IR 05000293/1992028

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Insp Rept 50-293/92-28 on 921124-1231.Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Maint & Surveillance,Emergency Preparedness, Security,Safety Assessment & Quality Verification
ML20128C441
Person / Time
Site: Pilgrim
Issue date: 01/28/1993
From: Eugene Kelly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20128C415 List:
References
50-293-92-28, NUDOCS 9302040021
Download: ML20128C441 (21)


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  • 1 U. S. NUCLEAR REGULATORY COMMISSION '

REGION I

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Docket No.: 50-293 Report No.: 92 28 Licensec: Boston lkilson Company 800 Boylston Street Boston, Massachusetts 02199 Facility: Pilgrim Nuclear power Station imcation: plymouth, Massachusetts Dates: November 24 December 31,1992 Inspectors: J. Macdonald, Senior Resident inspector A. Cerne, Resident inspector D. Kern, Resident I specto Approved by: MI E. Kelly, chi f, Reactor Pr ects Section 3A ' Date Scope: Resident inspection addressed the areas of plant operations, radiological controls, maintenance and surveillance, emergency preparedness, security, safet assessment and quality verification, and engineering and technical suppor Initiatives selected for inspection included: restoration from an electrical backfeed lineup; observation of an inplant emergency preparedness drill; control and testing of certain containment isolation valves; and, plant design changes associated with the reactor vessel head spray lines, inspections were performed on backshifts during November 30 and December 1 4,7,11,1318, and 2131,1992. " Deep" backshift inspections were performed on December 13 from 10:00 to 12:00 p.m. and December 14 from 00:01 to 05:45 Findings: Inspection results are summarized in the lhecutive Summar Procedure 3.M 2-7.6, "NUMAC Log Radiation Monitor Setpoint Change

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Procedure" was not properly performed. Technicians established incorrect RPS protective setpoints and management reviews failed to identify the associated discrepancies (Violation 92-28-01, see Section 4.4).

[ The technical basis for the deactivation of a head spray line remains unresolved (Unresolved item 92-28-02, see Section 8.2).

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EXECUTIVE SUhth1ARY l

Pilgrim inspution Report .50 293/92 28 Plant Operations Operations Section preparation for and response to the effects of a northeaster storm were comprehensive. Decisions to maintain reduced reactor power at the 80% rod pattern line and to separate the safety related buses from the distribution system demonstrated a strong safety perspectiv The immediate response by operators to two automatic reactor trips was appropriat Communications, use of procedures, and supervisory oversight of control room operations were excellent during post trip recovery activities and subsequent mactor startups. Also, the identification of loose or missing bolts on motor operated valve actuator limit switch covers during routine rounds indicated good questioning attitudes and attention to detail by plant operator Maintenance and Surveillance Act ons i taken to verify the presence of and trend the effect of steam leakage past safety relief valve (SRV) RV 203 3A were thorough. Although not required by Technical Specifications (TS), the decision to establish cold shutdown and replace the leaking SRV pilot valve following an unrelated plant shutdown demonstrated sound safety judgemen In addition, coordination between the materials & component engineering section, maintenance personnel, and system engineers to complete the repair during this unscheduled maintenance period was outstanding. Restoration from the backfeed electrical lineup following post trip corrective maintenance was performed. Maintenance and operations personnel demonstra'-d excellent procedural knowledge and communication ,

An automatic reactor trip on December 20 was caused by procedural weaknesses and poor work practices by technicians changing the main steam line (MSL) high radiation protective setpoint Also, the technicians failed to lower the MSL hi;;h radiation alarm setpoints following the reactor trip. As a result, the MSL high radiation alarm was not available to control room operators upon the subsequent plant restart. Failure to properly reestablish the MSL high radiation protective setpoints and associated failure of the management review process on two occasions indicates a need for greater management attentio Emergency Preparedness The capability to draw, analyze, and provide real time post-accident sampling system data under simulated emergency conditions was successfully demonstrated in a December dril Safety Assessment and Quality Verification Implementation of Phase 11 of a planned three phase structural reorganization, to become effective January 1,1993, was announced on December 16,1992. Licensee event reports (LERs) were of good detail, accurate, and clearly identified root cause and corrective action, detailed and properly addressed the required reporting criteri ' ii -

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(EXECUTIVE SUMMARY CONTINUED)

Engineering and Technleal Support Deactivated head spray line containment isoir. ion valves remain to be removed from the Type C localleak rate test program. Several questions regarding American Society of Mechanical Engineers (ASME) Code criteria anc! the technical basis of certain aspects of the head spray line deactivation plant design change remain unremtve Continuing NRC review of the licensee reactor vessel water levelinstrumentation spiking status determined the operability aswssment was consistent with the guidance of NRC generic documentation for degraded or nonconforming conditions on olerability, iii i

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TAHLE OF SUMMARY OF FACILITY ACTIVITIES At the start of the repor* period Pilgrim Nuclear Power Station was in the initial phase of power l ascension following the completion of a midcycle maintenance outag '

On November 24,1992, packing leakage from the reactor core isolation cooling (RCIC) system -

steam supply valve (1301-16) was identified during the drywell inspection with the reactor vessel pressurized. Post work testing of the RCIC system was completed and the system was retumed to service on November 2 Elevated tailpipe temperatures downstream of safety relief valve (SRV) FV 203-3A were observed on November 24 following reactor startup. Reactor pressure remained stable and operators commenced trending of tailpipe temperature on an increased frequency. Tailpipe temperature stabilized at approximately 218 degrees Full power operation began on November 30 until December 11 when reactor power was reduced to approximately 75 percent to allow for rapid power reduction in the event of condenser fouling as a result of a severe Northeaster storm. Power was periodically reduced further to support backwash of the main condenser. On December 13, the station experienced r. load rejection and resultant automatic reactor trip from approximately 50% of rated powe All systems responded to the trip as designed and the reactor was quickly stabilized in a hot - ,

