IR 05000259/2015003

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IR 05000259/2015003, 05000260/2015003, 05000296/2015003; on 07/01/15 - 09/30/15, Browns Ferry Nuclear Plant, Units 1, 2 and 3; Problem Identification and Resolution of Problems
ML15313A352
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 11/09/2015
From: Alan Blamey
Reactor Projects Region 2 Branch 6
To: James Shea
Tennessee Valley Authority
References
IR 2015003
Download: ML15313A352 (27)


Text

UNITED STATES ovember 9, 2015

SUBJECT:

BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2015003, 05000260/2015003, AND 05000296/2015003

Dear Mr. Shea:

On September 30, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. On October 16, 2015, the NRC inspectors discussed the results of this inspection with Mr. S. Bono and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented one finding which was determined to be of very low safety significance (Green) in this report. This finding involved a violation of NRC requirements.

The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Browns Ferry Nuclear Plant.

In addition, if you disagree with the cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, RII, and the NRC Senior Resident Inspector at Browns Ferry Nuclear Plant. In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Alan Blamey, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68

Enclosure:

NRC Integrated Inspection Report 05000259/2015003, 05000260/2015003 and 05000296/2015003

REGION II==

Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68 Report No.: 05000259/2015003, 05000260/2015003, 05000296/2015003 Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3 Location: Corner of Shaw and Nuclear Plant Road Athens, AL 35611 Dates: July 1, 2015, through September 30, 2015 Inspectors: D. Dumbacher, Senior Resident Inspector T. Stephen, Resident Inspector A. Ruh, Resident Inspector Approved by: Alan Blamey, Chief Reactor Projects Branch 6 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

05000259/2015003, 05000260/2015003, 05000296/2015003; Browns Ferry Nuclear Plant,

Units 1, 2 and 3; Problem Identification and Resolution of Problems.

The report covered a three-month period of inspection by resident inspectors. One NRC identified violation was identified. The significance of inspection findings are indicated by their color (i.e. Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC)0609, "Significance Determination Process" (SDP) dated April 29, 2015. Cross-cutting aspects are determined using IMC 0310, Components Within the Cross Cutting Areas dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy dated February 4, 2015. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 5.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

An NRC identified NCV of 10 CFR Part 50, Appendix B, Criterion XVI was identified for the licensee's failure to establish measures to promptly identify a condition adverse to quality involving the malfunction of the High Pressure Coolant Injection (HPCI) turbine exhaust system. Upon discovery of the malfunction, the licensee took action to determine that HPCI remained operable despite the degraded and nonconforming condition. The licensee is developing corrective actions to resolve the degraded and nonconforming condition. The licensee entered the violation into the licensee's corrective action program as CR 1098320.

The performance deficiency was more-than-minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and it adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, the performance deficiency resulted in the HPCI system being operated with an unidentified degraded/non-conforming condition which degraded the system capability and challenged system operabilty. The inspectors determined the finding was Green because the finding was a deficiency affecting the qualification of HPCI, but based on the licensees evaluations, operability was maintained. The inspectors determined that the finding had a cross-cutting aspect in the Problem Identification and Resolution area of Evaluation [P.2], because the licensee did not thoroughly evaluate an abnormal system condition to ensure that resolutions addressed causes commensurate with their safety significance. (Section 4OA2)

Licensee-Identified Violations

No findings were identified.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at 100 percent of rated thermal power (RTP) except for 5 unplanned downpowers and 3 planned downpowers. A July 14, 2015 unplanned downpower to 99 percent power was performed due to entry into LCO 3.0.3 (EN 51231). July 19, 2015 and July 28, 2015 unplanned downpowers to 95 percent power were performed to maintain vacuum in the main condenser. An August 29, 2015 unplanned downpower to 42 percent and an August 31, 2015 unplanned downpower to 38 percent power were performed due to tripping of the 1B recirculation pump. The 3 planned downpowers occurred on July 22, 2015, July 24, 2015, and September 11, 2015, for maintenance.

