05000266/LER-1997-026, Forwards LER 97-026-00 Re Failure to Establish Operability of RCS Average Temp Instrumentation Input to MSL Isolation Function During Plant Conditions Required by TS Table 15.3.5-4 Item 2.b Operability Requirements

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Forwards LER 97-026-00 Re Failure to Establish Operability of RCS Average Temp Instrumentation Input to MSL Isolation Function During Plant Conditions Required by TS Table 15.3.5-4 Item 2.b Operability Requirements
ML20141C254
Person / Time
Site: Point Beach NextEra Energy icon.png
Issue date: 06/19/1997
From: Dante Johnson
WISCONSIN ELECTRIC POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20141C260 List:
References
NPL-97-0364, NPL-97-364, NUDOCS 9706250076
Download: ML20141C254 (1)


LER-2097-026, Forwards LER 97-026-00 Re Failure to Establish Operability of RCS Average Temp Instrumentation Input to MSL Isolation Function During Plant Conditions Required by TS Table 15.3.5-4 Item 2.b Operability Requirements
Event date:
Report date:
2662097026R00 - NRC Website

text

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\ POWER COMPANY Point Decch Nuclear Plant (414) 755-2321 6610 Nuclear Rei. Two Rivers. WI 54241 NPL 97-0364 June 19,1997 Document Control Desk U.S. NUCLEAR REGULATORY COMMISSION Mail Station PI-137 -

Washington, D. C. 20555 Ladies / Gentlemen:

DOCKETS 50-266 AND 50-301 LICENSEE EVENT REPORT 97-026-00 TECIINICAL SPECIFICATION VIOLATION OF OPERABILITY REOUIREMENT FOR MAIN STEAM LINE ISOLATION POINT BEACH NUCLEAR PLANT. UNITS 1 AND 2 Enclosed is Licensee Event Report 97-026-00 for Point Beach Nuclear Plant, Units 1 and 2. This  ;

report is provided in accordance with 10 CFR 50.73(a)(2)(i)(B),"Any operation or condition .

prohibited by the plant's Technical Specifications." This report describes the identification of )

the failure to establish operability of the reactor coolant system average temperature instrumentation input to the main steam line isolation function during plant conditions required l by Technical Specification Table 15.3.5-4 item 2.b operability requirements. i New commitments within the report are indicated in italics. )

Please contact us if you require additional information.

Sincerely, 9

D. F. Johnson Manager - Regulatory Services & Licensing f

g'i Enclosure cc: NRC Resident inspector NRC Regional Administrator

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97062 970619 * * '

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