On November 13, 2015, at 1745 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.639725e-4 months <br /> during drywell entry, a leak was reported on the "B" Reactor Reactor Recirculation (RXR) Pump Lower Seal Cavity Vent piping. The leak was identified at the inboard pipe-to-union weld and required a weld repair prior to returning to service. The affected piping weld is for 3/4-inch piping, schedule 80 SA-479 TP304 or TP316, union 3000# SA-182 Gr F304 or F316. The affected piping had been in service for approximately 11 months following a previous repair of the weld at this location during the December 2014 forced outage, (e.g., LER 2014-011-00, issued February 11, 2015).
The condition was reported on November 13, 2015 in accordance with 10 CFR 50.72(b)(3)(ii)(A) as a principal safety barrier degradation (EN 51538). This Licensee Event Report (LER) is written in accordance with 10 CFR 50.73(a)(ii)(A) and 10 CFR 50.73(a)(2)(i)(B) as a condition that resulted in a principal safety barrier degradation with evidence of reactor coolant pressure boundary leakage, which is a condition prohibited by the Technical Specifications.
The previous December 2014 weld repair did not fully excavate the weld and remove the J-groove, and thereby eliminate the presence of the crack.
Repair of the cracked weld was performed prior to the restart of Unit 1. The safety significance of this condition is minimal. Given the size of the leak, there were no consequences to the health and safety of the public. |
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Category:Letter
MONTHYEARIR 05000387/20230042024-02-0707 February 2024 Integrated Inspection Report 05000387/2023004 and 05000388/2023004 PLA-8096, Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval2024-01-0404 January 2024 Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval PLA-8077, Emergency Plan Revision 67 (PLA-8077)2023-12-27027 December 2023 Emergency Plan Revision 67 (PLA-8077) IR 05000387/20230102023-12-11011 December 2023 Fire Protection Team Inspection Report 05000387/2023010 and 05000388/2023010 PLA-8089, Submittal of Revision to Inservice Testing Program Plan2023-12-0505 December 2023 Submittal of Revision to Inservice Testing Program Plan PLA-8084, Application to Revise Technical Specifications to Adopt TSTF-568, Revise Applicability of BWR TS 3.6.2.5 and TS 3.6.3.22023-11-29029 November 2023 Application to Revise Technical Specifications to Adopt TSTF-568, Revise Applicability of BWR TS 3.6.2.5 and TS 3.6.3.2 ML23345A0682023-11-28028 November 2023 Technical Specification Bases, Manual PLA-8091, Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inseervice Inspection Interval (PLA-8091)2023-11-0808 November 2023 Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inseervice Inspection Interval (PLA-8091) IR 05000387/20230032023-11-0303 November 2023 Integrated Inspection Report 05000387/2023003 and 05000388/2023003 PLA-8082, Proposed Amendment to Licenses NPF-14 and NPF-22: Application to Revise Technical Specifications to Adopt TSTF-563, Revise Instrument Testing Definitions to Incorporate the Surveillance Frequency Control Program2023-11-0202 November 2023 Proposed Amendment to Licenses NPF-14 and NPF-22: Application to Revise Technical Specifications to Adopt TSTF-563, Revise Instrument Testing Definitions to Incorporate the Surveillance Frequency Control Program ML23291A1132023-10-12012 October 2023 Submittal of Revision 71 to Updated Final Safety Analysis Report and Revision 25 to Fire Protection Review Report ML23279A0612023-10-0505 October 2023 Paragon Energy Solutions LLC, Part 21 Final Report Re Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) ML23277A0412023-10-0505 