shutdown condition. On December 14. the "A" reactor protective system (RPS) bus was momentarily deenergized due to personnel errer while attempting to shift power supplies. This resulted in multiple engineered safety feature actuations. Systems were properly restored to their intended lineup and notincation to the NRC was appropriately made. Reactor startup vias, performed on December 17 and the main generator was synchronized to the offsite distribution grid on December 18. Post work testing of RV-203-3A, which was replaced during the plant outage, was completed satisfactoril On December 20, the reactor tripped from 75 percent power in response to a main steam line (MSL) high radiation signal to the reactor protective system (RPS). The reactor plant responded as designed to the automatic trip signal. Control room personnel verified that MSL radiation levels were normal prior to and after the reactor trip. The trip resulted from incorrectly established protective trip setpoints. Wactor startup was performed on December 22 and full power was achieved at 3:55 a.m. on December 24, and maintained through the end of the reporting perio .0 PLANT OPERATIONS (71707,40500,90712) Plant Operations Review The inspector observed plant operations during regular and backshift hours of the following areas:

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Control Room Fence Line Reactor Building (Protected Area)

Diesel Generator Building Turbine Building Switchgear Rooms Screen llouse Security Facilities Control room instruments were independently observed by NRC inspectors and found to be in correlation amongst channels, prooerly functioning and in conformance with Technical Specifications. Alarms received in the control room were reviewed and discussed with the operators. Operators were found cognizant of control board and plant conditions. Control room and shift manning were in accordance with Technical Specincation requirements. Posting and control of radiation contamination and high radiation areas were appropriate. Use of and compliance with radiation work permits and use of required personnel monitoring devices were confirme Plant housekeeping controls, including control of Gammable and other hazardous m9terials, were observed. During plant tours, logs and records were reviewed to ensure compliance with station procedures, to determine if entries were correctly made, and to verify correct .communkation of equipment status. These records included various operating logs, turnover sheets, tagout, and lifted lead and jumper logs. The inspectors monitored control room operations during reactor startup and synchronization of the main generator to the electrical distribution gri Communications, use of procedures and supervisory oversight were excellen .2 lead Rejection and Automatic Reactor Trip On December 13,1992, at 5:23 p.m., the station experienced a load rejection and resultant automatic reactor trip from approximately 50% of rated thermal power. All systems responded to the trip as designed and the reactor was quickly stabilized in a hot shutdown conditio Anticipated Group 11 and Vi primary containment isolation system and reactor building isolation system actuations were experienced in response to normally low reactor vessel water level following the trip. Reactor pressure increased from 960 psig to 990 psig after the load rejection and remained below safety relief valve setpoint Following the trip, the licensee initiated a reactor cooldown and depressurization. A cooldown rate of 50-70 F/hr was maintained. On December 14,1992, at 20 psig reactor pressure and 240 F reactor coolant temperature, the plant initiated the shutdown cooling system mode of decay .

heat remova Since December 11, 1992, Southeastern Massachusetts had been battered by a severe winter northeaster storm accompanied by sustained winds in excess of 50 mph, torrential rains, and -

extremely high tides (+9ft to + 12 ft). The extreme weather and sea conditions necessitated the licensee to continuously operate the intake structure travelling screens and to conduct several main condenser backwashes to remove debris and marine life. As precautionary measures during the storm, the licensee reduced reactor power to approximately 75% (with further

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3 reductions to conduct condenser backwashing and per load dispatcher direction) and maintained the core con 6guration at the 80% tod pattern line. Additionally, on December 12,1992, for approximately seven hours (1:30 p.m. - 8:15 p.m.) during a period that included temporary loss of one of the two 345 KV lines (i.e., Bridgewater line) the licensee transferred the source of power to the two 4.16 KV safety related buses, (A 5 and A-6), from the unit auxiliary transformer to the associated emergency diesel generator (EDG). After the "A" EDG was secured (8:15 p.m.), the licensee identined that the belt had broken on the engine driven fuel pump. The belt was replaced, post maintenance testing was completed and the "A" EDG was returned to normal standby service within 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />, at 7:13 p.m. on December 13, 190 Additionally, on December 14,1992 at 4:50 a.m., power to the A 5 and A-6 buses was again transferred to the EDGs following further switchyard electrical instabilit Operations Section preparation for and mitigation of the potential effects of the storm were comprehensive. Backwash evolutions were well controlled. Sound safety perspectives were evidenced by the decision to maintain reduced reactor power at the 80% rod pattern lin Appropriete actions were taken to separate the safetyrre!ated buses from the distribution system during periods of high winds and distribution system instabilit Control room operator oversight of post reactor trip recovery activities was good. Reactor cooldown and depressurization were well controlled. The nuclear watch engineer (NWE)

maintained clear communications whh the offsite distribution system dispatcher. Additionally, after assessing preparations for washdown of switchyard equipment, the NWE concluded the continuing severe winds precluded safe conduct of the washdown and the activity was postponed and the safety related 4.16 KV buses were transferred to the EDG The licensee conducted a post-trip review to determine the root cause of the load rejection and reactor trip. The trip report,92-01, dated December 17, 1992, appropriately documented the event, root causes, and corrective actions. The report was supported by design and event dat The report concluded the load rejection was caused by Cashover in the switchyard due to salt

spray buildup.

i After the storm passed and the winds subsided, the licensee conducted a sequential freshwater washdown of the switchyard to remove salt spray deposit Visual inspection confirmed j evidence of one of the two 345 KV lines (355 line) Dashover on three bushings on the C phase between the air circuit breakers ACI 102 and ACB 105. Calibration setpoints for directional distance relay (21/MT), directional ground overcurrent relay (67N/MT), and overcurrent fault detector relay (50/MT) were verified to be correct. Additionally the main transformer secondary

relay wiring configuration was verified to be accurate. Continued lleensee troubleshooting identined damaged insulation on one of the conductors for the "C" phase current transformer supply to the 21/MT relay. It was questioned whether this condition could have caused the relay to actuate for a fault outside of its protective zone. Licensee electrical laboratory experts determined the damaged insulation would not have had any significant impact on the function

