ENS 40921
From kanterella
Jump to navigation
Jump to search
ENS Event | |
---|---|
14:24 Aug 4, 2004 | |
Title | Unexpected Reactor Trip During Maintenance Activities |
Event Description | At 1024 EDT a reactor trip occurred during maintenance activities involving the control rod drive trip breakers. All control rods fully inserted. The unit is currently stable with decay heat removal via the main steam system through the turbine bypass valves to the main condenser. Post trip response was normal with the following exceptions noted:
1. #4 main turbine stop valve may not have fully closed. 2. A #2 Steam Generator Safety Valve may be lifting early (lifted at 1010 psi rather than the 1050 psi setpoint). 3. Turbine Bypass valve SP13A3 stuck slightly open - isolated. All offsite power lines have been verified operable and both EDGs are available in standby, if needed. The licensee informed the local sheriff's department as required whenever a Steam Generator Safety valve lifts and the NRC Resident Inspector. |
Where | |
---|---|
Davis Besse Ohio (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-3.17 h-0.132 days <br />-0.0189 weeks <br />-0.00434 months <br />) | |
Opened: | Anthony Stallard 11:14 Aug 4, 2004 |
NRC Officer: | Steve Sandin |
Last Updated: | Aug 4, 2004 |
40921 - NRC Website | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 553462021-07-09T01:54:0009 July 2021 01:54:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Main Turbine Trip ENS 546112020-03-25T16:40:00025 March 2020 16:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to Loss of Reactor Coolant Pumps ENS 542632019-09-07T17:09:0007 September 2019 17:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 522322016-09-10T07:43:00010 September 2016 07:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Unit Trip Due to Main Generator Lock-Out ENS 516962016-01-29T18:22:00029 January 2016 18:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Reactor Protection System Actuation ENS 510612015-05-09T22:55:0009 May 2015 22:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Steam Leak in the Turbine Building ENS 491592013-06-30T01:20:00030 June 2013 01:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Reactor Coolant Pump Trip ENS 428282006-09-06T06:31:0006 September 2006 06:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip on Loss of Condenser Vacuum ENS 409212004-08-04T14:24:0004 August 2004 14:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unexpected Reactor Trip During Maintenance Activities 2021-07-09T01:54:00 | |
Retrieved from "https://kanterella.com/w/index.php?title=ENS_40921&oldid=93181"