6-22-2016 | On April 3, 2015, Prairie Island Nuclear Generating Plant ( PINGP) Unit 2 was operating at 100 percent power, when at 0652 CDT, an unexpected annunciator, 47510-0104 21 FEEDWATER PUMP LOCKED OUT was received. The reactor was manually tripped as required by the annunciator response procedure. This also resulted in a turbine trip as designed. The Operations crew entered the reactor trip emergency operating procedures and stabilized the unit in Mode 3, at normal operating pressure and temperature. All control rods fully inserted into the core following the trip. The Auxiliary Feedwater Pumps actuated as designed on low narrow range steam generator level. Steam Generator levels were returned to normal.
This event is reportable under 10 CFR 50.72(b)(2)(iv)(B), any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation, and 10 CFR 50.72(b)(3)(iv)(A), any event or condition that results in valid actuation of any of the systems listed in paragraph 10 CFR 50.72(b)(3)(iv)(B)(6), PWR auxiliary or emergency Feedwater system.
The cause evaluation determined that the event was caused by pressure fluctuation within the system which resulted in the bourdon tube movement at a high frequency causing wear of the internal components of the pressure switch.
Corrective actions: Pressure Switch (PS-16012) was replaced immediately on April 3, 2015, and to install snubbers to reduce process flow fluctuations experienced by Feedwater Pump pressure switches. |
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Category:Letter
MONTHYEARIR 05000282/20230042024-02-0101 February 2024 Integrated Inspection Report 05000282/2023004 and 05000306/2023004 ML23356A1232024-01-29029 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) ML24024A0722024-01-24024 January 2024 Independent Spent Fuel Storage Installation, Onticello, Supplement to Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML24017A0182024-01-19019 January 2024 Confirmation of Initial License Examination ML23356A0032024-01-17017 January 2024 Issuance of Amendments Revise Technical Specification 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR) L-PI-23-034, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.7.8, Cooling Water (Cl) System,2024-01-0202 January 2024 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.7.8, Cooling Water (Cl) System, L-PI-23-035, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specifications Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report2023-12-20020 December 2023 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specifications Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report IR 07200010/20234012023-12-20020 December 2023 Independent Spent Fuel Storage Installation Security Inspection Report 07200010/2023401 ML23349A0572023-12-15015 December 2023 and Independent Spent Fuel Storage Installation, Revision to Correspondence Service List for Northern States Power - Minnesota ML23215A1672023-12-15015 December 2023 Acceptance of Requested Licensing Action Amendment Request to Revise Surveillance Requirement 3.8.1.2 Note 3 IR 05000282/20234012023-12-13013 December 2023 Security Baseline Inspection Report 05000282/2023401 and 05000306/2023401 L-PI-23-033, Supplement to License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 32023-12-0505 December 2023 Supplement to License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 3 ML23304A1632023-11-15015 November 2023 Supplemental Information Needed for Acceptance of Requested Licensing Action Amendment Request to Revise SR 3.8.1.2 Note 3 ML23319A3182023-11-15015 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation IR 05000282/20230032023-11-0808 November 2023 Integrated Inspection Report 05000282/2023003 and 05000306/2023003 ML23311A3572023-11-0707 November 2023 Core Operating Limits Report (COLR) for Prairie Island Nuclear Generating Plant (PINGP) Unit 2. Cycle 33. Revision 0 ML23285A3062023-10-12012 October 2023 Implementation of the Fleet Standard Emergency Plan for the Monticello Nuclear Generating Plant and the Prairie Island Nuclear Generating Plant ML23270B9022023-09-29029 September 2023 Review of Reactor Vessel Material Surveillance Program Capsule N Technical Report L-PI-23-025, License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 32023-09-28028 September 2023 License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 3 ML23265A2532023-09-26026 September 2023 Review of Reactor Vessel Material Surveillance Program Capsule N Technical Report ML23262B0372023-09-19019 September 2023 Response to NRC Request for Additional Information Regarding the 2023 Monticello and Prairie Island Plant Decommissioning Funding Status Reports ML23256A1682023-09-13013 September 2023 Independent Spent Fuel Storage Installation and Monticello Nuclear Generating Plant - Voluntary