05000269/FIN-2017001-03
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Finding | |
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Title | Licensee-Identified Violation |
Description | Oconee Nuclear Station Technical Specification 3.0.4 requires that when a limiting condition of operation is not met, entry into a mode or other specified condition in the applicability shall not be made except when the associated actions to be entered permit continued operation in the mode or other specified condition in the applicability for an unlimited period of time. Oconee Nuclear Station Technical Specification 3.3.7, Engineered Safeguards Protective System (ESPS) Automatic Actuation Output Logic Channels, requires eight ESPS automatic actuation output logic channels to be operable in Modes 1 and 2 and Modes 3 and 4 when associated ES equipment is required to the operable. Contrary to the above, Oconee Nuclear Station Unit 1 entered Mode 4 on November 24, 2016 with ES protective system voters 1 and 2 in an abnormal configuration (bypassed) for the plant mode of operation. Operations shift personnel discovered this abnormal configuration on November 25, 2016 and restored voters 1 and 2 to an operate condition which met Technical Specification 3.3.7. This failure to maintain ESPS channels in the correct mode of operation for the required mode of applicability was a performance deficiency and was determined to be more than minor. The issue is more than minor because it was associated with the configuration control attribute of the mitigating system cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the issue challenged the configuration control attribute of ensuring operating equipment was available to respond to initiating events. The inspectors used IMC 0609, Att. 4, Initial Characterization of Findings, issued October 07, 2016, and IMC 0609, Appendix A, Significance Determination Process for Findings at Power, issued June 19, 2012, and determined the finding was of very low safety significance (Green) because the finding did not represent an actual loss of function of at least a single train for greater than its technical specification allowed outage time or two separate safety systems out-of-service for greater than its technical specification allowed outage time. The licensee has entered this issue into their corrective action program as NCR 02081523. |
Site: | Oconee |
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Report | IR 05000269/2017001 Section 4OA7 |
Date counted | Mar 31, 2017 (2017Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | E Crowe F Ehrhardt G Callaway J Parent M Bates M Toth N Childs |
Violation of: | Technical Specification |
INPO aspect | |
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Finding - Oconee - IR 05000269/2017001 | |||||||||||||||||||||||||||||||||||||||||
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Finding List (Oconee) @ 2017Q1
Self-Identified List (Oconee)
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