ENS 49926
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ENS Event | |
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17:02 Mar 17, 2014 | |
Title | |
Event Description | Ft. Calhoun station automatically tripped due to a loss of turbine load. The turbine tripped due to loss of stator cooling water. Maintenance was in progress on the stator cooling system when inventory was lost and low pump discharge pressure caused an automatic turbine trip and reactor trip. All systems operated as expected. Ft. Calhoun station is shutdown and stable in mode 3 at this time.
All control rods fully inserted into the core and decay heat is being removed using the normal condenser steam dump system. The licensee has notified the NRC Resident Inspector. |
Where | |
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Fort Calhoun Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.12 h-0.0467 days <br />-0.00667 weeks <br />-0.00153 months <br />) | |
Opened: | Scott Moeck 15:55 Mar 17, 2014 |
NRC Officer: | Dong Park |
Last Updated: | Mar 17, 2014 |
49926 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Fort Calhoun with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 520332016-06-22T13:41:00022 June 2016 13:41:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 506882014-12-17T16:14:00017 December 2014 16:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Load ENS 499262014-03-17T17:02:00017 March 2014 17:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip Initiated by Loss of Stator Cooling Water ENS 497172014-01-12T09:23:00012 January 2014 09:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Following Control Rod Position Deviation ENS 469882011-06-26T05:00:00026 June 2011 05:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Both Emergency Diesel Generators Supplying Plant Emergency Buses Per Plant Procedure ENS 465062010-12-23T16:50:00023 December 2010 16:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Uncomplicated Reactor Trip from 100% Power ENS 458282010-04-08T21:22:0008 April 2010 21:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Inoperable Steam Generator Inlet Isolation Valve ENS 440662008-03-15T13:33:00015 March 2008 13:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Turbine Trip ENS 429742006-11-08T17:06:0008 November 2006 17:06:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation - Emergency Diesel Generator Auto Start ENS 414462005-02-27T03:34:00027 February 2005 03:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Plant Had a Reactor Trip from 16.1% Power Due to a Loss of Turbine Load Signal ENS 401562003-09-13T01:55:00013 September 2003 01:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Unanticipated Negative Axial Shape Index (Asi). 2016-06-22T13:41:00 | |
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