ENS 46780
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ENS Event | |
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13:21 Apr 23, 2011 | |
Title | Valid Auxiliary Feedwater Pump Start While Cooling Down Reactor |
Event Description | At 0921 [EDT] on 4/23/11, CNS Unit-1 received an auxiliary feedwater pump auto start due to low-low level in the 1B steam generator. The 1A auxiliary feedwater pump started and restored steam generator level to the normal operating band.
A cooldown was in progress at the time of the event and the tagout isolated feedwater flow to the 1B steam generator. The licensee notified the NRC Resident Inspector. The states of North and South Carolina, and York, Gaston, and Mecklenburg Counties will be notified. |
Where | |
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Catawba South Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.73 h-0.0304 days <br />-0.00435 weeks <br />-9.99954e-4 months <br />) | |
Opened: | Donald Wisneiwski 12:37 Apr 23, 2011 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Apr 23, 2011 |
46780 - NRC Website | |
Unit 1 | |
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Reactor critical | Not Critical |
Scram | No |
Before | Hot Shutdown (0 %) |
After | Hot Shutdown (0 %) |
WEEKMONTHYEARENS 570262024-03-13T01:11:00013 March 2024 01:11:00
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