05000313/FIN-2016004-02
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Finding | |
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Title | Failure to Design Pipe Support for Vibration |
Description | Green. The inspectors documented a self-revealed finding and associated non-cited violation of 10 CFR 50 Appendix B Criterion III for the licensees failure to verify that the decay heat removal (DHR) system drain piping configuration and supports could withstand vibrations created during low pressure and high flow conditions. As a result, a cracked weld and unisolable leak in the DHR system occurred due to high cycle fatigue caused by those conditions. To correct this issue, the licensee repaired the leaking weld and designed and installed a new piping support and piping configuration to reduce vibrations during the expected operating conditions. The licensee entered this issue into the corrective action program as Condition Report CR-ANO-1-2016-03225. The failure to design the decay heat removal system piping to withstand expected vibrations from the systems cavitating venturis is a performance deficiency. The performance deficiency is more than minor because it was associated with the design control attribute of the initiating events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, inadequate design of the DHR system piping support resulted in a leak that could have challenged the capability of both trains of the DHR system during shutdown on September 29, 2016. The inspectors performed an initial screening of the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," issued October 7, 2016, and were directed to IMC 0609, Appendix G, Attachment 1, "Shutdown Operations Significance Determination Process Phase 1 Screening and Characterization of Findings, since the finding pertained to a degraded condition while the plant was shutdown. Using IMC 0609, Appendix G, Attachment 1, dated May 9, 2014, the inspectors determined that the finding required a Phase 2 evaluation. A senior reactor analyst performed a Phase 2 evaluation in accordance with IMC 0609, Appendix G, Attachment 2, Phase 2 Significance Determination Process Template for PWR during Shutdown, dated February 28, 2005. The senior reactor analyst performed a Phase 2 evaluation which used realistic break characteristics and plant configuration changes to determine the significance to be of very low safety significance (Green). The inspectors determined this finding did not have a cross-cutting aspect because the most significant contributor did not reflect current licensee performance. Specifically, the licensee last reviewed and modified the pipe support configuration in 1996 |
Site: | Arkansas Nuclear |
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Report | IR 05000313/2016004 Section 1R02 |
Date counted | Dec 31, 2016 (2016Q4) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.02 |
Inspectors (proximate) | B Correll B Tindell G Pick J Choate J Dixon J Mateychick M Phalen M Tobin N Greene N O'Keefe P Jayroe R Deese S Money M Kirk |
Violation of: | 10 CFR 50 Appendix B 10 CFR 50 Appendix B Criterion III, Design Control |
INPO aspect | |
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Finding - Arkansas Nuclear - IR 05000313/2016004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Arkansas Nuclear) @ 2016Q4
Self-Identified List (Arkansas Nuclear)
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