05000446/LER-2001-001

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LER-2001-001,
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
4462001001R00 - NRC Website

I. D DESCRIPTION OF REPORTABLE EVENT

A. REPORTABLE EVENT CLASSIFICATION

Any event or condition that resulted in manual or automatic actuation of the Reactor Protection System (RPS) including reactor trip or reactor scram.

B. PLANT OPERATING CONDITIONS PRIOR TO THE EVENT

On July 18, 2001, Comanche Peak Steam Electric Station (CPSES) Unit 2 was in Mode 1, Power Operation, operating at 100 percent power.

C. STATUS OF STRUCTURES, SYSTEMS, OR COMPONENTS THAT WERE

INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO

THE EVENT

Not Applicable — There were no structures, systems, or components that were inoperable at the start of the event which contributed to this event.

D. NARRATIVE SUMMARY OF THE EVENT, INCLUDING DATES AND

APPROXIMATE TIMES

On July 18, 2001, at approximately 7:00 a.m., Instrumentation and Controls (I&C) Personnel (Utility, Non-Licensed) were performing a Steam Generator (EIIS: (SB)) 2-01 Narrow Range Level 519 Channel Operability Test. During the test, a trouble alarm was generated on the Unit 2 AMSAC panel (EIIS: (JL)). AMSAC provides a backup to the Reactor Trip System (RTS) (EIIS:(JC)) and ESF Actuation System (ESFAS) (EIIS:(JE)) for initiating turbine trip and auxiliary feedwater flow in the event an anticipated transient results (e.g., the complete loss of main feedwater). The test procedure directed the I&C personnel to reset the alarm following completion of the test. While responding to the AMSAC trouble alarm, Operations personnel (Utility, Licensed) noticed that the Train A power light was not illuminated. At approximately 7:52 a.m., Operations personnel (Utility, Licensed) took AMSAC from normal to bypass and the bypass alarm was received as expected. While AMSAC remained in bypass, the I&C personnel (Utility, Non-Licensed) replaced the Train A power light. At 7:59 a.m, Operations personnel (Utility, Licensed) placed AMSAC back in the normal position. When the switch was placed in normal, a spurious AMSAC Train A actuation signal was generated that caused an automatic turbine trip and resulted in an automatic reactor trip from 100 percent power. All control rods (EIIS: (AA)) fully inserted. The reactor trip was followed by an automatic Auxiliary Feedwater (AFW) (EIIS:(BA)) actuation. During the reactor trip, two Facility Name (1) COMANCHE PEAK STEAM ELECTRIC STATION UNIT 2 Fase(3) Docket � LER Number (6) Sequential � Revision Number � Number Year Enclosure to TXX-01134 Feedwater Heater (EIIS: (SJ)) relief valves lifted and released steam into the Unit 2 Turbine Building (EIIS: (NM)). At 8:06 a.m., Operators (Utility, Licensed) in the Unit 2 Control Room were notified of the steam release and they closed the Main Steam (EIIS: (SB)) Isolation Valves (MSIV's) to isolate the steam leak. This action required the use of the Steam Generator (SG) Atmospheric Relief Valves (ARVs) to maintain temperature control of the Unit 2 Reactor. This resulted in a normal steam release to the atmosphere. Secondary activity levels were verified by procedure to be acceptable. The plant was stabilized in Mode 3 and all systems functioned as designed.

E. THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE,

OR PROCEDURAL OR PERSONNEL ERROR

Operators (Utility, Licensed) in the Unit 2 Control Room received a reactor trip greater than 50 percent power turbine trip alarm.

II. COMPONENT OR SYSTEM FAILURES

A. FAILURE MODE, MECHANISM, AND EFFECTS OF EACH FAILED COMPONENT

Since the AMSAC Train A relay coil power light bulb was initially not illuminated but was later demonstrated functional, a failed light socket is suspected. The spurious AMSAC Train A actuation was believed to have occurred when the bulb contactor on the center barrel of the socket separated from the current limiting resistor, and fell into a position that caused a short between the center post and the side of the light socket. When a new bulb was installed in the socket on July 18, 2001, the contact short was reinforced. The increase in current due to the loss of resistance of the bulb and the socket's current limiting resistor was enough to energize the AMSAC relays.

The design of the AC power lamp in the energized relay circuit did not prohibit a single point failure of the light socket from energizing the AMSAC relays. Review of the relay circuit design indicates that the AC power lamp is in series with the AMSAC relays. The design relies on the resistor built into the light socket to limit current through the circuit. When the light socket fails in a short circuit, the current to the relays is no longer limited and an AMSAC actuation will occur.

