ENS 48018
ENS Event | |
---|---|
18:56 Jun 12, 2012 | |
Title | Technical Specification Required Shutdown |
Event Description | At 1456 hours0.0169 days <br />0.404 hours <br />0.00241 weeks <br />5.54008e-4 months <br /> on June 12, 2012, the plant commenced a shutdown due to water leakage from the SIRW [Safety Injection Refueling Water] tank exceeding the operational decision-making issue process trigger point of 31 gallons per day causing it to be declared inoperable and requiring entry into Technical Specification (TS) 3.5.4, Condition B. TS 3.5.4 Condition B requires the SIRW Tank to be returned to operable status within one hour or entry into Condition C that requires the plant to be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and Mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
Actual leakage from the SIRW Tank was measured at approximately 31.4 gallons per day. This event had no impact on the health and/or safety of the public. The NRC Senior Resident Inspector has been notified. The licensee believes that the tank is leaking from several locations. However, at this time, they cannot determine exact locations. The refueling water has minor tritium contamination. The refueling water is being collected in a reservoir and then pumped into a holding tank. The licensee will be shutting down to cold shutdown.
Subsequent review concluded the condition did not meet reporting criteria. The rate of water leakage from the Safety Injection Refueling Water Tank had reached an administrative limit. Shutdown was not required by the Technical Specifications. The plant shutdown commenced in accordance with normal plant operating procedures. At 1849 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.035445e-4 months <br /> on June 12, 2012, the reactor was manually tripped. This event is not reportable as the reactor trip was part of a normal shutdown for corrective maintenance. Mode 5 was reached at 1745 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.639725e-4 months <br /> on June 13, 2012. The NRC Resident Inspector has been notified. Notified R3DO (Lipa). |
Where | |
---|---|
Palisades Michigan (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-1.48 h-0.0617 days <br />-0.00881 weeks <br />-0.00203 months <br />) | |
Opened: | Terry Davis 17:27 Jun 12, 2012 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Aug 7, 2012 |
48018 - NRC Website | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (50 %) |
WEEKMONTHYEARENS 490022013-05-05T05:12:0005 May 2013 05:12:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown - Safety Injection Refueling Water Tank Declared Inoperable Due to Leak ENS 487582013-02-15T18:00:00015 February 2013 18:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Component Cooling Water Train Out of Service ENS 484782012-11-04T16:30:0004 November 2012 16:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Secondary Side Steam Leak ENS 480182012-06-12T18:56:00012 June 2012 18:56:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown ENS 443852008-08-06T00:29:0006 August 2008 00:29:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Due to Excessive Unidentified Leakage ENS 429542006-11-01T23:05:0001 November 2006 23:05:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit Shutdown Required Due to Service Water Leak Involving a Containment Air Cooler ENS 424622006-03-29T17:15:00029 March 2006 17:15:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Hpsi Inoperability 2013-05-05T05:12:00 | |