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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000263/LER-1993-0081993-08-30030 August 1993 LER 93-008-00:on 930731,RPS Tripped from Reactor Low Water Level.Caused by Main Condensate Pump Trip.Condensate Pump 11 Motor Will Be Inspected & Preventive Maint Will Be Performed on Condensate Pump 11 breaker.W/930830 Ltr ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000263/LER-1984-011, Revised LER 84-011-01:on 840218,crack Indications Discovered in Listed Locations,Including RHR Sys & Recirculation Sys Pump Suction & Discharge Valves.Caused by Igscc.Stainless Steel 304 to Be Replaced1984-05-15015 May 1984 Revised LER 84-011-01:on 840218,crack Indications Discovered in Listed Locations,Including RHR Sys & Recirculation Sys Pump Suction & Discharge Valves.Caused by Igscc.Stainless Steel 304 to Be Replaced 05000263/LER-1982-013, Updated LER 82-013/01T-3:on 820928,1020,31 & 1102,during Preparation for Repair of E,C & F safe-ends,thru Wall Leaks Found on Each safe-end.Caused by Intergranular Stress Corrosion Cracking.Defects Repaired1982-12-0606 December 1982 Updated LER 82-013/01T-3:on 820928,1020,31 & 1102,during Preparation for Repair of E,C & F safe-ends,thru Wall Leaks Found on Each safe-end.Caused by Intergranular Stress Corrosion Cracking.Defects Repaired 05000263/LER-1982-004, Updated LER 82-004/01T-1:on 820410,inboard & Outboard 18-inch Dyrwell Vent Valves Failed to Close Upon Hand Switch Activation.Probably Caused by Solenoids Being Mounted Horizontally & Residual Core Magnetism.Solenoids Replaced1982-05-20020 May 1982 Updated LER 82-004/01T-1:on 820410,inboard & Outboard 18-inch Dyrwell Vent Valves Failed to Close Upon Hand Switch Activation.Probably Caused by Solenoids Being Mounted Horizontally & Residual Core Magnetism.Solenoids Replaced ML20062G2421978-12-21021 December 1978 /01T-0 on 781214:High Pressure Instrument Channel Relay Failed to Energize Due to Disengaged Agastat CR0095 Relay Socket Contact That Failed to Make Contact W/Agastat FPB750 Relay Contact.Contacts Were Reengaged ML20062G2571978-12-21021 December 1978 /03L-0 on 781121:during Normal Pwr Increase,Both Indicating Lights for MO-2014,LPCI a Loop Admission Valve Were Out Due to Blown Control Pwr Fuse.Fuse Had Opened on Slight Over Load for Extended Time Period & Was Replaced ML20062G2611978-12-21021 December 1978 /03L-0 on 781121:during Normal Oper a Steam Leak Was Found in Tee Downstream of MO-1197 on the 2 HP Turbine U Bend Drain Line to Condenser,Probably Due to Flow of Steam & Water from Restricting Orifice Into Tee ML20062D4941978-10-19019 October 1978 /03L-0 on 781002:during Routine Surveillance Test, HPCI Isolation Temp Switch Model 17023-6 Failed to Trip,Due to Loose Wire Inside Switch.Redundant Switches Tested Satisfatorily ML20058L5401977-12-21021 December 1977 Ler:On 771207,secondary Containment Isolation Dampers Associated W/Reactor Bldg Vent Supply Unit V-AH-4A Found Blocked in Open Position by Ice.Caused by Corrosion of Preheat Coil.Replacement Coils on Order ML20058L5411977-12-19019 December 1977 LER Update Rept M-RO-77-33.On 771031,number 15 Bus Auto Transfer Malfunctioned.Caused by Use of Incorrect Const Prints ML20058L5511977-11-30030 November 1977 Ler:On 771031,loss of 4 Kv Safeguards Bus Automatic Transfer Capability Occurred.Caused by Blown Control Fuses Due to Short Circuit.Short Removed & Fuses Replaced ML20058L5531977-11-29029 November 1977 Ler:On 771030,main Steam Line Low Pressure Switch Setpoint Drift Occurred.Switch Reset 05000263/LER-1977-0241977-11-18018 November 1977 LER 77-24-7:on 770910,A Outboard MSIV Found Leaking in Excess.Caused by Plug Being Slightly Out of Round.Seats Lapped & Valve Retested 05000263/LER-1977-0301977-11-0909 November 1977 LER 77-30:on 771010,discovered Leak from B RHR Loop Relief Valve 