October 2023 Notification of Commercial Grade Dedication Inspection (05000387/2024011 and 05000388/2024011) and Request for Information IR 05000387/20233012023-09-20020 September 2023 Initial Operator Licensing Examination Report 05000387/2023301 and 05000388/2023301 ML23254A0242023-09-0606 September 2023 Paragon Energy Solutions LLC, Potential Defect with Eaton Jd and Hjd Series Molded Case Circuit Breakers (Mccbs) IR 05000387/20230052023-08-31031 August 2023 Updated Inspection Plan for Susquehanna Steam Electric Station, Units 1 and 2 (Report 05000387/2023005 and 05000388/2023005) ML23228A1952023-08-21021 August 2023 Summary of August 10, 2023, Public Observation Meeting Re. Proposed Alternative PLA-8080, Proposed Relief for Valve 251130 (PLA-8080)2023-08-14014 August 2023 Proposed Relief for Valve 251130 (PLA-8080) PLA-8074, Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval2023-08-0303 August 2023 Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval IR 05000387/20230022023-08-0101 August 2023 Integrated Inspection Report 05000387/2023002 and 05000388/2023002 ML23195A1852023-07-27027 July 2023 Correction to Technical Specifications Page 3.3-73 in Amendment No. 265 PLA-8076, Unit 2 - 21st Refueling Outage Owner'S Activity Report (PLA-8076)2023-07-20020 July 2023 Unit 2 - 21st Refueling Outage Owner'S Activity Report (PLA-8076) ML23201A0152023-07-20020 July 2023 Operator Licensing Examination Approval ML23200A1012023-07-19019 July 2023 Notification of Conduct of a Fire Protection Team Inspection ML23193A0062023-07-12012 July 2023 Requalification Program Inspection PLA-8078, Submittal of Unit 2 Cycle 22 Core Operating Limits Report, Revision 1, PLA-80782023-07-0505 July 2023 Submittal of Unit 2 Cycle 22 Core Operating Limits Report, Revision 1, PLA-8078 ML23163A1012023-06-12012 June 2023 10 CFR 50.46 Annual Report (Pla 8065) PLA-8054, Proposed Amendment to Licenses NPF-14 and NPF-22: Remove Control Rod Operability Separation Criteria and Replace Reference to Banked Position Withdrawal Sequence with the Analyzed Rod Position Sequence2023-06-0808 June 2023 Proposed Amendment to Licenses NPF-14 and NPF-22: Remove Control Rod Operability Separation Criteria and Replace Reference to Banked Position Withdrawal Sequence with the Analyzed Rod Position Sequence IR 05000387/20234012023-06-0707 June 2023 Security Baseline Inspection Report 05000387/2023401 and 05000388/2023401 PLA-8073, Proposed Relief Request for the Fifth 10-Year Inservice Inspection Interval2023-06-0101 June 2023 Proposed Relief Request for the Fifth 10-Year Inservice Inspection Interval PLA-8064, Response to NRC Regulatory Issue Summary 2023-01 (PLA-8064)2023-05-17017 May 2023 Response to NRC Regulatory Issue Summary 2023-01 (PLA-8064) ML23132A3212023-05-17017 May 2023 Associated Independent Spent Fuel Storage Installation - Issuance of Amendment Nos. 285 and 269 Related to Order Approving Transfer of Licenses PLA-8067, Notification of Completion of Emergence from Bankruptcy (PLA-8067)2023-05-17017 May 2023 Notification of Completion of Emergence from Bankruptcy (PLA-8067) IR 05000387/20230012023-05-12012 May 2023 Integrated Inspection Report 05000387/2023001 and 05000388/2023001 PLA-8066, Notification of Planned Closing Date and Information Identified in March 30, 2023 Order, PLA-80662023-05-0808 May 2023 Notification of Planned Closing Date and Information Identified in March 30, 2023 Order, PLA-8066 PLA-8053, Radiation Exposure Information and Reporting System2023-04-27027 April 2023 Radiation Exposure Information and Reporting System PLA-8058, Annual Radiological Environmental Operating Report (PLA-8058)2023-04-26026 