05000388/LER-2016-004

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LER-2016-004, Unit 2 experienced an electrical transient resulting in a manual SCRAM
Susquehanna Steam Electric Station Unit 2
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material

10 CFR 50.73(a)(2)(iv)(A), System Actuation
3882016004R01 - NRC Website

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. LER NUMBER

CONDITIONS PRIOR TO EVENT

Unit 1 — Mode 1, 100 percent Rated Thermal Power Unit 2 — Mode 1, 100 percent Rated Thermal Power 2B246 Reactor Building Engineered Safeguard System (ESS) Division 2 480 volt Motor Control Center (MCC) (EIIS:B) and 2Y246 208/120 Volt Alternate Current (AC) Instrument Panel (EIIS:JL) were inoperable at the time of the scram.

It was discovered that the Manual Bypass Switch 2D666SW1 (EIIS:HS) was set to its alternate power source, via 2B246 AC ESS Bus (EIIS:JL). When the loss of 26246 (EIIS:JL) occurred, power could not be swapped back over to its primary power source via 2D666 vital uninterruptable power supply (UPS) since the Manual Bypass Switch (EllS:HS) was degraded. This led to the loss of power to panel 2Y629, which challenged operator response. The Manual Bypass Switch (EIIS:HS) had been in its degraded condition since May 6th 2015 when the UPS was being taken out of service and power was placed on its alternate supply via the Manual Bypass Switch (EllS:HS). This event was reported under the NRC Pls as a Scram with Complications.

EVENT DESCRIPTION

At 23:55 on 5/12/16, Unit 2 experienced an electrical transient resulting in a loss of 26246 Reactor Building Engineered Safeguard System (ESS) Division 2 480 volt Motor Control Center (MCC) (EIIS:B) and 2Y246 208/120 Volt Alternate Current (AC) Instrument Panel (EIIS:JL). With the loss of the Reactor Building ESS Division 480 volt MCC, several drywell cooling fans were lost leading to an increase in drywell pressure.

Drywell pressure increased to 1.3 psig when operators placed the mode switch to the shutdown position to manually scram the reactor. At 0110 on 5/13 Unit 2 was manually scrammed. The automatic start signal on high drywell pressure was received at 0312 for the A, C, and D Emergency Diesel Generators (EIIS:EK).

The B Emergency Diesel Generator was manually started from the control room. It did not automatically start in emergency mode due to the Unit 2 division 2 core spray not reaching an initiation signal on 1.72 psig. All rods inserted as expected. Reactor water level lowered to -27 inches and was immediately restored by normal feedwater level control. Level 3 (+13 inch) Primary Containment Isolation System isolations occurred, along with an initiation of the Reactor Core Isolation Cooling (RCIC) (EIIS:KI) system (- 30 inches). The 'A' and 'B' Emergency Service Water pumps were manually started. Once adequate level was verified, RCIC was overridden. Pressure was controlled with turbine bypass valves, and subsequently Main Steam Line Drains. All safety systems functioned as expected.

The power loss also tripped Reactor Building HVAC (EIIS:VA), causing a loss of secondary containment differential pressure resulting in a loss of safety function.

Due to the loss of drywell cooling, high drywell pressure actuations and a second reactor scram signal occurred at 0314 hours0.00363 days <br />0.0872 hours <br />5.191799e-4 weeks <br />1.19477e-4 months <br />. High Pressure Coolant Injection (EIIS code:BJ) was subsequently overridden and declared inoperable, resulting in a Loss of Safety Function.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

This event was determined to be reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event or condition that resulted in manual or automatic actuation of an ECCS system and 10 CFR 50.73(a)(2)(v)(C) as an event or condition that could have prevented fulfillment of a safety function.

CAUSE OF EVENT

The direct cause of the transient was found to be a phase to ground short between a cable and a protruding screw in MCC bucket 26246091, Drywell Area Unit Cooler 2V411B Breaker (EIIS: B). The protruding screw damaged and/or abraded the wire insulation until the short occurred. In 2005, Susquehanna did a receipt inspection on MCC buckets from Nuclear Logistics Incorporated (NLI) and found the wiring routed from the bucket connection stabs on the rear panel were in very close proximity or were in contact with the mounting screws. The vendor was contacted and the specification E1116, was revised to include that the screws should not protrude more than two threads from the back plate of the bucket. The apparent cause of the event is that the vendor did not comply with Specification E1116, Rev 3 with this order of buckets.

ANALYSIS/SAFETY SIGNIFICANCE

The actual consequences of this event were the Unit 2 loss of 2B246 and 2Y246 (EIIS:JL). With the loss of 2B246 (EIIS:JL), several drywell cooling fans were lost leading to an increase in drywell pressure. Operations manually scrammed the reactor prior to the Automatic Scram on high drywell pressure. Following the scram, drywell pressure continued to rise and the automatic start signal was received for the A, C, and D Emergency Diesel Generators.

The failure also resulted in four Maintenance Rule Functional Failures (MRFFs) and 12.58 hours6.712963e-4 days <br />0.0161 hours <br />9.589947e-5 weeks <br />2.2069e-5 months <br /> of 2B246 MCC unavailability.

The potential consequences are that other similar failures on safety related 480 Volt AC MCCs (EllS: B) could result in a loss of safety related equipment important for safe shutdown of either or both units depending on the affected MCC.

These events will not be counted as a safety system functional failure (SSFF) for the NRC performance indicator, based on the engineering analysis that shows there was no loss of ability to fulfill a safety function.

CORRECTIVE ACTIONS

Immediate corrective actions included the repair of 2B246 which has been completed. A plan has been developed to review a sample of the 480 VAC MCC breakers (EIIS: B) and is being tracked by maintenance and system engineering. Maintenance procedures are also being revised to ensure fasteners that are being used to mount components in MCC Buckets protrude approximately two thread lengths through the back of the bucket.

PREVIOUS SIMILAR EVENTS

There are no previous similar events