05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing

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Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing
ML20070M882
Person / Time
Site: Salem PSEG icon.png
Issue date: 12/29/1982
From: Heller R
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20070M877 List:
References
LER-82-002-01X, LER-82-2-1X, NUDOCS 8301250365
Download: ML20070M882 (1)


LER-2082-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing
Event date:
Report date:
2722082002R00 - NRC Website

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[ CRC FORM 366 U. S. NUCLE A/J RE1ULATCY COMMISSION 17 77) l UCENSEE EVENT REPORT

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74 75 7 60 61 DOCKET NUMBER 69 EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h g lOn January 19, 1982, while performing surveillance requirements to demonstrate l

,g,3, gateam generator operability, indications of tube thinning was detected by eddy l g gcurrent examination. No. 12 Steam Generator required two sample inspections. l

,g,3, lNo. 14 Steam Generator required three sample inspections, and reporting as required l 0 6 lby C-3 result in Technical Specification Table 4.4-2. l ,

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33 34 35 36 37 40 44 42 43 44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g lAll tubes degraded above 30% were plugged. Additional exams of Nos. 11 and 13 SG's l li j i j lwere conducted and all tubes degraded above 30% were plugged. Tube R44C62 was sent l

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