April 2023 Annual Radiological Environmental Operating Report (PLA-8058) PLA-8041, Radioactive Effluent Release Report and Offsite Dose Calculation Manual (PLA-8041)2023-04-25025 April 2023 Radioactive Effluent Release Report and Offsite Dose Calculation Manual (PLA-8041) PLA-8047, 2022 Annual Environmental Operating Report (Nonradiological), PLA-80472023-04-19019 April 2023 2022 Annual Environmental Operating Report (Nonradiological), PLA-8047 PLA-8062, Supplement to Relief Request 4RR-10 Relief from Code Seal Weld Requirement for Valve 252F007B, PLA-80622023-04-11011 April 2023 Supplement to Relief Request 4RR-10 Relief from Code Seal Weld Requirement for Valve 252F007B, PLA-8062 PLA-8061, Relief Request 4RR-10 Relief from Code Seal Weld Requirement for Valve 25F007B, PLA-80612023-04-10010 April 2023 Relief Request 4RR-10 Relief from Code Seal Weld Requirement for Valve 25F007B, PLA-8061 ML23090A2302023-03-31031 March 2023 NRC Decommissioning Funding Status Report PLA-8049 PLA-8060, Submittal of Unit 2 Cycle 22 Core Operating Limits Report (PLA-8060)2023-03-30030 March 2023 Submittal of Unit 2 Cycle 22 Core Operating Limits Report (PLA-8060) ML23095A0572023-03-29029 March 2023 NRC Decommissioning Funding Status Report December 31, 2022 PLA-8057, Application for Order Approving Indirect Transfer of Control of Licenses and Approving Conforming License Amendments- Supplemental Information, PLA-80572023-03-15015 March 2023 Application for Order Approving Indirect Transfer of Control of Licenses and Approving Conforming License Amendments- Supplemental Information, PLA-8057 ML23065A1962023-03-0202 March 2023 EN 56387 Paragon - Part 21 Report Re Defect Identified in Automatic Transfer Switch Pn: NLI-ATS480A400X1 IR 05000387/20220062023-03-0101 March 2023 Annual Assessment Letter for Susquehanna Steam Electric Station, Units 1 and 2 (Reports 05000387/2022006 and 05000388/2022006) PLA-8052, (Sses), Proof of Financial Protection and Guarantee of Payment of Deferred Premiums2023-02-13013 February 2023 (Sses), Proof of Financial Protection and Guarantee of Payment of Deferred Premiums IR 05000387/20220042023-02-0808 February 2023 Integrated Inspection Report 05000387/2022004 and 05000388/2022004 ML23010A0882023-01-15015 January 2023 Summary of Regulatory Audit in Support of License Amendment Request to Revise Control Rod Technical Specifications 2024-02-07
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000388/LER-2017-0102018-02-0202 February 2018 Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switches, LER 17-010-00 for Susquehanna, Unit 2 Regarding Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switches 05000387/LER-2017-0072017-10-0909 October 2017 Secondary Containment Declared Inoperable Due to the opening of a plenum., LER 17-007-00 for Susquehanna Steam Electric Station Regarding Secondary Containment Declared Inoperable Due to Supply Air Flow 05000387/LER-2017-0052017-10-0404 October 2017 Automatic Reactor Protection System Trip on High Neutron Flux, LER 17-005-01 for Susquehanna, Unit 1 Regarding Automatic Reactor Protection System Trip on High Neutron Flux 05000388/LER-2017-0082017-09-18018 September 2017 1 OF 3, LER 17-008-00 for Susquehanna, Unit 2, Regarding Condition Prohibited by Technical Specifications Due to a Loose Terminal Block Associated with a Primary Containment Isolation Valve 05000387/LER-2017-0062017-09-0606 September 2017 Control Room Envelope In-leakage Exceeded the Technical Specification Limit, LER 17-006-00 for Susquehanna, Unit 2, Regarding Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan 05000387/LER-2017-0042017-08-0404 August 2017 Secondary Containment Declared