06-24-2016 | Motor Operated (MO) HPCI Outboard Main Steam Isolation Valve (MO 2-2301-5). The packing leak was causing a two (2) foot steam plume to impinge on the valve limit switch compartment, potentially impacting the motor operator for the MO 2-2301-5 valve.
Due to the uncertainty on how the steam impingement would affect the valve limit switch compartment, Operations conservatively isolated the steam leak by closing the HPCI Inboard Main Steam Isolation Valve (MO 2-2301-4). With the steam supply isolated, HPCI was declared inoperable and Technical Specification (TS) 3.5.1 Condition G was entered.
The cause of the packing leak was a non-modern style packing installed in 2007 to repack valve MO 2-2301-5.
This packing material was susceptible to premature degradation.
Corrective actions included repacking the valve with modern packing and performance of valve diagnostic testing.
The safety significance of this event was minimal. Given the impact on the HPCI system, this report is submitted for Unit 2 in accordance with the requirements of 10 CFR 50.73 (a)(2)(v)(D), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. |
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Category:Letter
MONTHYEARIR 05000254/20230042024-02-0505 February 2024 Integrated Inspection Report 05000254/2023004 and 05000265/2023004 ML24004A0052024-01-17017 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0042 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) RS-24-001, Response to Request for Additional Information Regarding Relief Request I5R-26, Inservice Inspection Program Relief Request Regarding Examination Coverage for the Fifth Inservice Inspection Interval2024-01-0303 January 2024 Response to Request for Additional Information Regarding Relief Request I5R-26, Inservice Inspection Program Relief Request Regarding Examination Coverage for the Fifth Inservice Inspection Interval IR 05000254/20234032023-12-22022 December 2023 Public- Quad Cities Nuclear Power Station Security Baseline Inspection Report 05000254/2023403 and 05000265/2023403 IR 05000254/20230102023-12-20020 December 2023 Comprehensive Engineering Team Inspection Report 05000254/2023010 and 05000265/2023010 ML23349A1622023-12-17017 December 2023 Issuance of Amendment Nos. 298 and 294 Increase Completion Time in Technical Specification 3.8.1.B.4 (Emergency Circumstances) RS-23-128, Response to Request for Additional Information for the Emergency License Amendment Request Increase Technical Specifications Completion Time in TS 3.8.1.B.4 from 7 Days to 30 Days2023-12-15015 December 2023 Response to Request for Additional Information for the Emergency License Amendment Request Increase Technical Specifications Completion Time in TS 3.8.1.B.4 from 7 Days to 30 Days ML23305A1402023-12-13013 December 2023 Units 1 & 2; Nine Mile Point, Unit 2; Peach Bottom, Units 2 & 3; and Quad Cities, Units 1 and 2 - Issuance of Amendments to Adopt Traveler TSTF-580 RS-23-123, Emergency License Amendment Request - Increase Technical Specifications Completion Time in TS 3.8.1.B.4 from 7 Days to 30 Days2023-12-13013 December 2023 Emergency License Amendment Request - Increase Technical Specifications Completion Time in TS 3.8.1.B.4 from 7 Days to 30 Days ML23339A1762023-12-0505 December 2023 Notification of NRC Baseline Inspection and Request for Information (05000265/2024001) ML23319A3342023-11-20020 November 2023 Regulatory Audit in Support of License Amendment Requests to Adopt TSTF 505, Revision 2 and 10 CFR 50.69 RS-23-104, Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-11-17017 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23317A1192023-11-10010 November 2023 Constellation Energy Generation, LLC - 2023 Annual Report - Guarantees of Payment of Deferred Premiums IR 05000254/20230032023-11-0909 November 2023 Integrated Inspection Report 05000254/2023003 and 05000265/2023003 RS-23-113, Submittal of Updated Final Safety Analysis Report (Ufsar), Revision 17 and Fire Protection Report (Fpr), Revision 262023-10-20020 October 2023 Submittal of Updated Final Safety Analysis Report (Ufsar), Revision 17 and Fire Protection Report (Fpr), Revision 26 RS-23-097, Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans2023-10-12012 October 2023 Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans ML23206A0382023-09-21021 September 2023 Proposed Alternative to the Requirements of the ASME Code IR 05000254/20230112023-09-20020 September 2023 Safety-Conscious Work Environment Issue of Concern Team Inspection Report 05000254/2023011 and 05000265/2023011 RS-23-089, Sixth Ten-Year Interval Inservice Testing Program2023-09-0505 September 2023 Sixth Ten-Year Interval Inservice Testing Program RS-23-080, Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-264-A, Revision 0, 3.3.9 and 3.3.10 - Delete Flux Monitors Specific Overlap Requirement SRs2023-08-30030 August 2023 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-264-A, Revision 0, 3.3.9 and 3.3.10 - Delete Flux Monitors Specific Overlap Requirement SRs RS-23-086, Relief Request I5R-26, Inservice Inspection Program Relief Request Regarding Examination Coverage for the Fifth Inservice Inspection Interval2023-08-28028 August 2023 Relief Request I5R-26, Inservice Inspection Program Relief Request Regarding Examination Coverage for the Fifth Inservice Inspection Interval SVP-23-038, Owner'S Activity Report Submittal Fifth 10-Year Interval 2023 Refueling Outage Activities2023-08-14014 August 2023 Owner'S Activity Report Submittal Fifth 10-Year Interval 2023 Refueling Outage Activities IR 05000254/20230022023-08-0808 August 2023 Integrated Inspection Report 05000254/2023002 and 05000265/2023002 ML23178A0742023-08-0707 August 2023 Issuance of Amendment Nos. 296 and 292 Adoption of TSTF-416 Low Pressure Coolant Injection (LPCI) Valve Alignment Verification Note Location ML23216A0362023-08-0707 August 2023 Notification of an NRC Biennial Licensed Operator Requalification Program Inspection and RFI ML23216A0562023-08-0404 August 2023 Information Meeting (Open House) with a Question and Answer Session to Discuss NRC 2022 End-Of-Cycle Plant Performance Assessment of Quad Cities Nuclear Power Station, Units 1 and 2 SVP-23-031, Regulatory Commitment Change Summary Report2023-07-14014 July 2023 Regulatory Commitment Change Summary Report ML23181A1062023-06-30030 June 2023 Postponement- Information Meeting (Open House) with a Question-And-Answer Session to Discuss NRC 2022 End-Of-Cycle Plant Performance Assessment of Quad Cities Nuclear Power Station ML23178A2422023-06-28028 June 2023 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch III ML23179A1932023-06-28028 June 2023 07122023 Letter-Significant Public Meeting to Discuss NRC End-of-Cycle Performance Assessment of Quad Cities Nuclear Plant for Performance for 2022 Calendar Year IR 05000254/20234012023-06-26026 June 2023 Cyber Security Inspection Report 05000254/2023401 and 05000265/2023401 IR 05000265/20230402023-06-22022 June 2023 Reissue Quad Cities Nuclear Power Station 95001 Supplemental Inspection Supplemental Report 05000265/2023040 and Follow Up Assessment Letter RS-23-077, Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations2023-06-16016 June 2023 Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations ML23167B1722023-06-16016 June 2023 95001 Supplemental Inspection Report 05000265/2023040 and Follow-Up Assessment Letter RS-23-060, Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components for Nuclear Power Reactors2023-06-0808 June 2023 Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components for Nuclear Power Reactors RS-23-059, License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2023-06-0808 June 2023 License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b ML23144A3632023-05-26026 May 2023 Information Meeting (Open House) with a Question and Answer Session to Discuss NRC 2022 End-of-Cycle Plant Performance Assessment of Quad Cities Nuclear Power Station, Units 1 and 