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Category:INSPECTION REPORT
MONTHYEARIR 05000272/19990011999-04-0101 April 1999 Insp Repts 50-272/99-01 & 50-311/99-01 on 990117-0307.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities IR 05000272/19970031997-02-0505 February 1997 Attachment to Insp Repts 50-272/97-03 & 50-311/97-03 ,consisting of 970205 Slide Presentation Inadvertently Omitted from Repts IR 05000354/19960101997-01-27027 January 1997 Insp Rept 50-354/96-10 on 961110-1221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Security Program Plan IR 05000272/19960131996-12-0303 December 1996 Insp Repts 50-272/96-13 & 50-311/96-13 on 960812-0920. Violations Noted.Major Areas Inspected:Engineering Performance Issues That Require Resolution Prior to Plant Restart ML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 ML20247B6651989-05-0909 May 1989 Mgt Meeting Rept on 890307 & 0413.Major Areas Discussed: Status of Plant,Training & Safety Programs & Self Assessment Programs IR 05000272/19880061988-03-18018 March 1988 Partially Withheld Physical Security Insp Repts 50-272/88-06,50-311/88-06 & 50-354/88-04 on 880201-05 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Procedures,Security Organization & Mgt Effectiveness IR 05000254/19870251987-11-23023 November 1987 Insp Repts 50-254/87-25 & 50-265/87-25 on 870922-1105. Violations Noted.Major Areas Inspected:Licensee Implementation of Generic Ltr 85-06 Re ATWS Mitigation Sys (25020) & Onsite Followup Events IR 05000272/19870271987-10-20020 October 1987 Insp Rept 50-272/87-27 on 870921-25.No Violations Noted. Major Areas inspected:post-mod Test Program for Forthcoming Refueling Outage,Including Engineering Change (1EC) Packages,Mod Test Procedures & Test Specs IR 05000272/19870051987-03-23023 March 1987 Insp Repts 50-272/87-05 & 50-311/87-07 on 870224-27.No Violations Identified.Major Areas Inspected:Control of Internal Exposures,Processing of Routine Survey Data, Organization & Staffing & Control of Radioactive Matl IR 05000272/19870031987-03-11011 March 1987 Insp Repts 50-272/87-03 & 50-311/87-04 on 870127-0223. Violation Noted:Control & Testing of Containment Boundary Valves Incomplete IR 05000311/19870051987-03-10010 March 1987 Insp Rept 50-311/87-05 on 870203-06.No Violations Identified.Major Areas Inspected:Cycle 4 Startup Physics Testing Program,Precritical Tests,Low Power Physics Tests & Power Ascension Tests IR 05000272/19860231987-03-0404 March 1987 Mgt Meeting Repts 50-272/86-23 & 50-311/86-23 on 870203. Major Areas Discussed:Findings Re Equipment Qualification Insp,Including Equipment Qualification of Limitorque Operators & Exo Sensors Hydrogen Analyzers IR 05000272/19870021987-02-20020 February 1987 Insp Repts 50-272/87-02 & 50-311/87-02 on 870112-16. Violations Noted:Procedures Used in Performing Evaluation Found to Underestimate Anchor Bolt Loads When Compared to More Accurate Analytical Techniques IR 05000272/19870011987-02-11011 February 1987 Insp Repts 50-272/87-01 & 50-311/87-01 on 870101-26.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance & Review of Special Repts IR 05000272/19860331987-02-11011 February 1987 Radiation Safety Insp 50-272/86-33 Renumbered to Include 50-311.New Designation Is Combined Insps 50-272/86-33 & 50-311/86-33 IR 05000311/19870031987-02-0606 February 1987 Insp Rept 50-311/87-03 on 870112-23.Violation Noted:Rhr Flow Injected Into Only Two of Four RCS Cold Legs During LOCA IR 05000311/19860351987-01-0909 January 1987 Insp Rept 50-311/86-35 on 861119-27.No Violations or Deviations Noted.Major Areas Inspected:Test Witnessing, Preliminary Evaluation of Containment Integrated Leak Rate Test & Facility Tours IR 05000272/19860281986-11-0505 November 1986 Insp Repts 50-272/86-28 & 50-311/86-28 on 861001-27.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance,Special Repts & Licensee Events IR 05000272/19860221986-10-24024 October 1986 Insp Repts 50-272/86-22 & 50-311/86-22 on 860915-17.No Violations Noted.Major Areas Inspected:Licensee partial- Scale Emergency Exercise Conducted on 860916 IR 05000272/19860251986-10-15015 October 1986 Insp Repts 50-272/86-25 & 50-311/86-25 on 860908-12. Deviations Noted:Administrative Controls to Designate & Assure Quality of Bolt Matl Lubricants Did Not Meet Requirements of IE Bulletin 82-02 IR 05000311/19860261986-09-15015 September 1986 Insp Rept 50-311/86-26 on 860826-30.Unresolved Items Noted: Replacement of Dissimilar Metal Welded Joints & Overall Pipe Replacement Program on Svc Water Sys & Correction of Equipment Identified in 860826 Event IR 05000272/19860071986-04-0303 April 1986 Insp Repts 50-272/86-07 & 50-311/86-07 on 860224-28. Violation Noted:Inadequate Measures to Assure Design Bases Important to Safety Structures Correctly Translated Into Procedures IR 05000272/19860021986-03-14014 March 1986 Insp Repts 50-272/86-02 & 50-311/86-02 on 860210-14.No Noncompliance Noted.Major Areas Inspected:Liquid & Gaseous Effluents Control Program & Radiochemical Measurements Program ML20137N5861986-01-24024 January 1986 Corrected 851224 Insp Repts 50-272/85-29 & 50-311/85-27.Rept Numbers Revised & Should Read 50-272/85-27 & 50-311/85-29 IR 05000311/20080101986-01-23023 January 1986 Insp Rept 50-458/85-09 on 850311-0810.Violations Noted: Failure to Adequately Check Calculations,Document & Verify Assumptions & Provide Basis for Design Input IR 05000272/19850291985-12-23023 December 1985 Insp Repts 50-272/85-29 & 50-311/85-27 on 851203-05.No Violation Noted.Major Areas Inspected:Annual partial-scale Emergency Exercise on 851204 IR 05000272/19850161985-10-0707 October 1985 Insp Repts 50-272/85-16 & 50-311/85-18 on 850708-11.No Violation Noted.Major Areas Inspected:Emergency Preparedness Program W/Emphasis on Review of Deficient Areas Noted in Insp Repts 50-272/84-39 & 50-311/84-38 IR 05000311/20050171985-08-0101 August 1985 Insp Rept 50-458/85-19 on 850311-0517.Violation Noted: Failure to Incorporate Engineering & Design Coordination Rept Info Into Drawings & Use External Historical Data in Evaluation of Suppliers IR 05000272/19850121985-06-18018 June 1985 Insp Repts 50-272/85-12 & 50-311/85-13 on 850507-31. Violation in Area of Security & Two Unresolved Items Noted. Major Areas Inspected:Operational Safety Verification,Maint Observations & Licensee Event Followup Review IR 05000272/19850081985-05-29029 May 1985 Insp Repts 50-272/85-08 & 50-311/85-09 on 850401-04.No Violation or Deviation Noted.Major Areas Inspected:Followup of Unresolved Items Re Fire Protection/Prevention Program & Corrective Steps Taken IR 05000272/19850091985-05-16016 May 1985 Safety Insp Repts 50-272/85-09 & 50-311/85-11 on 850406- 