Security Clearance Program 2023 Insider Threat Program Self-Inspection L-PI-23-023, Baffle Former Bolts Alternate Aging Management Strategy2023-09-11011 September 2023 Baffle Former Bolts Alternate Aging Management Strategy IR 05000282/20230052023-08-30030 August 2023 Updated Inspected Plan for Prairie Island Nuclear Generating Plant Report 05000282/2023005 and 05000306/2023005 IR 05000282/20230102023-08-17017 August 2023 NRC Inspection Report 05000282/2023010 and 05000306/2023010 ML23222A0122023-08-10010 August 2023 Independent Spent Fuel Storage Installation and Monticello Nuclear Generating Plant - Changes in Foreign Ownership, Control or Influence IR 05000282/20230022023-08-0303 August 2023 Integrated Inspection Report 05000282/2023002 and 05000306/2023002 ML23214A2032023-08-0202 August 2023 Request for Information for an NRC Quadrennial Comprehensive Engineering Team Inspection: Inspection Report 05000282/2024010; 05000306/2024010 ML23206A2342023-07-25025 July 2023 Independent Spent Fuel Storage Installation, and Monticello Nuclear Generating Plant, Changes in Foreign Ownership, Control or Influence ML23202A0032023-07-21021 July 2023 Independent Spent Fuel and Independent Spent Fuel Storage Installation, Monticello Nuclear Generating Plant, Submittal of Quality Assurance Topical Report (NSPM-1) ML23199A0922023-07-18018 July 2023 Notification of NRC Baseline Inspection and Request for Information; Inspection Report 05000306/2023004 ML23195A1732023-07-14014 July 2023 Revision of Standard Practice Procedures Plan L-PI-23-018, License Amendment Request to Revise ISFSI Technical Specification 4.4 to Allow Use of a Code Alternative to ASME Code, NB-5130, Examination of Weld Edge Preparation Surfaces, for the TN-40HT2023-07-14014 July 2023 License Amendment Request to Revise ISFSI Technical Specification 4.4 to Allow Use of a Code Alternative to ASME Code, NB-5130, Examination of Weld Edge Preparation Surfaces, for the TN-40HT ML23181A0192023-06-30030 June 2023 Independent Spent Fuel Storage Installation, Revision to Correspondence Service List for Northern States Power - Minnesota ML23178A2422023-06-28028 June 2023 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch III L-PI-23-006, License Amendment Request to Revise Technical Specification 3.7.8 Required Actions2023-06-22022 June 2023 License Amendment Request to Revise Technical Specification 3.7.8 Required Actions L-PI-23-016, 2022 10 CFR 50.46 LOCA Annual Report2023-06-14014 June 2023 2022 10 CFR 50.46 LOCA Annual Report IR 05000282/20234202023-06-0101 June 2023 Security Baseline Inspection Report 05000282/2023420 and 05000306/2023420 ML23150A1722023-05-30030 May 2023 Preparation and Scheduling of Operator Licensing Examinations 2024-02-01
[Table view] Category:Licensee Event Report (LER)
MONTHYEARML19353A4092019-12-19019 December 2019 Technical Specification 5.6.8 Special Report: Inoperable Containment Isolation Valve Indication Supplemental Report 05000306/LER-2017-0032018-01-11011 January 2018 Both Containment SEa) Pump Control Switches in Pull-out in Mode 4, LER 17-003-00 for Prairie Island Nuclear Generating Plant, Unit 2 Regarding Both Containment Spray Pump Control Switches in Pull-Out in Mode 4 05000306/LER-2017-0022017-12-11011 December 2017 Reactor Coolant System Shutdown Communication Live Vent Through Wall Defect, LER 17-002-00 for Prairie Island, Unit 2, Regarding Reactor Coolant System Shutdown Communication Live Vent Through Wall Defect 05000306/LER-2017-0012017-11-29029 November 2017 23 Containment Fan Coil Unit Operability, LER 17-001-00 for Prairie Island, Unit 2, Regarding 23 Containment Fan Coil Unit Operability 05000282/LER-2016-0062017-02-15015 February 2017 121 Motor Driven Cooling Water Pump Auto Start, LER 16-006-00 for Prairie Island Nuclear Generating Plant, Units 1 and 2 Regarding 121 Motor Driven Cooling Water Pump Auto Start 05000306/LER-2015-0022016-06-22022 June 2016 21 Feedwater Pump Lockout, Unit 2 Reactor Trip Due to Pressure Switch Failure, LER 15-002-01 for Prairie Island, Unit, Regarding 21 Feedwater Pump Lockout, Reactor Trip Due to Pressure Switch Failure 05000282/LER-2016-0042016-06-21021 June 2016 1 OF 4, LER 16-004-00 for Prairie Island, Unit 1, Regarding Missing Fire Barrier Between Fire Area (FA) 59 and 85 / Fire Hazard Analysis Drawings Do Not Match Boundary Description 05000282/LER-2016-0022016-03-25025 March 2016 Listed System Actuation - Motor-Driven Cooling Water Pump Auto-Start, LER 16-002-00 for Prairie Island, Unit 1, Regarding Listed System Actuation - Motor-Driven Cooling Water Pump Auto-Start 05000306/LER-2016-0012016-02-12012 February 2016 Unit 2 Reactor Trip due to a Ground Fault resulting in a Generator Trip, LER 16-001-00 for Prairie Island, Unit 2, Regarding Reactor Trip Due to a Ground Fault Resulting in a Generator