation (URI 05000305/2009002-05).

(ii) Seismic Monitoring System Repeatedly Fails Surveillance
Introduction:

An unresolved item was identified by the inspectors for the inability of the seismic monitoring system to be maintained operable and support entry into the emergency plan.

Description:

While performing a plant status review of the relay room, the inspectors noticed that the seismic monitoring system was tagged as needing repair on multiple components, including the recording chart. Because this instrument was a TS-required instrument, it was used to determine reporting requirements for declaration of an unusual event, and its chart may be a necessary backup to assess reporting elements, the inspectors elected to review the next surveillance performed on the system.

The licensee performed SP-87-133, Seismic Monitoring System Calibration and Functional Test, Revision I, for seismic monitoring on January 8, through February 3, 2009. During the performance of the related surveillance, the two channels for horizontal motion had alarm triggers which were found to be non-conservatively out-of-specification. The inspectors reviewed the related data and determined that the instrument started performing erratically in 2005; with all of the trigger cards were found out-of-specification during the 2005 and 2007 surveillance tests.

The inspectors assessed the licensees instrumentation calibration practices and found that the licensee did write a CR when instrumentation was found out of specification; did not re-zero instruments to a reference value unless the instrument was found out of specification; did not consider replacing an instrument until the instrument experienced three consecutive failures; and did not trend instrument set-point data to assess the predictability of instrument failures.

The inspectors concluded that the seismic monitor failure was predictable and that the lack of a program to monitor instrument performance contributed to the failure. Because the instrument failure was predictable, the inspectors concluded that the ability of the licensee to use the seismic monitor as a reliable method to assess and enter the emergency plan was impaired, and that for some period of time during the calibration interval, the related instruments were inoperable.

Additionally, the surveillance procedure indicates reliance on the Point Beach Generating Station seismic monitors when the Kewaunee instruments were out-of-service. The inspectors did not review the Point Beach instrument outages to assess if there may have been periods when the Kewaunee seismic monitor were inoperable coincident with the Point Beach instrument.

The fact that the alarm cards for both operating and design basis earthquakes of the instrument were found out-of-specification in the non-conservative direction, during the last three surveillance tests, called into question the stations ability to ensure that the reporting requirements would be able to be met nor the applicable response plant equipment procedures would be entered in the event of an earthquake.

Because this issue is similar to the issue identified in September 2008 (AV 2008503-01)where radiation instrumentation was found to be incapable of supporting entry into the emergency plan, the inspectors are considering this as an unresolved item pending review during the inspection of the radiation instruments in June 2009 (URI 05000305/2009002-06).

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

.1 Training Observation

a. Inspection Scope

The inspector observed a simulator training evolution for licensed operators on March 10, 2009, which required emergency plan implementation by a licensee operations crew. This evolution was planned to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that the licensee evaluators noted the same issues and entered them into the corrective action program. As part of the inspection, the inspectors reviewed the scenario package and other documents listed in the Attachment to this report.

This training inspection constituted one sample as defined in IP 71114.06-05.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Review of Licensee Performance Indicators (PIs) for the Occupational Exposure

Cornerstone

a. Inspection Scope

The inspectors reviewed the licensees Occupational Exposure Control Cornerstone performance indicator to determine whether the conditions resulting in any PI occurrences had been evaluated and whether identified problems had been entered into the licensees CAP for resolution.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.2 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors assessed the adequacy of the licensees internal dose assessment process for internal exposures in excess of 50 millirem committed effective dose equivalent. There were no internal exposures greater than 50 millirem committed effective dose equivalent.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors also reviewed the licensees physical and programmatic controls for highly activated and/or contaminated materials (non-fuel) stored within the spent fuel pool or other storage pools.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.3 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed a sample of the licensees self-assessments, audits, Licensee Event Reports (LERs), and Special Reports related to the access control program to verify that identified problems were entered into the CAP for resolution.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors reviewed corrective action reports related to access controls and any high radiation area radiological incidents (issues that did not count as PI occurrences identified by the licensee in high radiation areas less than 1 Roentgen/hour. Staff members were interviewed and corrective action documents were reviewed to verify that follow-up activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk based on the following:

  • initial problem identification, characterization, and tracking;
  • disposition of operability/reportability issues;
  • evaluation of safety significance/risk and priority for resolution;
  • identification of repetitive problems;
  • identification of contributing causes;
  • identification and implementation of effective corrective actions;
  • resolution of NCVs tracked in the corrective action system; and
  • implementation/consideration of risk significant operational experience feedback.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors evaluated the licensees process for problem identification, characterization, and prioritization and verified that problems were entered into the CAP and resolved. For repetitive deficiencies and/or significant individual deficiencies in problem identification and resolution, the inspectors verified that the licensees self-assessment activities were capable of identifying and addressing these deficiencies.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.4 Job-In-Progress Reviews

a. Inspection Scope

The inspectors reviewed radiological work in high radiation work areas having significant dose rate gradients to evaluate whether the licensee adequately monitored exposure to personnel and to assess the adequacy of licensee controls. These work areas involved areas where the dose rate gradients were severe; thereby, increasing the necessity of providing multiple dosimeters or enhanced job controls.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.5 High Risk Significant, High Dose Rate, High Radiation Area and Very High Radiation

Area Controls

a. Inspection Scope

The inspectors held discussions with the Radiation Protection Manager concerning high dose rate, high radiation area, and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection, in order to assess whether any procedure modifications substantially reduced the effectiveness and level of worker protection.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors discussed with radiation protection supervisors the controls that were in place for special areas of the plant that had the potential to become very high radiation areas during certain plant operations. The inspectors assessed if plant operations required communication beforehand with the radiation protection group, so as to allow corresponding timely actions to properly post and control the radiation hazards.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors conducted plant walkdowns to assess the posting and locking of entrances to high dose rate, high radiation areas, and very high radiation areas.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified

.6 Radiation Worker Performance

a. Inspection Scope

The inspectors reviewed radiological problem reports for which the cause of the event was due to radiation worker errors to determine if there was an observable pattern traceable to a similar cause and to determine if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. Problems or issues with planned or completed corrective actions were discussed with the Radiation Protection Manager.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.7 Radiation Protection Technician Proficiency

a. Inspection Scope

The inspectors reviewed radiological problem reports for which the cause of the event was radiation protection technician error to determine if there was an observable pattern traceable to a similar cause and to determine if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Mitigating Systems Performance Index (MSPI) - Emergency Alternating Current (AC)

Power System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Emergency AC Power System PI for the first quarter through the fourth quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, MSPI derivation reports, issue reports, event reports, and NRC Integrated Inspection Reports to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI emergency AC power system sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.2 MSPI - High Pressure Injection Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - High Pressure Injection Systems PI for the first quarter through the fourth quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports, event reports, and NRC Integrated Inspection Reports to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI high pressure injection system sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.3 MSPI - Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for the first quarter through the fourth quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports, MSPI derivation reports, and NRC Integrated Inspection Reports to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the to this report.

This inspection constituted one MSPI heat removal system sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.4 MSPI - RHR System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal System performance indicator for the first quarter through the fourth quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports, event reports, and NRC Integrated Inspection Reports to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI residual heat removal system sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.5 MSPI - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems performance indicator for the first quarter through the fourth quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports, event reports, and NRC Integrated Inspection Reports to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one MSPI cooling water system sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

.1 Routine Review of Items Entered Into the CAP

a. Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily CAP Reviews

a. Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily CR packages.

These daily reviews were performed by procedure as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings of significance were identified.

.3 Selected Issue Follow-Up Inspection: Service Water Pump Circuit Breaker Failure

Leads to an Assessment of Breaker Problems

a. Scope

During a review of items entered in the licensees CAP, the inspectors found two recent corrective action items documenting service water pump breaker failures. The inspectors selected CR318324, SW [service water] Pump A1 Red Run Indication Not Lit in Control Room, dated December 29, 2008, for review. The inspectors found that the licensee had, as a result of this issue and other recent issues, identified a negative trend in breaker-performance. As a result of this issue the licensee performed an operational decision making (ODM) evaluation on breaker issues, ODM000079. This ODM identified several follow-on assignments to improve breaker performance. Activities proposed included procedural enhancements, strategies for rotating breakers, developing a breaker maintenance history tracking system, performing a circuit breaker self-assessment, and consulting with a breaker maintenance expert to improve overall breaker maintenance practices and performance. The inspectors concluded that the magnitude and types of historical failures observed on both 4160 and 480 volt safety-related circuit breakers warranted a future review to assess the effectiveness of the implemented corrective actions. The inspectors reviewed the related documentation and found that the licensee had scheduled an effectiveness review, CA126142, for this issue.