0506.No Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint Observations,Surveillance Observations & Review of Special Repts IR 05000311/20040191985-05-10010 May 1985 Insp Rept 50-458/85-22 on 850311-0419.No Violation or Deviation Noted.Major Areas Inspected:Maint Program,Test & Measurement Equipment,Surveillance Testing & Calibr Control Program,Design Changes & Mods & Document Control IR 05000311/20040011985-04-18018 April 1985 Insp Repts 50-348/85-18 & 50-364/85-18 on 850311-0401.No Violations or Deviations Noted.Major Areas Inspected: Licensee Action on Previous Enforcement Matters,Monthly Maint & Surveillance Observation & Independent Insp Effort IR 05000272/19820121982-06-14014 June 1982 IE Insp Repts 50-272/82-12 & 50-311/82-13 on 820512-0608. Noncompliance Noted:Failure to Review & Approve Procedures & Failure to Perform Surveillance Tests Re Containment Penetration Isolation Points IR 05000272/19820081982-05-27027 May 1982 IE Insp Repts 50-272/82-08 & 50-311/82-07 on 820122. Noncompliance Noted:Delivery of Shipment of Licensed Matl to Carrier for Transport W/Two Containers Not Strong,Tight Packages 1999-04-01
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000272/19990011999-04-0101 April 1999 Insp Repts 50-272/99-01 & 50-311/99-01 on 990117-0307.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities IR 05000272/19970031997-02-0505 February 1997 Attachment to Insp Repts 50-272/97-03 & 50-311/97-03 ,consisting of 970205 Slide Presentation Inadvertently Omitted from Repts IR 05000354/19960101997-01-27027 January 1997 Insp Rept 50-354/96-10 on 961110-1221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Security Program Plan IR 05000272/19960131996-12-0303 December 1996 Insp Repts 50-272/96-13 & 50-311/96-13 on 960812-0920. Violations Noted.Major Areas Inspected:Engineering Performance Issues That Require Resolution Prior to Plant Restart ML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 ML20247B6651989-05-0909 May 1989 Mgt Meeting Rept on 890307 & 0413.Major Areas Discussed: Status of Plant,Training & Safety Programs & Self Assessment Programs IR 05000272/19880061988-03-18018 March 1988 Partially Withheld Physical Security Insp Repts 50-272/88-06,50-311/88-06 & 50-354/88-04 on 880201-05 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Procedures,Security Organization & Mgt Effectiveness IR 05000254/19870251987-11-23023 November 1987 Insp Repts 50-254/87-25 & 50-265/87-25 on 870922-1105. Violations Noted.Major Areas Inspected:Licensee Implementation of Generic Ltr 85-06 Re ATWS Mitigation Sys (25020) & Onsite Followup Events IR 05000272/19870271987-10-20020 October 1987 Insp Rept 50-272/87-27 on 870921-25.No Violations Noted. Major Areas inspected:post-mod Test Program for Forthcoming Refueling Outage,Including Engineering Change (1EC) Packages,Mod Test Procedures & Test Specs IR 05000272/19870051987-03-23023 March 1987 Insp Repts 50-272/87-05 & 50-311/87-07 on 870224-27.No Violations Identified.Major Areas Inspected:Control of Internal Exposures,Processing of Routine Survey Data, Organization & Staffing & Control of Radioactive Matl IR 05000272/19870031987-03-11011 March 1987 Insp Repts 50-272/87-03 & 50-311/87-04 on 870127-0223. Violation Noted:Control & Testing of Containment Boundary Valves Incomplete IR 05000311/19870051987-03-10010 March 1987 Insp Rept 50-311/87-05 on 870203-06.No Violations Identified.Major Areas Inspected:Cycle 4 Startup Physics Testing Program,Precritical Tests,Low Power Physics Tests & Power Ascension Tests IR 05000272/19860231987-03-0404 March 1987 Mgt Meeting Repts 50-272/86-23 & 50-311/86-23 on 870203. Major Areas Discussed:Findings Re Equipment Qualification Insp,Including Equipment Qualification of Limitorque Operators & Exo Sensors Hydrogen Analyzers IR 05000272/19870021987-02-20020 February 1987 Insp Repts 50-272/87-02 & 50-311/87-02 on 870112-16. Violations Noted:Procedures Used in Performing Evaluation Found to Underestimate Anchor Bolt Loads When Compared to More Accurate Analytical Techniques IR 05000272/19870011987-02-11011 February 1987 Insp Repts 50-272/87-01 & 50-311/87-01 on 870101-26.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance & Review of Special Repts IR 05000272/19860331987-02-11011 February 1987 Radiation Safety Insp 50-272/86-33 Renumbered to Include 50-311.New Designation Is Combined Insps 50-272/86-33 & 50-311/86-33 IR 05000311/19870031987-02-0606 February 1987 Insp Rept 50-311/87-03 on 870112-23.Violation Noted:Rhr Flow Injected Into Only Two of Four RCS Cold Legs During LOCA IR 05000311/19860351987-01-0909 January 1987 Insp Rept 50-311/86-35 on 861119-27.No Violations or Deviations Noted.Major Areas Inspected:Test Witnessing, Preliminary Evaluation of Containment Integrated Leak Rate Test & Facility Tours IR 05000272/19860281986-11-0505 November 1986 Insp Repts 50-272/86-28 & 50-311/86-28 on 861001-27.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance,Special Repts & Licensee Events IR 05000272/19860221986-10-24024 October 1986 Insp Repts 50-272/86-22 & 50-311/86-22 on 860915-17.No Violations Noted.Major Areas Inspected:Licensee partial- Scale Emergency Exercise Conducted on 860916 IR 05000272/19860251986-10-15015 October 1986 Insp Repts 50-272/86-25 & 50-311/86-25 on 860908-12. Deviations Noted:Administrative Controls to Designate & Assure Quality of Bolt Matl Lubricants Did Not Meet Requirements of IE Bulletin 82-02 IR 05000311/19860261986-09-15015 September 1986 Insp Rept 50-311/86-26 on 860826-30.Unresolved Items Noted: Replacement of Dissimilar Metal Welded Joints & Overall Pipe Replacement Program on Svc Water Sys & Correction of Equipment Identified in 860826 Event IR 05000272/19860071986-04-0303 April 1986 Insp Repts 50-272/86-07 & 50-311/86-07 on 860224-28. Violation Noted:Inadequate Measures to Assure Design Bases Important to Safety Structures Correctly Translated Into Procedures IR 05000272/19860021986-03-14014 March 1986 Insp Repts 50-272/86-02 & 50-311/86-02 on 860210-14.No Noncompliance Noted.Major Areas Inspected:Liquid & Gaseous Effluents Control Program & Radiochemical Measurements Program ML20137N5861986-01-24024 January 1986 Corrected 851224 Insp Repts 50-272/85-29 & 50-311/85-27.Rept Numbers Revised & Should Read 50-272/85-27 & 50-311/85-29 IR 05000311/20080101986-01-23023 January 1986 Insp Rept 50-458/85-09 on 850311-0810.Violations Noted: Failure to Adequately Check Calculations,Document & Verify Assumptions & Provide Basis for Design Input IR 05000272/19850291985-12-23023 December 1985 Insp Repts 50-272/85-29 & 50-311/85-27 on 851203-05.No Violation Noted.Major Areas Inspected:Annual partial-scale Emergency Exercise on 851204 IR 