Unit 2 operated at 100 percent of RTP except for 2 unplanned and 3 planned downpowers. A July 14, 2015 unplanned downpower to 99 percent power was performed due to entry into LCO 3.0.3 (EN 51231). A September 21, 2015 downpower to 45 percent power was performed due to a bearing failure on the 2A Reactor Feed Pump Turbine (RFPT) while the 2B RFPT was out of service for repairs. The three planned downpowers occurred on August 20, 2015, August 21, 2015 and September 25, 2015, for maintenance.

Unit 3 operated at 100 percent of RTP except for 2 unplanned downpowers and 1 planned downpower. A July 14, 2015 unplanned downpower to 99 percent power was performed due to entry into LCO 3.0.3 (EN 51231). A July 19, 2015 unplanned downpower to 95 percent power was performed to maintain vacuum in the main condenser. The planned downpower occurred on August 28, 2015, for maintenance.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems, listed below, while the other subsystems were inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could affect operability of the redundant train or backup system. Documents reviewed are listed in the attachment. This activity constituted three Equipment Alignment Partial Walkdown inspection samples, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

.2 Complete Walkdown

a. Inspection Scope

The inspectors completed a detailed alignment verification of the Unit 3 Spent Fuel Pool Cooling and Cleanup system.

Also, the relevant operating instruction, 0-OI-78 and several other licensee analyses were used to verify equipment availability and operability. The inspectors reviewed relevant portions of the Updated Final Safety Analysis Report (UFSAR) and TS. This detailed walkdown also verified electrical power alignment, the condition of applicable system instrumentation and controls, component labeling, pipe hangers and support installation, and associated support systems status. The inspectors examined applicable System Health Reports, open Work Orders (WOs), and any previous Problem Evaluation Reports (PERs) that could affect system alignment and operability.

Documents reviewed are listed in the attachment. This activity constituted one Equipment Alignment Complete Walkdown inspection sample, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Fire Protection Tours

a. Inspection Scope

The inspectors reviewed licensee procedures for transient combustibles and fire protection impairments, and conducted a walkdown of the fire areas (FA) and fire zones (FZ) listed below. Selected FAs/FZs were examined in order to verify licensee control of transient combustibles and ignition sources; the material condition of fire protection equipment and fire barriers; and operational lineup and operational condition of fire protection features or measures. The inspectors verified that selected fire protection impairments were identified and controlled in accordance with procedures. The inspectors reviewed applicable portions of the Fire Protection Report, Volumes 1 and 2, including the applicable Fire Hazards Analysis, and Pre-Fire Plan drawings, to verify that the necessary firefighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, was in place. Documents reviewed are listed in the attachment. This activity constituted five Fire Protection Walkdown inspection samples, as defined in Inspection Procedure 71111.05.

  • Fire Area 3-1 Unit 3 Reactor Building, Elevation 519 - 565
  • Fire Area 22 Unit 3 Diesel Generator Building, Elevation 565.5 and 583.5, 4kv Shutdown Board Rooms 3EA and 3EB
  • Fire Area 25-1, Common Unit Intake Pumping Station
  • Fire Area 26, Radiological Waste Building
  • Fire Area 26, Unit 1, Unit 2 and Unit 3 Turbine buildings

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

Internal Flooding The inspectors reviewed related flood analysis documents and walked down the area listed below containing risk-significant structures, systems, and components susceptible to flooding. The inspectors verified that plant design features and plant procedures for flood mitigation were consistent with design requirements and internal flooding analysis assumptions. The inspectors also assessed the condition of flood protection barriers and drain systems. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the corrective action program. Documents reviewed are listed in the attachment. This activity constituted one Internal Flooding inspection sample, as defined in Inspection Procedure 71111.06.

  • Unit 1 A/C Equipment Room on elevation 606 of the Control Bay and Battery Room No. 1 on elevation 593 of the Control Bay

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification and Performance

.1 Licensed Operator Requalification

a. Inspection Scope

On August 3, 2015, the inspectors observed a licensed operator training session for an operating crew according to the Unit 2 Simulator Exercise Guide (SEG) OPL177(8).073, Power Reduction, Recirculation Pump Trip, Reactor Power Oscillations and Anticipated Transient Without SCRAM with Main Steam Isolation Valves open, Revision 0.

