ENS 50452
ENS Event | |
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21:48 Jul 26, 2014 | |
Title | Invalid Specified System Actuation |
Event Description | The following information is provided as 60 day telephone notification to the NRC in accordance with 10 CFR 50.73(a)(1) reported under 10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation of Division 1 Shutdown Service Water (SX) and an invalid actuation signal for Division 1 Containment Isolation Group 12. This event occurred on July 26, 2014, at 1648 CDT. As allowed by 10 CFR 50.73(a)(1) this notification is made via telephone.
(a) The specific train(s) and system(s) that actuated were: On July 26th, during lightning strikes on the switchyard grid system, the Division 1 SX (Shutdown Service Water) auto-started as a result of momentary loss of power to the Low Pressure Auto Start Relay. A lightning strike causing voltage transients also caused a Division 1 Group 12 Containment Isolation signal affecting DIV 1 Hydrogen monitor. (b) Whether each train actuation was complete or partial. Upon receiving the invalid signal from momentary loss of power, for Division 1 SX and Group 12 Containment Isolation signal, the systems responded as expected for existing plant conditions. For group 12 isolation, [Containment Monitoring] 1CM011/12/47 and 48 valves closed from their normally open position. For DIV 1 Shutdown Service Water (SX), the start of the Shutdown Service Water (SX) pump and alignment of valves operated as expected. The actuation was considered a complete Division 1 SX and Division 1 Group 12 Containment Isolation actuation. Containment Isolation Signals: The following Group 12 valves closed and associated shunt trips occurred on a loss of power to [Radiation Monitors] 1RIX-PR001A/1C: 1CM011, 1CM012, 1CM047, and 1CM048. (c) Whether or not the system started and functioned successfully. Upon receiving the invalid signal from momentary loss of power, Division 1 SX and Containment Isolation signals started and functioned successfully. The NRC Senior Resident Inspector has been notified. |
Where | |
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Clinton Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1142.28 h47.595 days <br />6.799 weeks <br />1.565 months <br />) | |
Opened: | Bob Rush 12:05 Sep 12, 2014 |
NRC Officer: | Vince Klco |
Last Updated: | Sep 12, 2014 |
50452 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (98 %) |
After | Power Operation (98 %) |
WEEKMONTHYEARENS 528622017-05-18T16:15:00018 May 2017 16:15:00
[Table view]10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generator ENS 512082015-05-11T06:19:00011 May 2015 06:19:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the Division 2 Emergency Diesel Generator ENS 504522014-07-26T21:48:00026 July 2014 21:48:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 475872011-12-04T12:09:0004 December 2011 12:09:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Signals and an Emergency Service Water Pump ENS 459012010-03-15T06:38:00015 March 2010 06:38:00 10 CFR 50.73(a)(1), Submit an LER Optional 60-Day Report of Invalid Specified System Actuation ENS 425952006-03-26T08:47:00026 March 2006 08:47:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Notification - Invalid Actuation of High Pressure Core Spray Pump ENS 424772006-02-08T03:59:0008 February 2006 03:59:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuations ENS 418212005-05-12T20:48:00012 May 2005 20:48:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the Division 2 Shutdown Service Water (Sx) System Pump. 2017-05-18T16:15:00 | |