2005 2 Boss Connection.Caused by Excess Cyclic Moment Induced by Unrestrained Vibration During Shutdown Cooling Operation.Relief Restraint installed.W/771109 Ltr 05000263/LER-1977-0291977-11-0101 November 1977 LER 77-29:on 771002,three Main Steam Line Area Temp Switches Found to Trip Above Allowable Tech Spec Setting.Switches recalibrated.W/771101 Ltr 05000263/LER-1977-0311977-10-27027 October 1977 LER 77-31:on 771013,noted Torus Internal Catwalk Sections Not Attached in Same Manner.All Locations Will Be Upgraded to Design Requirements Prior to End of outage.W/771027 Ltr 05000263/LER-1977-0271977-10-21021 October 1977 LER 77-27:on 770923,RHR Torus Cooling Valve Body Seat Ring Threads Found to Be Stripped.Caused by Rotation of Plug Which Unscrewed Seat.Mod in Process to Hold Seat in Place Using Bolding Ring Welded to Valve body.W/771021 Ltr 05000263/LER-1977-0261977-10-11011 October 1977 LER 77-26:on 770911,elbow on F SRV Discharge Line Found Deformed.Caused by Inadequate Restraint on Discharge Line. Addl Support Being Installed to Reduce Displacement of Line. W/771011 Ltr 05000263/LER-1977-0231977-10-0707 October 1977 LER 77-23:on 770909,RHR Torus Cooling Valve Mo 2009 Failed to Operate Properly.Caused by Inadequate Stem Clamp Set Screws for Unseating Torque.Stem Clamp W/Keyway Being installed.W/771007 Ltr 05000263/LER-1977-0251977-09-27027 September 1977 LER 77-25:on 770913,recalculated ECCS Thermal Limits Found to Be More Restrictive than Tech Spec Limits.Limiting Break Size & Revised Thermal limits.W/770927 Ltr 05000263/LER-1977-0221977-09-27027 September 1977 LER 77-22:on 770828,MO-2013 B RHR Injection Valve Failed to Open.Control Relays Installed in Breaker to Reduce Control Wire Voltage drop.W/770927 Ltr 05000263/LER-1977-0211977-09-0707 September 1977 LER 77-21:on 770810,CRD HCU 30-11 Nitrogen Charging Valve on Accumulator Would Not Hold Pressure.Caused by Leaking Stem Packing.Program Will Be Initiated to Replace Packing in Similar valves.W/770907 Ltr ML20058K5811977-09-0101 September 1977 Ler:On 770802,discovered Steam Leak Due to Erosion Caused by Flow of Steam/Water Through Failed Steam Trap Upstream of Elbow ML20058K5951977-07-11011 July 1977 Ler:On 770627,discovered Air Ejector Radiation Monitors Inoperable Following Startup After Outage ML20058K5931977-06-29029 June 1977 Ler:On 770530,discovered Failure of RHR Injection Valve Mo 2013 to Open ML20058K5991977-04-0404 April 1977 Ler:On 770321,discovered Air Ejector Radiation Monitors Inoperable During Startup Caused by Sample Sys Isolation ML20125B9541977-03-15015 March 1977 Ler:On 770315,following Installation of Redundant Torus Water Level Transmitter,Discrepancy Noted Between Two Torus Level Indicators.Torus Water Volume Returned to Normal Oprerating Volume 05000263/LER-1977-0031977-02-0909 February 1977 LER 77-03:on 770127,TIP Ball Valve Failed to Close During Use of Sys.Cause Undetermined.Valve Disassembled,Inspected & Found in Good condition.W/770209 Ltr ML20058K6211977-02-0909 February 1977 Ler:On 770127,discovered Number 3 Tip Ball Valve Failed to Close During Routine Use of Tip Sys.Cause Undetermined 05000263/LER-1976-0231976-11-24024 November 1976 LER 76-23:on 760912,surveillance Coordinator Could Not Locate Main Steam Line Radiation Monitor Functional Test Scheduled to Be Completed During Wk of 760912.Test Overlooked & Not Assigned for completion.W/761124 Ltr 05000263/LER-1976-011, Updated LER 76-011:on 760802 & 0830,during Test,Rcic Turbine Tripped on Overspeed.Caused by Steam Void in Discharge Piping Due to Valve Leakage from Feedwater Sys.Control Oil Sys Modified to Improve Control Valve Response1976-10-22022 October 1976 Updated LER 76-011:on 760802 & 0830,during Test,Rcic Turbine Tripped on Overspeed.Caused by Steam Void in Discharge Piping Due to Valve Leakage from Feedwater Sys.Control Oil Sys