At 0002 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> on April 26, 2005, the Donald C. Cook Nuclear Plant Unit 1 reactor automatically tripped while at 8% reactor power. Preparations were being made to synchronize the main generator with the offsite electrical power grid. The post-trip investigation determined that the trip was caused by an intermediate range high flux reactor trip signal. The intermediate range high flux reactor trip occurred below the reactor protection system actuation normally set at 22% reactor power. This reactor trip has a one-of-two channel trip logic. The trip is interlocked to be active below 10% reactor power. It was determined the cause was a spurious lowering of the trip setpoint due to age-related degradation of the level adjust potentiometer in the circuitry of 1-NRI-35, Nuclear Instrumentation Channel 1 Intermediate Range Neutron Flux Detector. The affected bistable and relay driver assembly, 1-NRI-35-NC35F, for the intermediate range channel 1-NRI-35, was replaced. Additionally, preventive maintenance tasks for periodic replacement of nuclear instrument bistable relay drivers will be developed.
All plant systems functioned normally following the reactor trip. The auxiliary feedwater system actuated and performed as expected during this event. This event was reported under event notification system number 41639 per 10 CFR 50.72(bX2)(iv)(B) and 10 CFR 50.72(b)(3XivXA), as a valid reactor trip and actuation of the auxiliary feedwater system, respectively.
This LER is being reported per requirements of 10 CFR 50.73(a)(2Xiv)(A). |
LER-2005-001, Reactor Trip Following Intermediate Range High Flux SignalDocket Number |
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3152005001R00 - NRC Website |
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Conditions Prior to Event Donald C. Cook Nuclear Plant (CNP) Unit 1 was at 8% reactor power and stable.
Description of Event
At 0002 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> on April 26, 2005, CNP Unit 1 reactor automatically tripped while at 8% reactor power.
Preparations were being made to synchronize the main generator with the offsite electrical power grid. The post-trip investigation determined that the trip was caused by an intermediate range high flux reactor trip signal. The intermediate range high flux reactor trip occurred below the reactor protection system actuation normally set at 22% reactor power. This reactor trip has a one-of-two channel trip logic. The trip is interlocked to be active below 10% reactor power. It was determined the cause was a spurious lowering of the trip setpoint due to age related degradation of the level adjust potentiometer in the circuitry of 1-NRI-35- DWR, Nuclear Instrumentation Channel 1 Intermediate Range Neutron Flux Detector Drawer [JD].
The automatic plant trip at low power functioned as expected. The auxiliary feedwater [BA] system actuated and operated as expected. Operators took procedurally directed actions and responded to the transient in an appropriate and timely manner, resulting in a safe and stable plant configuration. Automatic post-trip features functioned dependably with the exception of 1-FMO-242, West Motor Operated Auxiliary Feedwater Pump Supply to Steam Generator OME4-4 Control Valve, not throttling closed following the trip. An engineering evaluation concluded this was an expected response under the circumstance, and no equipment failure was indicated.
This event was reported under event notification system number 41639 per 10 CFR 50.72(b)(2Xiv)(B) and 10 CFR 50.72(b)(3Xiv)(A), as a valid reactor trip and actuation of the auxiliary feedwater system, respectively.
This LER is being reported per requirements of 10 CFR 50.73(aX2)(ivXA).
Cause of Event
The cause of the spurious reactor trip signal was determined to be drying out of the lubricant internal to the level adjust potentiometer (R4E) associated with 1-NRI-35-NC35F, Nuclear Instrumentation Intermediate Range Channel 1 High Neutron Flux Bistable, due to the age of the component and environmental conditions.
A recently completed single point vulnerability (SPV) study was not chartered to include conditions at less than 100% power operation. This was considered to be a contributing cause to this event.
The level adjust potentiometers, at the root of this event, are not a critical component above 10% power. The coincidence logic of the source and intermediate range instrumentation is a one-out-of-two trip logic, vice a two-out-of-four trip logic with the power range instrumentation. CNP will evaluate the need to expand the SPV study to operations less than 100% power.
Analysis of Event
An assessment of this event was performed and it was determined that this event was bounded by the existing accident analysis associated with unplanned reactor trips with the main condenser available. This assessment is based on the following considerations:
1. The automatic plant trip at low power, caused by Intermediate Range nuclear instrument 1-NRI-35, functioned as expected.
2. The reactor trip was inadvertent. The intermediate range nuclear instrument, 1-NRI-35, normally has a trip setpoint of 22%. In this event, a reactor trip was initiated at 7-8% power. This does not contribute to the increased likelihood of any initiators, other than transients that result in or from a reactor trip.
3. Neither the failure of the intermediate range nuclear instrument, nor the subsequent unit trip, degraded any system used to mitigate core damage, assure containment integrity, or maintain defense-in-depth and safety margins.
4. The low initial power level removes any risk contribution due to Anticipated Transient Without Scram (ATWS) initiators at 40% power or above. This initiator contributes about 90% of the ATWS core damage contribution, and corresponds to about 1% of the overall CDF.
Conclusion:
The significance associated with this event is non-risk significant. Additionally, there were no radiological or industrial safety risks created or affected by the event.
Corrective Actions
Immediate Corrective Actions:
Replaced the affected bistable and relay driver assembly, 1-NRI-35-NC35F, for the intermediate range channel 1-NRI-35 (JO 05116001, Activity 01).
High Level Trip bistables for the other Unit 1 nuclear instrumentation detector channels, 1-NRI-31, 1-NRI-32 and 1-NRI-36, were inspected. The potentiometers were manipulated to confirm they operated correctly (JO 05116001, Activity -02, -03, and -04).
Action to Address Extent of Condition:
CNP will evaluate expanding the single point vulnerability study to include operations less than 100% power.
(CR 05159006, duel/9/05).
Corrective Action to Prevent Recurrence:
Develop preventive maintenance tasks for periodic replacement of nuclear instrument bistable relay drivers (CRA 05116001-05, due 9/23/05).
Previous Similar Events
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Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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