05000316/LER-2003-005

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LER-2003-005, 1 of 4
Donald C. Cook Nuclear Plant Unit 2
Event date: 12-30-2003
Report date: 02-17-2004
3162003005R00 - NRC Website

Description of Event

On December 30, 2003, at approximately 1328 EST, the Unit 2 reactor automatically tripped on low steam generator water level coincident with feed flow less than steam flow for Steam Generator #22.

Just prior to the trip, Instrument and Control Technicians were performing a calibration of 2-IFC-325 [BP - FCV], West Residual Heat Removal Pump (PP-35W) Discharge Flow Switch. While connecting a lead, a momentary ground occurred at the terminal box. The resulting ground fault current and subsequent inrush current caused the Control Room Instrument Distribution (GRID) IV [ED - INVT] inverter to transfer to the alternate power supply. The voltage transient on the GRID IV bus was enough to open the Feedwater Isolation Relay (K666X2). The opening of the relay initiated a seal-in closure signal to Steam Generator #22 and #23 Feedwater Isolation Valves (2-FMO-202 and 2-FMO-203) [ISV]. Control Room personnel observed the GRID IV abnormal annunciator and Steam Generator water level alarms and immediately implemented actions to respond to the alarms. An automatic reactor trip occurred due to a low steam generator level coincident with feed flow less than steam flow.

Following the reactor trip, the Unit 2 Output Breakers failed to automatically open due a Main Turbine Stop Valve [SB] position indicator failing to provide a closed indication. The Unit Output Breakers were manually opened in accordance with the reactor trip response procedure. All safety components started and performed as expected.

At 1501 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.711305e-4 months <br /> on December 30, 2003, Indiana Michigan Power Company (I&M) made a four-hour notification to the NRC Operations Center, in accordance with 10 CFR 50.72(b)(2)(iv)(B) to report the actuation of the reactor protection system and resultant reactor scram.

Cause of Event

The cause of the Unit 2 automatic reactor trip was the loss of feedwater flow to Steam Generator #22. The cause of the loss of feedwater flow was the closure of the Feedwater Isolation Valve when the Feedwater Isolation Relay opened following a momentary electrical disturbance on GRID IV. The electrical disturbance was caused by a momentary ground fault created while connecting a lead during the calibration of 2-IFC-325, which is powered by CRID IV.

The root cause of the Unit 2 trip was inattention on the part of the Instrument & Control Technician performing the connection of live leads in the terminal box for 2-IFC-325. The technician brought the lead in close proximity to the terminal box edge and caused a ground fault. The current drawn as a result of the fault caused a voltage transient resulting in an unanticipated voltage drop below the design opening value of relay 2-K666-X2-B. The opening of this relay sent a dose signal to the Feedwater Isolation Valves, which subsequently resulted in the reactor trip.

2003 � 005 � 00 17. TEXT (If more space Is required, use additional copies of NRC Form (366A)

Analysis of Event

An assessment of this event was performed and it was determined that this event was bounded by the existing accident analysis associated with unplanned reactor trips with the main condenser available. The change in risk with respect to core damage and large early release frequency due to the inadvertent CRID inverter automatic transfer, together with the associated inadvertent closure of the Feedwater Isolation Valves and subsequent plant trip, have been qualitatively assessed and judged no different than any other unplanned reactor trips with the main condenser available. This assessment is based on the following considerations:

  • The automatic plant trip, due to low main feedwater flow, functioned properly. The automatic trip features also functioned dependably, with the exception of a failed Main Turbine Stop Valve limit switch, which resulted in failure of the Unit Output Breaker to automatically open. However, the operators responded in an appropriate and timely manner, resulting in a safe and stable plant configuration.
  • The inadvertent CRID inverter automatic transfer did not contribute to the increased likelihood of any initiators, other than transients that result in or from a reactor trip.
  • Neither the CRID inverter automatic transfer nor the associated inadvertent closure of the Feedwater Isolation Valves degraded any system used to prevent core damage, assure containment integrity, or maintain defense- in-depth and safety margins.

Accordingly, l&M concludes that there was no impact on the health and safety of the public as a result of this event.

Corrective Actions

Plant Equipment:

  • Verification of proper operation of the CRID.
  • Replacement of Main Turbine Stop Valve position indicator and verification of its proper operation.

Immediate Actions:

  • An event specific causal evaluation was performed.
  • A human performance root cause was performed for this human error event as well as other recent similar human performance events within the Maintenance Department.
  • As a result of the unacceptable human performance trend associated with maintenance work activities, a Stop Work Order was issued effective immediately to the Maintenance Department for all maintenance activities.

This Stop Work Order is documented in Condition Report 04009044. The Stop Work Order will be rescinded when permanent preventive actions have been put into place to address barrier failures that occurred leading up to this event. The approval of the Plant Manager and the Site Vice President or Chief Nuclear Officer is required for rescinding this Stop Work Order.

  • Enhanced standards were established for disconnecting and connecting leads.

1. FACIUTY NAME 2. DOCKET NUMBER 6. LER NUMBER 3. PAGE 2003 _ 005 _ 00 17. TEXT (If more space Is required, use additional copies of NRC Form (366A) Corrective Action to Prevent Recurrence:

  • Incorporation of the enhanced standards for disconnecting and connecting leads into Procedure 12-IHP-5021-IMP-001, "Lead Lifting/Landing And Electrical Jumper/Fuse Installation And Removal.

(Reference Corrective Action Item 3 of CR 03365009)

  • Incorporation of the enhanced standards for disconnecting and connecting leads into Procedure PMP-2291-PLN-001, "Work Control Activity Planning Process." (Reference Corrective Action Item 4 of CR 03365009)

Previous Similar Events

None. A review of the LERs issued by I&M from 1998 to present, for both units, identified no similar occurrences (i.e., reactor trips due to maintenance personnel errors).