05000315/FIN-2018002-05
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Finding | |
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Title | Minor Violation |
Description | While there did appear to be a reduction in operational errors being made in the field while manipulating equipment (such as during clearance activities and in performing certain evolutions) the inspectors noted a trend in configuration control issues. Most of these dealt with some kind of operation department interface or coordination with another department. In one case, valves associated with feedwater heater level control were left closed following a project to replace some of the heaters, which contributed to a manual reactor trip due to high moisture-separator drain tank level when starting the plant following the Unit 2 refueling outage. Other examples were Chemistry and Operations department coordination on an non-essential service water (NESW) valve alignment which led to NESW being isolated to generator seal oil cooling during plant startup, poor coordination between Maintenance and Operations which resulted in a containment penetration being left open, a pressure gauge remaining isolated after the Projects department completed the heater drain pump replacements, and the failure to ensure that valve-closure tests were done following the feedwater heater replacements. Another identified trend was in the area of post-maintenance testing (PMT). During the refueling outage on Unit 2, both the NRC and the licensee identified instances of improper PMTs being scheduled for safety-related equipment. Inspectors identified work on an EDG fuel oil transfer pump that did not have an in-service test (IST) scheduled. The licensee identified the lack of a time response test following a motor-driven AFW pump motor replacement, was a repeat issue from the previous outage. The licensee also identified the lack of an IST following a seal replacement on a CCW pump. In each case, the issues were discovered and corrected before equipment was restored to fully operable status. In response to the trend, the licensee reviewed other work on safety-related equipment for the outage to confirm the proper PMTs would be done. No other issues were identified. Finally, early in the observation period, the inspectors noted a trend in procedure quality for maintenance activities on safety-related equipment. There were instances regarding Turbine-Driven Auxiliary Feedwater (TDAFW) pump linkages where better procedure direction could have precluded binding and governor-valve travel issues. Additionally, while replacing a TDAFW governor, a snap ring was inadvertently left out of a coupling due to insufficient procedure detail. Regarding the EDGs, the licensee discovered instructions for assembly of air start check valves did not contain the torque guidance that the vendor drawings stipulated. In response to this trend, the licensee started to perform deliberate reviews of OE before maintenance on some safety-related equipment, to verify maintenance instructions had up-to-date guidance before starting work. No violations or findings were identified by the inspectors. 12 Licensee management acknowledged the issues discussed by the inspectors. |
Site: | Cook |
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Report | IR 05000315/2018002 Section 4OA2 |
Date counted | Jun 30, 2018 (2018Q2) |
Type: | Violation: Severity level Minor |
cornerstone | No Cornerstone |
Identified by: | NRC identified |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | J Ellegood T Taylor S Bell J Bozga J Cassidy T Go M Holmberg L Smith K Riemer |
INPO aspect | |
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Finding - Cook - IR 05000315/2018002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Cook) @ 2018Q2
Self-Identified List (Cook)
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