05000272/19850161985-10-0707 October 1985 Insp Repts 50-272/85-16 & 50-311/85-18 on 850708-11.No Violation Noted.Major Areas Inspected:Emergency Preparedness Program W/Emphasis on Review of Deficient Areas Noted in Insp Repts 50-272/84-39 & 50-311/84-38 IR 05000311/20050171985-08-0101 August 1985 Insp Rept 50-458/85-19 on 850311-0517.Violation Noted: Failure to Incorporate Engineering & Design Coordination Rept Info Into Drawings & Use External Historical Data in Evaluation of Suppliers IR 05000272/19850121985-06-18018 June 1985 Insp Repts 50-272/85-12 & 50-311/85-13 on 850507-31. Violation in Area of Security & Two Unresolved Items Noted. Major Areas Inspected:Operational Safety Verification,Maint Observations & Licensee Event Followup Review IR 05000272/19850081985-05-29029 May 1985 Insp Repts 50-272/85-08 & 50-311/85-09 on 850401-04.No Violation or Deviation Noted.Major Areas Inspected:Followup of Unresolved Items Re Fire Protection/Prevention Program & Corrective Steps Taken IR 05000272/19850091985-05-16016 May 1985 Safety Insp Repts 50-272/85-09 & 50-311/85-11 on 850406- 0506.No Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint Observations,Surveillance Observations & Review of Special Repts IR 05000311/20040191985-05-10010 May 1985 Insp Rept 50-458/85-22 on 850311-0419.No Violation or Deviation Noted.Major Areas Inspected:Maint Program,Test & Measurement Equipment,Surveillance Testing & Calibr Control Program,Design Changes & Mods & Document Control IR 05000311/20040011985-04-18018 April 1985 Insp Repts 50-348/85-18 & 50-364/85-18 on 850311-0401.No Violations or Deviations Noted.Major Areas Inspected: Licensee Action on Previous Enforcement Matters,Monthly Maint & Surveillance Observation & Independent Insp Effort IR 05000272/19820121982-06-14014 June 1982 IE Insp Repts 50-272/82-12 & 50-311/82-13 on 820512-0608. Noncompliance Noted:Failure to Review & Approve Procedures & Failure to Perform Surveillance Tests Re Containment Penetration Isolation Points IR 05000272/19820081982-05-27027 May 1982 IE Insp Repts 50-272/82-08 & 50-311/82-07 on 820122. Noncompliance Noted:Delivery of Shipment of Licensed Matl to Carrier for Transport W/Two Containers Not Strong,Tight Packages 1999-04-01
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000272/19990011999-04-0101 April 1999 Insp Repts 50-272/99-01 & 50-311/99-01 on 990117-0307.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities IR 05000272/19970031997-02-0505 February 1997 Attachment to Insp Repts 50-272/97-03 & 50-311/97-03 ,consisting of 970205 Slide Presentation Inadvertently Omitted from Repts IR 05000354/19960101997-01-27027 January 1997 Insp Rept 50-354/96-10 on 961110-1221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Security Program Plan IR 05000272/19960131996-12-0303 December 1996 Insp Repts 50-272/96-13 & 50-311/96-13 on 960812-0920. Violations Noted.Major Areas Inspected:Engineering Performance Issues That Require Resolution Prior to Plant Restart ML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 ML20247B6651989-05-0909 May 1989 Mgt Meeting Rept on 890307 & 0413.Major Areas Discussed: Status of Plant,Training & Safety Programs & Self Assessment Programs IR 05000272/19880061988-03-18018 March 1988 Partially Withheld Physical Security Insp Repts 50-272/88-06,50-311/88-06 & 50-354/88-04 on 880201-05 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Procedures,Security Organization & Mgt Effectiveness IR 05000254/19870251987-11-23023 November 1987 Insp Repts 50-254/87-25 & 50-265/87-25 on 870922-1105. Violations Noted.Major Areas Inspected:Licensee Implementation of Generic Ltr 85-06 Re ATWS Mitigation Sys (25020) & Onsite Followup Events IR 05000272/19870271987-10-20020 October 1987 Insp Rept 50-272/87-27 on 870921-25.No Violations Noted. Major Areas inspected:post-mod Test Program for Forthcoming Refueling Outage,Including Engineering Change (1EC) Packages,Mod Test Procedures & Test Specs IR 05000272/19870051987-03-23023 March 1987 Insp Repts 50-272/87-05 & 50-311/87-07 on 870224-27.No Violations Identified.Major Areas Inspected:Control of Internal Exposures,Processing of Routine Survey Data, Organization & Staffing & Control of Radioactive Matl IR 05000272/19870031987-03-11011 March 1987 Insp Repts 50-272/87-03 & 50-311/87-04 on 870127-0223. Violation Noted:Control & Testing of Containment Boundary Valves Incomplete IR 05000311/19870051987-03-10010 March 1987 Insp Rept 50-311/87-05 on 870203-06.No Violations Identified.Major Areas Inspected:Cycle 4 Startup Physics Testing Program,Precritical Tests,Low Power Physics Tests & Power Ascension Tests IR 05000272/19860231987-03-0404 March 1987 Mgt Meeting Repts 50-272/86-23 & 50-311/86-23 on 870203. Major Areas Discussed:Findings Re Equipment Qualification Insp,Including Equipment Qualification of Limitorque Operators & Exo Sensors Hydrogen Analyzers IR 05000272/19870021987-02-20020 February 1987 Insp Repts 50-272/87-02 & 50-311/87-02 on 870112-16. Violations Noted:Procedures Used in Performing Evaluation Found to Underestimate Anchor Bolt Loads When Compared to More Accurate Analytical Techniques IR 05000272/19870011987-02-11011 February 1987 Insp Repts 50-272/87-01 & 50-311/87-01 on 870101-26.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance & Review of Special Repts IR 05000272/19860331987-02-11011 February 1987 Radiation Safety Insp 50-272/86-33 Renumbered to Include 50-311.New Designation Is Combined Insps 50-272/86-33 & 50-311/86-33 IR 05000311/19870031987-02-0606 February 1987 Insp Rept 50-311/87-03 on 870112-23.Violation Noted:Rhr Flow Injected Into Only Two of Four RCS Cold Legs During LOCA IR 05000311/19860351987-01-0909 January 1987 Insp Rept 50-311/86-35 on 861119-27.No Violations or Deviations Noted.Major Areas Inspected:Test Witnessing, Preliminary Evaluation of Containment Integrated Leak Rate Test & Facility Tours IR 05000272/19860281986-11-0505 November 1986 Insp Repts 50-272/86-28 & 50-311/86-28 on 861001-27.