Modified to Improve Control Valve Response 05000263/LER-1976-0181976-09-22022 September 1976 LER 76-18:on 760909,investigation of Drywell Torus Pressure Differential Effect on Torus Water Level Vol Correllation Disclosed Vol Slightly Below Tech Spec Limit.Water Vol Increased & New Vol Vs Level Correlation Issued 05000263/LER-1976-012, Updated LER 76-012:on 760805,generic ECCS Model Analysis Indicated 2200 F PCT May Be Exceeded at Reduced Core Flows. MAPLHGR 5% Reduction at Less than 90% Core Flow implemented.W/760910 Ltr1976-09-0303 September 1976 Updated LER 76-012:on 760805,generic ECCS Model Analysis Indicated 2200 F PCT May Be Exceeded at Reduced Core Flows. MAPLHGR 5% Reduction at Less than 90% Core Flow implemented.W/760910 Ltr ML20058K9521976-03-19019 March 1976 Ler.On 760220,elbow Leaking on Condensate Return Line Down Stream of Trap.Caused by Elbow Wall Erosion Due to Hot Steam Flashing After Passing Through Trap.Elbow Replaced ML20058K9541975-12-31031 December 1975 Ler.On 751227,hydraulic Snubber on Isolable Section of Core Spray Discharge Line Discovered Inoperable.Caused by Loose & Improper Orientation of Pipe Clamp.Clamp Adjusted & Tightened ML20058L0451975-11-26026 November 1975 Ler.On 751118,during Test,Rcic Turbine Failed to Start When Given Fast Start.Caused by Valve Binding Due to Corrosion Products & Crud on Valve Stem & Pivots.Stem & Pivots Polished & Lubricated ML20058L0341975-11-26026 November 1975 Ler.On 751117,while Preparing for Containment Leak Testing, Number 3 TIP Ball Valve Failed to Close Completely.Caused by Stuck Wiper on wafer-type Limit Switch.Valve Replaced ML20058L0311975-11-26026 November 1975 Ler.On 751116,auto Blow Down Delay Relay for a Logic Channel Failed to Energize in Required Time Interval.Time Delay Reset Per Tech Specs ML20058L0291975-11-26026 November 1975 Ler.On 751116,during Test,Number 12 Diesel Generator Tripped on Overspeed During Fast Start.Caused by Maladjusted Cam Operated Switch in Fast Start Control Circuitry.Adjustment Made ML20058L1051975-11-11011 November 1975 Ler.On 750930,while Performing Local Leak Rate Test,Crd Isolation Valve CRD-31 Found Leaking in Excess of Acceptance Criteria.Caused by Accumulation of Scale on Seating Surface. Cleaned & Lapped Valve Seats ML20058L1071975-11-11011 November 1975 Ler.On 750912,during Local Leak Rate test,HPCI-9 Turbine Exhaust Line Check Valve Leaking in Excess of Tech Spec Acceptance Criteria.Caused by Scratched Seating Surface. Seating Surfaces Lapped ML20058L1161975-11-11011 November 1975 Ler.On 750923,while Performing Local Leak Rate Tests,Standby Liquid Control Outboard Isolation Valve XP-6 Found Leaking in Excess of Acceptance Criteria.Caused by Accumulation of Scale on Seating Surface.Cleaned & Lapped Valve Seat ML20058L0791975-11-11011 November 1975 Ler.On 750913,while Performing Local Leak Rate Tests,Core Spray Check Valves AO 14-13A & AO 14-13B Found Leaking in Excess of Acceptance Criteria.Caused by Accumulation of Scale on Seating Surfaces.Cleaned Valve Seats ML20058L0891975-11-11011 November 1975 Ler.On 750920,local Leak Rate Test Indicated Combined Leakage of Drywell Equipment Drain Sump Isolation Valves AO-2561A & B in Excess of Acceptance Criteria.Caused by Lodged Flexitallic Gasket Piece.Seat Cleaned ML20058L0531975-11-11011 November 1975 Ler.On 751101,during Cold Shutdown,Crack Discovered in 1-inch Inlet Nipple to Rv 2005,B Loop LPCI Relief Valve. Caused by Excess Cyclic Movement Induced by Unrestrained Relief Valve Discharge Line ML20058L0591975-11-11011 November 1975 Ler.On 750912,while Conducting Local Leak Rate Test,Msivs AO-2-80A & AO-2-86A Found Leaking in Excess of Tech Specs. Cause Unknown.Pilot & Poppet Seats Lapped ML20058L0671975-11-11011 November 1975 Ler.On 750912,while Conducting Local Leak Test,Msivs AO-2-80C & 86C Found Leaking in Excess of Tech