2 RS-23-042, Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling2023-05-25025 May 2023 Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling ML23033A4042023-05-15015 May 2023 Exemption from the Requirements of 10 CFR Part 2, Section 2.109(B) Related to Submission of Subsequent License Renewal Application Letter IR 05000254/20234022023-05-15015 May 2023 Security Baseline and ISFSI Inspection Reports 05000254/2023402, 05000265/2023402, 07200053/2023401 ML23132A2022023-05-12012 May 2023 Annual Radiological Environmental Operating Report ML23125A0612023-05-0808 May 2023 Proposed Alternative to the Requirements of the ASME Code IR 05000254/20230012023-05-0808 May 2023 Integrated Report 05000254/2023001 and 05000265/2023001 RS-22-067, 10 CFR 50.46 Annual Report2023-05-0404 May 2023 10 CFR 50.46 Annual Report ML23118A3472023-05-0101 May 2023 County, 1 & 2; Nine Mile Point, 2; and Quad Cities, 1 & 2 - Correction of Amendment No. 193 Adoption of TSTF-306, Revision 2, Add Action to LCO 3.3.6.1 to Give Option to Isolate the Penetration EPID L-2022-LLA-0143 RS-23-068, Response to Request for Additional Information for Quad Cities Relief Request I6R-11, Proposed Alternatives for a Temper Bead Weld Repair of the Mating Surfaces of the Reactor Pressure Vessel Head and Shell2023-04-28028 April 2023 Response to Request for Additional Information for Quad Cities Relief Request I6R-11, Proposed Alternatives for a Temper Bead Weld Repair of the Mating Surfaces of the Reactor Pressure Vessel Head and Shell SVP-23-018, Radioactive Effluent Release Report for 20222023-04-28028 April 2023 Radioactive Effluent Release Report for 2022 ML23114A2522023-04-28028 April 2023 Request to Use a Provision of a Later Edition of the ASME Boiler & Pressure Vessel Code, Section XI ML23110A0622023-04-25025 April 2023 Transmittal of Final Quad Cities Nuclear Power Plant, Unit 1 Accident Sequence Precursor Report (Licensee Event Report 254-2022-001) ML23081A0382023-04-25025 April 2023 County, 1 & 2; Nine Mile Point, 2; and Quad Cities, 1 & 2 - Issuance of Amendments to Adopt TSTF-306, Rev. 2, Add Action to LCO 3.3.6.1 to Give Option to Isolate the Penetration 2024-02-05
[Table view] Category:Licensee Event Report (LER)
MONTHYEARSVP-22-072, Manual Scram Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level2022-12-30030 December 2022 Manual Scram Due to Feedwater Regulator Valve Failure Increasing Reactor Water Level 05000254/LER-2017-0042018-01-0505 January 2018 Unit 1 HPCI Did Not Trip Due to Wear Debris in the Turbine Stop Valve Oil Resetting Solenoid, LER 17-004-00 For Quad Cities Nuclear Power Station, Unit 1 re: Unit 1 HPCI Did Not Trip Due to Wear Debris in the Turbine Stop Valve Oil Resetting Solenoid 05000254/LER-2017-0032017-11-17017 November 2017 Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue, LER 17-003-00 for Quad Cities, Unit 1, Regarding Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue 05000265/LER-2017-0012017-07-13013 July 2017 High Pressure Coolant Injection Minimum Flow Valve Failed to Open, LER 17-001-00 for Quad Cities, Unit 2, Regarding High Pressure Coolant Injection Minimum Flow Valve Failed to Open 05000254/LER-2017-0022017-05-26026 May 2017 Four Main Steam Isolation Valves (MSIVs) Closure Times Exceeded, LER 17-002-00 for Quad Cities, Unit 1, Regarding Four Main Steam Isolation Valves (MSIVs) Closure Times Exceeded 05000254/LER-2017-0012017-03-22022 March 2017 Secondary Containment Interlock Doors Opened Simultaneously, LER 17-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Interlock Doors Opened Simultaneously 05000265/LER-2016-0022016-06-24024 June 2016 High Pressure Coolant Injection System Declared Inoperable Due to Valve Packing Leak, LER 16-002-00 for Quad Cities Nuclear Power Station Unit 2 - RE: High Pressure Coolant Injection System Declared Inoperable Due to Valve Packing Leak 05000265/LER-2016-0012016-05-19019 May 2016 Main Steam Isolation Valve Local Leak Rate Tests Exceed Technical Specification