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simultaneous switchyard Dashovers between ring bus air circuit breakers ACil 102 and ACB 105 as well as between ACB 104 and ACH 105 and the main transformer. Finally, during reactor ;

startup the licensee verined the proper polarity of the 21/MT rela .3 Reactor Protective System Automalle Reactor Trip On December 20,1992 at 2:33 a.m., the reactor tripped from 75 percent power in response to a main steam line (MSL) high radiation signal to the reactor protective system (RPS). The reactor plant responded as designed to the automatic trip signal. The Group I primary containment isolation system (PCIS) actuated in response to the high radiation signal. Group 11 and VI PCIS and reactor build:ng isolation 6/ stems actuated as expected in response to the transitory low reactor water level immediately following the trip. Control room personnel reviewed MSL radiation level recorders and verified that normal MSL radiation levels existed prior to and after the reactor trip. No high MSL radiation condition had actually occurred. The licensee initiated an event critique to determine the root cause of the trip and correspondi corrective actions as described in further detail in Section .4 Loose Motor Operated Valve Limit Switch Cover Holts Noted During Operator Tour Operators identified loose or missing closure bolts on four motor operated valve (MOV) limit switch compartment covers during the reactor building tour on December 29,1992. The covers remained inplace, held Ormly by the remaining bolts which were tight. The loose bolts were tightened and problem report (PR) 92-9296 was initiated to determine the cause and appropnate corrective actions. The Nuclear Engineering Department performed an engineering evaluation that concluded that the MOVs in question were operable for the period during which the bolts were not correctly installed. The inspector ieviewed the engineering evaluation and determined that it was technically soun The four MOVs on which loose bolts were identined had each been worked on during the recent midcycle maintenance outage. The licensee therefore initiated an inspection of the remaining 48 MOVs on which maintenance had been performed during the recent outage. This inspection identified four additional MOVs with loose limit switch cover bolts which were promptly-tightened. Eight of the 48 MOVs were not accessible for inspection in the present plant operating condition; however, inspections have been properly scheduled for when plant

! conditions are appropriate. Identification of the loose or missing bolts was indicative of detailed l and questioning tours by plant operators. The inspector concluded that initial corrective actions l

were appropnate and that the plant report process was properly initiated to address root caus .0 RADIOLOGICAL CONTROLS (71707)

The inspector reviewed radiological controls in place as well as the radiological conditions of selected areas of the plant. Management tours of the radiological controlled area continued to be thorough and directed toward minimizing total personnel radiation exposure. Survey postings, radiological conditions and controls were appropriate with no discrepancies noted,

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, MAINTENANCE AND SURVEILI.ANCE (37828,61726,62703,93702)

' Replacement of Defective Safety Relief Pilot Yalve  ;

i On November 24, 1992, control room operators observed elevated tailpipe temperatures  ;

downstream of safety relieve valve (SRV) RV 203-3A. Reactor pressure remained stable and i operators commenced trending of tailpipe temperature on an increased frequency. The SRV is '

designed to relleve reactor vessel pressure directly to the suppression pool in the event of a high pressure transient, an automatic. signal frt,m the automatic depressuritation system (ADS), or

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a manual actuation of ADS. The elevated temperature was characteristic of steam leakage past '

the normally closed SRV or SRV pilot valve. Excessive SRV _ leakage can result in SRV actuation setpoint drift and response time degradation. While the drywell was open. Operations personnel locally verified the elevated tallpipe temperatur As required by Technical Specifications, an engineering evaluation was performed to determine 1 whether continued power operation with elevated SRV tailpipe temperature (above 212 degrees ;

F) was acceptable. The completed evaluation concluded that the SRV was operable as it would_ ~

still open upcm demand to pc: form its intended safety function and that continued operation was justified with elevated SRV tailpipe temperatures up to 255 degrees F. The inspector noted the engineering evaluation to be detailed and technically sound. Operations response to the elevated -

RV 203 3A tailpipe temperature was appropriate. During a control room inspection, the inspector noted and discussed with operations personnel the alarm status for the continuing- 3 clevated tailpipe temperature, in order to prevent this condition from masking elevated tahr.pe temperature alarms from the other SRVs, t!,e alarm for RV-203-3A was disabled and the temperature recorder for this point checked hourly to establish a temperatere trend and ensure the 255 degrees F limit was not exceeded. The inspector considered this operator action to bei .

prudent and responsive to the existing plant condition :

Maintenance work packages were prepared and replacement of the RV-203 3A pilot valve was -

scheduled for the next refueling outage. Operators continued to trend RV-203-3A tailpipe _ ,

f temperature, which remained below 220 degrees F. The reactor trip on December 13, 1992, provided an unscheduled opportunity to replace the leaking pilot valve. Maintenance work plans - ,

were ready and' contained an appropriate level ofinstruction for the intended work. Although not required by Technical Specifications.(TS), the licensee decided to place the plant in a cold-shutdown _ condition following the trip and to replace the SRV pilot valve. This decision-demonstrated a conservative safety perspective, in addition, the inspector noted effective -

coordination between the Materials & Component Engineering Section, maintenance personnel, and system engineers to complete the repair during this' unscheduled maintenance period.'

