05000277/FIN-2012004-01
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Finding | |
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Title | Inadequate Preplanning and Performance of Maintenance/Modifications Resulted in Unavailability of RHR B Loop |
Description | The inspectors identified a Green, self-revealing non-cited violation (NCV) of Technical Specification (TS) 5.4.1, Procedures. The inspectors determined that PBAPS did not properly preplan and perform maintenance/modifications to the Unit 2 low pressure coolant injection (LPCI) swing bus B motor control cabinet (MCC) while energized. Specifically, PBAPS did not appropriately consider the potential plant impact due to sensitive energized components within the MCC that could be activated and did not utilize sufficient physical barriers to prevent such activation. Consequently, on July 25, 2012, the B loop of the residual heat removal (RHR) system was declared inoperable and unavailable after workers pulling an electrical cable into the Unit 2 energized LPCI swing bus B MCC inadvertently contacted and actuated the LPCI inboard injection valve motor relay. The motor operated valve (MOV) relay actuation caused a potential over-thrust event and had the potential to impact the valves qualification and reliability. PBAPS conducted detailed examinations and diagnostic stroke testing on the MOV assembly and concluded that the design limits of the MOV assembly were not exceeded. This finding was more than minor because it was associated with the equipment performance attribute of the Mitigating System cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined that this finding was of very low safety significance (Green) because it did not represent an actual loss of safety function of a single LPCI train for greater than its TS allowed outage time. The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance, work control, because PBAPS did not appropriately incorporate risk insights and job site conditions that could impact plant structures, systems, and components (SSCs) into its work activities. Specifically, PBAPS did not appropriately consider and reduce the potential for an over-thrust event on the B loop LPCI inboard injection valve MO-2-10-25B when performing work in the LPCI swing bus B MCC while it was energized. |
Site: | Peach Bottom |
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Report | IR 05000277/2012004 Section 1R13 |
Date counted | Sep 30, 2012 (2012Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71111.13 |
Inspectors (proximate) | J Furia A Rosebrook S Hansell A Ziedonis H Gray P Krohn S Ibarrola |
CCA | H.5, Work Management |
INPO aspect | WP.1 |
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Finding - Peach Bottom - IR 05000277/2012004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Peach Bottom) @ 2012Q3
Self-Identified List (Peach Bottom)
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