03-16-2016 | On January 25, 2016 at 0147 hours0.0017 days <br />0.0408 hours <br />2.430556e-4 weeks <br />5.59335e-5 months <br /> an automatic reactor trip occurred at Millstone Power Station Unit 3 while the unit was in Mode 1, operating at 100 percent power due to a trip of the 'B' Reactor Coolant Pump. The 'B' Reactor Coolant Pump tripped on a ground fault, which in turn caused the Unit 3 reactor to trip on reactor coolant system low loop flow ( Reactor Protection System actuation). All control rods fully inserted into the reactor. The auxiliary feedwater pumps started as designed on low steam generator level and operators maintained steam generator level.
All other post trip actions were standard and all safety systems operated as expected.
The 'B' Reactor Coolant Pump trip was caused by failure of one of three motor capacitors on the Reactor Coolant Pump motor. The failed capacitor on the affected Reactor Coolant Pump motor was replaced and the integrity of the motor windings, cabling, breaker, and associated protective relays were verified. Based on an assessment of the event, the risk impact was determined to be very small. There were no radiological challenges and the health and safety of the public were not affected.
The actuation of the reactor protection system and the automatic start of the auxiliary feedwater pumps is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in manual or automatic actuation of systems listed in 10 CFR 50.73(a)(2)(iv)(B). |
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Category:Letter
MONTHYEARML24030A7522024-01-30030 January 2024 Technical Specification Bases Pages IR 05000336/20234022024-01-30030 January 2024 Security Baseline Inspection Report 05000336/2023402 and 05000423/2023402 (Cover Letter Only) ML23341A0172024-01-12012 January 2024 Issuance of Amendment No. 288 Revision to Applicability Term for Reactor Coolant System Heatup and Cooldown Pressure-Temperature Limitations Figures IR 05000336/20234402024-01-11011 January 2024 Special Inspection Report 05000336/2023440 and 05000423/2023440 (Cover Letter Only) ML24004A1052024-01-0404 January 2024 Request for Information for a Biennial Problem Identification and Resolution Inspection; Inspection Report 05000336/2024010 & 05000423/2024010 ML23361A0942023-12-21021 December 2023 Response to Request for Additional Information Regarding Proposed License Amendment Request to Revise Technical Specifications for Reactor Core Safety Limits, Fuel Assemblies and Core Operating Limits Report . ML23283A3052023-12-20020 December 2023 Review of Appendix F to DOM-NAF2, Qualification of the Framatome ORFEO-GAIA and ORFEO-NMGRID CHF Correlations in the Dominion Energy VIPRE-D Computer Code (EPID L-2022-LLT-0003) (Nonproprietary) ML23361A0312023-12-20020 December 2023 Intent to Pursue Subsequent License Renewal ML23352A0202023-12-18018 December 2023 Senior Reactor and Reactor Operator Initial License Examinations ML23334A2242023-11-30030 November 2023 Request for Exemption from Enhanced Weapons Firearms Background Checks, and Security Event Notifications Implementation ML23324A4222023-11-20020 November 2023 Reactor Vessel Internals Inspections Aging Management Program Submittal Related to License Renewal Commitment 13 ML23324A4302023-11-20020 November 2023 Alloy 600 Aging Management Program Submittal Related to License Renewal Commitment 15 ML23317A2702023-11-13013 November 2023 Core Operating Limits Report, Cycle 23 IR 05000336/20230032023-11-0606 November 2023 Integrated Inspection Report 05000336/2023003 and 05000423/2023003 ML23298A1652023-10-26026 October 2023 Requalification Program Inspection IR 05000336/20234202023-10-0404 October 2023 Security Inspection Report 05000336/2023420 and 05000423/2023420 ML23230A0502023-10-0202 October 2023 5 of the Quality Assurance Topical Report - Review of Program Changes ML23226A0052023-09-26026 September 2023 Issuance of Amendment No. 287 Supplement to Spent Fuel Pool Criticality Safety Analysis IR 05000245/20230012023-09-19019 September 2023 Safstor Inspection Report 05000245/2023001 IR 05000336/20230102023-09-0808 September 2023 Commercial Grade Dedication Report 05000336/2023010 and 05000423/2023010 IR 05000336/20230052023-08-31031 August 2023 Updated Inspection Plan for Millstone Power Station, Units 2 and 3 (Report 05000336/2023005 and 05000423/2023005) ML23248A2132023-08-30030 August 2023 Response to Request for Additional Information Regarding Proposed License Amendment Request to Revise the Applicability Term for Reactor Coolant System Heatup and Cooldown Pressure-Temperature. ML23242A0142023-08-30030 August 2023 Operator Licensing Examination Approval ML23223A0552023-08-18018 August 2023 Request for Withholding Information from Public Disclosure for License Amendment Request to Revise Technical Specifications for Reactor Core Safety Limits, Fuel Assemblies, and COLR Related to Framatome Gaia Fuel ML23223A0482023-08-18018 August 2023 Request for Withholding Information from Public Disclosure for License Amendment Request to Use Framatome Small Break and Realistic Large Break LOCA Evaluation