ENS 43226
ENS Event | |
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19:23 Mar 9, 2007 | |
Title | Unusual Event Declared Due to Rcs Leakage Greater than Tech Spec Limit |
Event Description | A Notification of Unusual Event has occurred on Unit 2 due to Reactor Coolant System (RCS) unidentified leakage greater than 10 gallons per minute.
The licensee notified NRC Resident Inspector. Notified USDA (Brzostels).
No actual RCS leakage occurred and the RCS always remained intact. The additional water injection occurred and the RCS always remained intact. The additional water injection into the Reactor Coolant System was required to makeup for gases that came out of solution and accumulated in the reactor vessel head and were being vented from the RCS during a planned drain down. The licensee terminated the Unusual Event at 1751 on 3/9/07. The licensee notified the NRC Resident Inspector, state, and local government agencies. The licensee will remain in Mode 5 for their planned outage. Notified R2DO (G. Hopper), NRR EO (M. Case), IRD (T. Blount), NRR (J. Dyer), DHS (McKentry), FEMA (Biscoe), DOE (Wyatt), EPA (Burgess), HHS (Dalviel), USDA (Giles).
This report is retracted based on the following: On 3/9/07, an NOUE was declared while Unit 2 was in Mode 5, draining the RCS to support Rx Vessel disassembly, due to what was then diagnosed as an RCS Unidentified Leak greater than 10 gpm. Subsequent review of the event revealed that no leak existed and the mismatch between charging and letdown, which was the basis of the leak determination, was caused by a nitrogen bubble being vented from the Rx Vessel Head and the additional charging volume was displacing the nitrogen volume as it was being vented. As a result, Vogtle Unit 2 is retracting the NOUE classification that was made on 3/9/07. The licensee informed the NRC Resident Inspector. Notified R2DO (Ernstes). |
Where | |
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Vogtle Georgia (NRC Region 2) | |
Reporting | |
Emergency class: | Unusual Event |
10 CFR 50.72(a) (1) (i), Emergency Class Declaration | |
Time - Person (Reporting Time:+-4.58 h-0.191 days <br />-0.0273 weeks <br />-0.00627 months <br />) | |
Opened: | Timothy Thompson 14:48 Mar 9, 2007 |
NRC Officer: | Pete Snyder |
Last Updated: | May 12, 2007 |
43226 - NRC Website | |
Unit 2 | |
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Reactor critical | Not Critical |
Scram | No |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 512192015-07-09T21:32:0009 July 2015 21:32:00
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