07-18-2005 | On March 2, 2005, during performance of the as-found LLRT for the 'A' RHR Shutdown Cooling containment penetration X-13A line, the penetration failed to pressurize. During the as-found LLRT for the 'B' RHR Shutdown Cooling containment penetration X-13B line on March 4, 2005, the penetration failed to pressurize.
Subsequent investigation identified leakage past the inboard HV251F050A and B RHR Shutdown Cooling testable check valves. Both valves were disassembled for examination and were found to have significant damage on the body and disk seats.
The cause of the LLRT failure was determined to be HV251F050A and B gross seat leakage. The seat damage was caused by fretting of the valve seats due to cyclic disk motion during plant operation. The valve disks were permitted to move due to pressure across the valves being equalized during the operating cycle and vibration and/or pump pressure pulses from the Reactor Recirculation system provided the motive force for the cyclic disk motion.
The valves were repaired and satisfactory as-left LLRT results were obtained. Core flow restrictions were imposed for Unit 2 fuel cycle 13 to prevent damage to the HV251F050A and B valves. Planned corrective actions include evaluation of a possible modification solution to provide a differential pressure across the check valve.
Also, Unit 2 procedure TP-264-034, Reactor Recirculation/RHR Injection Loop Hydraulic Response evaluation will be performed to allow stroking of the Unit 2 HV251F015A and B outboard isolation valves at power, and monitoring of vibration effects. There were no actual safety consequences as a result of the damage found in the check valves. |
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PLANT CONDITIONS AT TIME OF EVENT
Unit 2, Mode 5, 0% power
EVENT DESCRIPTION
On March 2, 2005, the containment penetration for the 'A' RHR Shutdown Cooling line failed to pressurize during as-found Local Leak Rate testing (LLRT). On March 4, 2005, during performance of the as-found LLRT for the 'B' RHR Shutdown Cooling containment penetration line, the penetration failed to pressurize. An investigation concluded that the LLRT failures were due to leakage past the inboard HV251F050A and B RHR Shutdown Cooling testable check valves. Both valves were disassembled for examination and were found to have significant damage on the body and disk seats.
PPL conducted an investigation, including analysis performed by Structural Integrity and Kalsi Engineering, to determine the cause of the valve damage. The investigation was completed on May 31, 2005, and concluded that the damage was caused by fretting of the valve seats due to cyclic disk motion during plant operation.
This LER is being submitted in accordance with 10 CFR 50.73(a)(2)(vii) for any event where a single cause or condition resulted in at least one independent train or channel to become inoperable in multiple systems or two independent trains or channels to become inoperable in a single system.
CAUSE OF THE EVENT
The cause of the body seat and disk seat damage was due to relative motion between the disk and the seat, which resulted from a combination of the following circumstances:
- Leakage through the Unit 2 inboard RHR HV251F050A and B testable check valves and/or leakage past the F122 bypass valve enables the section of pipe between the check valves and the HV251F015A and B outboard isolation valves to pressurize, eventually to a point of equilibrium with pressure on the reactor side. Upon reaching the point of equilibrium, the only force keeping the swing check valve disk closed is gravity. The valve disk is then free to move relative to the seat as a result of structural vibration and/or hydraulic Recirculation System pump pressure pulsations.
- Extended operation at high core flows accelerates the damage mechanism. Since there is an incubation period associated with fretting failure, the damage was only observed after cumulative operation at high Recirculation System pump speeds associated with high core flow.
- Side-to-side disk clearance greater than vendor recommended specification on the HV251F050B valve aggravated the relative motion of the valve disk.
ANALYSIS / SAFETY SIGNIFICANCE
The Unit 1 and 2 inboard RHR testable check valves HV151(251)F050A and B are 24-inch Atwood-Morrill swing check valves with cast stainless steel bodies and disks, and stellite hard facing on the body and disk seats. The testable check valves are typically in standby service. The valves are stroked approximately eight times per operating cycle for surveillance testing and are opened with system flow for shutdown cooling for approximately 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> per cycle.