Enclosure to TXX-01134

B. CAUSE OF EACH COMPONENT OR SYSTEM FAILURE

The wire that connects the current limiting resistor to the bulb contactor on the center barrel of the socket was found to be broken. Evidence of tinning was found in the cross section of this wire, and TXU Electric believes that this indicates a discontinuity existed in the wire at the time the socket was manufactured. A break in the wire allowed the contactor to fall out of it's barrel location. Based on the lack of any evidence of mishandling of the socket, TXU Electric believes that CPSES maintenance practices did not cause or contribute to the broken wire.

C. SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE

OF COMPONENTS WITH MULTIPLE FUNCTIONS

Not applicable — No failures of components with multiple functions have been identified.

D. FAILED COMPONENT INFORMATION

Dialight Corp.

Model Number 137-8836-0931-552 Light Bulb Socket

III. ANALYSIS OF THE EVENT

A. SAFETY SYSTEM RESPONSES THAT OCCURRED

The Reactor Protection System (EIIS:(JC)) and The Auxiliary Feedwater System (EIIS:(BA)) actuated during the event.

The Motor Driven Auxiliary Feedwater (MDAFW) pump (EIIS: (P)(BA)) number 1 and the Turbine Driven Auxiliary Feedwater (TDAFW) pump (EIIS: (P)(BA)) automatically started without Steam Generator Lo-Lo water level (EIIS: (JB)) signals. This is the expected response during an AMSAC actuation. Motor Driven Auxiliary Feedwater (MDAFW) pump (EIIS:

(P)(BA)) number 2 automatically started on a Lo-Lo water level signal in Steam Generator number 3.

Facility Name (1) COMANCHE PEAK STEAM ELECTRIC STATION UNIT 2 LER Number (6) Year � Sequential � Revision Number � Number 01 1 1 001 1 1 00 Docket Fage(3) Enclosure to TXX-01134

B. DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY

Not Applicable — No safety system trains were inoperable during this event.

C. SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT

This event is bounded by the FSAR accident analysis which assumes conservative initial conditions which bound the plant operating range and other assumptions which reduce the capability of safety systems to mitigate the consequences of the transient.

This event is bounded by the analysis of the turbine trip presented in Section 15.2.3 of the CPSES Final Safety Analysis Report (FSAR). The analysis uses conservative assumptions to demonstrate the capability of pressure relieving devices and to demonstrate core protection margins. The event of July 18, 2001, occurred at 100 percent reactor power, and all systems and components functioned as designed.

After the reactor trip and during the stabilization of the plant, a Main Steam Isolation was manually initiated due to a report of steam in the Turbine Building, and the Steam Generator Atmospheric Relief Valves were used for temperature control. Both Main Feedwater Pumps tripped, and Feedwater flow was adequately maintained by the Auxiliary Feedwater System.

Secondary activity levels were verified by procedure to be acceptable.

There were no safety system functional failures associated with this event.

Based on the above, it is concluded that the event of July 18, 2001, did not adversely affect the safe operation of CPSES Unit 2 or the health and safety of the public.

IV. CAUSE OF THE EVENT

TXU Electric believes that the event was caused by a short circuit in a light bulb socket during replacement of an apparently burned out AC power lamp in the AMSAC panel. The short circuit caused a spurious AMSAC Train A actuation that resulted in a turbine trip and automatic reactor trip.

The design of the AC power lamp in the energized relay circuit did not prohibit a single point failure of the light socket from energizing the AMSAC relays. TXU Electric believes that the failed light socket may have been degraded since manufacture.

Facility Name (1) COMANCHE PEAK STEAM ELECTRIC STATION UNIT 2 LER Number (6) Year � Sequential � Revision Number � Number 01 1 1 001 � 00 Docket Page(3) Enclosure to TXX-01134

V. CORRECTIVE ACTIONS

The Unit 2 Train A AMSAC AC power light bulb and socket have been replaced and verified functional. The other Unit 2 AMSAC panel light sockets were inspected and no discrepancies were found. Although TXU Electric believes that the problem with the Unit 2 Train A AMSAC AC power light socket was isolated, the light sockets in the Unit 1 AMSAC panel will be inspected to ensure the center contactors are intact. The power light circuits in the Unit 1 and Unit 2 AMSAC panels will be modified to prevent future similar spurious relay actuations. The need for a bulb list for use by Operations will be evaluated. This list would be used to approve or cause an evaluation of certain indicating light bulb replacements while the plant is at power.

VI. PREVIOUS SIMILAR EVENTS

There have been other previous events which resulted in a turbine trip followed by an automatic reactor trip. However, the causes of those events were sufficiently different such that the corrective actions taken for the previous events would not have prevented this event.