This review constituted one in-depth problem identification and resolution sample as defined in IP 71152-05.

b. Findings

No findings of significance were identified.

.4 Selected Issue Follow-Up Inspection: CCW Surge Tank Level Transmitter Calibration

Failures

a. Scope

During a review of items entered in the licensees CAP, the inspectors found recent corrective action items documenting repetitive occurrences where LT-618, the CCW surge tank level transmitter, was found out of calibration during the performance of ICP-31-01, CC - Surge Tank Level Loop 618 Calibration. The inspectors reviewed the adequacy of the corrective actions and assessed the licensees instrumentation calibration practices.

This review constituted one in-depth problem identification and resolution sample as defined in IP 71152-05.

b. Observations The inspectors concluded that level transmitter failures were predictable based on the recurring frequency. The inspector also found that transmitter output is a QA-2 function and that alternate methods for identifying changes to the CCW system water level were available. The licensee replaced the transmitter during the week of March 30, 2009.

No findings of significance were identified.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 Notice of Enforcement Discretion (NOED)

a. Inspection Scope

The licensee submitted an oral request for enforcement discretion for TS 3.7.a.7, Auxiliary Electrical Systems, on January 23, 2009. The licensee requested enforcement discretion for a 14-day period until a license amendment request to change TS 3.7.a.7 could be submitted and approved. This request was for not meeting the required 35,000 gallons of fuel oil available to either diesel generator. The NRC staff granted approval during a teleconference with the licensee, on January 23, at approximately 3:42 p.m. The licensee sent a follow-up letter on January 27, 2009.

On January 23, 2009, during a teleconference with the NRC, the licensee declared the siphon line that connects the two underground fuel oil storage tanks for the diesel generators inoperable. With the siphon line inoperable and neither storage tank capable of providing at least 35,000 gallons of fuel, Kewaunee could not meet the requirement to supply at least 35,000 gallons of fuel to an EDG. With the condition of Kewaunee not being able to provide 35,000 gallons of fuel to either EDG, both EDGs would be inoperable. Technical Specification 3.7.b.7 requires that if two EDGs are inoperable for more than two hours, then Kewaunee must initiate action within one hour to achieve Hot Standby within the next six hours. As the result of additional specifications that applied, the licensee entered TS 3.0.c, which directs that actions be initiated within one hour to place the unit in a mode in which the specification does not apply by placing it, as applicable, in at least hot standby within the next six hours, hot shutdown within the following six hours, and cold shutdown within the subsequent 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. The one hour action time expired at 2:58 p.m.; the licensee entered its shutdown procedure at 2:45 p.m. and the NOED was granted at 3:42 p.m. Although preparations were made to shutdown, no reactivity manipulations were performed. The NOED was used until 3:15 p.m. on February 6, 2009, at which time License Amendment No. 203 was approved by the NRC. The amendment provided fuel oil storage requirements that would provide for a 7-day supply of fuel to either EDG without credit for the siphon line connection between the two underground tanks.

Prior to approval for granting the NOED, the inspectors (from the site, headquarters and the region) reviewed the licensees basis for the NOED in accordance with Regulatory Information Summary RIS 2005-01, Changes to NOED Process and Staff Guidance.

The inspectors also reviewed the scheduled work activities, environmental conditions, compensatory actions planned, and the sites readiness to implement the NOED. Prior to and during the period when the NOED was in effect, the inspectors verified that the licensee appropriately managed plant risk and that the licensee implemented the compensatory measures identified during the telephone call that verbally granted the NOED. The review of these items is also documented in the NRC approval letter for NOED 09-3-01, dated January 29, 2009.

b. Findings

There were no findings related to the NOED implementation. There was one finding related to the cause of the siphon line inoperability which is discussed below in section 4OA3.2, Siphon Line Which Interconnected Two Diesel Generator Emergency Fuel Oil Storage Tanks Was Not Functioning as Designed.

