05000354/LER-2002-003

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LER-2002-003, PSEG Nuclear LLC
P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236
0 PSEG
Nuclear LLC
JUN 12 2002
LR-NO2-0201
U. S. Nuclear Regulatory Commission
Document Control Desk
Washington, DC 20555
SPECIAL REPORT 354/2002-003-00
HOPE CREEK GENERATING STATION
FACILITY OPERATING LICENSE NO. NPF-57
DOCKET NO. 50-354
Gentlemen:
This Special Report entitled "License Condition Violation — Reactor Power and Minimum
Feedwater Temperature Limits", is being submitted pursuant to the requirements of
License Conditions 2.C. (1), (11), and 2.F. The attached Special Report contains no
commitments.
D. F. Garcho
Vice Presiden - Operations
Attachment
/MGM
C � Distribution
LER File 3.7
95-2168 REV. 7/99
NRC FORM 366 6 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004
(7-2001) ) COMMISSION 6 Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to
industry. Send comments regarding burden estimate to the Records Management Branch (7-6
E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to
LICENSEE EVENT REPORT (LER) 6bjs1@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-
10202 (3150-0104), Office of Management and Budget Washington, .DC 20503. If a means (See reverse for required number of
digits/characters for each block) used to impose information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the
Hope Creek Generating Station I 05000354 I 1 OF 5
License Condition Violation - Reactor Power and Minimum Feedwater Temperature Limits
Docket Number
Event date:
Report date:
3542002003R00 - NRC Website

2002 0 FACILITY NAME (1) Hope Creek Generating Station DOCKET (2) LER NUMBER (6 0 3 00 PAGE 3)

PLANT AND SYSTEM IDENTIFICATION

General Electric — Boiling Water Reactor (BWR/4) Feedwater System — EIIS Identifier {SJ/--} * Reactor Water Cleanup System — EIIS Identifier {CE/--}* Emergency Core Cooling SystemEIIS Identifier {Bot--}* Electrohydraulic Control System — EIIS Identifier {TG/--}* Technical Support Center Ventilation System — EIIS Identifier {VF/--}* Fuel Pool Cooling System — EIIS Identifier {DA/--}* Safety Auxiliaries Cooling System — EIIS Identifier {CC/--}* Control Room Ventilation System — EIIS Identifier {V1/--}* Hydrogen Water Chemistry Injection System — EIIS Identifier {KDA-}* Radiation Monitoring System — EIIS Identifier {IU--}* Switchyard System — EIIS Identifier {FIV--}* Drywell Unit Coolers - EIIS Identifier {VB//—}* Turbine Building Chillers - EIIS Identifier {viv--}* *Energy Industry Identification System {EIIS} codes and component function identifier codes appear as (SS/CCC)

IDENTIFICATION OF OCCURRENCE

Date of occurrence: May 13, 2002

CONDITIONS PRIOR TO OCCURRENCE

Mode 1 — 100% power. No structures, systems, or components were inoperable at the time of the occurrence that contributed to the event.

DESCRIPTION OF OCCURRENCE

At approximately 0025, May 13, 2002, the Hope Creek Generating Station (HCGS) experienced a major electrical transient. The cause of the transient was attributed to the clearing and rapid re- powering of the 5024 (New Freedom) Line, which ties into the Salem switchyard. Per the Load Dispatcher, New Freedom breakers {FK/52} 2-8 & 7-8 opened concurrently with the Salem 2-6 & 5-6 breakers {FK/52}. The 2-6 and 2-8 breakers subsequently re-closed in a rapid fashion re-powering 2002 0 FACILITY NAME (1) Hope Creek Generating Station DOCKET (2) (1 SEQUENTIAL REVISION LER NUMBER6) 0 3 00 DESCRIPTION OF OCCURRENCE (Cont'd) the 5024 line. Several site personnel subsequently reported a lightning strike in the vicinity of the 5024 line at 0025. The resulting electrical transient had the following impact on HCGS Plant Equipment: trip of the "A" Electrohydraulic Control (EHC) Pump {TG/P}, loss of all drywell unit coolers {VB/CHU}, trip of the 6A, B, & C feedwater heaters {SJ/HX}, loss of all turbine building chillers {VK/CHU}, trip of the "B" Fuel Pool Cooling (FPC) pump {DA/P}, trip of the "A" & "B" Reactor Water Cleanup (RWCU) pumps {CE/P} and loss of the filter-demineralizer precoats, trip of the "C" Emergency Core Cooling System (ECCS) jockey pump {BO/P}, Hydrogen Water Chemistry Injection (HWCI) system trip, loss of the North Plant Vent (NPV), South Plant Vent (SPV), Drywell Leak Detection (DLD), and Cooling Tower Blowdown (CTB) Radiation Monitoring System (RMS) skids {IU- -}, trip of the "B" Technical Support Center (TSC) ventilation train with auto start of the "A" train, auto start of the "A" Safety Auxiliaries Cooling System (SACS) pump {CC/P}, trip of the "A" Control Room (CR) ventilation train with auto start of the "B" train, trip of the "B" Reactor Feedpump (RFP) main lube oil pump {SJ/P} with auto start of the auxiliary and emergency lube oil pumps {SJ/P}, and trip of the circulating water hypochlorination system. Power peaked at approximately 105% during the transient due to reduced feedwater temperature. Abnormal Operating procedures were entered for Reactor Power, Feedwater heating, Turbine Hydraulic Pressure, and Drywell Pressure. Power was immediately reduced to 100% and the plant stabilized, and all equipment was returned to normal service. Power was further reduced to 80% in accordance with abnormal operating procedures associated with the loss of feedwater heating. Reactor power peaked at 105.23% and feedwater reached 347degrees F due to the loss of feedwater heating. The operating crew restored extraction steam to the 6A, 6B and 6C feedwater heaters at 0123 and feedwater temperature returned to 394 degrees F. Limiting Conditions for Operation (LCO) were entered for the 15%/hr power change, "A" offgas pretreatment RMS alarm, HWCI trip, "C" ECCS jockey pump, NPV, SPV, CTB, DLD, and RWCU continuous conductivity. This event was terminated more quickly than a similar event that occurred in 1999 due to proper operator recovery action during this event.