(- The_ inspector observed the licensee drywell :loscout inspection prior to reactor startup at the i conclusion of SRV pilot valve replacement, in addition to inspection of RV-203 3A', the air ;

isolation supply valve to the RV-203-3A pilot valve was verified open. The drywell inspection

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was thorough and properly addressed the minor material discrepanc:es noted. Post maintenance l

testing (pMT) was successfully completed in accordance with procedure 8.5.6.2, " ADS System L = . = - . - --

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Manual Opening of Relief Valves" following reactor startup and pressurization. The inspector witnessed the conduct of the PMT of RV-203 3A in the control room on December 18 with the reactor mode select switch in the STARTUP position and the reactor at approximately 10%

power. A thorough pre-evolution brienng was observed and contingency actions for a stuck open SRV, (i.e., procedure 2.4.29), were available for ready reference. The inspector noted good coordination of test activities among the operators stationed at control room panels 903, ,

905, C10 and C171. In accordance with procedures HV 203-3A was opened and immediately closed upon receipt of the acoustic monitor alarm and verincation of partial bypass valve ,

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Preliminary licensee inspection of the failed SRV pilot valve concluded that the failure mechanism was unrelated to the failure of RV-203 3D which occurred in August 1991. The licensee intends to ship the defective SRV pilot valve to an off-site test facility for detailed root cause failure analysis and testing. The inspector determined that the lleensee's response to the elevated tailpipe temperature of RV-203 3A was in compliance with TS 3.6.D, ir.cluding plans for testing the as found condition of the pilot valv .2 Repair of Minor RCIC Valve Packing leakage During the drywell inspection (with the reactor pressurized), a minor packing leak was identified on RCIC steam supply containment isolation valve RCIC 16. The licensee initiated maintenance request (MR) 19200103 to documerd the repair. On November 24,1992, maintenance personnel applied Hve turns to the packing gland nut to isolate the leak, llecause the RCIC-16 valve constitutes a primary containment isolation system boundary, motor operated valve diagnostic testing was included as a ponion of the post maintenance testing requirements. The valve was time tested for the open and closed stroke travel, with maximum motor current recorded. The valve opened in 6.7 seconds with a maximum current of 1.3 amperes. Iloth values met the acceptance criteria of open stroke not to exceed 12 seconds at a running current of 1.4 ampere The valve closed in 8.2 seconds with a maximum current of 1.4 amperes floth values met the acceptance criteria of closed stroke not to exceed 12.5 seconds at a running current of amperes. Voltages recorded for the 480V power supply were recorded to be between 481-484V and remained below the overvoltage limit of 486V. post maintenance testing was completed satisfactorily and the RCIC system was declared operable and the plant startup continue During conduct of the post maintenance te-ting, two electrical technicians appeared to suffer from the effects of heat exhaustion and required medical assistance. The reactor was at approximately 900 psig and drywell temperatures at the 41 ft. elevation in the vicinity.of th-RCIC-16 valve were recorded at approximately 100 degrees F at the time the testing was conducted and the testing was considered to be of rr ulum metabolic physical demand. Station safety yrsonnel established a 60 minute stay time and the individuals involved wore personnel heat stress monitors. The work crew entered the drywell at approximate 1v 11:00 a.m. (on November 24,1992). Approximately 15 minutes later the crew exited the drywell because an A.C. cable for the test equipment was missing. The cable was located and the crew returned to the drywell at approximately 11:40 a.m. Approximately 35-40 minutes later, the cognizant L

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test engineer stopped the work effort upon the feeling of fatigue. The test engineer exited the drywell without need for assistance. One of two electrical technicians reported becoming weak and lightheaded and required assistance exiting the drywell work area. At approximetely 12:20 p.m., station emergency medical technicians (EMTs) responded to the drywell control point and administered to the technician. The technician was helped from his protective clothing and the EMTs assisted him omo a stretcher. Oxygen at 6 liters was applied vir the nasal passage and wet towels were applied to the technician's chest. The technielan was frisked by radiological protection personnel and was determined to be free of contamination and was then transported to (Se licensee medical facility. At approximately 12:32 p.m., the technician arrived at the medical facility and additional treatment was initiated but the technician declined the treatment and icquested that an ambulance be dispatched so that he could seek further evaluation and treatment at the Jordan 11ospital. A Town of Plymouth ambulance responded and transported the technician to Jordan 11ospital where he was treated and released later in the day. The second tcchnician apparently traveled to Jordan llospital via a private vehicle where he was similarly treated and release immediately following the event, the licensee convened an event critique in accordance with station procedure 1.3.6.1, " Conduct of Critiques and incident Investigations," to determine what factors contributed to the technicians' heat exhaustion. The critique included statements from involved individuals and event timeliness reconstructed from security computer records and radiation protection control logs. Initial critique findings documented by memorandum (ISD 92 62) dated December 4,1992, indicated that due to the emerging nature of the maintenance activity, normal practices prescribed by procedure 1.4.43, "licat Stress Management," such as planning and communications and technician preparations auch as pre-job heat stress briefing _

were expedited and may have contributed to the event. The practice of self determination of .

physical condition during the work activity was determined to be partially effective and due to work area equipment noise levels, the work crew could not hear the personal heat stress monitor alarms. Additionally, the report identified some ambiguity regarding what constitutes a recovery period as it relates to stay time. The inspector reviewed the critique report and all submitted reference material, including statements of record from involved individuals. The critique was very detailed and effectively developed potentially contributing factors to the event. The inspector found the initial report findings and concludons acceptable. No violations were "

identifie .3 Restoration of Normal Shutdown Electrical I,lneup from Backfeed I,ineup The plant tripped on December 13,1992, due to an electrical transient and turbine load reject signal as discussed in Section 2.2. A contributing factor to the electrical transient had been execisive salt buildup on electrical components in the switchyard during a severe stor Con ective action prior to reactor restart included washdown of switchyard components with cleai water to remove the excessive salt residue. The station was placed in an alternate electr..a backfeed lineup to support isolation and washdown of the start-up transformer (the preferred power source while shutdown). In the backfeed lineup, station electrical busses are supplied with offsite power via the main and auxiliary transformers. in this lineup the main