.2 (Closed) URI 05000305/2008003-03, Siphon Line Which Interconnected Two Diesel

Generator Emergency Fuel Oil Storage Tanks Was Not Functioning as Designed

a. Inspection Scope

Inspection Report (IR) 05000305/2008003 identified a URI associated with the EDG fuel oil storage tank design and licensing basis following the licensee issuing event notification (EN) EN#44182. This EN stated that a siphon line interconnecting the two EDG emergency fuel oil storage tanks was not functioning as designed. The purpose of the siphon line, as part of EDG fuel oil system, was to feed fuel oil from either storage tank to the adjacent tank; thereby, interconnecting the tanks such that both EDGs had access to fuel from both tanks.

The inspectors reviewed the licensing basis of the EDG fuel oil system as described in the TSs, USAR and other licensing basis documents. This review included consideration of seismic, single failure, and fuel oil storage volume requirements. The inspectors concluded that the siphon line was part of the current licensing basis (CLB).

However, the licensees position was that the siphon line was not part of the CLB.

b. Findings

Introduction:

A finding of very low safety significance (Green) and associated Severity Level IV, NCV of 10 CFR 50.59 was identified by the inspectors.

Description:

On April 30, 2008, with the reactor shutdown, the licensee identified that the siphon line was malfunctioning. Subsequently, the licensee established a procedure and a temporary modification to enable transfer of fuel oil from one storage tank to the other in the event that one of the safety-related installed pumps was not available. The inspectors noted that the temporary modification was not safety-related, was not seismically qualified, consisted of commercial grade components, and was not stored in a seismically controlled location.

The inspectors review of the CLB identified that the licensees safety analysis report from May 12, 1972, described the use of the siphon line to provide for a total of over 7 days of fuel for both EDGs. This was acknowledged by the NRC in its May 10, 1973, safety evaluation (Kewaunees operating license was issued in December 1973). In an update to the USAR dated July 20, 1993, the licensee identified that the siphon line was not working and removed reference to it in the USAR, stating incorrectly that its inoperability did not adversely affect plant safety. The removal of this reference was accomplished by referencing elements of a ASME code relief request that had not been incorporated into the licensing basis for this purpose. The inspectors reviewed the related change request and concluded that USAR change request, UCR 93-031, inappropriately answered question Number 3, Could the change increase the probability of occurrence of a malfunction of equipment important to safety previously evaluated in the UASR? as No. Specifically, the licensee should have determined that the proposed activity degraded the SSC reliability because the activity reduced system/equipment redundancy or independence. As a result of the inappropriate assumption, the licensee did not submit a license amendment request as required by 10 CFR 50.59.

The inspectors also noted that with the siphon line inoperable and loss of one of the transfer pumps in either of the tanks, there would not be a 7-day supply of fuel oil to one of the EDGs during a postulated accident. Discussions with the licensee indicated that the problem with the siphon line that occurred on April 30, 2008, was related to the problem mentioned in the1993 submittal to the NRC that the line was not working and reflected a problem with the siphon line that has existed since initial plant operations.

The inspectors attributed the identification of the problem in April to the strong questioning attitude of new plant staff.

Analysis:

The inspectors determined that the licensees failure to perform a proper 10 CFR 50.59 was a performance deficiency warranting further review. Because violations of 10 CFR 50.59 are considered to be violations that potentially impede or impact the regulatory process, they are dispositioned using the traditional enforcement process. As described in Supplement I of the Enforcement Policy, to determine the severity of a 10 CFR 50.59 violation, the underlying technical issue was evaluated under the SDP.