Limits, LER 2016-001-00 for Quad Cities Nuclear Power Station, Unit 2 Regarding Main Steam Isolation Valve Local Leak Rate Tests Exceed Technical Specification Limits 05000254/LER-2016-0022016-03-14014 March 2016 Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Pump Rm), LER 16-002-00 for Quad Cities Units 1 and 2, Regarding Secondary Containment Different Pressure Momentarily Lost due to Air Failure (RWCU pump Rm) 05000254/LER-2016-0012016-03-10010 March 2016 Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm), LER 16-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm) 05000254/LER-2015-0102016-02-0505 February 2016 Loss of Control Room Emergency Ventilation System Due to Differential Pressure Switch Failure, LER 15-010-00 for Quad Cities, Unit 1, Regarding Loss of Control Room Emergency Ventilation System Due to Differential Pressure Switch Failure SVP-03-036, LER 03-S01-00, Security Event Report for Quad Cities, Unescorted Protected Area Access Granted Based on Falsified Information and Inadequate Screening Caused by a Failure of Administrative Controls.2003-03-0303 March 2003 LER 03-S01-00, Security Event Report for Quad Cities, Unescorted Protected Area Access Granted Based on Falsified Information and Inadequate Screening Caused by a Failure of Administrative Controls. ML17252B4771976-09-15015 September 1976 LER 76-059-00 for Dresden, Units 2 and 3 Re Review of Quad-Cities Unusual Event Letter Led to Discovery That Dresden'S Standby Gas Treatment System Deviated from Single Failure Criteria That Disabled the SBGT System ML18348A2401976-08-0606 August 1976 LER 1976-027-00, Reportable Occurrence of Control Rods for Quad-Cities, Unit 1 ML18348A2391976-08-0404 August 1976 LER 1976-026-00, Reportable Occurrence of Control Rods for Quad-Cities, Unit 1 2022-12-30
[Table view] |
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
EVENT IDENTIFICATION
High Pressure Coolant Injection System Declared Inoperable Due to Valve Packing Leak
A. CONDITION PRIOR TO EVENT
Unit: 2 Reactor Mode: 1 Event Date: April 25, 2016 Event Time: 06:07 hours Mode Name: Power Operation Power Level: 100%
B. DESCRIPTION OF EVENT
On April 25, 2016 at 04:50, while performing Reactor Building basement rounds, an Equipment Operator (EO) identified a small puddle of water in Bay 2 of the Unit 2 Torus area with water actively leaking from the overhead area at 2 drops per minute (dpm). An additional, much larger, puddle was discovered in Bay 3 with approximately 15 dpm leaking from the overhead area. A second EO was dispatched to the top of the Unit 2 Torus to inspect for leaks. The EO on top of the Torus reported a two foot steam plume coming from the packing of the MO 2-2301-5, Unit 2 HPCI Outboard Main Steam Isolation Valve. It was noted that the steam was impinging on the MO 2-2301-5 limit switch compartment, but not directly on any other components.
At 06:07, Operations isolated the identified steam leak by closing the MO 2-2301-4, Unit 2 HPCI Inboard Main Steam Isolation Valve. Operations declared Unit 2 HPCI inoperable and unavailable at this time and entered TS 3.5.1 Condition G.
At 12:05, Operations closed the MO 2-2301-5 valve as part of the Clearance Order (CO) boundary. The valve closed as expected and no ground alarms were received.
At 12:39, ENS #51880 was made to the NRC under 10 CFR 50.72(b)(3)(v)(D) to report this event as an event or condition that could have prevented the fulfillment of a safety function.
On April 27, 2016 at 05:44, after repacking the valve with a modern packing set (AP Services 6000/6300J) and diagnostic testing, Unit 2 HPCI was returned to the standby line-up and declared operable; TS LCO 3.5.1 Condition G was exited.
C. CAUSE OF EVENT
Non-modern style packing (Crane 387-I) was used in 2007 to repack the MO 2-2301-5 valve. This packing material was susceptible to premature degradation and hardening. At the time of installation, the long term temperature effects on Crane 387-I packing were not yet discovered.