Inoperable Due to Failure of an Exhaust Fan Breaker., LER 17-004-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Failure of an Exhaust Fan Breaker 05000388/LER-2017-0022017-05-0505 May 2017 Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 during Unit 2 Refueling, LER 17-002-00 for Susquehanna, Unit 2, Regarding Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 During Unit 2 Refueling 05000387/LER-2017-0032017-05-0505 May 2017 Susquehanna Steam Electric Station Unit 1 05000387, LER 17-003-00 for Susquehanna, Units 1 and 2, Regarding Loss of Secondary Containment Zone 3 Due to Fan Trip 05000387/LER-2017-0012017-05-0505 May 2017 Secondary Containment Breach Due to Simultaneous Opening of Airlock Doors, LER 17-001-00 for Susquehanna, Unit 2, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Sticking Door Latch 05000387/LER-2017-0022017-04-12012 April 2017 Secondary Containment Breach due to Simultaneous Opening of Airlock Doors, LER 17-002-00 for Susquehanna, Unit 1, Regarding Secondary Containment Breach due to Simultaneous Opening of Airlock Doors 05000388/LER-2016-0052016-07-12012 July 2016 Unit 2 HPCI Manually Overridden Prior to a Manual Scram During a Plant Transient, LER 16-005-00 for Susquehanna, Unit 2, Regarding HPCI Manually Overridden Prior to a Manual Scram During a Plant Transient 05000387/LER-2016-0152016-06-15015 June 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error, LER 16-015-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error 05000387/LER-2016-0142016-06-0909 June 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error, LER 16-014-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error 05000387/LER-2016-0132016-06-0909 June 2016 Secondary Containment Declared Inoperable Due to Simultaneous Opening of Double Airlock Doors, LER 16-013-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Simultaneous Opening of Double Airlock Doors 05000387/LER-2016-0102016-05-31031 May 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Medical Emergency, LER 16-010-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Medical Emergency 05000387/LER-2016-0092016-05-26026 May 2016 Valid Primary Containment Isolation Actuation during Local Leak Rate Testing due to Human Performance Error, LER 16-009-00 for Susquehanna, Unit 1, Regarding Valid Primary Containment Isolation Actuation During Local Leak Rate Testing Due to Human Performance Error 05000387/LER-2016-0082016-05-19019 May 2016 Inoperability of Diesel Generator Due to Misalignment of MOC Switch Contacts Due to Inadequate Post Maintenance Testing, LER 16-008-00 for Susquehanna, Unit 1, Regarding Inoperability of Diesel Generator Due to Misalignment of MOC Switch Contacts Due to Inadequate Post Maintenance Testing 05000387/LER-2016-0112016-05-16016 May 2016 Valve inoperability for a period longer than allowed by Technical Specifications, LER 16-011-00 for Susquehanna, Unit 1, Regarding Valve Inoperability for a Period Longer Than Allowed by Technical Specifications 05000387/LER-2016-0052016-05-16016 May 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Human Performance Error, LER 16-005-00 for Susquehanna, Units 1 and 2, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Human Performance Error 05000387/LER-2016-0062016-05-10010 May 2016 Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, LER 16-006-00 for Susquehanna, Unit 1, Regarding Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 05000387/LER-2016-0042016-05-10010 May 2016 Momentary Loss of Secondary Containment due to Both Airlock Doors on Elevation 779 of the Unit 2 Reactor Building being Opened at the Same Time, LER 16-004-00 for Susquehanna, Unit 