12-08-2016 | On October 9, 2016 at 0254 hours0.00294 days <br />0.0706 hours <br />4.199735e-4 weeks <br />9.6647e-5 months <br />, with Unit 1 and Unit 2 at 100 percent power, Unit 2 experienced an automatic reactor trip initiated by a turbine trip due to generator differential lockout relay actuation. At the time of the trip, high wind and heavy rain conditions existed due to the effects of Hurricane Matthew. All three auxiliary feedwater pumps automatically started on low-low steam generator water level as expected. All plant systems functioned as required, and Unit 2 was stabilized at hot shutdown. The trip response was not affected by any previously inoperable systems, structures, or components.
The direct cause of the generator differential lockout was an electrical ground overcurrent initiated by water accumulation in the "A" phase of the "A" station service transformer leads termination enclosure. Affected electrical enclosures were drained, the system was tested, and modifications to the enclosures to prevent recurrence of water intrusion were completed prior to returning Unit 2 to power operation on October 13, 2016.
This report is being submitted pursuant to 10CFR50.73(a)(2)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System' and the Auxiliary Feedwater System. |
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Category:Letter
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[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000281/LER-2020-001, Cancellation of LER 2020-001-00 for Surry Power Station Unit 2 Re Loss of Containment Cooling Affecting Containment Partial Pressure Indication2020-11-0606 November 2020 Cancellation of LER 2020-001-00 for Surry Power Station Unit 2 Re Loss of Containment Cooling Affecting Containment Partial Pressure Indication 05000280/LER-2019-0022020-02-0404 February 2020 LER 2019-002-00 for Surry Power Station Unit 1, Items Non-Conforming to Design for Tornado Missile Protection 05000280/LER-2017-0012017-10-0606 October 2017 1 OF 3, LER 17-001-00 for Surry, Unit 1, Regarding Shutdown due to an Unisolable Leak in Reactor Coolant Pressure Boundary 05000281/LER-2016-0012016-12-0202 December 2016 Unit 2 Reactor Trip due to Generator Differential Lockout, LER 16-001-00 for Surry Power Station, Unit 2, Regarding Reactor Trip Due to Generator Differential Lockout 05000280/LER-2016-0012016-07-11011 July 2016 1 OF 4, LER 16-001-00 for Surry Power Station, Unit 1 and 2, Regarding Emergency Service Water Pump Inoperable Due to Corrosion of Valve Support ML1015505662009-03-0404 March 2009 Event Notification for Surry on Relief Valve Failure Results in Tritium and Cesium Spill ML0702501902007-01-17017 January 2007 Special Report on Qpt Not Less than Two Percent for Twenty Four Hours ML19105B1281979-08-21021 August 1979 LER 1979-011-03X for Surry Units 1 & 2 Loss of Power with Both Units at Cold Shutdown, Observed Radiation Monitors Without Power ML19093B4141978-09-26026 September 1978 Reporting Condenser Cooling Water Outlet Temperature to James River Decreased by 3.5oF as Measured at Station Discharge Structure ML19105A3001978-09-0808 September 1978 LER 78-013-03X-1, LER 78-029-03L-0, & LER 78-031-03L-0 for Surry 2 Re Critical Below Minimum Insertion Limit on D Control Bank ML19105A3011978-09-0101 September 1978 LER 1978-028-03L-0 for Surry 2 Re Containment Pressure Exceeded Allowable Limit ML19095A4971978-08-25025 August 1978 Submit Licensee Event Report No. LER 78-024/03L-0 Re No Alarm During a Planned Release of Liquid Radioactive Waste ML19095A4981978-08-22022 August 1978 Submit Licensee Event Report Nos. LER 1978-019/03L-0, LER 1978-021/03L-0, LER 1978-022/03L-0, LER 1978-023/03L-0, LER 1978-025/03L-0, LER 1978-026/03L-0 for Surry Unit No. 1 ML19105A0771978-08-16016 August 1978 Submit LER 78-027/03L-0 Re Seven Snubbers Not Meeting Inspection Criteria ML19105A0781978-08-16016 August 1978 Submit LER 78-027/03L-0 Re Seven Snubbers Not Meeting Inspection Criteria ML19105A0791978-08-11011 August 1978 LER 78-026/03L-0. Follow-up Inspection for Valve Cleanliness, Discovered That Containment Spray Isolation Valves (MOV-CS-201C and D) Contained No More That Five Milliliters. Technical Specification TS 6.6.2.b.