The inspectors specifically evaluated the following attributes related to the operating crews performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of procedures including Abnormal Operating Instructions (AOIs), Emergency Operating Instructions (EOIs) and Safe Shutdown Instructions (SSI)
  • Timely control board operation and manipulation, including high-risk operator actions
  • Timely oversight and direction provided by the shift supervisor, including ability to identify and implement appropriate technical specifications actions such as reporting and emergency plan actions and notifications
  • Group dynamics involved in crew performance The inspectors assessed the licensees ability to assess the performance of their licensed operators. The inspectors reviewed the post-examination critique performed by the licensee evaluators, and verified that licensee-identified issues were comparable to issues identified by the inspector. The inspectors reviewed simulator physical fidelity (i.e., the degree of similarity between the simulator and the reference plant control room, such as physical location of panels, equipment, instruments, controls, labels, and related form and function). Documents reviewed are listed in the attachment. This activity constituted one Observation of Requalification Activity inspection sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Control Room Observations

a. Inspection Scope

Inspectors observed and assessed licensed operator performance in the plant and main control room, particularly during periods of heightened activity or risk and where the activities could affect plant safety. Inspectors reviewed various licensee policies and procedures covering Conduct of Operations, Plant Operations and Power Maneuvering.

Inspectors utilized activities such as post maintenance testing, surveillance testing and other activities to focus on the following conduct of operations as appropriate;

  • Operator compliance and use of procedures.
  • Control board manipulations.
  • Communication between crew members.
  • Use and interpretation of plant instruments, indications and alarms.
  • Use of human error prevention techniques.
  • Documentation of activities, including initials and sign-offs in procedures.
  • Supervision of activities, including risk and reactivity management.
  • Pre-job briefs.

This activity constituted one Control Room Observation inspection sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine

a. Inspection Scope

The inspectors reviewed the specific structures, systems and components (SSC) within the scope of the Maintenance Rule (MR) (10CFR50.65) with regard to some or all of the following attributes, as applicable:

(1) Appropriate work practices;
(2) Identifying and addressing common cause failures;
(3) Scoping in accordance with 10 CFR 50.65(b) of the MR;
(4) Characterizing reliability issues for performance monitoring;
(5) Tracking unavailability for performance monitoring;
(6) Balancing reliability and unavailability;
(7) Trending key parameters for condition monitoring;
(8) System classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2);
(9) Appropriateness of performance criteria in accordance with 10 CFR 50.65(a)(2); and
(10) Appropriateness and adequacy of 10 CFR 50.65 (a)(1) goals, monitoring and corrective actions. The inspectors compared the licensees performance against site procedures. The inspectors reviewed, as applicable, work orders, surveillance records, PERs, system health reports, engineering evaluations, and MR expert panel minutes; and attended MR expert panel meetings to verify that regulatory and procedural requirements were met.

Documents reviewed are listed in the attachment. This activity constituted two Maintenance Effectiveness inspection samples, as defined in Inspection Procedure 71111.12.

  • 2A Reactor Feed Pump Turbine failure.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

For planned online work and/or emergent work that affected the combinations of risk significant systems listed below, the inspectors examined on-line maintenance risk assessments, and actions taken to plan and/or control work activities to effectively manage and minimize risk. The inspectors verified that risk assessments and applicable risk management actions (RMA) were conducted as required by 10 CFR 50.65(a)(4) and applicable plant procedures. As applicable, the inspectors verified the actual in-plant configurations to ensure accuracy of the licensees risk assessments and adequacy of RMA implementations. Documents reviewed are listed in the attachment. This activity constituted five Maintenance Risk Assessment inspection samples, as defined in Inspection Procedure 71111.13.