1, Regarding Momentary Loss of Secondary Containment Due to Both Airlock Doors on Elevation 779 of the Unit 2 Reactor Building Being Opened at the Same Time 05000387/LER-2016-0032016-05-0606 May 2016 Unit 2 Zone 3 HVAC unable to maintain Zone 3 differential pressure greater than 0.25 in wg, LER 16-003-00 for Susquehanna, Unit 1, Regarding Unit 2 Zone 3 HVAC Unable to Maintain Zone 3 Differential Pressure Greater Than 0.25 in wg 05000387/LER-2016-0072016-05-0303 May 2016 Inoperability of Swing Bus Transfer Switch Due to Deformed Bolt on Linkage, LER 16-007-00 for Susquehanna, Unit 1, Regarding Inoperability of Swing Bus Transfer Switch Due to Deformed Bolt on Linkage 05000387/LER-2016-0012016-04-18018 April 2016 Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence, LER 16-001-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence 05000387/LER-2016-0022016-04-18018 April 2016 Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence, LER 16-002-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence 05000387/LER-2015-0062016-03-30030 March 2016 Loss of Safety Function due to Inoperability of Both Trains of the Standby Gas Treatment System and a Loss of Safety Function of the Control Room Emergency Outside Air Supply System due to Air Flow Controller found in Manual, LER 15-006-01 for Susquehanna, Unit 1, Regarding Loss of Safety Function due to Inoperability of Both Trains of the Standby Gas Treatment System and a Loss of Safety Function of the Control Room Emergency Outside Air Supply System due to Air Flow... 05000387/LER-2015-0012016-02-10010 February 2016 Inoperability of the 'B' Emergency Diesel Generator due to Fuel Oil Leakage, LER 15-001-01 for Susquehanna, Unit 1, Regarding Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Steam Dome - Low Switches 05000387/LER-2015-0032016-01-26026 January 2016 Secondary Containment Inoperability Due to Failure to Meet Technical Specification Surveillance Requirement 3.6.4.1.1, LER 15-003-01 for Susquehanna, Unit 1, Regarding Secondary Containment Inoperability Due to Failure to Meet Technical Specification Surveillance Requirement 3.6.4.1.1 05000387/LER-2015-0092016-01-11011 January 2016 Pressure Boundary Leakage From an Inadequate Weld Repair in Small Bore Pump Seal Vent Piping, LER 15-009-00 for Susquehanna, Unit 1, Regarding Pressure Boundary Leakage From an Inadequate Weld Repair in Small Bore Pump Seal Vent Piping 05000387/LER-2015-0072016-01-0808 January 2016 Unit 1 'B' Inboard Main Steam Isolation Valve, HV141F022B closed during surveillance test which caused a SCRAM on Unit 1, LER 15-007-00 for Susquehanna, Unit 1, Regarding 'B' Inboard Main Steam Isolation Valve, HV141 F022B Closed During Surveillance Test Which Caused a SCRAM PLA-7323, LER 015-001-00 for Susquehanna Regarding Inoperability of the B Emergency Diesel Generator Due to Fuel Oil Leakage2015-04-28028 April 2015 LER 015-001-00 for Susquehanna Regarding Inoperability of the B Emergency Diesel Generator Due to Fuel Oil Leakage 2018-02-02
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
CONDITIONS PRIOR TO THE EVENT
Unit 1 — Mode 4, Unplanned shutdown, 0 Percent Other than the leaking weld itself there were no systems, structures, or components at the start of the event that contributed to the event. Prior to this condition on November 12, 2015, at 1132 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.30726e-4 months <br />, the Unit 1 reactor automatically scrammed due to one Main Steam Isolation Valve (MSIV) unanticipated closure causing a High Pressure Reactor Protection System trip. During the unplanned forced outage, a drywell entry and drywell leakage investigation were performed.
