05000272/FIN-2017001-03
From kanterella
Jump to navigation
Jump to search
Finding | |
---|---|
Title | Failure to Conduct Post-Maintenance Testing Required by Procedure and Work Order Resulting in Inoperable Containment Fan Coil Units |
Description | Green. A self-revealing Green non-cited violation (NCV) of Technical Specification (TS) 6.8.1, Procedures and Programs; TS 3.6.2.3, Containment Cooling Fans; TS 3.6.1.1, Primary Containment Integrity; and TS 3.0.4, Applicability, was identified. Specifically, PSEG did not perform a specified post-maintenance test (PMT) after replacing the air supply valve for service water (SW) system accumulator discharge valve 11SW535. As a result, valve 11SW535 failed its subsequent technical specification (TS) required stroke time to close surveillance, and rendered two of the five containment fan coil units (CFCUs) inoperable. PSEG entered this issue in the corrective action program (CAP) as NOTF 20736868 and completed corrective actions (CAs) included coaching the senior operator involved in closing the work order (WO) without ensuring the PMT was completed and a review of similar retest activities (no additional deficiencies identified). This issue was more than minor because it was associated with the human performance attribute of the Mitigating Systems corner stone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the incomplete PMT resulted in a delay in identifying a degraded stroke time and resultant inoperability of two CFCUs. The inspectors determined that this finding was Green in accordance with IMC 0609, Appendix A, Exhibit 2, because the finding did not result in an actual loss of function of a system or train. The finding had a cross-cutting aspect in the area of Human Performance, Work Management, because the organization did not implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. Specifically, PSEG did not execute WO instructions to conduct the appropriate PMT following maintenance on an air supply valve for SW accumulator discharge valve 11SW535, which resulted in 11SW535 stroking closed too fast and required declaring two CFCUs inoperable. [H.5] |
Site: | Salem |
---|---|
Report | IR 05000272/2017001 Section 4OA3 |
Date counted | Mar 31, 2017 (2017Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | A Ziedonis F Bower J Furia J Schoppy P Boguszewski P Finney S Pindale |
Violation of: | Technical Specification Technical Specification - Procedures |
CCA | H.5, Work Management |
INPO aspect | WP.1 |
' | |
Finding - Salem - IR 05000272/2017001 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Salem) @ 2017Q1
Self-Identified List (Salem)
| ||||||||||||||||||||||||||||||||||||||||||||||||||||||||