X-13P(B) Containment Penetration To Reckc Loop 'A' M251FD15P(B) RHR Outboard Isolation Valve Testable Check Valve HI25IFO5ONIE9 Figure 1 HV2S1F122/01 Bypass Valve The LLRT is performed such that it tests the leakage through both the RHR HV151(251)F050A (or B) testable check valves and the HV151(251)F122A (or B) bypass valves (Figure 1). A review of previous Unit 2 LLRT results show that the Unit 2 RHR HV251F050A testable check valve successfully passed its LLRT or the 1000# leak test during the last two refueling outages. However, prior to this recent LLRT failure, the 'B' RHR testable check valve failed its LLRT during the last two refueling outages. One of the failures was attributed to the RHR 50B bypass valve F122B. No seat damage was noted, but due to radiation dose considerations, the 'B' RHR testable check valve disk was replaced and the valve rebuilt. The second failure was attributed to the 'B' RHR check valve. Although no seat damage was found, the valve seat was lightly lapped and the disk was replaced.
A review of the Unit 1 LLRT history identified that the RHR testable check valves (i.e., HV151F050A and B) were tested during the last three refueling outages and the results were acceptable. The valves have no prior record of seat damage. The Unit 1 RHR injection check valves are not expected to be subject to the same Susquehanna Steam Electric Station Unit 2 05000388 2005 - 04 - 00 damage mechanism observed in the Unit 2 valves because the Unit 2 recirculation pumps operate at higher pump speeds than the Unit 1 pumps to achieve the same core flow.
Actual Consequences The HV251F050A and B testable check valves are Primary Containment Isolation Valves (PCIVs) and have a function to open to allow Low Pressure Coolant Injection (LPCI) and Shutdown Cooling flow to the reactor vessel. Additionally, these valves are part of the reactor coolant pressure boundary (RCPB).
The disassembly and inspection of the Unit 2 RHR HV251F050A and B valves during the recent refueling outage revealed significant as-found damage to only the body and disk seats. Internal hardware such as the disk nut and pin, hinge arm, washers and bushings, were found in generally good condition. In the HV251F050B valve, one shaft bushing was cracked and there was evidence of wear at the shaft end cover.
However, this wear would not have adversely impacted the valve's operation. No internal parts were found to be missing and therefore damage due to loose parts was not a concern.
refueling outage and the valves would have opened to allow flow for LPCI, if required. There was no challenge to primary containment that would have required the valves to perform their primary containment isolation function. Additionally, there was no evidence of leakage noted at the pressure seal or shaft packing area, so the RCPB function was not compromised. Therefore, there were no actual safety consequences as a result of the damage found in the RHR HV251F050A and B testable check valves.
Potential Consequences In the event an accident had occurred which required the affected valves to perform their PCIV function, the affected penetrations could have been isolated by the outboard PCIVs (i.e., the HV251F015A and B valves).
These are normally closed valves and were operable for the primary containment function when they were opened (e.g. for shutdown cooling). The HV251F015A and B outboard isolation valves are not routinely stroked at power. Any potential consequence would have required an accident with primary containment isolation during the time one of the outboard PCIVs was open, and a failure of the outboard PCIV to close. In this unlikely case, one penetration would not have been completely isolated. The HV251F050A and B testable check valves would still have closed, but significant seat leakage would be expected. However, any leakage through this penetration would have been contained by the closed system of RHR piping beyond the outboard PCIVs. Therefore, any potential consequence of this condition would have been minimal.
CORRECTIVE ACTIONS
Completed Actions
- The Unit 2 RHR HV251F050A and B testable check valves were disassembled and repaired. Satisfactory as-left LLRT results were obtained.