EVENT DESCRIPTION
On November 13, at 1745 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.639725e-4 months <br /> during drywell entry, a leak was reported on the "B" Reactor Recirculation (RXR) [EIIS System Identifier: AD] Pump [EIIS Component Identifier: P] Lower Seal Cavity Vent piping [EllS Component Identifier: PSP]. The leak was identified at the inboard pipe-to-union weld and required a weld repair prior to returning Unit 1 to service. The leaking weld was attached to the vendor supplied replacement pump seal chamber. The affected piping weld is for 3/4-inch piping, schedule 80 SA-479 TP304 or TP316, union 3000# SA-182 Gr F304 or F316. The affected piping had been in service for approximately 11 months following a previous repair of the weld at this location during the December 2014 forced outage of Unit 1, (e.g., LER 2014-011-00, issued February 11, 2015). A timeline of relevant events follows:
Mid-1990s April 2013 April 2014 December 2014 December 2014 through 2015 November 12, 201 Replacement RXR pump shafts and related components were procured from FLOWSERVE (formerly BW/IP). The replacement shafts were stored in the warehouse until installed (one on the 2A RXR pump in 2013 and the other on the 1B RXR pump in 2014). The weld discovered to have cracking and leakage in December 2014 was a vendor weld that existed at the time of procurement.
The 2A RXR pump shaft and related components were replaced with components procured form FLOWSERVE in the mid-1990s.
The 1B RXR Pump shaft and related components were replaced with components procured from FLOWSERVE in the mid-1990s.
Unit 1 initiation of a plant shutdown due to unidentified drywell leakage, discovery of weld cracking at this location, and its repair.
Unit 1 drywell leakage took a step increase from 0.1 to 0.2 gallons per minute (GPM) on December 28, 2014. Subsequently, gradual increases in excess drywell leakage were observed, (e.g., 0.2 to 0.6 GPM).
5 Unit 1 reactor scram due to 'B' inboard MSIV closure during surveillance testing, (unrelated to this condition).
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
November 13, 2015 Drywell leakage is identified again to be at the 1P401B Reactor Recirculation Pump Seal Connection No. 8.
November 21, 2015 A weld repair was again performed on the 1B reactor recirculation pump seal.
This condition was reported on November 13, 2015, at 0022 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />, in accordance with 10 CFR 50.72(b)(3)(ii)(A) as a principal safety barrier degradation (EN 51538). This License Event Report (LER) is written in accordance with 10 CFR 50.73(a)(ii)(A) and 10 CFR 50.73(a)(2)(i)(B) as a condition that resulted in a principal safety barrier degradation with evidence of reactor coolant pressure boundary leakage, which is a condition prohibited by Technical Specifications.
CAUSE OF THE EVENT
The cause of this event is a decision making process that did not consider the technical merits of prudent versus allowable repair options. More specifically, the previous December 2014 weld repair did not fully excavate the weld and remove the J-groove, and thereby eliminate the presence of the crack.
A lack of fusion between original vendor weld passes, or at the root of the weld at the interface with the remaining vendor weld, is also considered to be a causal factor, contributing to further weld cracking and resulting reactor coolant pressure boundary leakage. This lack of fusion remaining within in the vendor weld, not in the December 2014 weld repair itself, created an initiating site for fatigue cracking to worsen.
ANALYSIS/SAFETY SIGNIFICANCE
The consequence of this condition was a violation of the Unit 1 Technical Specification (TS), Section 3.4.4, "Reactor Coolant System (RCS)," a reportable condition. The TS requires RCS leakage be limited to no pressure boundary leakage.
The safety significance of this condition is minimal. A 3/4-inch unisolable pipe leak from the reactor coolant pressure boundary from this condition is unlikely, given the drywell leakage observed prior to this repair, e.g., 0.6 GPM. Allowable reactor coolant system operational leakage limits are based on the predicted and experimentally observed behavior of pipe cracks. The probability is small that the imperfection or crack associated with such leakage would grow rapidly. The unidentified leakage flow limit of Technical Specifications allows time for corrective action before the reactor coolant pressure boundary could be significantly compromised. The five GPM limit is a small fraction of the calculated flow from a critical crack in the primary system piping. Crack behavior from experimental programs shows that leakage rates of hundreds of gallons per minute will precede crack instability. In summary, given the size of the leak, there were no actual consequences to the health and safety of the public.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
CORRECTIVE ACTIONS
Completed - Repair of the cracked weld was performed prior to the restart of Unit 1.