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance,Special Repts & Licensee Events IR 05000272/19860221986-10-24024 October 1986 Insp Repts 50-272/86-22 & 50-311/86-22 on 860915-17.No Violations Noted.Major Areas Inspected:Licensee partial- Scale Emergency Exercise Conducted on 860916 IR 05000272/19860251986-10-15015 October 1986 Insp Repts 50-272/86-25 & 50-311/86-25 on 860908-12. Deviations Noted:Administrative Controls to Designate & Assure Quality of Bolt Matl Lubricants Did Not Meet Requirements of IE Bulletin 82-02 IR 05000311/19860261986-09-15015 September 1986 Insp Rept 50-311/86-26 on 860826-30.Unresolved Items Noted: Replacement of Dissimilar Metal Welded Joints & Overall Pipe Replacement Program on Svc Water Sys & Correction of Equipment Identified in 860826 Event IR 05000272/19860071986-04-0303 April 1986 Insp Repts 50-272/86-07 & 50-311/86-07 on 860224-28. Violation Noted:Inadequate Measures to Assure Design Bases Important to Safety Structures Correctly Translated Into Procedures IR 05000272/19860021986-03-14014 March 1986 Insp Repts 50-272/86-02 & 50-311/86-02 on 860210-14.No Noncompliance Noted.Major Areas Inspected:Liquid & Gaseous Effluents Control Program & Radiochemical Measurements Program ML20137N5861986-01-24024 January 1986 Corrected 851224 Insp Repts 50-272/85-29 & 50-311/85-27.Rept Numbers Revised & Should Read 50-272/85-27 & 50-311/85-29 IR 05000311/20080101986-01-23023 January 1986 Insp Rept 50-458/85-09 on 850311-0810.Violations Noted: Failure to Adequately Check Calculations,Document & Verify Assumptions & Provide Basis for Design Input IR 05000272/19850291985-12-23023 December 1985 Insp Repts 50-272/85-29 & 50-311/85-27 on 851203-05.No Violation Noted.Major Areas Inspected:Annual partial-scale Emergency Exercise on 851204 IR 05000272/19850161985-10-0707 October 1985 Insp Repts 50-272/85-16 & 50-311/85-18 on 850708-11.No Violation Noted.Major Areas Inspected:Emergency Preparedness Program W/Emphasis on Review of Deficient Areas Noted in Insp Repts 50-272/84-39 & 50-311/84-38 IR 05000311/20050171985-08-0101 August 1985 Insp Rept 50-458/85-19 on 850311-0517.Violation Noted: Failure to Incorporate Engineering & Design Coordination Rept Info Into Drawings & Use External Historical Data in Evaluation of Suppliers IR 05000272/19850121985-06-18018 June 1985 Insp Repts 50-272/85-12 & 50-311/85-13 on 850507-31. Violation in Area of Security & Two Unresolved Items Noted. Major Areas Inspected:Operational Safety Verification,Maint Observations & Licensee Event Followup Review IR 05000272/19850081985-05-29029 May 1985 Insp Repts 50-272/85-08 & 50-311/85-09 on 850401-04.No Violation or Deviation Noted.Major Areas Inspected:Followup of Unresolved Items Re Fire Protection/Prevention Program & Corrective Steps Taken IR 05000272/19850091985-05-16016 May 1985 Safety Insp Repts 50-272/85-09 & 50-311/85-11 on 850406- 0506.No Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint Observations,Surveillance Observations & Review of Special Repts IR 05000311/20040191985-05-10010 May 1985 Insp Rept 50-458/85-22 on 850311-0419.No Violation or Deviation Noted.Major Areas Inspected:Maint Program,Test & Measurement Equipment,Surveillance Testing & Calibr Control Program,Design Changes & Mods & Document Control IR 05000311/20040011985-04-18018 April 1985 Insp Repts 50-348/85-18 & 50-364/85-18 on 850311-0401.No Violations or Deviations Noted.Major Areas Inspected: Licensee Action on Previous Enforcement Matters,Monthly Maint & Surveillance Observation & Independent Insp Effort IR 05000272/19820121982-06-14014 June 1982 IE Insp Repts 50-272/82-12 & 50-311/82-13 on 820512-0608. Noncompliance Noted:Failure to Review & Approve Procedures & Failure to Perform Surveillance Tests Re Containment Penetration Isolation Points IR 05000272/19820081982-05-27027 May 1982 IE Insp Repts 50-272/82-08 & 50-311/82-07 on 820122. Noncompliance Noted:Delivery of Shipment of Licensed Matl to Carrier for Transport W/Two Containers Not Strong,Tight Packages 1999-04-01
[Table view] Category:UTILITY
MONTHYEARML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 ML20247B6651989-05-0909 May 1989 Mgt Meeting Rept on 890307 & 0413.Major Areas Discussed: Status of Plant,Training & Safety Programs & Self Assessment Programs IR 05000272/19880061988-03-18018 March 1988 Partially Withheld Physical Security Insp Repts 50-272/88-06,50-311/88-06 & 50-354/88-04 on 880201-05 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Procedures,Security Organization & Mgt Effectiveness IR 05000254/19870251987-11-23023 November 1987 Insp Repts 50-254/87-25 & 50-265/87-25 on 870922-1105. Violations Noted.Major Areas Inspected:Licensee Implementation of Generic Ltr 85-06 Re ATWS Mitigation Sys (25020) & Onsite Followup Events IR 05000272/19870271987-10-20020 October 1987 Insp Rept 50-272/87-27 on 870921-25.No Violations Noted. Major Areas inspected:post-mod Test Program for Forthcoming Refueling Outage,Including Engineering Change (1EC) Packages,Mod Test Procedures & Test Specs IR 05000272/19870051987-03-23023 March 1987 Insp Repts 50-272/87-05 & 50-311/87-07 on 870224-27.No Violations Identified.Major Areas Inspected:Control of Internal Exposures,Processing of Routine Survey Data, Organization & Staffing & Control of Radioactive Matl IR 05000272/19870031987-03-11011 March 1987 Insp Repts 50-272/87-03 & 50-311/87-04 on 870127-0223. Violation Noted:Control & Testing of Containment Boundary Valves Incomplete IR 05000311/19870051987-03-10010 March 1987 Insp Rept 50-311/87-05 on 870203-06.No Violations Identified.Major Areas Inspected:Cycle 4 Startup Physics Testing Program,Precritical Tests,Low Power Physics Tests & Power Ascension Tests IR 05000272/19860231987-03-0404 March 1987 Mgt Meeting Repts 50-272/86-23 & 50-311/86-23 on 870203. Major Areas Discussed:Findings Re Equipment Qualification Insp,Including Equipment Qualification of Limitorque Operators & Exo Sensors Hydrogen Analyzers IR 05000272/19870021987-02-20020 February 1987 Insp Repts 50-272/87-02 & 50-311/87-02 on 870112-16. Violations Noted:Procedures Used in Performing Evaluation Found to Underestimate Anchor Bolt Loads When Compared to More Accurate Analytical Techniques IR 05000272/19870011987-02-11011 February 1987 Insp Repts 50-272/87-01 & 50-311/87-01 on 870101-26.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance & Review of Special Repts IR 05000272/19860331987-02-11011 February 1987 Radiation Safety Insp 50-272/86-33 Renumbered to Include 50-311.New Designation Is Combined Insps 50-272/86-33 & 50-311/86-33 IR 05000311/19870031987-02-0606 February 1987 Insp Rept 50-311/87-03 on 870112-23.Violation Noted:Rhr Flow Injected Into Only Two of Four RCS Cold Legs During LOCA IR 05000311/19860351987-01-0909 January 1987 Insp Rept 50-311/86-35 on 861119-27.No Violations or Deviations Noted.Major Areas Inspected:Test Witnessing, Preliminary Evaluation of Containment Integrated Leak Rate Test & Facility Tours IR 05000272/19860281986-11-0505 November 1986 Insp Repts 50-272/86-28 & 50-311/86-28 on 861001-27.No Violations Noted.Major Areas Inspected:Followup on Outstanding Insp Items,Operational Safety Verification, Maint,Surveillance,Special Repts & Licensee Events IR 05000272/19860221986-10-24024 October 1986 Insp Repts 50-272/86-22 & 50-311/86-22 on 860915-17.No Violations Noted.Major Areas Inspected:Licensee partial- Scale