  • Elevated risk due to an extended out of service for 2-year preventative maintenance on 3A Emergency Diesel Generator on July 26, 2015
  • Reviewed Risk management actions associated with out of service to 1A Residual Heat Removal (RHR) train on August 5, 2015
  • Reviewed risk management actions associated with 3E Shutdown Board, 3 Emergency Diesel Generator and C Standby Gas Treatment inoperable on August 21, 2015
  • Elevated trip risk due to major switchyard work making Bus 2 unavailable on August 18, 2015
  • Elevated risk due to maintenance window for Unit 3 HPCI system on September 9, 2015

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessment

a. Inspection Scope

The inspectors reviewed the operability/functional evaluations listed below to verify technical adequacy and ensure that the licensee had adequately assessed TS operability. The inspectors reviewed applicable sections of the UFSAR to verify that the system or component remained available to perform its intended function. In addition, where appropriate, the inspectors reviewed licensee procedures to ensure that the licensees evaluation met procedure requirements. Where applicable, inspectors examined the implementation of compensatory measures to verify that they achieved the intended purpose and that the measures were adequately controlled. The inspectors reviewed PERs on a daily basis to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the attachment. This activity constituted seven total Operability Evaluation inspection samples, one being an Operator Work Around inspection sample, as defined in Inspection Procedure 71111.15.

  • Unit 1 HPCI Steamline Inboard Injection Valve 1-FCV-73-2 closing stroke time exceeded Inservice Test limit (CR 1061051)
  • Unit 2 RCIC system oil leaks (CR 1043271 and 1048485)
  • EDG B 7 day tank level gauge reading incorrectly (CR 1059820)
  • Unit 3 HPCI evaluation of potential water cannon effects on turbine exhaust line (CR 1071880)
  • Dried concrete density for the Holtec International Storage Module (HI-STORM)

Flood and Wind (FW) casks was less than the required range (CR 1049026)

  • HPCI Operator Work Around (OWA) for auxiliary oil pump running.

b. Findings

No findings were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors witnessed and reviewed post-maintenance tests (PMT) listed below to verify that procedures and test activities confirmed Structure, System, or Component (SSC) operability and functional capability following the described maintenance. The inspectors reviewed the licensees completed test procedures to ensure any of the SSC safety function(s) that may have been affected were adequately tested, that the acceptance criteria were consistent with information in the applicable licensing basis and/or design basis documents. The inspectors witnessed and/or reviewed the test data, to verify that test results adequately demonstrated restoration of the affected safety function(s). The inspectors verified that problems associated with PMTs were identified and entered into the Corrective Action Program (CAP). Documents reviewed are listed in the attachment. This activity constituted seven Post Maintenance Test inspection samples, as defined in Inspection Procedure 71111.19.

  • WOs 11666097,115638101 Unit 3 HPCI PMT following calibration and troubleshooting on valve 3-LCV-73-8

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed portions of, and/or reviewed completed test data for the following surveillance tests of risk-significant and/or safety-related systems to verify that the tests met technical specification surveillance requirements, UFSAR commitments, and in-service testing and licensee procedure requirements. The inspectors review confirmed whether the testing effectively demonstrated that the SSCs were operationally capable of performing their intended safety functions and fulfilled the intent of the associated surveillance requirement. Documents reviewed are listed in the attachment.

This activity constituted two Surveillance Testing inspection samples: one routine test, and one in-service test, as defined in Inspection Procedure 71111.22.

Routine Surveillance Test:

  • 2-SR 3.5.3.3, RCIC System Rated Flow at Normal Operating Pressure (WO 115435510)

In-service Test:

116965233)

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness (EP)

1EP6 Drill Evaluation

.1 EP Radiological Emergency Plan (REP) training drill

a. Inspection Scope

The inspectors observed an EP REP training drill that contributed to the licensees Drill/Exercise Performance and Emergency Response Organization performance indicator (PI) measures on September 2, 2015. This drill was intended to identify any licensee weaknesses and deficiencies in classification, notification, dose assessment and protective action recommendation (PAR) development activities. The inspectors observed emergency response operations in the Technical Support Center (TSC) and the Operations Support Center (OSC) to verify that event classification and notifications were done in accordance with EPIP-1, Emergency Classification Procedure, and licensee conformance with other applicable Emergency Plan Implementing Procedures.