Crane 387-I (non-modern style) packing has a history of drying out and becoming very hard. This typically happens when Crane 387-I packing is used in high temperature and pressure systems. The materials used in this packing are susceptible to drying out. When the packing dries out, and is no longer flexible, it typically leads to packing leaks.
This is especially true with the Crane 387-I (I indicates that there is Inconel wire impregnated in the rope). This was initially believed to be used as a reinforcement material; however, it was later discovered to be a potential foreign material issue. During valve unpacking, the Inconel wire may break apart and the wire pieces can potentially enter into the system.
D. SAFETY ANALYSIS
System Design Per the Updated Final Safety Analysis Report (UFSAR) Section 6.3.2.3, the HPCI subsystem is designed to pump water into the reactor vessel under Loss of Coolant Accident (LOCA) conditions which do not result in rapid depressurization of the pressure vessel. The loss of coolant might be due to a loss of reactor feedwater or to a small line break which does not cause immediate depressurization of the reactor vessel. The sizing of the HPCI subsystem is based upon providing adequate core cooling during the time that the pressure in the reactor vessel decreases to a value that the Core Spray subsystem and/or the Low Pressure Coolant Injection (LPCI) subsystem become effective.
The HPCI subsystem is designed to pump 5600 gallons per minute into the reactor vessel within a reactor pressure range of about 1120 psig to 150 psig. Initiation of the HPCI subsystem occurs automatically on signals indicating reactor low-low water level or high drywell pressure. HPCI injection into the reactor vessel may be accomplished manually by the operator or without operator action by the HPCI automatic initiation circuitry. HPCI can also operate in a pressure control mode of consuming steam from the reactor vessel without providing full injection into the vessel (down to and including zero injection).
Per UFSAR Section 6.3.3.1.3.2, the LOCA analysis by Westinghouse at 2957 MWt for SVEA-96 Optima2 fuel analyzed the entire break spectrum. This analysis included the various combinations of single failures as described in Table 6.3-7D. The HPCI turbine oil cooler and gland seal condenser are cooled by water from the suppression pool.
Since these components are rated at 140°F, continued operation above a suppression pool temperature of 140°F is not permitted. Also, operation of HPCI above 140°F would exceed the current net positive suction head (NPSH) calculations for rated HPCI pump flows. Another limitation on the HPCI system is related to the dependence of the HPCI room cooler on the unit emergency diesel generator (EDG). Therefore, any single failures of the unit EDG need to assume consequential loss of the HPCI system after 10 minutes of operation. As a result of these considerations, the HPCI system is not credited when any of these conditions are exceeded. The results of the analysis show that the HPCI system met its requirements before the 10 minute mission time was exceeded and the suppression pool temperature exceeded 140°F.
Safety Impact The safety impact of this condition was low. Valve MO 2-2301-5 is normally open and required to remain open during HPCI initiation. Due to the potential impact of the steam plume on the valve's motor operator, Operations conservatively closed the HPCI Inboard Main Steam Isolation Valve (MO 2-2301-4) to stop the packing leak. The valve actuator area did have some condensation from the steam but did not exhibit any 250 VDC grounds or any other abnormalities. The valve closed satisfactorily during placement of the CO and showed no signs of electrical or mechanical degradation. The identified packing leak would not have affected the valve's ability to remain open if HPCI was required for injection into the reactor vessel. The MO 2-2301-5 valve has a normal open position for the HPCI System and must remain open for the HPCI System to perform its intended safety function. Even though the packing had failed within the valve, based on the leakage observed, the valve remained in the normal open position.
The HPCI System remained capable of performing its intended design/safety function. The packing leak was
CONTINUATION SHEET
considered insignificant compared to the total steam consumption of the HPCI System and would not have hindered the system from fulfilling any required safety function or injection over the required 10 minute mission time.
Per UFSAR Table 6.2-7, valve MO 2-2301-5 is considered a primary containment isolation valve with a normal position of open. Valve MO 2-2301-5 is one of two primary containment isolation valves present in line 2-2305-10"-B, the other is the MO 2-2301-4 valve. As with valve MO 2-2301-5, the normal position for the MO 2-2301-4 valve is open. At the time the leak was identified on valve MO 2-2301-5, the MO 2-2301-4 valve was closed to stop the leak.