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generator Dexible links are removed to prevent damage to the generator. Pronciency at safely establishing and restoring from a backfeed electrical lineup is important with regard to maximizing availability of off site power sources during varied shutdown condition The laspe-tor observed restoration from the backfeed electrical lineup in accordance with procedure 3.M.3-9, " Main Generator or Main Transformer Flexible Connectors Removal and Restoration' Main and Unit Auxiliary Transformer Back Scuttling", following completion of the startup transformer washdown. Proper verincation while posting and clearing tagouts was demonstrated (Stoughout the evolution. The procedure was well written to an appropriate level N &>>il and clearly understood by both epmtions and maintenance personnel. However, the inspecto not<.xl that the procedure did not direct the removal of the control key following reposiacning of the Turbine Auxiliary Trip Rel Cutoff Switch. This was discussed with the Chief Operating Engineer and properly addresse Sound personr.cl safety practices were utilized when removing electrical fuses and " racking out" circuit breakers. Operations and electrical maintenance personnel demonstrated excellent knowledge of the procedure and equipment being operated. Minor discrepancies, such as improperly terminated electrical connectors and relay covers adrift inside electrical cabinets, were no'n! and correctly addressed by technicians performing this procedure. The evolution was performed in a controlled manner, with excellent communications between maintenance and opeia* ions personnel. The licensee demonstrated the capability to effectively establish the electrical backfeed lineup and to restore the normal shutdown electrical lineu .4 Reactor Trip Resulting from Incorrectly Adjusted Protective Setpoints Technical Speci0 cations require the MSL high radiation trip setpoints to be set at a value less than or equal to seven times the normal full power background radiation level. As described in Section 2.3, the reactor trlpped on December 20, 1992, in response to a main steam line (MSL) high radiation signal to the reactor protective system (RPS). Control room recorders.

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Indicated normal MSL radiation levels and no MSL high radiation alarm occurred prior to the l RPS tnp. The licensee promptly initiated an event critique to determine the root cause of the l trip. Inspector review of radiological monitor data confirmed that MSL radiation levels were

normal at the time of the tri Procedure 3.M 2-7.6, "NUMAC log Radiation Monitor Setpoint Change Procedure" was performed following reactor startup on December 19.1992 in order to raise both the MSL high radiation alarm and MSL high radiation trip setpoint The setpoints were changed to correspond to the increase in normal background MSL radiation levels that exist when hydrogen water chemistry injection is in service. The event critique team determined that the trip occurred as a result of Instrumentation and Control (I&C) technicians adjusting trip setpoints to an incorrect value during performance of procedure 3.M.2 7.6. It was noted that the procedure documented the required setpoints in decimal notation while the NUMAC instrument screen

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displayed the setpoints in scientific notation. Despite secord person verification of the setpoint

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adjustment, the trip setpoints of all four instrumtnt channels were erroneously adjusted (lowered)

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to values which were a factor of ten below the intended setpoints. inspector review of the completed procedure noted that in addition to the incorrect trip setpoints, the "C" MSL high  :

radiation trip reset point, which clears the trip signal, was documented as being a factor of one thousand too high. Although the reset value error had no safety consequence, this was also a setting requiring verincation by a second person, and provided further indication that technicians did not afford appropriate attention to the work being performed. Personnel error was identified as the root cause of the trip, with human factors and procedural weaknesses noted as contributing factors. Initial corrective actions included counseling of the technicians and revision of procedure 3.M.2 7.6 (revision 3) to address the procedural weaknence which most directly contributed to the trip. Significant procedure improvements were implemented prior to the subsequent reactor startu After reactor startup and performance of revised procedure 3.M.2-7.6 on December 23,1992, the inspector verified that the existing MSL high radiation alarm and trip setpoluts were correct, llowever, the inspector noted that the instrument downscale trip reset poln's were not set in accordance with the revised procedure. The error was not of safety concern, but indicated that the revised procedure may not have been thoroughly reviewed by persor,nel performing the maintenance or by I&C supervisory review of the completed maintenanen documentation. In addition, the inspector identified severa! further inconsistencies in proccoure 3.M 2-7.6 which the 1&C division manager planned to address as part of the ongoing critique team review of the -

even The MSL high radiation alarm setpoint is established well below the MSL high radiation trip setpoint to provide control room personnel with advance indication to initiate operator action to mitigate the cause or effect of the increasing radiation condition and climinate unnecessary safety system challenges. The incorrect setpoint adjustment on December 19, lowered the MSL trip setpoints to a value below the MSL high radiation alarm setpoint. Therefore control room personnel had no advance warning of the reactor trip. Inspector review of additional maintenance documents determined that the MSL high radiation alarm setpoints were not lowered following the reactor trip on December 20 as required by procedure. As a result, the .

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MSL high radiation alarm was not available upon plant restart until after the MSL high radiation trip setpoints were raised to support hydrogen water chemistry injection. These discrepancies were not identified by the technicians performing the maintenance nor by required management review of the completed procedure. The inspector reviewed documentation of procedure 3.M.2-7.6 performance for the past 18 months and identified no other similar discrepancie Technical Specification 6,8.A requires the proper implementation of procedures recommended in Appendix A of USNRC Regulatory Guide 1.33. - Appendix A- -Section 4 recommends

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establishment of procedures for startup, operation, and shutdown of safety related systems including the RPS system, The licensee failed to properly implement procedure 3.M 2-7.6, in that technicians established incorrect RPS protective setpoints and management reviews failed to identify associated discrepancies. This failure to follow procedural instruction directly resulted in the December 20,1992, reactor trip and challenged several safety related systems, in addition, as identified by NRC inspection upon review of completed procedure records, MSL

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high radiation alarrns were unavailable to operators on two occasions. Failure to properly i

implement procedure 3.M 2-7.6 adversely affected the establishment of the correct RPS i

protective setpoints and is a violation of Technical Specification 6.8 A (VIO 50 293/92-28-01), EMERGENCY PREPAREDNESS (40500)