The inspectors evaluated the finding using the SDP in accordance with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of Findings, Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008. The inspectors answered yes to Question 2 in the Mitigation System Cornerstone column, which required the issue to be evaluated in accordance with Appendix A, of IMC 0609. Using Appendix A, the inspectors screened the issue as very low safety significance (Green) because the quantity of fuel to the diesel generators that was historically available always exceeded that needed for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of operation, thereby, resulting in the probabilistic risk assessment (PRA) function for the diesels being met.

The inspectors determined that the issue had a cross-cutting aspect in problem identification and resolution, Corrective Action Program, because the licensee had identified similar deficiencies with accurately applying or interpreting the CLB, since June 2005 (IRs 2005008, 2005011, 2006004, 2006016, and 2007002), and failed to take timely action to complete corrective actions, or establish barriers to prevent recurrence of this deficiency (P.1(d)),

Enforcement:

10 CFR 50.59(a)(1) states in part, that the licensee may make changes in the facility as described in the final safety analysis report without prior Commission approval unless the proposed change involves an unreviewed safety question.

10 CFR 50.59(a)(2) states, in part, that a proposed change shall be deemed to involve an unreviewed safety question if the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased. Contrary to this, the licensee failed to obtain Commission approval via a license amendment when it incorrectly determined that the subject change did not constitute an unreviewed safety question and subsequently modified the safety analysis report.

The licensee entered this issue into its CAP as CR 321056 for evaluation and development of corrective actions, as appropriate. Because this violation was of very low safety significance and it was entered into the licensees corrective action program, this violation is being treated as a Non-Cited Severity Level IV Violation consistent with Section VI.A of the NRC Enforcement Policy (NCV 05000305/2009002-07).

.3 Follow-up of 10 CFR 50.72 Notification: Steam Exclusion Door Failure Results In

Multiple Safety Systems Being Declared Inoperable

a. Inspection Scope

The inspectors reviewed the licensee's event notifications and corrective actions for various losses of barrier integrity which impacted risk-significant and safety-related equipment. The inspectors reviewed the scope of the report, and corrective actions to determine if the station response was appropriate for each identified issue. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one sample as defined in IP 71153.

b. Findings

Introduction:

A finding of very low safety significance (Green) and associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the licensees failure to follow the CAP procedure to implement corrective actions that could have prevented a December 30, 2008, door seal failure.

Description:

Between October 30, 2008, and January 28, 2009, the licensee experienced multiple problems with hazard barriers, specifically doors providing HELB, fire, and control room exclusion boundary protection. Multiple event notifications and LERs were made associated with the problems with the doors. The inspectors noted that corrective actions for the first occurrence, LER 05000305/2008-002-00, Blocked Open Steam Exclusion Door Results in Postulated Inoperability of Safety Systems, included actions to revise surveillance procedures for critical doors and for require operations to perform a walk-down of doors identified as a single-point-vulnerability for equipment (CR 116752). Subsequent to the October 30, 2008, door failures, there have been more than five degraded door issues, including two which resulted in LERs.

In addition to the October 30, 2008, door failure, the inspectors noted that CR 117765, dated November 6, 2008, CR 117879, dated November 7, 2008, and CR 319052, dated January 7, 2009, were written for door issues and seal failures. While performing a plant walk-down, the inspectors also identified a door seal failure, which the licensee documented in CR 322644, dated January 12, 2009. The inspectors elected to assess the December 30, 2008, door failure and associated LER 05000305/2008-003-00, Door Bottom Seal Failure Results in Inoperability of Control Room Ventilation System, because it represented a second nearly identical failure to the October 30, 2008, door failure.

For the corrective actions for the October 30, 2008, failure, the inspectors noted that a new procedure to inspect doors was not scheduled to be completed until March 2, 2009, with first performance of the modified procedure due in April 2009. Because door issues continued to manifest after the issuance of the first condition report, CR 116752, the inspectors were concerned that the corrective actions may not be timely. Additionally, a prior corrective action related to a HELB single point vulnerability study that occurred in advance of the October 30, 2008, door failure had increased the inspection frequency via the use of operator rounds, but was closed without action taken (CA 077972).

Closure of CA 077972 occurred because a related corrective action, CA 072073, determined that it was inappropriate to use the 18-month surveillance as a 12-hour door inspection tool.