The inspectors attended the post-drill critique to compare any inspector-observed weaknesses with those identified by the licensee in order to verify whether the licensee was properly identifying EP related issues and entering them in to the CAP, as appropriate. Documents reviewed are listed in the attachment. This activity constituted one EP evaluation inspection sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1 Cornerstone: Mitigating Systems

a. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and reporting the following PIs. The inspectors examined the licensees PI data for the specific PIs listed below for the third quarter 2014 through second quarter of 2015.

Additional data was also reviewed for the second quarter of 2014 for Safety System Functional Failures. The inspectors reviewed the licensees data and graphical representations as reported to the NRC to verify that the data was correctly reported.

The inspectors validated this data against relevant licensee records (e.g., PERs, Daily Operator Logs, Plan of the Day, Licensee Event Reports, etc.), and assessed any reported problems regarding implementation of the PI program. The inspectors verified that the PI data was appropriately captured, calculated correctly, and discrepancies resolved. The inspectors used the Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, to ensure that industry reporting guidelines were appropriately applied. This activity constituted twelve PI inspection samples, as defined in Inspection Procedure 71151.

  • Units 1, 2, and 3 Emergency AC power system
  • Units 1, 2, and 3 Cooling Water systems
  • Units 1, 2, and 3 Safety System Functional Failures

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution of Problems

.1 Review of items entered into the Corrective Action Program:

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished by reviewing daily CR reports, and periodically attending Management Review Committee (MRC) and Plant Screening Committee (PSC) meetings.

b. Findings

1.

Introduction:

The NRC identified a Green non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XVI for the licensee's failure to establish measures to promptly identify a condition adverse to quality involving the malfunction of the HPCI turbine exhaust system. Specifically, on multiple occasions the licensee had indications of water entering the HPCI turbine casing following surveillance runs, but failed to recognize that the water intrusion was indicative of a degraded and nonconforming condition of the HPCI turbine exhaust system.

Description:

On May 15th, 2014, September 15th, 2014 and March 12th, 2015, the licensee documented that the HPCI turbine casing needed to be manually drained following surveillance testing due to a high level alarm that would not clear. In each case, the actions of the annunciator response procedure were taken. This procedure required engineering to evaluate the condition; however, until March 12th, 2015, the amount of water drained from the turbine was not documented in order to support these evaluations. After the amount of water drained from the turbine was documented to be an estimated 250 gallons, operators and engineering incorrectly evaluated the condition as being caused by water collecting due to abnormal amounts of steam condensation following turbine shutdown. It was later determined that exhaust steam condensation would only amount to approximately 1 gallon of water. Following questioning by the inspectors, the licensee performed additional troubleshooting on May 7th, 2015, which led to the discovery that 100 gallons of water were found in the turbine casing shortly following turbine shutdown. An engineering evaluation determined that the water was siphoned from the suppression pool due to the malfunction of the HPCI turbine exhaust system. Prior to the inspectors questioning, the licensees actions were not sufficient to promptly identify the condition adverse to quality associated with the malfunctioning HPCI turbine exhaust system. On June 11th, 2015, following HPCI testing, the licensee discovered approximately that 190 gallons of water were present in the turbine casing upon turbine shutdown. Because the additional water was not within the bounds of a previous evaluation, the licensee declared the HPCI system inoperable between June 12th, 2015 and June 20th, 2015 while further analysis was being performed to evaluate system operation with approximately 190 gallons of water in the turbine casing.

The inspectors questioned the licensee on the potential of having a large volume of water in the HPCI turbine prior to turbine startup and whether the HPCI turbine exhaust piping would be subjected to water hammer forces that could render the equipment inoperable. With support from the system vendor, the licensee determined that potential water hammer forces would not be excessive, that system piping integrity would be maintained, that the turbine would not be damaged and that the turbine exhaust rupture discs would not be adversely affected. Based on these evaluations, the licensee concluded that, although degraded/non-conforming, the HPCI system maintained operability.