The licensee conducted a post accident sampling system (PASS) drill on December 3,1992, to evaluate the capability of station personnel to draw, analyze, and provide real time PASS data under simulated emergency conditions.- The inspector reviewed the drill scenario prior to the evolution and concluded that the scenario was appropriate to support assessment of the stated objectives. Nuclear Watch Engineer verification that the scenario did not conflict with existing -

plant conditions prior to authorizing drill ecmmencement was thorough. The inspector observed initial staffing and deployment of response personnel from the Operations Support Center. ' No discrepancies were identified. Licensee assessment of this drill concluded that areas of concern - 3 noted during the previous PASS drill (92-01) had been effectively addresse l

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" SECURITY (71707)

Selected aspects of plant physical security were reviewed during regular and backshift hours to verify that controls were in accordance with the security plan and tpproved procedures. This review included the following security measures; security force staffing, vital and protected areas barrier integrity, maintenance ofisolation zones, behavioral observation, and implementation of access control including access authorization and badge issue, searches of personnel, packages and vehicles and escorting of visitors. Security force personnel continued to perform their duties in an alert manne l

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n SAFETY ASSESSMENT AND QUALITY YERIFICATION (92701) .

- Licensee Event Report (LER) Review 7.1.1 LER 92-11 LER 92-11, " Unplanned Actuation of a Portion of the _ Residual Heat Removal (RIIR) System Logic Circuitry During Surveillance Testing," describes the August 21, 1992, inadvertent initiation of portions of the RHR system due to personnel error while the reactor was at powe The actuation occurred when a technician inadvertently operated an incorrect relay during a l planned surveillance. An immediate result was the trip of the "A" recirculation pump and entry i; into single loop operation. Operator response to_ the event was appropriate and in accordance .

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with Technical Specifications. . Further discussion _of licensee response to the event .and corrective actions are documented in NRC Inspection Report 50-293/92-16; The LER accurately detailed the event and addressed the reporting criteri e l-

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7.1.2 LER 92-12 LER 92-12, " Failure to Perform Calibration Test of Neutron Monitoring System Recirculation Flow Converters," describes the licensee determination that they did not have documentation to verify that an instrument calibration was performed within the Technical Specification required periodicity. On September 16,1992, during a review of documentation, an engineer could not kicate the calibration resulb from a surveillance which was signed offin the Master Surveillance Tracking Program (MSTP) as having been completed on February 12, 1992, immediate corrective actions included initiation of a search for the missing data, and reperformance of the calibration tes Problem Report 92.9170 was initiated to determine whether or not the instrument calibration had been performed as documented on the MSTP. The licensee determined that the instrument functional test had been performed on February 12, 1992, but that the calibration was not performed. The supervisor who signed-off the MSTP for completion of the calibration had incorrectly believed that completion of the functional test would also satisfy testing requirements for the calibration. A contributing factor was the inclusion of both the functional test and the calibration test within the same procedure. The calibration test was reperformed on September 16, 1992 with satisfactory results, the supervisor was counselled regarding calibration test requirements, and a procedure revision was initiated to more clearly differentiate between functional test and instrument calibration requirements. Corrective actions were appropriat The LER eifectively developed the causal contributors and documented licensee corrective action .2 Phase II Organizational Restructuring On December 3,1992, Mr. Roy A. Anwrson, Senior Vice President Nuclear (SVP,N)

announced his resignation from BECo to accept a similar position with the Carolina Power and Light Company at the Dnmswick Facility. Dr. E. Thomas Boulette, Vice President of Nuclear Operations and Station Director was appointed to act as SVP,N upon Mr. Anderson's departur On December 16, 1992, the licensee officially announced the selection of various managerial positions to be effective January 1,1993 consistent with Phase 11 of the three phase structural reorganization. Phase I was initiated on June 29,1992 and is documented in NRC inspection Report 50 293/92-14, Section 7.1. Initially, as previously announced, Mr, E. Thomas Boulette will continue to serve as Acting Senior Vice President, Nuclear and Mr. Edward Kraft will serve as Acting Vice President of Nuclear Operations and Station Director. Mr. Les Schmeiing was selected as Plant Manager, with the plant department remaining unchanged. Mr. William Rethert was selected as General Manager, Technical, with the Nuclear Engineering Department managed by Mr. Robert Fairbanks and the new Regulatory Affairs and Emergency Planning l Department managed by Mr. Vern Oheim as direct reports. Mr. Frank Famulari remains the

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Quality Assurance Manager and continues to report to the Senior Vice President, Nuclear. M Leon Olivier was selected as Nuclear Services Manager. The Nuclear Services Department maintains the radiologica, radwaste and chemistry sections and will gain most plant support

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functions in Phase 111. Finally, Mr. Jack Alexander remains the Nuclear Training Manage The Nuclear Training Department remains unchanged in Phaw 11 but will gain most management support functions in Phase 111. Phase til is planned to be implemented in the summer of 1993 following completion of the next refueling outag Two significant reorganization highlights are the climination of the Vice President, Technical position and the merge of Emergency Planning (EP) into one department with Regulatory Affairs. Prior to Phase I, !!P reported as a department directly to the Senior Vice Presiden In Phase I, EP remained a separate department but was realigned to report to the Vice President, Technica .3 Sinff Qualificatiom Technical Specification (TS) 6.3 requires that station staff meet the educational and experience requirements described in ANSI N18.1 1971, " Selection and Training of Personnel for Nuclear Power Plants," at the time of appointment to an active position. The licensee implements the requirements of TS 6.3 through station procedure 1.3.78, " Procedure to Qualify llEco Employee to ANSI Requirements," in conjunction with a position description manual for every position requiring ANSI certifications. A qualification matrix is established that delineates the requirements of thejob description, ANSI N18.1-1971. ANSI /ANS 3.1-1987 and the educational experience background of the candidate. ANSI /ANS 3.1-1987, "American National Standard for Selection, Qualification and training of Personnel for Nuclear Power Plants," was issued to reflect the improvement in the selection and training practices in the industry. Candidates for ANSI certified positions must be verified to fulfill the matrix requirements before being appointed to the respective position The inspector reviewed the job description manual and verified that ANSI certified positions were properly identined with appropriate requirements identified. The inspector also reviewed the qualification matrixes for various department, section, and division managers. The matrices were well maintained and reflected the current organizational structure. Additionally, the inspector determined that the qualitications of the managers who matrices were reviewed were consistent with the ANSI requirements. The inspector had no questions in this are .0 ENGINEERING AND TECilNICAl, SUPPORT (71707) Containment isolation Valves The inspector checked the testing and handling of specific containment isolation valves (CIVs)

whose status had either been modified by a plant design change (PDC) or was defined by a unique system categorization. SpeciGeally, the inspector reviewed the status of motor operated valves, MO-1001-60 & 63, whose function as CIVs in the reactor head spray system piping was climinated by field revision notice FRN 196 to PDC 86-5211(see section 8.2 of this report for additional inspection of this plant modification); and also checked the status of air operated