Spec Limits. Cause Unknown.Pilot & Poppet Seats Lapped ML20058L0741975-11-11011 November 1975 Ler.On 750912,during Local Leak Rate Testing,Inboard Main Steam Line Drain Isolation Valve MO-2373 Leaking in Excess of Tech Spec Limits.Valve Not Inspected Due to High Radioactivity.Replaced Valve in Kind ML20058L1221975-10-23023 October 1975 Ler.On 751015,during Test,Number 2 Start Sys on Number 11 Diesel Generator Failed.Caused by Loose Fitting on Control Air Line to Air Start Motors.Fitting Tightened 1993-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20202F7901999-01-25025 January 1999 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20198J4451998-10-22022 October 1998 Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153F0511998-09-21021 September 1998 Rev 2 to MNGP Colr,Cycle 19 ML20153E9361998-09-0808 September 1998 Rev 1 to MNGP Colr,Cycle 19 ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236W5041998-07-21021 July 1998 ISI Exam Summary Rept - Refueling Outage 19 ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant ML20217D8731998-04-13013 April 1998 Rev 0 to MNGP Colr,Cycle 19 ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant ML20216D1041998-03-0505 March 1998 Rev 21 to Operational QA Plan ML20216H6481998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Monticello Nuclear Generating Plant ML20203G1431998-02-10010 February 1998 Rev 2 to Inservice Insp Exam Plan,Third Interval,920601- 020531 ML20203B2821998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Monticello Nuclear Generating Station ML20202F9161998-01-29029 January 1998 Special Rept:On 980128,two of Three Fire Protection Pumps Were Removed from Svc as Result of Sys Configuration Necessary to Support Planned Maintenance.Fire Pumps Were Returned to Svc on 980128 ML20216D2071997-12-31031 December 1997 1997 Annual Rept for Northern States Power Co ML20197J8131997-12-31031 December 1997 Revised Evacuation Time Estimates for Plume Exposure Pathway Emergency Planning Zone at Monticello Nuclear Power Plant. W/One Oversize Drawing ML20198P2201997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Monticello Nuclear Generating Plant ML20203J7131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Monticello Nuclear Generating Plant ML20199G7051997-11-19019 November 1997 Safety Evaluation Authorizing Relief Request 8 of Third 10 Yr Inservice Insp Interval ML20199H8181997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Monticello Nuclear Generating Plant ML20217K2081997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Monticello Nuclear Generating Plant ML20216H7771997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Monticello Nuclear Generating Plant ML20217K2741997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Monticello Nuclear Generating Plant ML20196H1081997-07-0808 July 1997 Rev 20 to Operational QA Plan ML20141B9271997-06-30030 June 1997 LOCA Containment Analyses for Use in Evaluation of NPSH for RHR & Core Spray Pumps ML20149E2921997-06-30030 June 1997 Monthly Operating Rept for June 1997 for MNGP ML20148S6341997-06-23023 June 1997 NPSH - Rept of Sulzer Bingham Pump 1999-09-30
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j Narthem States Power Company i 414 Nicollet Mall Minneapolis, Minnesota 55401 1927 Telephone (612) 330-5500 j August 30, 1993 Report Required by ,
10 CFR Part 50, Section 50.73 US Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 MONTICELLO NUCLEAR GENERATING PIANT Docket No. 50-263 License No. DPR-22 Reactor Protection System Actuation From Low f Reactor Level Caused by Main Condensate Pump Trin !
I The Licensee Event Report for this occurrence is attached. This report l contains the following new NRC commitments. '
- 1. The No. 11 Condensate Pump motor will be inspected for any internal degradation during the 1994 refueling outage.