Trip L-PI-15-071, Cancellation of License Event Report (LER)50-282/2015-001-00, 14 Fan Coil Unit Leak2015-09-0303 September 2015 Cancellation of License Event Report (LER)50-282/2015-001-00, 14 Fan Coil Unit Leak L-PI-11-023, Reinstatement of Licensee Event Reports Associated with Flooding Scenarios2011-03-31031 March 2011 Reinstatement of Licensee Event Reports Associated with Flooding Scenarios L-PI-07-101, LER 07-03-001 for Prairie Island, Unit 1 Regarding Unanalyzed Condition Due to Breached Fire Barrier2008-01-25025 January 2008 LER 07-03-001 for Prairie Island, Unit 1 Regarding Unanalyzed Condition Due to Breached Fire Barrier L-PI-06-046, Cancellation of Licensee Event Report (LER) 1-05-01, Discovery of Single Failure Vulnerability of Unit 1 Safeguards Buses2006-06-0909 June 2006 Cancellation of Licensee Event Report (LER) 1-05-01, Discovery of Single Failure Vulnerability of Unit 1 Safeguards Buses 2019-12-19
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by interne( e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
CONTINUATION SHEET
05000- 2 306 2015 002 01 On April 3, 2015, at 0652 CDT, the Unit 2 reactor was manually tripped while operating at 100 percent power, due to a lockout trip of 21 Main Feedwater Pump (245-261) as required by the Annunciator Response Procedure (ARP 47510-01 04) for the lockout alarm. This also resulted in a turbine trip as designed. The Operations crew entered the reactor trip emergency operating procedures and stabilized the unit in Mode 3 at normal operating pressure and temperature. All control rods fully inserted into the core following the trip. The Auxiliary Feedwater System (EIIS System Code - BA) actuated to start the Auxiliary Feedwater Pumps as designed on low narrow range Steam Generator level and provided makeup flow to the Steam Generator.
Steam Generator levels were returned to normal. The Auxiliary Feedwater Pumps were subsequently secured and returned to automatic. Steam Generators were being supplied by 22 Main Feedwater Pump and decay heat was removed by the condenser steam dump system. This event was entered into the Corrective Action Program (AR 01472846).
This event is reportable under 10 CFR 50.72(b)(2)(iv)(B), any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation, and 10 CFR 50.72(b)(3)(iv)(A), any event or condition that results in valid actuation of any of the systems listed in paragraph 10 CFR 50.72(b)(3)(iv)(B)(6), PWR auxiliary or emergency Feedwater system.
EVENT ANALYSIS
The PS-16012 was identified as a Mercoid, Model DSW-7223-153S1-10S pressure switch. A failure analysis was performed of the failed switch. The switch was disassembled and observations were made of the internal components. The results of this evaluation concluded that a C-clip that secures the linkage connecting the bourdon tube to the switch mechanism had fallen off the pin allowing the linkage to become disconnected from the switch mechanism. Wear was observed on the pin at the interface of the C-clip to the pin. The wear on the pin connected to the intermediate linkage was the cause for the switch failure.
There were no complications during the shutdown as all control rods fully inserted and Reactor Pressure Vessel pressure was maintained by normal means. All systems actuated as required. The Auxiliary Feedwater Pumps actuated as designed on low Steam Generator level. This is reportable under 10 CFR 50.73(a)(2)(iv) (A), any event or condition that results in manual or automatic actuation of any of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B)(1), RPS including: reactor scram or reactor trip, and in paragraph 10 CFR 50.73(a)(2)(iv)(B)(6), PWR auxiliary or emergency Feedwater system.
SAFETY SIGNIFICANCE
This event did not challenge nuclear safety as all plant systems responded as designed. The reactor was manually tripped in accordance with the annunciator response procedure. There were no radiological, environmental, or industrial impacts associated with this event and PINGP did not affect the health and safety of the public.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
05000- 2 306 2015 002 01
CAUSE
The causal evaluation determined that pressure fluctuation within the system is resulting in the bourdon tube movement at a high frequency causing wear of the internal components of the pressure switch.
CORRECTIVE ACTION
- Immediate action to replace Pressure Switch PS-16012 per Work Order (WO) 00519920-01. Complete.
- Implement interim action monitoring plan for all Feedwater Pump suction pressure switches. Complete.
- Install pressure snubbers on the four Feedwater Pump suction pressure switches. Complete.
PREVIOUS SIMILAR EVENTS
A LER historical search was conducted and no similar LER events at PINGP with the same apparent cause were identified in the last three years.