(3) ML19095A4991978-08-0404 August 1978 Sutmit Licensee Event Report No. LER 78-018/03L-0 Re Two Main Steam Safety Valves Were Not within Plus or Minus 3% of Setpoint as Required ML19105A0801978-07-28028 July 1978 LER 1978-022-03L-0 Re Axial Power Distribution Monitoring Was Exceeded,& Three LERs 1978-021-03L-0, LER 1978-023-03L-0, & LER 1978-024-03L-0 Re Inlet Circulating Water Temperature Exceeded ML19095A5001978-07-28028 July 1978 Submit Licensee Event Report Nos. LER 78-017/03L-0 Re Not Documenting Four Electric Maintenance Procedures & Two Periodic Tests, & 78-020/03L-0 Re Suspended Air Bubbles in Reservoir Fluid ML19095A2281978-07-27027 July 1978 Reporting & Providing Additional Information on Incidence of Missing Two Steam Generator Tube Plugs Found During Inspection ML19095A2291978-07-26026 July 1978 Reporting of Cooling Water Discharge Temperature Change Rate on 7/9/1978 & Found No Evidence of Any Detrimental Effects in River or Its Inhabitants ML19095A5011978-07-21021 July 1978 Submit Licensee Event Report No. LER 78-016/03L-0 Re Valve MOV-RH-100 Was Not Opening ML19105A0821978-07-17017 July 1978 LER 1978-025-03L for Surry Unit 2 Excessive Gap Around Battery Room Ventilation Duct ML19105A0811978-07-17017 July 1978 LER 1978-025-03L for Surry Unit 2 Excessive Gap Around Battery Room Ventilation Duct ML19095A5021978-07-0707 July 1978 Submit Licensee Event Report Nos. LER 78-013/03L-0 Re Six Snubbers Not Meeting Test Criteria, & 78-014/03L-0 Re Mount Plate Was Warped, & 3 of 8 Bolts Were Insufficiently Embedded ML19095A5031978-06-27027 June 1978 Submit Licensee Event Report No. LER-78-015/03L-0 Re Valve Cleanliness Inspection Found Foreign Material on Valve Seating Surfaces ML19095A5041978-06-27027 June 1978 Submit Licensee Event Report No. LER-78-015/03L-0 Re Valve Cleanliness Inspection Found Foreign Material on Valve Seating Surfaces ML19105A0831978-06-23023 June 1978 LER 1978-017-03L, LER 1978-018-03L, LER 1978-019-03L, & LER 1978-020-03L for Surry Unit 2 Related to Snubbers ML19095A2481978-06-19019 June 1978 06/19/1978 Letter Reporting Increase of Condenser Cooling Water Discharge ML19095A5051978-06-0707 June 1978 Submit Licensee Event Report No. LER-78-012/03L-0 Re Inside Recirculation Spray Pump 1-RS-P-1A, Failure to Rotate by Hand ML19105A0851978-05-23023 May 1978 LER 1978-015-03L for Surry Unit 2 Finding of Air Leak on Header of Control Room Emergency Air Supply Bank ML19095A5061978-05-23023 May 1978 Submit Licensee Event Report Nos. LER-78-008/03L-0, LER-78-009/03L-0, LER-78-010/03L-0, LER-78-011/03L-0 for Surry Unit No. 1 ML19105A0861978-05-12012 May 1978 LER 1978-013-03L for Surry Unit 2 Reactor Brought Critical Below Minimum Insertion Limit on D Control Bank ML19105A0871978-05-0505 May 1978 LER 1978-014-03L for Surry Unit 2 Charging Pump Service Water Pump a Tripped on High Current ML19095A5071978-05-0505 May 1978 Submit Licensee Event Report No. LER-78-007/03L-0 Re Leak on Body to Bonnet Joint Diaphragm Valve 1-CH-98 ML19105A0881978-04-19019 April 1978 LER 1978-006-01T for Surry Unit 2 Review of Fire Protection Yard Piping Revealed That Two Pipe Extensions May Not Have Been Seismically Qualified ML19095A5081978-04-19019 April 1978 