- 2. Preventive maintenance will be performed on the No. 11 Condensate !
Pump breaker during the 1994 refueling outage. l Please contact Marv Engen, Sr Licensing Engineer, at (612) 295-1291 if you [
require further information. !
, +
/*
( ,t[ h h M 7L-Ro.er 0 Anderson i Director '
Licensing and Management Issues ;
c: Regional Administrator - III, NP,C !
NRR Project Manager, NRC Sr Resident Inspector, NRC State of Minnesota Attn: Kris Sanda f
Attachment l
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PDR ADOCK 05000263 OJ l i S PDR W ) ;
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f NRC FOPM 366 U S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 ,
ts na , EXPIRES $/31/95 f E5NATED BJRDEN PER RESP 3NSE TO CDUMY MTH TH$
P# oRVA'ON CoLLECDON RIQUEST: 60 0 HRS FORAARD LICENSEE EVENT REPORT (LER) cwomS ntwow BUoN EmnE TO wE youum AND RE*ARDS VANAGEMENT BRANCH (MNBB 7714), US NJOLEAR PEGULATOW COMM.SSON, WASHINGTON. DC M.55 030L AND TC THE PAPERWORK REDUCTION FFGJECT Q 153-0104!, orflCE OF !
(See reverse for required nurnber of dig >ts/ Characters for each block) MANAGEVENT AND BJDGET. W ASHINTON, DC 20503 r i
f ACILITV NAME (1) DOCALT NUMBER (2) PAGE (3) ,
MONTICELLO NUCLEAR GENERATING PLANT 05000-263 1 OF 4 ;
t "5 8*' Reactor Protection System Actuation From Low i Reactor Level Caused by Main Condensate Pump Trin [
EVENT DATE (5) LER NUMBER (6' REPORT NUMBER (7) OTHER F ACILITIES INVOLVED (8) i St OJL N1A1 REVCON I Mus an ma vE An y.,yg, y, ex" Du vE**
05000 j f AOiUTY NMR DOCKET NUMBER !
07 31 93 93 - 008 00 08 30 93 05000 l
f0PERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR O (Check one or more) (11) f N
MODE (9) 20 402fb) 20 405tc) m 50 73(aH2)(w) 73 71(b) ,
POWER 20 405MH1)D) 50.36(cH1) 50.73(a)(2Hvl 73.71(c)
LEVEL (10) 100 20 4cs:aln Hn) 50.asrc)(2) 50 73(aH2)(vn) OTHER I 20 4051a H1 Hm) 50 73ta)(2)(0 50.73(aH2Hvud(A) >+g m Abut ,
betow and m Test NRC f 20 4DStaH110v) 50.73(aH2)OO 50.73(a)(2Hvm](B) So,m 3m j 20 405;aH11tv) 50.73(aH2HW) 50.73taH2)(a1 (
LICENSEE CONTACT F OR THIS LER {12) I f NAMt. TELiPHONE NUMBE.h thusoe Area Coce) I Steve Engelke, Superintendent, Elec & Inst Systems Eng (612) 295-1329 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) ;
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cut.c frsu v avw N- eANw ACM AE D CAUSE SYrEM COMPONE NT MANur ACTURE R J !
i X SD 50 G080 Yes i i, !
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l SUPPLEMENT AL REPORT EXPECTED (14) EXPECTED "N" D" " EAR l
YE5 NO m y.s mem rwr C'rD sa noN rcri y DATE (15) l j ABSTRACT (Umit to 1430 spaces. i e., appronmatey 15 single-spaced typeuntien knes) (16) ;
(
l During normal full power operation a Reactor Protection System trip from low ;
i reactor water level occurred. The Standby Gas Treatment System and several {
j containment isolation groups were also initiated on lew reactor level. Normal j
- post trip procedures were followed to restore stable conditions. One ;
j condensate and one feedwater pump remained in operation during the event. f Level remained well above the ECCS initiation setpoint. There were no !
failures or other complications. The immediate cause was a reduction in ;
. reactor feedwater flow due to a ground fault relay trip of a main condensate {
pump. The cause of the ground fault relay trip has not been determined. l Extensive investigation and testing was conducted. No abnormal conditions ;
were found. A motor inspection and breaker maintenance are scheduled for the I next refueling outage.
4 a
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i
i REQUIRED NUMBER OF DIGITS / CHARACTERS !