Methodologies for Establishing COLR Limits IR 05000336/20230022023-08-0909 August 2023 Integrated Inspection Report 05000336/2023002 and 05000423/2023002 ML23188A0432023-07-31031 July 2023 Authorization and Safety Evaluation for Alternative Request No. IR-04-11 ML23208A0922023-07-26026 July 2023 Request for Approval of Appendix F of Fleet Report DOM-NAF-2-P Qualification of Framatome ORFEO-GAIA and OORFE-NMGRID CHF Correlations in the Dominion Energy Vipre-D Computer Code Response ML23188A0202023-07-26026 July 2023 Closeout of Generic Letter 2004-02, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized-Water Reactors ML23207A1102023-07-26026 July 2023 NRC Regulatory Issues Summary 2023-01 Preparation and Scheduling of Operator Licensing Examinations IR 05000336/20234012023-07-17017 July 2023 Material Control and Accounting Program Inspection Report 05000336/2023401 and 05000423/2023401 - (Cover Letter Only) ML23175A0052023-07-12012 July 2023 Alternative Request P-07 for Pump Periodic Verification Testing Program for Containment Recirculation Spray System Pumps ML23193A8562023-06-28028 June 2023 Submittal of Updates to the Final Safety Analysis Reports ML23178A1682023-06-26026 June 2023 2022 Annual Report of Emergency Core Cooling System (ECCS) Model Changes Pursuant to the Requirements of 10 CFR 50.46 ML23153A1732023-06-16016 June 2023 Correction to Amendment Nos. 346 & 286 Millstone, 294 & 277 North Anna, 311 & 311 Surry, and 225 Summer to Revise Technical Specifications to Adopt TSTF-554,Rev Reactor Coolant Leakage Requirement ML23151A0742023-06-12012 June 2023 Review of the Spring 2022 Steam Generator Tube Inspection Report ML23159A2202023-06-0808 June 2023 Associated Independent Spent Fuel Storage Installation Revision to Emergence Plan - Report of Changes IR 07200047/20234012023-06-0808 June 2023 NRC Independent Spent Fuel Storage Installation Security Inspection Report No. 07200047/2023401 2024-01-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000423/LER-2019-0012020-02-13013 February 2020 LER 2019-001-00 for Millstone Power Station Unit 3 Regarding Plant Shutdown Required by Technical Specifications, Emergency Diesel Generator Exceeded Allowed Outage Time 05000423/LER-2017-0012017-03-20020 March 2017 Loss of Safety Function - Secondary Containment, LER 17-001-00 for Millstone, Unit 3 Regarding Loss of Safety Function - Secondary Containment 05000336/LER-2016-0022016-09-20020 September 2016 Manual Reactor Trip Due to Loss of Two Circulating Water Pumps, LER 16-002-00 for Millstone Power Station Unit 2 Regarding Manual Reactor Trip Due Loss Of Two Circulating Water Pumps 05000423/LER-2016-0052016-08-0909 August 2016 Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation, LER 16-005-00 for Millstone Power Station Unit 3 RE: Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation 05000423/LER-2016-0042016-07-13013 July 2016 Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator, LER 16-004-00 for Millstone Power Station Unit 3 RE: Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator 05000336/LER-2016-0012016-06-27027 June 2016 Turbine Driven Auxiliary Feedwater Putnp Room HELB Door Left Open, LER 16-001-00 for Millstone Power Station Unit 2 RE: Turbine Driven Auxiliary Feedwater Pump Room HELB Door Left Open 05000423/LER-2016-0032016-06-0808 June 2016 Loss of Safety Function- Supplementary Leak Collection and Release System, LER 16-003-00 for Millstone Power Station, Unit 3, Regarding Loss of Safety Function-Supplementary Leak Collection and Release System 05000423/LER-2016-0022016-03-23023 March 2016 Feedwater Isolation Signal Defeated Due to Wiring Error, LER 16-002-00 for Millstone Power Station Unit 3 Regarding Feedwater Isolation Signal Defeated Due to Wiring Error 05000423/LER-2016-0012016-03-16016 March 2016 Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump, LER 16-001-00 for Millstone Power Station Unit 3, Regarding Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump 05000336/LER-2015-0032016-01-0707 January 2016 Valid Actuation of the Reactor Protection System, LER 15-003-00 for Millstone, Unit 2, Regarding Valid Actuation of the Reactor Protection System ML0925900552009-09-0808 September 2009 Special Report for Seismic Instrumentation ML0719302812007-04-11011 April 2007 Final ASP Analysis- Millstone (LER 336/06-002) ML0622802402006-08-0808 August 2006 Special Report for Inoperable Radiation Monitor 2020-02-13
[Table view] |
1. EVENT DESCRIPTION:
On January 25, 2016 at 0147 hours0.0017 days <br />0.0408 hours <br />2.430556e-4 weeks <br />5.59335e-5 months <br /> an automatic reactor trip occurred at Millstone Power Station Unit 3 (MPS3) while the unit was in Mode 1, operating at 100 percent power. The Reactor Protection System (RPS) was initiated due to a reactor coolant system loop low flow. All control rods fully inserted into the reactor. The auxiliary feedwater pumps started as designed on low steam generator level and operators maintained steam generator level. All other post trip actions were standard and all safety systems operated as expected, stabilizing the plant.