Emergency Exercise Conducted on 860916 IR 05000311/19860261986-09-15015 September 1986 Insp Rept 50-311/86-26 on 860826-30.Unresolved Items Noted: Replacement of Dissimilar Metal Welded Joints & Overall Pipe Replacement Program on Svc Water Sys & Correction of Equipment Identified in 860826 Event IR 05000272/19860071986-04-0303 April 1986 Insp Repts 50-272/86-07 & 50-311/86-07 on 860224-28. Violation Noted:Inadequate Measures to Assure Design Bases Important to Safety Structures Correctly Translated Into Procedures IR 05000272/19860021986-03-14014 March 1986 Insp Repts 50-272/86-02 & 50-311/86-02 on 860210-14.No Noncompliance Noted.Major Areas Inspected:Liquid & Gaseous Effluents Control Program & Radiochemical Measurements Program ML20137N5861986-01-24024 January 1986 Corrected 851224 Insp Repts 50-272/85-29 & 50-311/85-27.Rept Numbers Revised & Should Read 50-272/85-27 & 50-311/85-29 IR 05000311/20080101986-01-23023 January 1986 Insp Rept 50-458/85-09 on 850311-0810.Violations Noted: Failure to Adequately Check Calculations,Document & Verify Assumptions & Provide Basis for Design Input IR 05000272/19850291985-12-23023 December 1985 Insp Repts 50-272/85-29 & 50-311/85-27 on 851203-05.No Violation Noted.Major Areas Inspected:Annual partial-scale Emergency Exercise on 851204 IR 05000272/19850161985-10-0707 October 1985 Insp Repts 50-272/85-16 & 50-311/85-18 on 850708-11.No Violation Noted.Major Areas Inspected:Emergency Preparedness Program W/Emphasis on Review of Deficient Areas Noted in Insp Repts 50-272/84-39 & 50-311/84-38 IR 05000311/20050171985-08-0101 August 1985 Insp Rept 50-458/85-19 on 850311-0517.Violation Noted: Failure to Incorporate Engineering & Design Coordination Rept Info Into Drawings & Use External Historical Data in Evaluation of Suppliers IR 05000272/19850121985-06-18018 June 1985 Insp Repts 50-272/85-12 & 50-311/85-13 on 850507-31. Violation in Area of Security & Two Unresolved Items Noted. Major Areas Inspected:Operational Safety Verification,Maint Observations & Licensee Event Followup Review IR 05000272/19850081985-05-29029 May 1985 Insp Repts 50-272/85-08 & 50-311/85-09 on 850401-04.No Violation or Deviation Noted.Major Areas Inspected:Followup of Unresolved Items Re Fire Protection/Prevention Program & Corrective Steps Taken IR 05000272/19850091985-05-16016 May 1985 Safety Insp Repts 50-272/85-09 & 50-311/85-11 on 850406- 0506.No Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint Observations,Surveillance Observations & Review of Special Repts IR 05000311/20040191985-05-10010 May 1985 Insp Rept 50-458/85-22 on 850311-0419.No Violation or Deviation Noted.Major Areas Inspected:Maint Program,Test & Measurement Equipment,Surveillance Testing & Calibr Control Program,Design Changes & Mods & Document Control IR 05000311/20040011985-04-18018 April 1985 Insp Repts 50-348/85-18 & 50-364/85-18 on 850311-0401.No Violations or Deviations Noted.Major Areas Inspected: Licensee Action on Previous Enforcement Matters,Monthly Maint & Surveillance Observation & Independent Insp Effort IR 05000272/19820121982-06-14014 June 1982 IE Insp Repts 50-272/82-12 & 50-311/82-13 on 820512-0608. Noncompliance Noted:Failure to Review & Approve Procedures & Failure to Perform Surveillance Tests Re Containment Penetration Isolation Points IR 05000272/19820081982-05-27027 May 1982 IE Insp Repts 50-272/82-08 & 50-311/82-07 on 820122. Noncompliance Noted:Delivery of Shipment of Licensed Matl to Carrier for Transport W/Two Containers Not Strong,Tight Packages 1989-08-15
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-I-99-043, on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power1999-09-16016 September 1999 PNO-I-99-043:on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power IR 05000272/19990011999-04-0101 April 1999 Insp Repts 50-272/99-01 & 50-311/99-01 on 990117-0307.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support PNO-I-98-057, on 981130,util Commenced Shutdown of Salem Unit 2 to Repair 21 RCP Seal.Resident Inspectors Observed Portions of Plant Shutdown & Plan to Observe Continuing Maint Activities on RCP Seal1998-12-0101 December 1998 PNO-I-98-057:on 981130,util Commenced Shutdown of Salem Unit 2 to Repair 21 RCP Seal.Resident Inspectors Observed Portions of Plant Shutdown & Plan to Observe Continuing Maint Activities on RCP Seal IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities ML20217N6221998-04-24024 April 1998 Notice of Violation from Investigation Conducted by Oi. Violation Noted:Safeguard Event Log,Required to Be Maintained by Licensee,Was Not Complete & Accurate in All Matl Aspects ML20217E7851997-07-25025 July 1997 Investigation Rept 1-96-024 on 970725.No Noncompliance Noted.Major Areas Investigated:Allegations Re Failure to Make 10CFR73.71 Notification by Station Security Dept ML20202D0971997-03-31031 March 1997 Investigation Rept 1-95-013 on 970331.No Noncompliance Noted.Major Areas Investigated:Allegation Re Pse&G Intentionally Operated Outside Design Basis & Failed to Make Timely Notification to Nrc,Per 10CFR50.72 ML20137B6021997-03-18018 March 1997 Notice of Violation Identified in Correspondence Between 961105 & 970212.Violations Noted:Conducted Requalification Program Such That Annual Operating Test Not Provided for Fourteen Plant Licensed Operators in CY96 IR 05000272/19970031997-02-0505 February 1997 Attachment to Insp Repts 50-272/97-03 & 50-311/97-03 ,consisting of 970205 Slide Presentation Inadvertently Omitted from Repts ML20134B6741997-01-27027 January 1997 Notice of Violation from Insp on 961110-1221.Violations Noted:Vital Area Access Control & Badge Sys Requirements of Util Security Plan Were Not Implemented for Listed Examples IR 05000354/19960101997-01-27027 January 1997 Insp Rept 50-354/96-10 on 961110-1221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Security Program Plan ML20133A4491996-12-11011 December 1996 Notice of Violation from Insp on 960815-0903.Violation Noted:On 960814,vital Area Access Not Physically Controlled in That Positive Access Control Over Photobadge Keycards Compromised,Creating Opportunity for Unauthorized Access ML20133A4341996-12-11011 December 1996 Notice of Violation from Investigation Repts 1-94-006R & 1-94-053 on 940218-960430 & 941121-960425.Violation Noted: Licensee Through Former Manager of Nsr,Discriminated in Nov 93 & May 94 Against Former Onsite Safety Review Engineer IR 05000272/19960131996-12-0303 December 1996 Insp Repts 50-272/96-13 & 50-311/96-13 on 960812-0920. Violations Noted.Major Areas Inspected:Engineering Performance Issues That Require Resolution Prior to Plant Restart ML20135B2681995-04-11011 April 1995 Notice of Violation from Investigation 