- Vibration monitoring instrumentation was installed inside the Unit 2 drywell on selected points in the RHR and Reactor Recirculation systems to allow for vibration monitoring during the fuel cycle.
RHR HV251F050A and B inboard testable check valves.
Planned Actions
- Procedure TP-264-034, Reactor Recirculation/RHR Injection Loop Hydraulic Response evaluation will be performed allow stroking of the Unit 2 HV251F015A and B outboard isolation valves at power and monitoring of the vibration effects.
- Evaluate a possible modification solution to upgrade the Unit 1 RHR HV151F015A and B outboard isolation valves and/or the Unit 2 RHR HV251F050A and B testable check valves to solve the issue of swing check valve disk positive closure.
ADDITIONAL INFORMATION
Past Similar Events: None
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05000387/LER-2005-001 | R. A. Saccone PPL Susquehanna, LLC Vice President - Nuclear Operations 769 Salem Boulevard Berwick, PA 18603 Tel. 570.542.3959 Fax 570.542-1504 rasaccone@pplweb.com PP SEP 2 0 2005 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Station OP1-17 Washington, DC 20555 SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 50-387/2005-001-01 PLA-5938 Docket 50-387 Reference:� Susquehanna Steam Electric Station — Licensee Event Report 50-387/2005-001-00, dated, Januar), 20, 2005 Susquehanna Steam Electric Station — NRC Integrated Inspection Report 05000387/2004005 and 05000388/2004005, dated, January 28, 2005 Attached is Licensee Event Report 50-387/2005-001-01. This report supplements the referenced Licensee Event Report which identified that primary containment instrument lines found penetrating the Unit 1 Reactor Building's Railroad Bay (an area not normally maintained within Secondary Containment) could prevent structures or systems needed to control the release of radioactive material from fulfilling their safety function. Accordingly, this event was reported in accordance with 10 CFR 50.73(a)(2)(v)(C). By virtue of Susquehanna's ventilation system design, PPL was able to eliminate the non-conforming condition by reconfiguring Secondary Containment in a manner that encompassed the Railroad Bay. On four occasions, however, as noted in the Inspection Report referenced above, PPL temporarily returned the Railroad Bay to its normal configuration (e.g., ventilation outside of secondary containment) to support plant maintenance activities. A misinterpretation of Generic Letter 91-18 guidance, and PPL's belief that the Secondary Containment function was not affected by returning the plant to its normal and customary ventilation alignment, caused PPL to complete the reconfiguration without entering the Secondary Containment LCO 3.6.4.1. Because the Secondary Containment was not restored within LCO Required Action completion times, this situation also constitutes an operation prohibited by the plant's Technical Specifications and is reportable per 10 CFR 50.73(a)(2)(i)(B). .!;;C-a'at>
2- Document Control Desk PLA-5938 or There were no actual consequences to the health and safety of the public as a result of this event. No new regulatory commitments have been created through issuance of this report. Robe A. Saccone Vice President - Nuclear Operations Attachment cc:-Mr. S. J. Collins Regional Administrator U. S. Nuclear Regulatory Commission
475 Allendale Road
King of Prussia, PA 19408
Mr. F. W. Jaxheimer
Sr. Resident Inspector
U. S. Nuclear Regulatory Commission P.O. Box 35
Berwick, PA 18603-0035
Mr. R. Osborne
Allegheny Electric Cooperative
P. 0. Box 1266
Harrisburg, PA 17108-1266
Mr. R. R. Janati
Bureau of Radiation Protection
Rachel Carson State Office Building
P. 0. Box 8469
Harrisburg, PA 17105-8469
NRC FORM 366 APPROVED BY OMB: NO. 3150-0104 . .��EXPIRES: 06/30/2007 (6-2004) U.S. NUCLEAR REGULATORY Estimated burden per response to comply with this mandatory collection request 50 hours. Reported lessons learned are incorporated into theCOMMISSION licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to infocoltects@nrc oov and to the Desk Officer, Office of Information LICENSEE EVENT REPORT (LER) andR egulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Wathington, DC 20503. If a means used to impose an Information collection does not display a currently valid OMB control number, the NRC(See reverse for required number of may not conduct or sponsor, and a person is not required to respond to, thedigits/characterS for each block) information collection. 1. FACILITY NAME Susquehanna Steam Electric Station - Unit 1 2. DOCKET NUMBER 3. PAGE
