05000277/LER-1982-008, Revised LER 82-008/01X-1:on 820328,auxiliary Boiler Operated on Diesel Fuel 2 Instead of Fuel Oil 6,decreasing Diesel Fuel Inventory Below Tech Spec Limit of 104,000 Gallons. Caused by Failure to Monitor Fuel Tank Inventory

From kanterella
Jump to navigation Jump to search
Revised LER 82-008/01X-1:on 820328,auxiliary Boiler Operated on Diesel Fuel 2 Instead of Fuel Oil 6,decreasing Diesel Fuel Inventory Below Tech Spec Limit of 104,000 Gallons. Caused by Failure to Monitor Fuel Tank Inventory
ML20054E091
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 04/15/1982
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20054E084 List:
References
LER-82-008-01X, LER-82-8-1X, NUDOCS 8204260122
Download: ML20054E091 (1)


LER-2082-008, Revised LER 82-008/01X-1:on 820328,auxiliary Boiler Operated on Diesel Fuel 2 Instead of Fuel Oil 6,decreasing Diesel Fuel Inventory Below Tech Spec Limit of 104,000 Gallons. Caused by Failure to Monitor Fuel Tank Inventory
Event date:
Report date:
2772082008R00 - NRC Website

text

,

. . - .. . ~ - . ~ .

.nCf onu ins ,

u.s not.u an neuo u.. u.. o.w....... .

' !!l Unit 2 ,

LICENSEE EVENT REPORT R; port N3. 82-08-01X-1 ROL SLOCC ' l l l l l IPLE ASE PRINT OR TYPE ALL REQUIRED INF OHMAltONI

'M l* P* l AuCe=== l P 151812 COOe i<

@is Ol0 l- 10oCEnn lo loouM.ER lo 1010 l ol 01@l n 2. 4loCE~n 1111ivPE Il ll@l, a o,l wl @

.ex t E 0 "E

s L e l 0 l 5 l0 l- l0 l2 l 7 l7 l@l 0 l 3 l 2 l 8 l 812 l@l OM la 11

$1 DOCKET NUMegn 80 e9 EVENT DAf g 74 1 ; I R 12_}6)

REPORT DATI "O EVENT DESCRIPTION AND PROSASLE CONSEQUENCES h

~ifil l Wi t h Un i t 2 in refuel mode and Unit 3 at full nownv nvnhinmc with nny i M l boilers resulted in operatine one boiler on #2 diesel fun 1 instead of # 63

<>loilfuel oil Diesel fuel tank inventory decreased helnw Toch enne limit nf _1 JO l s i 1104. 000 callons by approximatelv 3.000 callons. Fuel level was below I RITE l 11 im i t for maximum of 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Additinnni fuel wnc neniinhin in Unit i l y ldiesel fuct oil storace tank and 1R_000 en11ons of dinent funt were _]

I

['O TT'l l d e l i v e r e d within nine hours a f t er identificatinn nf nenhinm ao SYSTGM CAueE CAUSE COMP. VALVE COOE COOG SueCODE COMPONENT CODE SUSCODE SUSCODE E. '

i n i ElO

. io LM@n La_J@ Iz I z I zi z I zi z l@ L:_J@ LzJ is SEOUENTI AL is i.

OCCUR R E NCE CODE i.

REPORT TYPE 2o REVl510N NO LE R/liO EVENTVEAR REPORT NO.

O,aj,T; is 12 1 28 22 p- 10 101 al 24 26 Ld 27 to l i i 2e 29 po x L-1 31 LlJ 32 MAN FACTUREH W

AK N ACT T MET HOURS 5 IT POR US. EU L LxJ@LZ_l@ Lz_.J@ loI oloI ol 37 Ll@

48 LN_j@

ey

[Z_jh lZ l Z l Zl Z lh g3 31 34 36 40 4e of CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o IDiesel fuel tank inventory was not properly monitored durine neriod whenI i i lauxiliary hoiler was usine diesel fu e l oil. Stens were innodinen1v entnd i 7 lto obtain additional oil deliveries. Aux boiler fuel oil sunniv was I g l transferred to #6 oil within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />. Data sheet was added to ST 9.1 tol i 4 lealculate inventory once per day and to reorder at 122.000 callons. I i a e so STA  % POWER OTHER$1ATUS Di$ RV DISCOVERY DESCRIPTION i 6 8

Wh l 0l 0 l 0l@lU/ 3-Fu l l Power l g,,,, $3 $1 '

W@*s Operator Observation so l

g?n y,,,

RELE Asto OF RELEASE LOCADON OF Rf LE ASE @

l 6 h l AMOUNT N/A OF ACUVITY l

.s N/A @ l so I

e e e to n 4.

PERSONNEL EMPOSUREE NUMBER TYPE DE SCRl# TION i 7' l' 0 l0 l 0 hdh" '

N/A l

PERsONNE L iNau'Rits NUUe E R OEsCRiPfiONh N/A .

E 1010

' s 9 lOl@l 11 12 80 l

LOSS OF OR OAMAGE TO P ACiLITY tvPE DESCRIPTION 3 W@i N/A _

l Pusua' 8204 2 6 0 /d4, ,l .x , ~nc us< o~ < v mCR.P,.@.s 8 ,',N_jhl , Uto

[ N/A // / /A ^< l l l l l l I I l l l I l ! :?

r e e to ,y J 6e 69 RO 5

- ,u .. m .

  1. M. J. Cooney _ (215) 841-5020 . ;'