1-93-021R.Violation Noted:C Vondra Deliberately Caused Pse&G to Violate 10CFR50.7 by Discriminating Against Two Employees for Engaging in Protected Activities ML20135A9461994-03-0909 March 1994 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Noncompliance Noted:On 931012,maint on Breaker for electro-hydraulic Pump Was Conducted W/O Supervisor Ensuring Equipment Was Tagged & Safe to Work on PNO-I-93-068, on 931203,ALCO Emergency Diesel Generator Cylinder Cracking Discovered.Health Physics Technician Noticed Coolant Leaking from Number 3 Cylinder Sleeve on Right Bank of Cylinders (3R)1993-12-0707 December 1993 PNO-I-93-068:on 931203,ALCO Emergency Diesel Generator Cylinder Cracking Discovered.Health Physics Technician Noticed Coolant Leaking from Number 3 Cylinder Sleeve on Right Bank of Cylinders (3R) PNO-I-93-062, on 931112,informed That Current 30-day Contract Extension W/United Govt Security Officers of America Will Expire on 931115.Licensee Indicated That They Have Adequate Personnel Trained & Available to Satisfy Security Plan1993-11-12012 November 1993 PNO-I-93-062:on 931112,informed That Current 30-day Contract Extension W/United Govt Security Officers of America Will Expire on 931115.Licensee Indicated That They Have Adequate Personnel Trained & Available to Satisfy Security Plan PNO-I-93-060, on 931102,fire Reported in 230 Volt Lighting Transformer in Turbine Bldg.Caused by Loose Electrical Connection.State of Nj Has Been Notified1993-11-0303 November 1993 PNO-I-93-060:on 931102,fire Reported in 230 Volt Lighting Transformer in Turbine Bldg.Caused by Loose Electrical Connection.State of Nj Has Been Notified ML20058P9361993-10-15015 October 1993 Notice of Violation from Insp on 920614-0725.Violation Noted:Licensee Determined Several Instances in Which Personnel Assigned to Fire Watch Patrols Failed to Perform or Complete Function as Required by TS & Falsified Records IR 05000272/19910991993-07-29029 July 1993 Initial Draft SALP Repts 50-272/91-99,50-311/91-99 & 50-354/91-99 for 911229-930619 IR 05000272/19920211993-01-27027 January 1993 Exam Repts 50-272/92-21OL & 50-311/92-21OL on 921214-17.Exam Results:All Six SRO Candidates Passed All Portions of Exam & Issued Licenses PNO-I-92-075, upon Investigation of Alarm Printed Out on Auxiliary Typewriter on 921213,operators Determined That Cpu for Overhead Annunciator (Oha) Had Failed to Perform, Resulting in Loss of Oha Sys for 1 H & 41 Minutes1992-12-15015 December 1992 PNO-I-92-075:upon Investigation of Alarm Printed Out on Auxiliary Typewriter on 921213,operators Determined That Cpu for Overhead Annunciator (Oha) Had Failed to Perform, Resulting in Loss of Oha Sys for 1 H & 41 Minutes PNO-I-90-056, on 900722,potential Design Deficiency in Main Steam Isolation Sys Noted.Units Shut Down Until Final Analysis & Appropriate Corrective Actions Completed1990-07-23023 July 1990 PNO-I-90-056:on 900722,potential Design Deficiency in Main Steam Isolation Sys Noted.Units Shut Down Until Final Analysis & Appropriate Corrective Actions Completed ML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 ML20247B6651989-05-0909 May 1989 Mgt Meeting Rept on 890307 & 0413.Major Areas Discussed: Status of Plant,Training & Safety Programs & Self Assessment Programs IR 05000272/19880061988-03-18018 March 1988 Partially Withheld Physical Security Insp Repts 50-272/88-06,50-311/88-06 & 50-354/88-04 on 880201-05 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Procedures,Security Organization & Mgt Effectiveness IR 05000354/19860991988-03-0404 March 1988 SALP Rept 50-354/86-99 on 861201-880115 PNO-I-88-020, on 880216,CA Mcneill Named Executive Director - Nuclear W/Responsibility of Directing Nuclear Operations, Including Nuclear Dept Reorganization & Restart Efforts of Peach Bottom1988-02-16016 February 1988 PNO-I-88-020:on 880216,CA Mcneill Named Executive Director - Nuclear W/Responsibility of Directing Nuclear Operations, Including Nuclear Dept Reorganization & Restart Efforts of Peach Bottom IR 05000272/19860991988-02-0505 February 1988 SALP Repts 50-272/86-99 & 50-311/86-99 for Oct 1986 - Dec 1987 IR 05000254/19870251987-11-23023 November 1987 Insp Repts 50-254/87-25 & 50-265/87-25 on 870922-1105. Violations Noted.Major Areas Inspected:Licensee Implementation of Generic Ltr 85-06 Re ATWS Mitigation Sys (25020) & Onsite Followup Events IR 05000272/19870261987-11-0909 November 1987 Exam Repts 50-272/87-26OL & 50-311/87-26OL on 870915-17.Exam Results:All Four Senior Reactor Operator Candidates Passed Written & Operating Exams ML20217F8541987-10-27027 October 1987 PNS-I-87-017:on 871026,fireman Received Call of Bomb Threat at Plant.Search of Facility Proved Negative PNO-I-87-099, on 871023,licensee Notified Region I of Addl Uncertainties in Onsite Electrical Distribution Sys Design W/Potential for Breaker Coordination Problems.Unit Shutdown Commenced on 871023.Analysis Underway1987-10-26026 October 1987 PNO-I-87-099:on 871023,licensee Notified Region I of Addl Uncertainties in Onsite Electrical Distribution Sys Design W/Potential for Breaker Coordination Problems.Unit Shutdown Commenced on 871023.Analysis Underway IR 05000272/19870271987-10-20020 October 1987 Insp Rept 50-272/87-27 on 870921-25.No Violations Noted. Major Areas inspected:post-mod Test Program for Forthcoming Refueling Outage,Including Engineering Change (1EC) Packages,Mod Test Procedures & Test Specs IR 05000272/19870211987-08-17017 August 1987 Requalification Evaluation Repts 50-272/87-21OL & 50-311/87-26OL on 870615-19.Exam Results:Two Senior Reactor Operators & Three Reactor Operators Passed All Portions of Exam.Program Found Unsatisfactory,Per NUREG-1021 PNO-I-87-075A, on 870812,visual Insp Identified No Significant Corrosion of Reactor Vessel Studs After Finding Leak on 870807.Further Insp of Degraded Vessel Components Will Be Formalized After Cleaning Affected Areas1987-08-13013 August 1987 PNO-I-87-075A:on 870812,visual Insp Identified No Significant Corrosion of Reactor Vessel Studs After Finding Leak on 870807.Further Insp of Degraded Vessel Components Will Be Formalized After Cleaning Affected Areas PNO-I-87-060, on 870703,unit Removed from Svc to Make Repairs to Low Pressure Turbines 21 & 22.Unit Being Maintained in Hot Shutdown.Licensee Expects to Complete Turbine Gasket Repairs within 14 Days1987-07-0606 July 1987 PNO-I-87-060:on 870703,unit Removed from Svc to Make Repairs to Low Pressure Turbines 21 & 22.Unit Being Maintained in Hot Shutdown.Licensee Expects to Complete Turbine Gasket Repairs within 14 Days PNO-I-87-059, on 870626,operators Received High Vibration Alarm on Bearing 6 of Low Pressure Turbine 22.Bearing Vibration Increased & High Pitched Noise Discovered.Licensee Elected to Remove Unit from Svc1987-06-26026 June 1987 PNO-I-87-059:on 870626,operators Received High Vibration Alarm on Bearing 6 of Low Pressure Turbine 22.Bearing Vibration Increased & High Pitched Noise Discovered.Licensee Elected to Remove Unit from Svc ML20154D4561987-06-15015 June 1987 Notice of Violation from Insp on 831205-06 & 840116-20. Violations Noted:Fire Protection Features Not Provided for Certain Redundant Trains of Equipment &/Or Cabling Located Outside Primary Containment PNO-I-87-038, on 870429,licensee Learned That Control Room Operator Tested Positive for Use of Controlled Substance. Employee Will Be Terminated.Individual Acceptance Into Rehabilitation Program Under Consideration1987-04-29029 April 1987 PNO-I-87-038:on 870429,licensee Learned That Control Room Operator Tested Positive for Use of Controlled Substance. Employee Will Be Terminated.Individual Acceptance Into Rehabilitation Program Under Consideration IR 05000272/19870051987-03-23023 March 1987 Insp Repts 50-272/87-05 & 50-311/87-07 on 870224-27.No Violations Identified.Major Areas Inspected:Control of Internal Exposures,Processing of Routine Survey Data, Organization & Staffing & Control of Radioactive Matl ML20207S4181987-03-12012 March 1987 Notice of Violation from Insp on 870127-0223 IR 05000272/19870031987-03-11011 March 1987 Insp Repts 50-272/87-03 & 50-311/87-04 on 870127-0223. Violation Noted:Control & Testing of Containment Boundary Valves Incomplete IR 05000311/19870051987-03-10010 March 1987 Insp Rept 50-311/87-05 on 870203-06.No Violations Identified.Major Areas Inspected:Cycle 4 Startup Physics Testing Program,Precritical Tests,Low Power Physics Tests & Power Ascension Tests IR 05000311/19870061987-03-0909 March 1987 Exam Rept 50-311/87-06OL on 870213.Exam Results:One Candidate Administered Oral Exam Failed Due to Lack of Knowledge of Tech Specs Unique to Unit 2 IR 05000272/19860231987-03-0404 March 1987 Mgt Meeting Repts 50-272/86-23 & 50-311/86-23 on 870203. Major Areas Discussed:Findings Re Equipment Qualification Insp,Including Equipment Qualification of Limitorque Operators & Exo Sensors Hydrogen Analyzers IR 05000272/19850981987-02-27027 February 1987 Corrected SALP Repts 50-272/85-98 & 50-311/85-98 for Oct 1985 - Sept 1986 ML20212B9751987-02-20020 February 1987 Notice of Violation from Insp on 870112-16 IR 05000272/19870021987-02-20020 February 1987 Insp Repts 50-272/87-02 & 50-311/87-02 on 870112-16. Violations Noted:Procedures Used in Performing Evaluation Found to Underestimate Anchor Bolt Loads When Compared to More Accurate Analytical Techniques 1999-09-16
[Table view] |
Inspection Report - Salem - 1986023 |
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U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Report No. 86-23 50-272 Docket N DPR-70 License No. OPR-75 Category C Licensee: Public Service Electric and Gas Company 80 Park Place Newark, New Jersey 07101
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Facility Name: Salem Generating Station, Units 1 and 2 Meeting At: NRC Region I Office, King of Prussia, PA Prepared by: b 7O C. Ande/ son, Chief, Plant Systems date Section, DRS Meeting Summary: Meeting at NRC Region I on February 3,1987 to discuss several of the findings related to the Equipment Qualification inspection 50-272/86-23; 50-311/86-2 The major items discussed were items 86-23-04, 05 and 06 in inspection report 86-23 related to the equipment qualification of Limitorque operators, Exo Sensors Hydrogen Analyzers and ASCO Solenoid valves respectivel PDR ADOCK 05000272 O PDR
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DETAILS Participants 1.1 Public Service Electric and Gas Company C. McNeill, Vice President, Nuclear B. Preston, Manager-Licensing and Regulation R. Gura, Manager-Engineering R. Smith, Engineer G. Lambert, Principal Engineer 1.2 Nuclear Regulatory Commission S. Ebneter, Director Division of Reactor Safety W. Kane, Director Division of Reactor Projects R. Gallo, Chief, Projects Branch 2 L. Norrholm, Chief, Reactor Projects Section 2B C. Anderson, Chief, Plant Systems Section G. Hubbard, Engineer, IE R. Paolino, Lead Reactor Engineer L. Cheung, Reactor Engineer Purpose and Background An inspection was conducted on August 11-15, 1986, at Salem Nuclear Generating Station, Units 1 and 2 of their program to meet the require-ments of 10 CFR 50.49. The licensee responded to the inspection findings in two letters from C. McNeill of PSE&G to J. Taylor of NRC dated November 7, 1986 and December 15, 1986. In these letters they indicated that they disagreed with some of the inspection finding This meeting was held at the request of Public Service Electric and Gas Company so they could provide their views on several of the findings of the inspectio . Presentation and Discussion A copy of the meeting notice and the meeting agenda is attached. The licensee indicated that they wished to discuss items 86-23-04, 05 and 06 l in inspection 86-23. They indicated that they were not contesting the inspection findings for items 03 and 09. A copy of the licensee's presentation slides for items 04, 05 and 06 is attache Items 86-23-04 related to the equipment qualification of Limitorque operators. The NRC concern related to the absence of operator gear case grease relief valves. Public Service Electric and Gas, PSE&G, personnel stated that they had determined through a phone call with Limitorque,
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prior to the inspection, that grease relief valves were not required to satisfy the EQ requirements for their application at Salem. They provided the technical basis for their conclusion. The NRC agreed that their arguments had technical merit. However, it was noted by the NRC that PSE&G should have documented these arguments in the Limitorque EQ file prior to the time of the inspectio Items 86-23-05 related to the equipment qualification of Exo Sensors Hydrogen Analyzers. The NRC concern was that the files did not provide