Analysis:

The inspectors determined that the failure to promptly identify a condition adverse to quality associated with the HPCI turbine exhaust system, as required by 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was a performance deficiency. Specifically, the licensee failed to identify that the HPCI turbine exhaust system was malfunctioning and causing water intrusion into the HPCI turbine casing following surveillance runs. The performance deficiency was more-than-minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and it adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, the performance deficiency resulted in the HPCI system being operated with an unidentified degraded/non-conforming condition which degraded the system capability and challenged system operabilty. This finding was evaluated in accordance with NRC IMC 0609, Appendix A, Exhibit 2 Mitigating Systems Screening Questions, dated June 19th, 2012. The inspectors determined the finding was Green because the finding was a deficiency affecting the qualification of HPCI, but based on the licensees evaluations, operability was maintained. The inspectors determined that the finding had a cross-cutting aspect in the Problem Identification and Resolution area of Evaluation [P.2],

because the licensee did not thoroughly evaluate an abnormal system condition to ensure that resolutions addressed causes commensurate with their safety significance.

Enforcement:

10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, that measures shall be established to assure that conditions adverse to quality, such as malfunctions, are promptly identified. Contrary to the above, from May 15th, 2014 to May 7th, 2015, the licensee failed to maintain measures to promptly identify that the HPCI turbine exhaust system was malfunctioning. Upon discovery of the malfunction, the licensee took action to determine that HPCI remained operable despite the degraded and nonconforming condition. The licensee is developing corrective actions to resolve the degraded and nonconforming condition. The licensee entered the violation into the licensee's corrective action program as CR 1098320. This violation is being treated as an NCV consistent with Section 2.3.2 of the Enforcement Policy. (NCV 05000296/2015003-01, Failure to Promptly Identify a Condition Adverse to Quality Associated with HPCI Turbine Exhaust System).

4OA3 Follow-up of Events and Notices of Enforcement Discretion

.1 (Closed) Licensee Event Report (LER) 05000259/2015-002-00 High Pressure Coolant Injection

System Inoperable Due to Slow Containment Isolation Valve Closing Time

a. Inspection Scope

On July 22, 2015, the licensee was performing a valve timing surveillance on the HPCI inboard steam isolation valve. The closure time for the valve was in the high alert range and the licensee was unable to analyze the stroke time deviation within the TS 3.6.1.3 Primary Containment Isolation Valves time limit of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The TS LCO 3.6.1.3 required closing the inboard steam isolation valve rendering HPCI inoperable. The licensee has reported a safety system functional failure for the High Pressure Coolant Injection (HPCI) system from July 22, 2015 until July 25, 2015. The time HPCI was inoperable was within the Technical Specification allowed outage time. The inspectors reviewed the licensees reports and the CAP documents for this issue.

b. Findings

No findings were identified. This licensee event report is closed.

.2 (Closed) Licensee Event Report (LER) 05000296/2015-004-00 High Pressure Coolant Injection

System Inoperable Due to Failed Pressure Switch

a. Inspection Scope

On May 12, 2015, the licensee performed a Steam Line Low Pressure Functional Test on the Unit 3 HPCI steam supply line pressure switches. Due to a spurious actuation of one switch, while testing was being done on a second switch, a Primary Containment Isolation System (PCIS) Group 4 isolation of the HPCI system occurred. The isolation resulted in the inoperability of the HPCI system. Operations reset the system isolation 21 minutes later and declared HPCI operable. The licensee has reported a safety system functional failure for the High Pressure Coolant Injection (HPCI) system. The time HPCI was inoperable was within the Technical Specification allowed outage time.

The inspectors reviewed the licensees reports and the CAP documents for this issue.

b. Findings

No findings were identified. This licensee event report is closed.

These activites constituted completion of two event follow-up samples, as defined in Inspection Procedure 71153. Documents reviewed are listed in the attachment.