FOR EACH BLOCK j BLOCK NUMBER OF NUMBER DIGITS / CHARACTERS 1 UP TO 46 FACILITY NAME ;
2 DOCKET NUMBER I
- - m ADDITiOf4 o 05000 3 VARIES PAGE NUMBER I
4 UP TO 76 TITLE 5 DATE 2 PER BLOCK 7 TOTAL 6 LER NUMBER 3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 6 TOTAL -
7 REPORT DATE !
2 PER BLOCK !
UP TO 18 - FACILITY NAME
- I 8 OTHER FACILITIES INVOLVED 8 TOTAL- DOCKET NUMBER 3 IN ADDITION TO 05000 l t
r 9 1 OPERATING MODE l I
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'I REQUIREMENTS OF 10 CFR I CHECK BOX THAT APPLIES UP TO 50 FOR NAME
$- 12 LICENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COVPONENT F. ALLURE
] 4 FOR MANUFACTURER l
- NPRDS VARIES {
1 i 14 SUPPLEMENT AL REPORT EXPECTED t CHECK BOX THAT APPLIES i c
6 TOTAL 15 EXPECTED SUBMISSION DATE 2 PER BLOCK i
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EXPlRES 5/31/95 l t
E5 tMAND BURDEN PER RESPONSE To covPLY W4H TMS i INFoR*AATON Cou EC'CN REQUEST: 50 0 MRS. FORA ARD t LICENSEE EVENT REPORT (LER) couvres uEcARoma asnotN EsnuATE To T-E wroRuiTCN
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TEXT CONTINUATION PEGULATON COMM $3CN W ASNtNGTON, DC 20558Kr#1. AND TO i TME PAPERWORK MLDUCT)N PROJECT (315H10dj, OFFICE OF MANAGEMEN'T AND BJD3ET, WASM;NGTON. DC 20503 4
7 ACIUTY 84AME (1) DOCKE1 NUMBER (2) LER NUMBER (6) I P AGE (3)
SEQUENTA. HE vtSON ,
NVMBER WUVBER 05000 -263 op l Monticello Nuclear Generating Plant 93 - 008 -
00 2 4 f
i r
Description i i
On July 31, 1993, at 0234 hours0.00271 days <br />0.065 hours <br />3.869048e-4 weeks <br />8.9037e-5 months <br />, with the plant at 100% thernal power, the j Reactor Protection System (EIIS System: JC) tripped from reactor low water level. The low water level also initiated the Standby Gas Treatment System (EIIS System: BH). Secondary Containment (EIIS System: NG), Reactor Water l Cleanup (EIIS System: CE)(Group 3) and Primary Containment (Group 2) ,
isolations.
9 The event began when a ground fault relay tripped (EIIS Component: 50) the No. '
11 Condensate (EIIS System: SD) pump. This subsequently resulted in a low suction pressure trip of No. 11 Reactor Feedwater (EIIS System: SJ) pump. In response to the condensate pump trip, the control room operator initiated a j reduction of reactor recirculation flow to reduce reactor power and thereby reduce feedwater requirements to within the capability of the remaining pumps. :
However, the feedwater pump tripped and reactor level reached the scram ,
I setpoint before a sufficient reduction was achieved. The operating crew I l performed normal post scram and isolation follow-up procedures to place the plant in a stable condition and restore isolated systems. l The event is reportable per 10CFR50.73 as an unplanned automatic actuation of Engineered Safety Features. !
Cause The cause of the condensate pump ground fault trip is unknown. The breaker was inspected, the pump motor and leads were meggered, resistance of each '
phase was measured, the ground fault current transformer was inspected and tests were conducted to verify proper operation. The ground fault relay was tested for setpoint and sensitivity to mechanical shock. An induction motor l rotor c. .dition test was conducted. A sample of the motor oil was analyzed.
4KV bus .itages prior to and during the event, as recorded by the plant computer, were evaluated. Cable terminations and connections were inspected.
I Everything indicated that the pump, motor and associated electrical equipment were operating properly. Subsequent operation of the pump appears normal.
There was one person near the back side of the breaker at the time of the trip. A review of the movements of this individual indicated that the breaker cabinet containing the ground fault relay was not bumped.