Submit Licensee Event Report No. LER-78-006/01T-0 Re Seismically Disqualified Two Pipe Extensions on Fire Protection Yard Piping ML19095A5091978-04-0707 April 1978 Forwarding Licensee Event Report No. LER-78-005/01T-0 Re Westinghouse'S Error in LOCA-ECCS Evaluation Model, Which Will Result in Higher Calculated Peak Clad Temperature ML19105A0901978-04-0606 April 1978 LER 1978-012-01T for Surry Unit 2 Failure to Meet Containment Integrity ML19105A0921978-04-0404 April 1978 LER 1978-011-03L for Surry Unit 1 Loss of Service Water Flow Through Charging Pump Intermediate Seal Cooler ML19095A5101978-04-0404 April 1978 Submit Licensee Event Report No. LER-78-004/03L-0 Re Loss of Service Water Flow Through Charging Pump Intermediate Seal Cooler ML19105A0931978-03-30030 March 1978 LER 1978-008-03L Re Snubber Body in Contact with Structure; LER 1978-009-03L Re Trip of Boric Acid Transfer Pump; & LER 1978-010-03L Re Failure of Pressurizer Channel ML19095A5111978-03-28028 March 1978 Submit Licensee Event Report No. LER-78-003/03L-0 Re Failed Heat Tracing, Panel 8 Circuit 24 ML19095A5121978-03-21021 March 1978 Submit Licensee Event Report No. LER-78-002/01T-0 Re Additional Radial Peaking Factor Surveillance ML19105A0941978-02-27027 February 1978 LER 1978-006-03L Re Failure of Sola Transformer, & LER 1978-007-03L Re Trip of Boric Acid Transfer Pump on Thermal Overload ML19095A5131978-02-24024 February 1978 Submit Licensee Event Report No. LER-78-001/03L-0 Re Hydraulic Shock Suppressor Found Inverted with Empty Reservoir ML19105A0951978-02-16016 February 1978 LER 1978-003-03L Re Erroneous Readings of Loop a Hot Leg Temperature Protection Channel; LER 1978-004-03L Re Unqualified Welding of Two Diaphragm Welds on Heat Exchanger; & LER 1978-005-03L Re Low Current Condition from Heat Tracing ML19105A0971978-02-0202 February 1978 LER 1978-001-03L for Surry Unit 2 Inoperability of Condenser Circulating Water Outlet Valve ML19095A5141978-01-0909 January 1978 Submit Licensee Event Report Nos. LER-77-021/03L-0 & LER-77-022/03L-0 ML19105A0991978-01-0909 January 1978 LER 1977-021-03L Re Routine Sampling of Bast a Revealed Tank Was at Concentration of 11.5%, & LER 1977-022-03L Re Failure of Comparator to Trip During Routine Test of a Steam Generator Level Protection Channel II 2020-02-04
[Table view] |
Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc,gov, and to the Desk Officer, Office of Information and Regulatory Affairs, used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
1.0 DESCRIPTION OF THE EVENT On October 9, 2016 at 0254 hours0.00294 days <br />0.0706 hours <br />4.199735e-4 weeks <br />9.6647e-5 months <br />, with Unit 1 and Unit 2 at 100 percent power, Unit 2 experienced an automatic reactor trip initiated by a turbine trip due to generator differential lockout relay actuation. At the time of the trip, high wind and heavy rain conditions existed due to the effects of Hurricane Matthew. All three auxiliary feedwater (AFW) pumps [EIIS-BA-P] automatically started on low-low steam generator (SG) [EIIS-AB-SG] water level providing flow to the SGs as expected. Operation of the main steam power operated relief valves (PORVs) [EIIS-SB-RV] and the main steam dump valves [EIIS-SB-TCV], coincident with the initiation of AFW, resulted in the Unit 2 reactor coolant system (RCS) temporarily cooling to 542 degrees F. RCS temperature was restored to nominal average temperature of 547 degrees,,Fat 0320 hours0.0037 days <br />0.0889 hours <br />5.291005e-4 weeks <br />1.2176e-4 months <br />. Main feedwater flow was re-established to control SG level, and AFW was secured at 0336 hours0.00389 days <br />0.0933 hours <br />5.555556e-4 weeks <br />1.27848e-4 months <br />.