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an adequate basis for the qualified life for the pressure transmitters and the RTDs used in the analyzer PSE&G personnel indicated that information included in the file at the time of the inspection supported a ten year life for these subcomponents. In addition, at the end of the inspection, they provided information to the NRC to support the subcomponent lif The NRC stated that the information provided near the end of the inspection appeared to support the subcomponent ten year life. However, the NRC noted that the technical basis for the analyzer subcomponents' life of ten years should have been documented in the Exo Sensors Hydrogen analyzer EQ file prior to the NRC inspectio Item 86-23-06 related to the qualification of ASCO solenoid valves. The NRC concern was that the EQ file for this item was not clear regarding support of a 120 day post-accident operability requirement. PSE&G personnel provided clarification regarding the information in the fil The NRC agreed that this clarification appeared adequate to support the required post-accident operating tim The NRC requested an opportunity to conduct a summary review of a report documenting the review of the PSE&G EQ program that PSE&G personnel had performed by an outside consultant. PSE&G personnel stated their view that their contractor's review went beyond the requirements of 10 CFR 50, Appendix B for licensee internal audits. The NRC conducted a summary review of the subject report. The staff concluded that the report identified deficiencies similar to those identified by the NRC EQ inspection tea The licensee indicated that they planned to take a closer look at the EQ findings identified by their consultant. They also indicated that they plan to develop an engineering manual which will address some of the EQ documentation deficiencies identified by the EQ tea . Concluding Remarks The NRC staff thanked the licensee for their presentation. The informa-tion presented by the licensee during the meeting will be considered in the NRC review of potential enforcement actions related to the EQ in-spectio . -
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MEETING ;,GENDA DISCUSSION OF POTENTIAL ENFORCEMENT / UNRESOLVED ITEMS
- SALEM EQUIPMENT GUALIFICATION INSPECTION LOCATION: NRC Region I OATE: February 3, 1987 TIME: 9:30 '
PURPOSE OF MEETING To discuss the status of those items identified as Potential Enforcement / Unresolved Items in Inspection Report 50-272/86-23; 50-311/86-23 under the enforcement criteria delineated in NRC Generic Letter 86-1 ITEMS OF OISCUSSION 1 Introduction of attendees -
2. Current status of EQ Enforcement Criteria
- Clarifications
- Enforcement Actions
- Regulatory implications NRC Representatives 3. PSE&G Responses to IR 50-272/86-23: 50-311/86-23 Potential Enforcement / Unresolved Items identified unden Generic Letter 86-15 enforcement criteri Rockbestos coaxial and EPR cables
-- 86-23-04 Limitorque Operator Gear Case Grease Relief Valves
- 86-23-05 Exo' Sensors Hydrogen Analyzers
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- 86-23-06 ASCO Solenoid Valves
- 86-23-09 Scotch 70/ construction electric wiring splices PSE&G Representatives
, Summary Discussion l - NRC response to technical resentation l - Projection of enforcement action and schedule l
l PSE&G Attendees C.A. NcNeill, Jr./ R.A. Burricelli i
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R.L Gura C.U. Lambert i
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R. Smith 8.A. Preston/ 0.J.Vito
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LIMITOROUE OPERATORS POTENTIAL ENFORCEMENT / UNRESOLVED ITEM 86-23-04:
PSE8G HAD NOT ESTABLISHED QUALIFICATION OF INSIDE CONTAINMENT LIMITORQUE OPERATORS BECAUSE PSE&G HAD NOT DEMONSTRATED THAT THE USE OF OPERATORS WITHOUT GEAR CASE GREASE RELIEF VALVES WAS ACCEPTABL JUSTIFICATION FOR USE OF THE OPERATORS WITHOUT THE RELIEF VALVES WAS PROVIDED DURING THE INSPECTIO PSE8G'S POSITIUk PSE&G CONTACTED LIMITOROUE BY PHONE IN APRIL 1986, REQUESTING CLARIFICATION ON THE ISSUE OF CORRECT INSTALLATION OF GREASE RELIEF VALVE PHONE CONVERSATION LEAD PSE86 TO BELIEVE THAT THE USE OR NON-USE OF GREASE RELIEF VALVES WOULD:
- NOT AFFECT THE OPERABILITY OR SAFETY FUNCTION OF THE OPERATOR
- NOT AFFECT THE QUALIFICATION STATUS OF THE OPERATOR NOT MANDATORY, BASED ON ENGINEERING JUDGEMENT LIMITORQUE DOES NOT ISSUE WRITTEN INSTRUCTIONS ON THE PROPER INSTALLATION OF GREASE RELIEFS ENGINEERING JUDGEMENT, BASED ON AVAILABLE INFORMATION, DETERMINED GREASE RELIEFS WERE NOT A SIGNIFICANT PROBLEM FOR THE SALEM STATION AND NO CORRECTIVE ACTION WAS REQUIRE SUPPLEMENTAL ANALYSIS WAS PROVIDED TO THE INSPECTORS AND WAS JUDGED ACCEPTABL SUPPLEMENTAL ANALYSIS CONFIRMED PSE&G'S POSITIO .
s DA9
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EX0 SENSURS HYDROGEN ANALYZER POTENTIAL ENFORCEMENT / UNRESOLVED ITEM 86-23-05:
AT THE TIME OF THE INSPECTION, THE QUALIFICATION FILES DID NOT PROVIDE ADEQUATE BASIS FOR THE QUALIFIED LIFE FOR THE PRESSURE TRANSMITTERS AND THE RTDS USED IN THE Ex0 SENSORS HYDROGEN ANALYZER PSE&G'S POSITION -
PSE8G BELIEVES.THIS POTENTIAL ENFORCEMENT ITEM IS UNWARRANTED FOR THE FOLLOWING REASONS:
COMPONENT DESIGN LIFE WAS ORIGINALLY STATED AS SIGNIFICANTLY IN EXCESS OF THE LEVELS REQUIRED, THEREFORE, THE VENDOR DETERMINED AGING TESTS WERE NOT REQUIRED TO BE EXTENDED PAST 2 YEAR IHE Ex0 SENSOR STATED MAINTENANCE CYCLE OF 120 MONTHS FOR THE PRESSURE TRANSDUCER AND RTD WAS CONTAINED IN THEIR OPERATION AND MAINTENANCE (O&M) MANUA THE QUALIFICATION REPORT WAS MARKED TO SHOW THAT THE EQUIVALENT AGE FOR THE PRESSURE TRANSDUCER AND RID WAS 10 YEARS PER TELECON WITH EXO-SENSOR ON 9/5/84 IESTING TO SUPPORT THE LIFE EXTENSION WAS AVAILABLE TO SUPPORT THE TELECON DISCUSSION OF 9/5/84 08M MANUAL REPLACEMENT PERIOD OF 10 YEARS CORRELATED WITH
- 10 YEARS EQUIVALENT AGE OBTAINED DURING VENDOR TELECO SUMMARY DATA SUPPORTING THE EXTENDED LIFE WAS MADE AVAILABLE FROM Ex0-SENSOR'S FILES DURING THE INSPECTION SUPPORTING THIS POSITION.
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ASCO SOLEN 0ID VALVES POTENTIAL ENFORCEMENT / UNRESOLVED ITEM 86-23-06:
AT THE TIME OF THE INSPECTION, THE QUALIFICATION FILES FOR ASCO SOLEN 0ID VALVES FAILED TO DEMONSTRATE THAT THE VALVES COULD MEET THE SPECIFIED POST-ACCIDENT OPERABILITY REQUIREMENT .
PSE&G'S POSITION ANFORMATION IN THE QUALIFICATION FILE DID ADEQUATELY DEMONSTRATE, BY AN ACCEPTABLE MEANS, THAT THE VALVE POST-ACCIDENT OPERABILITY TIME ENVELOPED THE 120 DAY REQUIREMEN PART OF THE PACKAGE REVIEWED BY THE INSPECTORS WAS A GENERAL PURPOSE DOCUMENT LISTING EXAMPLES OF EXTRAPOLATION METHODS TO THE 10 C RULE AND ARRHENIUS THEOR (00 ANALYSIS 1 AND 2)
4D ANALYSIS 3 IS " FILE SPECIFIC" AND ADEQUATELY DEMONSTRATES THAT THE VALVES MEET THE 120 DAY REQUIREMEN SALEM STATION REACHES A STEADY STATE CONDITION AFTER 24 HOURS (1 DAY). ACTUAL TEST DATA MUST BE USED FOR THIS PERIO EXTRAPOLATION MUST DEMONSTRATE THAT (120-1 = 119) 119 DAYS CAN BE OBTAINED BY THE ARRHENIUS METHODOLOG RESULT OF' ANALYSIS INDICATES THAT "T PLANT >> 119 DAYS"
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EXTRAPOLATION GREATER THAN 119 DAYS PLUS 1 DAY ACTUAL TEST DATA = 120 DAYS DA10
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