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l ilRC FORM 366A . U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 31504104 fW)
EXPIRES 5/31/95 ;
ESTIMMED BJRDEN PER RESPONSE To COMPLY W'TH THIS INFoRMATON COLLECTON HEQUEST: S:: 0 HHS. FORWARD LICEf1SEE EVEtJT REPORT (LER) covuons RE2 ara,NG BUR 3tN Ec.ucs Tas NucaAR x.), u,NroRMcCN TEXT CONTINUATION """ "E
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REGJLATORY """" E"",# 8New mBB m ESCN WASHrNGTON. DC 205S5-0001, AND TO THE F APERWORK REDUCTON PROJECT (3160 0104;. OFFICE oF i MANAGEMENT AND BJDGET. WuHtNGToN. DC 20S33 l 1
f ACIUTY NAME (1) DOCKET NUMBER (2) LER HUMBER (6) FAGE (3) l EEQJENTAL RE w4CN l l
NUMBER NUMBER i 05000-263 OF l Monticello Nuclear Generating Plant 93 008 00 3 4 l TEXT w n,w ,w. a nw.a .aonsm . n8c w m on l Analysis This event represents an unnecessary challenge to the reactor protection and isolation systems and an unnecessary plant transient. It occurred at full l rated power which is the most severe condition for a loss of feedwater. l l Iloweve r , all systems responded as designed and all parameters remained within l l analyzed values. The No. 12 Condensate and No. 12 Feedwater pumps remained in l set ice during the event. Reactor level remained well above the ECCS in;;iation lesel. Therefore, there were no consequences directly affecting ,
! pu ile health and safety. j i
Corrective Actions The following activities were performed to determine immediate corrective $
actions. However, no abnormal conditions were found. j i
l 1. Megger of the motor and leads from the breaker cubicle. l l
I 1
- 2. Rcsistance checks of each phase of the motor from the breaker cubicle. l
- 3. Breaker tests including mc s , contact resistance, and close/ trip operation.
l 4 Set point verification of the ground fault relay. l l
S. Visual inspection of the ground fault cucrent transformer, bresker terminations, and current transformer cabling at the breaker cubicle.
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- 6. Current transformer test with data compared to previous data.
- 7. An induction motor rotor condition test.
- 8. Motor oil sample analysis.
- 9. Evaluation of 4KV. bus voltage levels prior to and during the event, as recorded by the plant computer.
l l 10. Inspection of cable connection condition at the *3rmination box.
- 11. With the ground fault relay isolated, it was jarred . etermine sensitivity to mechanical shock.
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 5 83 i
. EXPlRES S/31/95 ESTIMA*ED BURDEN PE A RESPONSE To c0MPLY Wr!H THIS INFORMATON cOMI N N REQUEST; 50.0 HRS. FORWARD i LICENSEE EVENT REPORT (LER) COMME,c5 REaAeN2 oun0EN ESTum To TsE ~FoRucow TEXT CONTINUATION AND RECOFOS MANAGEMENT BRANCH (MNBB 7714), U.S NUCLEAR i REcuuToa< covu:ESow. wASesTm. oc ms.omi. ANo To :
1 TME PAPERWORK REDUCTON PRNECT 13150C104), OFFICE or +
u ANAGEMENT AND BJDGET, WASH!NGTON. DC 20503 I F ACluTY NAME (1) DOCKET NUMBEH (2) LE R HUMBE R (5) PAGE(3) bEQJENT4AL Ftyrs.ON g
NUMBER NUMBER 05000 - 263 OF
- 93. ~ 008 Monticello Nuclear Generating Plant 00 4 4 i Ttma mw ,P.e <, ,aw.m a. . mon ees e wc ram ym o r; ;
1
- 12. The individual near the breaker when it tripped was interviewed. ,
- 13. Vibration testing and thermographic inspection cf the motor and breaker cubicle after restarting the motor.
The following actions are scheduled for completion during the 1994 refueling ,
outage:
.i
- 1. The motor will be inspected for any internal degradation.
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- 2. Preventive maintenance will be performed on the breaker '
i Additional Information Failed Nmponent Identification:
l A Ground Fault Rely i Manufacturer: General Electric -
Model: 12PJC11AVIA a "*evious Simulator Events:
1 Ne previous event, Licensee Event 87-009, Scram Following Closure of ;
i sV Preaker Door, involved a trip of the condensate pump breaker. '
Ilowever, unlike the recent event, that event cas caused by a forceful l closure of the breaker door which initiated the condensate pump trip relays.
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