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valve, AO-5025, a normally sealed-closed isolation valve in the direct torus vent system. These valves a:e currently listed in Table 11 of procedure 8.7.1.5 as requiring Type C local leak rate testing in accordance with 10 CFR 50, Appendix J requirements, liased upon the nonfunctionality of valves, MO 1001-60 & 63, the inspector verified that cognizant licensee personnel are aware of the need to revise procedure 8.7.1.5 to eliminate the categorization of these reactor head spray valves as CIVs. Additionally, the inspector con 0rmed that the containment penetration, X 17, for the reactor head spray system would still be appropriately Type 11 tested, in accordance with 10 CFR 50, Appendix J, because the expansion bellows original design was required to accommodate the thermal movement of the piping (reference: PNPS FSAR section 5.2.3.4.2).

For valve AO-5025, the inspector also verified acceptable local leak rate testing provisions, and noted a position indication test requirement in accordance with the ASMll Code Section XI in-service testing program. Since procedure 8.7.1.5 specifies cycling of the valve for the position indicatien test prior to the conduct of the Type C leakage test, periodic stroking of valve AO-5025 is assured by the PNPS CIV testing program. Ilowever, since the opening of the direct torus vent valve is not stroke timed and done only coincidentally to the Type C testing, the inspector questioned whether the other safety function of the valve, i.e., venting versus containment isolation, has been appropriately addressed by the PNPS in service testing program, in response to the inspector's question, the licensee initiated an integrated action data base (IADil) item, GM 93-0002, to evaluate the need for a procedural requirement to conduct and document the stroke time testing of valve AO 5025. The inspector reviewed the 1ADil data entry form for this item and determined that this issue was being tracked to an appropriate technical resolution. Since the normal direct torus vent system con 0guration maintains valve AO-5025 as a scaled closed CIV, representing its fail-r,afe position, the inspector had no additional questions regarding the current status or isolation capability of the valve. The licensee resolution of item GM 93-0002 is due prior to the start of the next refueling outage (RFO 9),

when valve AO 5025 is again scheduled for testing, Plant Design Change Review - Removal of Reactor llead Spray System Previous NRC review (Report 50 293/90 25) of plant design change (PDC) 86-20 cvaluated cutting and capping of the reactor head spray line from the standpoint of continued protection of the primary containment boundary. During the last (August 1991) refueling outage (RFO 8),

new design change PDC 86 5211 was implemented which involved the removal of piping which included an inboard containment isolation valve (CIV); the capping of containment penetmtion-X-17; and, the abandonment of piping and another CIV outside of the containment. While the abandoned piping remained seismically' qualified and in accordance with safety-related Class "ll over 1" criteria, the safety class of the components was downgraded and no provision for continued maintenance and testing of the valves was required. During this inspection, the inspector reviewed field revision notice (FRN) 196 to PDC 86-5211 to deteanine the existing status of the systems, components and material affatal by the head spray design change, as implementa . -

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The inspector also checked the compatibility of the Residual lleat Removal (RllR) system confi;;uration, as left after implementation of PDC 86-20 with the design intent of PDC 86-5211-

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196 and, in this regard, additionally reviewed drawings M100 llc-2821, M100-38 7, MIN 40-12, M241 and an earlier FRN 191 to PDC 86-52I1. During a plant inspection tour, the inspector noted that the electrical supply breaker (H2003) for the head spray valve (MO-100163) which had been removed during RFO 8 was still danger-tagged open. The inspector reviewed the PNPS tagout sheet T9010-21 and determined that this open tag status was inconsistent with the handling of the electrical supply to the other head spray CIV (MO 100160), where the breaker had been left open, but the tagout cleared. The inspector discussed this inconsistency with cognizant TA ant personnel who initiated action to query the nuclear engineering department as to whether the entire tagout *190-10 21 could be closed and cleare In review of PDC 86-5211196 design change criteria, the inspector identined a statement which implied that the abandoned piping in the reactor head spray system outside containment would temain vented, liowever, since PDC 86-20 installed a pipe cap or, one side of this piping and PDC 86-5211-196 capped the piping at penetration X 17 on the other side, the reviewed licensee documentation provided no indication how such venting was implemented in that the valves identified in the PDC relating to this piping appeared to have been left in the closed positio Furthermore, since valve MO 1001-60, as identined in tagout "19010-21 was chained closed, two vent paths, one on either side of the closed valve, would have to have been provided for the as-!cft piping to be consistent with the PDC design criteri .