The inspectors reviewed licensee procedure, PI-KW-200, Corrective Action, and noted for level 1 or 2 condition reports, step 3.7.2 stated that, If the threat is continuous, implement corrective actions immediately, or implement compensatory actions to reduce the threat or mitigate the consequences. Because of the continuing door issues and because the failures impacted safety-related equipment operability, the inspectors concluded that the implementation of corrective actions was not timely nor in accordance the intent of implementing corrective or compensatory actions to remove the threat.

Specifically, the December 30, 2008, self-revealing door seal failure that caused both trains of control room ventilation to be inoperable was preventable.

Analysis:

The inspectors concluded that the failure to implement timely or effective interim corrective actions that could have prevented the December 30, 2008, self-revealing door seal failure was a performance deficiency warranting further review.

The inspectors determined that the performance deficiency was more than minor in accordance with IMC 0612, Appendix B, Issue Disposition Screening, dated December 4, 2008, because it was associated with the Barrier Integrity Cornerstone attribute of Configuration Control and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. The inspectors evaluated the finding using the SDP in accordance with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of Findings, dated January 10, 2008, and determined the finding represented a degradation of the barrier function to protect against radiological hazards, toxic gas, and smoke that required a Phase 3 analysis. A Region III Senior Reactor Analyst completed a qualitative Phase 3 analysis and determined that because the duration of the event was small, forty-four minutes, the issue screened as having very low safety significance (Green).

The inspectors determined that the finding had a cross-cutting aspect in the corrective action program component element of problem identification and resolution because the licensee failed to take appropriate corrective actions to address safety issues and adverse trends in a timely manner (P.1(d)).

Enforcement:

10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, states, in part, that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances. Kewaunee procedure PI-KW-200, Corrective Action, step 3.7.2, requires that, If the threat is continuous, implement corrective actions immediately, or implement compensatory actions to reduce the threat or mitigate the consequences. Contrary to this, the licensee failed to implement compensatory actions to preclude subsequent occurrences of similar events when corrective actions for an October 30, 2008, door seal failure were developed.

The licensee entered this issue into its CAP as CR 318446. Corrective actions implemented and planned included an apparent cause evaluation, increased monitoring of doors for potential failure mechanisms, and a scoping study to assess permanent modifications for upgrading doors that act as hazard barriers for single point vulnerabilities. Because this violation was of very low safety significance and it was entered into the licensees CAP, this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000305/2009002-08).

.4 (Closed) LER 05000305/2008-002-00: Blocked Open Steam Exclusion Door Results in

Postulated Inoperability of Safety Systems On October 30, 2008, when a technician was transiting through the door to the spent fuel pool cooling room the bottom door seal fell off and wedged the door open. This door provided a steam exclusion function and was stuck open for less than one minute.

During the time when the steam exclusion function protecting safety-related equipment in both trains was inoperable, the plant was in both an unanalyzed condition and a condition that could have prevented the fulfillment of a safety function. With the door closed, the safety function was effective. The door remained closed until it was repaired.

Section 1R15 above discusses the repetitive nature and related issues for the loss of hazard barriers. This LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

.5 (Closed) LER 05000305/2008-003-00: Door Bottom Seal Failure Results in Inoperability

of Control Room Ventilation System On December 30, 2008, when an operator was transiting through the door to the control room air conditioning room the bottom door seal fell off. This door provided a steam exclusion function and was a control room exclusion zone barrier; the door was inoperable for approximately 44 minutes until repairs were completed. During the time the doors function was impaired, the door was incapable of protecting safety-related equipment in both trains of control room emergency ventilation and the plant was in both an unanalyzed condition and a condition that could have prevented the fulfillment of a safety function. Section 1R15 above discusses the repetitive nature and related issues for the loss of hazard barriers. This LER is closed.

This event follow-up review constituted 1 sample as defined in IP 71153-05.

.6 (Closed) LER 05000305/2009-002-00: Steam Exclusion Door Blocked Open During

Maintenance Activities On January 28, 2009, contrary to procedural requirements, a door chock was utilized to hold a door to the carbon dioxide room open, thus rendering the door incapable of automatic closure if released. The door being chocked open rendered it incapable of performing its HELB function of protecting the safety-related 4160-volt switchgear. This condition lasted for approximately 15 minutes. During the time the doors function was impaired, the plant was in a condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. Section 1R15 above discusses the repetitive nature and related issues for the loss of hazard barriers.