At 0609 hours0.00705 days <br />0.169 hours <br />0.00101 weeks <br />2.317245e-4 months <br />, a four-hour report to the NRC was made pursuant to 10CFR50.72(b)(2)(iv)(B) due to valid automatic actuation of Reactor Protection Systems and an eight-hour report was made pursuant to 10CFR50.72(b)(3)(iv)(A) due to automatic actuation of the AFW system.
2.0 SIGNIFICANT SAFETY CONSEQUENCES AND IMPLICATIONS This event resulted in no safety consequences or implications. There were no testing or surveillance procedures in progress when the reactor trip occurred. Appropriate operator actions were taken in accordance with station procedures, and the unit was brought to a stable condition. Station equipment relied upon to mitigate the event responded as designed. Normal offsite and emergency power supplies were available during the event. The health and safety of the public were not affected.
3.0 CAUSE The 22 KV electric output of the main generator is sent to the Main Transformers and the Station Service Transformers (SST) [EIIS-EA-XFMR] through the Isolated Phase Bus Duct (IPBD) [EIIS-EA-IPBU] System.
The current Unit 2 IPBD system and SST leads termination enclosures were installed by design changes in 2011 and 2015, respectively. As part of the October 2016 post-trip inspection, water was found in two leads termination enclosures and in some IPBD horizontal runs. Water appears to have entered the system during ongoing heavy rain and wind conditions through gaps at mechanical joints associated with the SST leads termination enclosure and the IPBD.
The direct cause of the reactor trip was a ground of the 'A' phase on the high side (22 KV) of the 'A' SST due to water accumulation in the 'A' SST leads box, resulting in the actuation of the generator differential lockout relay. Without a drain path, the water level in the enclosure increased up the insulator creating a path to ground.
The root cause for the water intrusion and the resulting trip was the lack of testing and inspection of mechanical joints to ensure a weather tight system was accomplished after modifications. The design change specifications included provisions to ensure weather tightness, including detailed instructions for testing of welds and an array of electrical tests. However, no guidance was provided for inspection or testing of mechanical connections for the bus duct insulator hardware and gaskets, or for the termination enclosures.
4.0 IMMEDIATE CORRECTIVE ACTIONS Following the reactor trip, control room operators acted promptly to stabilize the unit in a safe, hot shutdown condition in accordance with station procedures.
5.0 ADDITIONAL CORRECTIVE ACTIONS A root cause evaluation (RCE) team was assembled to determine the cause of this event and to recommend corrective actions. While Unit 2 was shut down, water was removed from the IPBD and leads termination enclosures, and breaches that allowed water intrusion were sealed. Additionally, the 'A' phase SST and IPBD systems were dried using forced dehumidified air. Weep holes were installed at low points in the SST leads termination enclosures and Generator Step-Up transformer (GSU) [El IS-EL-XFMR] leads termination enclosures to allow drainage of potential moisture intrusion. All three phases of the IPBD system were meggered to verify no further grounds existed.
6.0 ACTIONS TO PREVENT RECURRENCE Weep holes installed in the transformer termination enclosures as described in section 5.0 above will prevent the possibility of creating a ground path by water accumulation. Design change testing procedures will be revised to include more rigorous instructions for non-safety design changes and common tests for electrical enclosures. Engineering qualification requirements will be updated to ensureAhat engineers are trained on lessons learned from this event. Additionally, upcoming design changes associatedmith Reserve Station Service Transformers (RSST) [EIIS-EA-XFMR] will be reviewed and revised as neededAo capture lessons learned from this event.
7.0 SIMILAR EVENTS None 8.0 MANUFACTURER/MODEL NUMBER AZZ — Calvert Isolated Phase Bus / 7085 9.0 ADDITIONAL INFORMATION Unit 1 was at 100 percent power at the time of this event and was unaffected by the Unit 2 reactor trip. Unit 1 entered a refueling outage on October 23, 2016. The corresponding Unit 1 IPBD and SST leads termination enclosures were inspected for the accumulation of water. Water was identified on the low side (4 KV) of the 'B' SST leads termination enclosure on Unit 1. As in Unit 2, weep holes were installed on the Unit 1 SST and GSU, leads termination enclosures, and connections were inspected and sealed as necessary. Other transformer terminations (including those associated with emergency power supplies) are not enclosed by bus ducts, and therefore are not affected by this event.