05000387 1 OF 3
4. Tm.E Primary Containment Instrument Lines Located Outside Secondary Containment | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000387/LER-2005-002 | R. A. Saccone PPL Susquehanna, LLC Vice President - Nuclear Operations 769 Salem Boulevard Berwick, PA 18603 Tel. 570.542.3959 Fax 570.542-1504 rasaccone@ pplweb.com PP TM ULU 21 2005 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Station OP1-17 Washington, DC 20555 SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 50-387/2005-002-00 PLA-5997 Docket 50-387 Attached is Licensee Event Report 50-387/2005-002-00. This event was determined to be reportable per 10 CFR 50.73(a)(2)(i)(A) because the plant was shutdown as required by Technical Specification action statements. On October 28, 2005 at 1600 hours, Susquehanna operators began the process of shutting down Unit 1 for a planned maintenance outage to address known control cell friction issues. Four control rods had previously been declared inoperable because of excessive rod to fuel channel friction. Other rods, previously known to exhibit slow settling characteristics, would be inserted during the controlled shutdown. Rather than delay the shutdown to perform operability testing if these rods again experienced long settling times, it was conservatively determined that any slow settling rods would be declared inoperable and that Technical Specification 3.1.3, Control Rod Operability, would be entered when nine rods had been classified as such. As anticipated, Technical Specification 3.1.3.f was entered at 2332 hours when the ninth control rod was declared inoperable. Entry into this specification requires that the unit be taken to Mode 3, Hot Shutdown, within 12 hours. The controlled shutdown continued until 0805 hours on October 29, 2005, when insertion of all rods was completed and Mode 3 had been entered by placing the mode switch to the Shutdown position. There were no actual consequences to the health and safety of the public as a result of this event. �-2 Document Control Desk PLA-5997 No new regulatory commitments have been created through issuance of this report. 1;0441 Sz. Robert A. Saccone Vice Piesident - Nuclear Operations Attachment cc:�Mr. S. J. Collins
Regional Administrator
U. S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19408 Mr. B. A. Bickett Sr. Resident Inspector U. S. Nuclear Regulatory Commission P.O. Box 35 Berwick, PA 18603-0035 Mr. R. Osborne Allegheny Electric Cooperative P. 0. Box 1266 Harrisburg, PA 17108-1266 Mr. R. R. Janati Bureau of Radiation Protection Rachel Carson State Office Building P. 0. Box 8469 Harrisburg, PA 17105-8469 NRC FORM 3660 APPROVED BY OMB: NO. 3150-0104 . EXPIRES: 06/30/2007 (5-2oo4) U.S. NUCLEAR REGULATORY Estimated burden per response to comply with this mandatory collection request: 50 hours. Reported lessons learned are incorporated into theCOMMISSION licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20556-0001, or by Internet e-ma jnfocoll ctsa c oov, and o h D O ce ,O eLICENSEE EVENT REPORT (LER) and Regula o Affa r , NEOB-10202, ( 50 010)Office anaoemonmt ann Budget Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC(See reverse for required number of may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME Susquehanna Steam Electric Station - Unit 1 2. DOCKET NUMBER 3. PAGE 05000387 1 OF 3 4. -mix TS Required Shutdown Due to Excessive Control Cell Friction | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000388/LER-2005-004 | Common Mode Failure of the Inboard 'A' and 'B' Loop RHR Shutdown Cooling Testable Check Valves due to Vibration-Induced Seat Damage | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
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