Since the line could effectively be isolated utilizing one of two primary containment isolation valves, the primary containment integrity could be assured, therefore, the primary containment system remained capable of performing its intended design/safety function.
With MO 2-2301-4 closed, HPCI was declared inoperable and TS 3.5.1 Condition G was entered. Required action G.2 is to, restore HPCI System to OPERABLE status, with a completion time of 14 days. The valve was repacked with a modern packing set, post maintenance tested and the HPCI system declared operable in approximately 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. There were no other issues or problems identified with valve MO 2-2301-5 during the packing replacement.
No other repairs were required or performed. The valve closed satisfactorily during placement of the CO and showed no signs of electrical or mechanical degradation. Electrical and Mechanical visual inspections were performed with no issues identified. The Post Maintenance Testing was performed satisfactorily with no identified issues. Since valve MO 2-2301-5 showed no signs of electrical degradation due to the steam impingement, the HPCI System remained capable of performing its intended design/safety function.
Since HPCI is a single train safety system, this notification is being made per NUREG-1022, Revision 3, Section 3.2.7 (Event or Condition that Could Have Prevented Fulfillment of a Safety Function), which states, "There are a limited number of single-train systems that perform safety functions (e.g., the HPCI system in BWRs). For such systems, inoperability of the single train is reportable even though the plant TS may allow such a condition to exist for a limited time.
The engineering analysis that was performed demonstrated this event did not constitute a Safety System Functional Failure (SSFF). (Reference NEI 99-02, Revision 7, Regulatory Assessment Performance Indicator Guideline, Section 2.2, Mitigating Systems Cornerstone, Safety System Functional Failures, Clarifying Notes, Engineering analyses.) As such, this event will not be reported in the NRC Performance Indicator (PI) for SSFF since an engineering analysis was performed which determined that the system was capable of performing its safety function during this event.
Risk Insights The plant Probabilistic Risk Assessment (PRA) model was reviewed with respect to this event. Since HPCI was unavailable for only 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, the incremental change in risk was minimal.
In conclusion, the overall safety significance and impact on risk of this event were minimal.
E. CORRECTIVE ACTIONS
Immediate:
1. Mechanical Maintenance replaced the packing in the valve with a modern packing set, and Electrical Maintenance performed a post maintenance valve diagnostic thrust test.
Follow-up:
2. Component Maintenance Organization will verify modern packing sets are installed in all primary containment isolation valves.
F. PREVIOUS OCCURRENCES
The station events database, LERs, and INPO Consolidated Event System (ICES) were reviewed for similar events at the Quad Cities Nuclear Power Station. This event was attributed to non-modern style packing material that was susceptible to premature degradation. Based on the nature of this failure, the event listed below, although similar in topic, are not considered significant station experience that would have directly contributed to preventing this event.
- INPO ICES #199278 "HPCI Inboard Steam Supply Isolation Valve Packing Leak Causes Reactor Shutdown to Repair" — During a MOV valve timing test on July 24, 2002, at Quad Cities Unit 1, the HPCI Steam Supply Inboard Drywell in-leakage increased from approximately 1.5 gpm to approximately 2.2 gpm. During the subsequent troubleshooting for the cause of the increased in-leakage, MOV 1-2301-4 was closed. The Drywell in-leakage then decreased from approximately 2.2 gpm to approximately 0.38 gpm. The as-found valve condition was steam leaking from the stuffing box. The packing gland nuts were not at rated torque and the live-load washers were not in complete compression when the valve packing was disassembled. The apparent cause of this event was the gradual loss of packing gland force. The loss of gland force allowed the packing to decompress and steam to eventually escape.
G. COMPONENT FAILURE DATA
Failed Equipment: High Pressure Coolant Injection Outboard Steam Supply Primary Containment Isolation Valve MO 2-2301-5 Component Manufacturer: Crane Valve Corporation.
Component Model Number: SPL783U-10-900-SR-A-N Component Part Number: LIMITORQUE, 783 U, 10.0 This event will not be reported to ICES due to not meeting the INPO reporting criteria (14 day unplanned LCO; not 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or less).