The 'B' Reactor Coolant Pump (RCP) trip was caused by failure of one of three motor capacitors on the RCP motor. The failed capacitor on the affected RCP motor was replaced and the integrity of the motor windings, cabling, breaker, and associated protective relays were verified.
Based on an assessment of the event, the risk impact was determined to be very small. There were no radiological challenges and the health and safety of the public were not affected.
The actuation of the reactor protection system and the automatic start of the auxiliary feedwater pumps is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in manual or automatic actuation of systems listed in 10 CFR 50.73(a)(2)(iv)(B).
2. CAUSE:
The direct cause of the 'B' RCP trip, which resulted in an automatic reactor trip due to partial loss of forced reactor coolant flow, was due to the failure of one of the three RCP motor capacitors. Failure of the capacitor provided a short to ground.
3. ASSESSMENT OF SAFETY CONSEQUENCES:
Final Safety Analysis Review (FSAR) Section 15.3.1 presents an analysis of a Partial Loss of Forced Reactor Coolant Flow (one RCP). The analysis presented spans 10 seconds from the onset of the flow coast down to beyond the time of minimum Departure from Nucleate Boiling Ratio (3.6 seconds).
The event as presented in the FSAR contains conservative assumptions typical of safety analysis.
These include rapid coast down characteristics, maximum trip delay times, most adverse time in cycle reactivity feedbacks, etc.
Plant computer data and log entries were examined to verify that the actual plant response was bounded with respect to that in the safety analysis. Examination of the plant response showed that the January 25th partial loss of forced reactor coolant flow due to the loss of 'B' RCP transient was well bounded by the FSAR analysis.
The event was considered uncomplicated as defined by the Reactor Oversight Process. In addition, all equipment designed to remove decay heat was available prior to the event and functioned properly during the event. The event was not a significant operational event. Therefore, the event posed no actual or potential hazard to public health and safety.
4. CORRECTIVE ACTION:
The failed motor capacitor was replaced on the 'B' RCP.
Additional corrective actions are being taken in accordance with the Millstone Corrective Action Program.
5. PREVIOUS OCCURRENCES:
Millstone Power Station Unit 3 has no previous occurrences.
6. Energy Industry Identification System (EIIS) codes:
7. MANUFACTURER/PART NUMBER
- Capacitor: Westing house/6060B7H01N
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05000423/LER-2016-001 | Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump LER 16-001-00 for Millstone Power Station Unit 3, Regarding Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2016-001 | Turbine Driven Auxiliary Feedwater Putnp Room HELB Door Left Open LER 16-001-00 for Millstone Power Station Unit 2 RE: Turbine Driven Auxiliary Feedwater Pump Room HELB Door Left Open | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000423/LER-2016-002 | Feedwater Isolation Signal Defeated Due to Wiring Error LER 16-002-00 for Millstone Power Station Unit 3 Regarding Feedwater Isolation Signal Defeated Due to Wiring Error | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2016-002 | Manual Reactor Trip Due to Loss of Two Circulating Water Pumps LER 16-002-00 for Millstone Power Station Unit 2 Regarding Manual Reactor Trip Due Loss Of Two Circulating Water Pumps | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000423/LER-2016-003 | Loss of Safety Function- Supplementary Leak Collection and Release System LER 16-003-00 for Millstone Power Station, Unit 3, Regarding Loss of Safety Function-Supplementary Leak Collection and Release System | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000423/LER-2016-004 | Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator LER 16-004-00 for Millstone Power Station Unit 3 RE: Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000423/LER-2016-005 | Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation LER 16-005-00 for Millstone Power Station Unit 3 RE: Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
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