4OA5 Other Activities

Temporary Instruction 2515/190 - Inspection of the Proposed Interim Actions Associated with Near-Term Task Force Recommendation 2.1 Flooding Hazard Evaluations The inspectors completed a verification that the licensees interim actions would perform their intended functions for some beyond design basis flooding events. The inspectors reviewed licensee responses to specific Office of Nuclear Reactor Regulation areas of interest. The inspectors walked down specific flood control measures for the Diesel Generator buildings and the Intake Pumping Station. The inspectors also reviewed controls for the following activities to ensure sufficient guidance is available to successfully complete the tasks.

  • Watertight door seal inspection and maintenance program for the Diesel Generator Buildings, Intake Pumping Station, and the Radiological Waste Building
  • Unit 1, 2, and 3 Diesel Generator Buildings flood mitigation strategy and required manual actions
  • Diesel Generator seven day tank fill connection seals
  • Re-evaluation of the design basis Local Intense Precipitation (LIP) event and required actions to verify watertight doors closed
  • Preventative maintenance program to maintain Radiological Waste Building and Diesel Generator Building drains There were no finding identified, however the inspectors made the following observations which were achnowledged by the licensee. The licensee did not maintain any portable dewatering equipment. The licensees procedures require the use of installed sump pumps to remove flood water. The licensees flooding procedure focuses on a response to external flooding and not internal flooding. Inspection associated with this TI is complete, as defined in Inspection Procedure TI 2515/190.

.2 Operation of an Independent Spent Fuel Storage Installation (ISFSI) (60855.1)

a. Inspection Scope

The inspectors performed a walkdown of the onsite ISFSI and monitored the activities associated with the dry fuel storage campaign that is scheduled to be completed on October 23, 2015. The inspectors reviewed changes made to the ISFSI programs and procedures, including associated 10 CFR 72.48, Changes, Tests, and Experiments, screens and evaluations to verify that changes made were consistent with the license or certificate of compliance. The inspectors observed the loading activities to verify that the licensee recorded and maintained the location of each fuel assembly placed in the ISFSI. The inspectors also reviewed surveillance records to verify that daily surveillance requirements were performed as required by technical specifications. Documents reviewed are listed in the attachment. This activity constituted one dry cask campaign inspection sample, as defined in Inspection Procedure 60855.1.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On October 16, 2015, the resident inspectors presented the quarterly inspection results to Mr. Steve Bono, Site Vice President, and other members of the licensees staff, who acknowledged the findings. The inspectors verified that all proprietary information was returned to the licensee.

ATTACHMENT: Supplementary Information

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Bono, Site Vice President
L. Hughes, General Plant Manager
P. Summers, Director of Safety and Licensing
J. Paul, Nuclear Site Licensing Manager
M. McAndrew, Manager of Operations
D. Campbell, Superintendent of Operations
L. Slizewski, Ops Shift Manager
M. Hunter, FIN Manager
M. Kirschenheiter, Assistant Director for Site Engineering
B. L. McCoy, Spent Fuel Storage Program Manager
M. Oliver, Licensing Engineer
E. Bates, Licensing Engineer
M. Acker, Licensing Engineer
M. Lawson, Radiation Protection Manager
J. Smith, System Engineer
P. Campbell, System Engineer
J. Kulisek, EP Manager
K. Skinner, System Engineer
L. Holland, System Engineer
D. Jackson, System Engineer
D. Ford, System Engineer

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000296/2015-003-01 NCV Failure to Promptly Identify a Condition Adverse to Quality Associated with HPCI Turbine Exhaust System (Section 4OA2)

Closed

05000259/2015-002-00 LER High Pressure Coolant Injection System Inoperable Due to Slow Containment Isolation Valve Closing Time (Section 4OA3.1)
05000296/2015-004-00 LER High Pressure Coolant Injection System Inoperable Due to Failed Pressure Switch (Section 4OA3.2)

2515/190 TI Inspection of Interim Actions of Near-Term Task Force Recommendation 2.1 Flooding Reevaluations (Section 4OA5.1)

Discussed

None

LIST OF DOCUMENTS REVIEWED