Because the duration of the event was small this issue was considered minor. This LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

4OA6 Management Meetings

.1 Exit Meeting Summary

On April 8, 2009, the inspectors presented the inspection results to S. Scace and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

.2 Interim Exit Meetings

An interim exit was conducted for:

  • Access Control to Radiologically Significant Areas with Mr. S. Scace on January 16, 2009, and with Mr. J. Hale on February 25, 2009.

The inspectors confirmed that none of the potential report input discussed was considered proprietary.

4OA7 Licensee-Identified Violations

None.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Scace, Site Vice-President
M. Crist, Plant Manager
J. Hale, Radiation Protection Manager
C. Olson, Radiation Protection General Supervisor
M. Peroutka, Radiation Protection Supervisor
D. Shannon, Radiation Protection General Supervisor
J. Dillich, Site Engineering Director
J. Gadzala, Licensing Engineer
R. Repshas, Licensing Engineer
W. Henry, Maintenance Manager
T. Breene, Manager of Licensing
J. Madden, System and Component Engineering
K. Karr, Director Performance Improvement
D. Bouche, Nuclear Specialist
D. Lawrence, Operations Manager
S. Yuen, Programs Engineering Manager
J. Stafford, Organizational Effectiveness Manager
C. Chovan, Outage and Planning Manager
J. Palmer, Maintenance Training Supervisor
J. McNamara, Design Engineering Supervisor

Nuclear Regulatory Commission

M. Kunowski, Chief, Division of Reactor Projects, Branch 5

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

05000305/2009002-01 NCV Potential Debris Could Clog a Drain Credited During Internal Floods (Section 1R06)
05000305/2009002-02 URI Inappropriate Application of a Dedicated Operator During a CCW Surveillance (Section 1R13)
05000305/2009002-03 NCV Inappropriate Application of a Dedicated Operator During a CCW Surveillance (Section 1R13)
05000305/2009002-04 URI Multiple Component Cooling Water Pipes in Close Proximity to High Energy Feedwater Lines (1R15)
05000305/2009002-05 URI Emergency Diesel Generator Air System May Not Be Appropriately Qualified (Section 1R22)
05000305/2009002-06 URI Seismic Monitoring System Repeatedly Fails Surveillance (Section 1R22)

Attachment

05000305/2009002-07 NCV Siphon Line Which Interconnected Two Diesel Generator Emergency Fuel Oil Storage Tanks Was Not Functioning as Designed (Section 4OA3.2)
05000305/2009002-08 NCV Steam Exclusion Door Failure Results In Multiple Safety Systems Being Declared Inoperable (Section 4OA3.3)

Closed

05000305/2008-002-00 LER Blocked Open Steam Exclusion Door Results in Postulated Inoperability of Safety Systems (Section 4OA3.4)
05000305/2008-003-00 LER Door Bottom Seal Failure Results in Inoperability of Control Room Ventilation System (Section 4OA3.5)
05000305/2009-002-00 LER Steam Exclusion Door Blocked Open During Maintenance Activities (Section 4OA3.6)
05000305/2008003-03 URI Siphon Line Which Interconnected Two Diesel Generator Emergency Fuel Oil Storage Tanks Was Not Functioning as Designed (Section 4OA3.2)
05000305/2009002-01 NCV Potential Debris Sources Could Clog a Drain Credited During Internal Floods (Section 1R06)
05000305/2009002-03 NCV Inappropriate Application of a Dedicated Operator During a CCW Surveillance (Section 1R13)
05000305/2009002-07 NCV Siphon Line Which Interconnected Two Diesel Generator Emergency Fuel Oil Storage Tanks Was Not Functioning as Designed (Section 4OA3.2)
05000305/2009002-08 NCV Steam Exclusion Door Failure Results In Multiple Safety Systems Being Declared Inoperable (Section 4OA3.3)

Attachment

LIST OF DOCUMENTS REVIEWED