Planned - The procedure for control of welding will be revised to include additional requirements for addressing repair of cracked welds on small bore reactor coolant pressure boundary piping, such that the cognizant weld engineer consults with the Non-Destructive Examination (NDE) supervision, and/or manager of programs engineering to:
- identify possible repair options with respect to removal of the weld metal defects (e.g., excavate unacceptable defects to sound metal, remove entire weld to base metal, etc.),
- assess risk for each identified repair option, (e.g., potential consequences if the method is ineffective),
- document selected repair option, and
- ensure the planner assigned to plan a weld repair work document is provided a specific repair option that documents their instruction.
PREVIOUS SIMILAR EVENTS
This event is similar to the following event, involving a weld crack repair and leakage at this same location.
- LER 50-387/2014-011-00: "Degraded Condition Due to Reactor Coolant Pressure Boundary Leakage Caused by an Inadequate Weld," issued February 11, 2015.
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05000387/LER-2015-001 | Inoperability of the 'B' Emergency Diesel Generator due to Fuel Oil Leakage LER 15-001-01 for Susquehanna, Unit 1, Regarding Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Steam Dome - Low Switches | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000388/LER-2015-001 | Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Steam Dome - Low Switches | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000387/LER-2015-002 | Secondary Containment Inoperability Due to Failure to Meet Technical Specification Surveillance Requirement 3.6.4.1.1 | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2015-002 | Secondary Containment Inoperability Due To Failure to Meet Technical Specification Surveillance Requirement 3.6.4.1.1 | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2015-003 | Secondary Containment Inoperability Due to Failure to Meet Technical Specification Surveillance Requirement 3.6.4.1.1 LER 15-003-01 for Susquehanna, Unit 1, Regarding Secondary Containment Inoperability Due to Failure to Meet Technical Specification Surveillance Requirement 3.6.4.1.1 | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2015-003 | Unit 2 Automatic Reactor Scram Caused by Main Turbine Trip Due to Loss of Main Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000387/LER-2015-004 | Secondary Containment Inoperable due to Secondary Containment Boundary Door Found Ajar | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2015-004 | Degraded Condition Due to Reactor Coolant Pressure Boundary Leakage Caused by Vibration and Stiff Pipe Connection | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000388/LER-2015-005 | Condition Prohibited by Technical Specifications Due to Implementation of Enforcement Guidance Memorandum (EGM) 11-003 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000387/LER-2015-006 | Loss of Safety Function due to Inoperability of Both Trains of the Standby Gas Treatment System and a Loss of Safety Function of the Control Room Emergency Outside Air Supply System due to Air Flow Controller found in Manual LER 15-006-01 for Susquehanna, Unit 1, Regarding Loss of Safety Function due to Inoperability of Both Trains of the Standby Gas Treatment System and a Loss of Safety Function of the Control Room Emergency Outside Air Supply System due to Air Flow... | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2015-006 | Secondary Containment Declared Inoperable Due to Secondary Containment Boundary Door 104-R Breached. | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2015-007 | Unit 1 'B' Inboard Main Steam Isolation Valve, HV141F022B closed during surveillance test which caused a SCRAM on Unit 1 LER 15-007-00 for Susquehanna, Unit 1, Regarding 'B' Inboard Main Steam Isolation Valve, HV141 F022B Closed During Surveillance Test Which Caused a SCRAM | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000388/LER-2015-007 | 1 of 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000387/LER-2015-008 | 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000387/LER-2015-009 | Pressure Boundary Leakage From an Inadequate Weld Repair in Small Bore Pump Seal Vent Piping LER 15-009-00 for Susquehanna, Unit 1, Regarding Pressure Boundary Leakage From an Inadequate Weld Repair in Small Bore Pump Seal Vent Piping | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded |
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