The following summarizes the effect on the plant and actions taken: power was immediately reduced to 100% on identification of the power excursion in accordance with reactor power Abnormal Operating Procedure, "B" EHC pump was immediately placed in service upon identification that "A" EHC pump was no longer in service (lowest EHC pressure 1460 psig), power was further reduced to 80% upon identification of a greater than 10 degrees F change in FW heating due to loss of multiple #6 FW heaters, as drywell pressure rose to approximately 0.75 psig, drywell unit coolers were restored (peak drywell pressure reached 0.8-0.9 psig before turning). Subsequently, 3 turbine building chillers were reset locally and returned to service, "B" FPC pump was returned to service, both RWCU pumps were isolated per procedure, the "C" ECCS jockey pump immediately auto restarted and the RHR "A", "C" and core spray "A" fill and vents were inspected with no evidence of air in the system. In addition, HWCI was returned to service, the NPV and SPV RMS were returned to service, and the DLD and CTB RMS auto started when acknowledged. The SACS system was DOCKET (2) DESCRIPTION OF OCCURRENCE (Cont'd) returned to normal alignment and the "B" RFP lube oil line-up was returned to normal. Chemistry was informed of the circulating water hypochlorination system trip, control board walkdowns and alarm chronology reviews were conducted.

CAUSE OF OCCURRENCE

The apparent cause of the event is attributed to equipment malfunction resulting from the electrical transient following a lightning strike.

PRIOR SIMILAR OCCURRENCES

Prior Hope Creek and Salem LERs and SRs were reviewed for similar events. A similar event was reported in LER 354/1999-009-00, "License Condition Violation — Minimum Feedwater Temperature Limits." The cause of this event was attributed to equipment malfunction resulting from the electrical transient following a lightning strike. The safety lockout of the Primary Containment Instrument Gas (PCIG) compressors and the isolation of the number 6 Feedwater Heater resulted in the immediate entry into Technical Specification 3.0.3 for two inoperable Main Steam Isolation Valve (MSIV) Sealing System subsystems and violation of the Operating License condition for required minimum feedwater heater capacity, respectively. Less than adequate operator response to the plant transient extended the license condition violation for approximately six hours following the lightning strike.

SAFETY CONSEQUENCES AND IMPLICATIONS

The minimum feedwater temperature reported during the transient was 347 degrees F (421 degrees F nominal). The reload licensing analysis for the current cycle of operation assumes a 110 degrees F temperature loss (to 311 degrees F), while operating at rated power, without violation of the fuel cladding integrity Safety Limit. Based on the above, there was no impact to the health and safety of the public.

A review of this condition determined that a Safety System Functional Failure (SSFF) has not occurred as defined in Nuclear Energy Institute (NEI) 99-02.

DOCKET (2)

CORRECTIVE ACTIONS

A design change to revise the logic for the 6A, 6B and 6C Feed Water Heaters to provide complete UPS protection of these FW Heaters has been implemented.

COMMITMENTS

The corrective actions cited in this Special Report are voluntary enhancements and do not constitute commitments.