ENS 48936
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ENS Event | |
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01:42 Apr 17, 2013 | |
Title | Specified System Actuation During Turbine Stop Valve Logic Testing While Shutdown |
Event Description | During outage main turbine stop valve RPS logic surveillance testing, an invalid RPS actuation occurred due to an error in executing main turbine surveillance testing procedures. A Turbine Stop Valve closure RPS signal occurred due to an error in the restoration sequence of restoring the RPS bypass signal and a subsequent manual trip of the main turbine. This resulted in a full scram and a trip of both reactor recirculation pumps.
The site post-scram response procedure was entered, which required that the mode switch be placed in the locked SHUTDOWN position. This caused an expected but valid RPS actuation. No control rod motion occurred due to all control rods were inserted at the time of the invalid RPS actuation and subsequent valid RPS actuation. The license has notified the NRC Resident Inspector. |
Where | |
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Limerick Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000353/LER-2013-001 |
Time - Person (Reporting Time:+0.48 h0.02 days <br />0.00286 weeks <br />6.57504e-4 months <br />) | |
Opened: | Chris Giambrone 02:11 Apr 17, 2013 |
NRC Officer: | Bill Huffman |
Last Updated: | Apr 17, 2013 |
48936 - NRC Website | |
Unit 2 | |
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Reactor critical | Not Critical |
Scram | No |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 511682015-06-21T20:25:00021 June 2015 20:25:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Secondary Containment Isolation ENS 509812015-04-13T06:20:00013 April 2015 06:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Initiated ENS 489362013-04-17T01:42:00017 April 2013 01:42:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation During Turbine Stop Valve Logic Testing While Shutdown ENS 481212012-07-19T19:37:00019 July 2012 19:37:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Protection Signal Actuation Due to Changing Mode Switch Position During Surveillance Testing ENS 478882012-05-02T11:24:0002 May 2012 11:24:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Initiation of Secondary Containment Isolation ENS 469062011-05-30T15:50:00030 May 2011 15:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation - Manual Reactor Scram Due to Dual Recirc Pump Trip During Startup ENS 449482009-03-31T22:50:00031 March 2009 22:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Diesel Start Signal Received During Maintenance Testing of Diesel ENS 438982008-01-12T14:04:00012 January 2008 14:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Specified System Actuation During Edg Governor Testing ENS 433152007-04-24T06:10:00024 April 2007 06:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Scram with Eccs Injection on Lowering Reactor Vessel Water Level ENS 432312007-03-13T11:30:00013 March 2007 11:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Low Main Condenser Vacuum Isolation Signal Received During Plant Shutdown ENS 421932005-12-09T14:01:0009 December 2005 14:01:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Trip of a Startup Bus Breaker Results in Start of Emergency Diesel Generators ENS 415732005-04-06T21:55:0006 April 2005 21:55:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Partial Loss of Offsite Power Resulting in Autostart of Emergency Diesel Generators 2015-06-21T20:25:00 | |
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