Additionally, the inspector confirmed that the pipe cap for the penetration X-17 piping had been procured to ASME Code, Section 111, Class 2 criteria as " impact tested material." 110 wever, it appeared that an impact tested weld procedure had not been used to install the pipe cap as would be required by the ASME Code, Section IX, unless certain conditio.is of exemption allowed by Section 111 of the code were satisfied. Given that the PNPS FSAR documents the containment drywell shell material to be fabricated of impact tested plate and forgings, the licensee issued problem report 93-9005 to resolve this question regarding the weld procedure qualificatio The inspector determined through the review of PDC 86-52B-196 and related supporting documentation that the current configuration of the teactor head spray piping was acceptable, in that the continued safe operation of PNPS had not been adversely affected by the design modification. Ilowever, as noted above, certain questions, regarding the existing pipe venting and the containment penetration weld qualification criteria, remain open. Pending the licensee presentation of evidence that the installed configuration is in compliance with the intended PDC design criteria, these issues remain unresolved (92-28-02). Reactor Vessel Water imel Instrumentation Update NRC Inspection Report 50-293/92 23, Section 8.1,' provided a detailed status of licensee

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activities in response to reactor vessel water level instrumentation spiking experienced during l recent reactor shutdown evolutions. Specifically, the issue has been addressed in terms of the l generic concern for les el instrumentation inaccuracies during rapid depressuriration eventa due l to the evolution of noncondensible gases from the reference leg _

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The NRC conducted review of BECo operability determination of the levelinstrumentation, with particular attention on the instrumentation associated with the two-thirds (2/3) core height containment spray interlock. The safety function of this instrumentation is to provide level signals and indication such that adequate core cooling can be achieved for cenain classes of accidents. The NRC staffindependently concluded that this safety function would be satisfied

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at Pilgrim based upon the following:

  • If flow is diverted to containment spray after 2/3 core coverage is achieved, one core spray pump alone is adequate to maintain 2/3 level and core cooling. Thus, even the diversion of all available low pressure coolant injection (LPCI) would not preclude adequate core coolin * It is unlikely that significant diversion of flow would occur prior to renooding the vessel to 2/3 core height, because:

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the interlock does not cause any automatic actuations; that is, satisfying the interlock does not automatically divert LPCI now to containment spra according to the Pilgrim Reload Analysis (SAFER /GESTR Report NEDC-31852),

for design basis loss of coolant accidents, the core is renooded to 2/3 core height within approximately.60 to 150 seconds; therefore, the operator would have to immediately divert LPCI for such erroneous action to occur prior to renooding the vessel. Moreover, operators are directed by proccdure to assure adequate core cooling prior to initiation of containment spray, and operators have been sensitized to potential errors in level indication. Station Emergency Operating Procedures (ie, EOP 03, " Primary Containment Control") which govern the decision to divert LPCI now and spray the containment would require the presence of a high drywell pressure above 2.5 psig. Also, the EOPs direct that only "those RilR pumps not required to assure adequate core cooling by continuous operation in the LPCI mode" be used for containment spray diversio over 20 linear feet of reference leg volume, including both horizontal and vertical sections, must be voided and not recovered at Pilgrim to cause a continuous 14 inch level error, and an error of this amplitude is already considered in the interlock setpoin it is expected that the magnitude of error in the level indication following an actual depressurization event would be significantly less than that estimated by conservative assumptions used in the calculations performed by the General Electric Company and the BECo consultants.

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the potential for level' errors has likely been lessened by actions taken by the l licensee to reduce external reference leg leakage (ie, tighten fittings and packing at the

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instrument racks),

e Ifit was postulated that LPCi flow was prematurely diverted to containment spray, the safety function of the interlock would still be fulfilled, because:

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-- at Pilgrim the diversion of LPCI flow to containment spray (both drywell and torus) represents only approximately 25% of thc capacity of one LPCl/RHR pum Appendix K analysis from the current Pilgrim Reload Analysis for the most limiting case for which LPCI flow is creGited (ie, battery failure case), indicate a 1694

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degrees F peak clad temperature (PCF), which represents a 506 degrees F margin to the 2200 degrees F PCT limi NRC staff reviewed analysis for a similar BWR13 plant in which 100% of the Dow of one Rilk pump was assumed to be diverted from the core from the onset of the accident. These analysis support the staff judgement that, using Appendix K analysir ,

assumptions, diversion of 25% of the Dow of one RHR pump would not result in exceeding 2200 degrees F PC Based on the above, the NRC staff concluded that any manual actuation of containment spray which is based upon an erroneous level signal to this interlock is both highly unlikely and of low safety significance, and that the safety function of the level instrumentation system at Pilgrim

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would therefore be fulfille The NRC staff also concluded that the DECO operability determination was performed consistent with the guidance of NRC Generic Letter No. 91-18,

"Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and on Operability," dated November 7,199 During reactor depressurization following the two automatic trips that occurred during this inspection period, no reactor vessel water level instrumentation " spiking" was observed. The ,

reactor tripped on December 13,1992, after 20 days of operation and again on December 20,1992, shortly after startup from the previous trip. The NRC will continue to monitor DECO's progress in resolving the problem of noncondensible gas cccumulation in the level instrumentation system at Pilgri .0 NRC MANAGEMENT MEETINGS AND OTIIER ACTIVITIFS (30702) Routine Meetings ,

At periodic intervals during this inspection, meetings were held with senior plant management to discuss licensee activities and areas of concern to the inspectors. At the conclusion of the reporting period, the resident inspector staff conducted an exit meeting on January 7,1993 with licensee management, summarizing inspection activity and preliminary findings for this report period. No proprietary information was identified as being included in the repor Other NRC Activilles During the weeks of . November 30 - December 4,1992 and December 1418,1992 a Probabilistic Risk Assessment team inspection was conducted. Inspection esults will be documented in NRC Inspation Report 50-293/92-8 .

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17-On December 17,1992, Messrs. Jacque Durr, Region 1, Division of Reactor Safety, Engineering -

Branch Chief, Eutene Kelly, Region I, Division of Reactor Projects, Chief Section 3A, Ronald B. Eaton, NRR, Project Directorate 1-3, Senior Project Manager, and Jefferey Harold, NRR, Project Directorate 1-3, Project Engineer conducted a site visit. . Activities during the visit'

included discussions with the Resident inspector staff, observation of PRA inspection team performance, meeting with station management to discuss the Phase 11 reorganization, attendance a. a Town of Plymouth Nuclear Matters Committee Meeting and attendance at the PRA inspection exit meeting on December 18, 1992.

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