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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000254/LER-1993-0131993-08-27027 August 1993 LER 93-013-00:on 930729,identified Deviation from TS & Reg Guide 1.52 Requirements for Methyl Iodide Testing of Charcoal Sample Canisters.Caused by Failure to Implement Proper Canister Testing.Canisters Tested by Nucon 05000254/LER-1993-0121993-08-24024 August 1993 LER 93-012-00:on 930726,light Socket Shorted Out When Operator Reset HPCI Logic Power.Caused by Short Circuit in Light Socket.Light Socket & Blown Fuses replaced.W/930824 Ltr 05000254/LER-1993-0101993-08-19019 August 1993 LER 93-010-00:on 930720,HPCI Declared Inoperable & HPCI Outage Rept Qcos 2300-2 Initiated Because IST Flow Rate Fell in IST Required Action Range Due to New Procedure. Surveillance Procedure Will Be revised.W/930819 Ltr 05000254/LER-1993-0111993-08-18018 August 1993 LER 93-011-00:on 930721,discovered That 4kV Breaker 68 Feeding CS 1B Motor Pump Open & Discharged,Resulting in CS 1B Being Declared Inoperable.Wr Written to Investigate & repair.W/930813 Ltr 05000254/LER-1993-0091993-08-13013 August 1993 LER 93-009-00:on 930714,SBGT Methyl Iodide Test Failed Due to Age of Charcoal Combined W/Stringent Test Criteria. Replaced Charcoal Absorber in Both Trains of Sbgt. W/930806 Ltr 05000254/LER-1993-0081993-08-11011 August 1993 LER 93-008-00:on 930709,reactor Bldg Ventilation Radiation Monitor Setpoints Set non-conservatively Four Times in Five Yrs.Caused by Instrument Maint Program Error. New Computer Program developed.W/930805 Ltr 05000265/LER-1988-006, Errata to LER 88-006-02:on 880404,station Notified That Eleven Flued Head Anchors Did Not Meet Design Requirements. Caused by Misinterpretation of Scope & Design Structures.Mod Initiated to Revise Structure1992-06-0404 June 1992 Errata to LER 88-006-02:on 880404,station Notified That Eleven Flued Head Anchors Did Not Meet Design Requirements. Caused by Misinterpretation of Scope & Design Structures.Mod Initiated to Revise Structure 05000254/LER-1990-0131990-07-24024 July 1990 LER 90-013-00:on 900626,annunciators on Both Units & Reactor Recirculation Loop Sample Valve Closed.Caused by Actuation of Primary Containment Isolation Valve When Lightning Struck 345 Kv Line.Valve reopened.W/900724 Ltr 05000254/LER-1988-001, Sanitized Version of LER 88-001-00:on 880114,records Review Found Two Apparent Overexposures of Contractor Personnel During Fourth Quarter 1980.Caused by Inaccurate Secondary &/ or Primary Dosimetry.Dosimetry Sys Upgraded1988-01-28028 January 1988 Sanitized Version of LER 88-001-00:on 880114,records Review Found Two Apparent Overexposures of Contractor Personnel During Fourth Quarter 1980.Caused by Inaccurate Secondary &/ or Primary Dosimetry.Dosimetry Sys Upgraded ML20203L0281986-04-25025 April 1986 Informs of Planned Site Visit to Obtain Info Supporting Implementation of Emergency Response Data Sys,Including Availability of PWR or BWR Parameters in Digital Form & Characterization of Available Data Feed Points 05000254/LER-1984-018, :on 840922 & 24,reactor Bldg Fuel Pool Channel B Area Radiation Monitor 1705-16B Spiked High, Tripping Ventilation.Cause Unknown.Corrective Actions for Both Events Will Be Documented in Suppl to LER 84-0181984-10-11011 October 1984
- on 840922 & 24,reactor Bldg Fuel Pool Channel B Area Radiation Monitor 1705-16B Spiked High, Tripping Ventilation.Cause Unknown.Corrective Actions for Both Events Will Be Documented in Suppl to LER 84-018
05000265/LER-1983-021, Revised LER 83-021/01T-5:on 831028,ultrasonic Exams of Large Bore Stainless Steel Pipe Welds Identified 11 Welds W/Crack Indications.Caused by Intergranular Stress Corrosion Cracking.Weld Overlay Performed1984-02-28028 February 1984 Revised LER 83-021/01T-5:on 831028,ultrasonic Exams of Large Bore Stainless Steel Pipe Welds Identified 11 Welds W/Crack Indications.Caused by Intergranular Stress Corrosion Cracking.Weld Overlay Performed 05000265/LER-1983-018, Revised LER 83-018/01T-1:on 831011,discovered 1-1/4 Inch long,20% through-wall Linear Indication in Weld 12S-S27. Caused by Intergranular Stress Corrosion Cracking.New Welds & Elbow Installed1984-02-0202 February 1984 Revised LER 83-018/01T-1:on 831011,discovered 1-1/4 Inch long,20% through-wall Linear Indication in Weld 12S-S27. Caused by Intergranular Stress Corrosion Cracking.New Welds & Elbow Installed 05000265/LER-1983-020, Revised LER 83-020/01T-1:on 831028,weld 02B-S9,22-inch Pipe to Cap,Weld 02BS-S12,28-inch Elbow to Pipe & Weld 02BS-F14, 28-inch Pipe to Elbow Weld Had Circumferential Linear Indications1983-12-0909 December 1983 Revised LER 83-020/01T-1:on 831028,weld 02B-S9,22-inch Pipe to Cap,Weld 02BS-S12,28-inch Elbow to Pipe & Weld 02BS-F14, 28-inch Pipe to Elbow Weld Had Circumferential Linear Indications 05000265/LER-1982-018, Supplemental LER 82-018/03L-1:on 821006,emergency Diesel Generator Tripped on High Temp After Loading.Caused by Fouling of Diesel Generator Cooling Water Sys.Both HX Replaced1982-12-0101 December 1982 Supplemental LER 82-018/03L-1:on 821006,emergency Diesel Generator Tripped on High Temp After Loading.Caused by Fouling of Diesel Generator Cooling Water Sys.Both HX Replaced 05000254/LER-1982-022, Supplemental LER 82-022/03L-1:on 820816,maint Outage for 1/2B Diesel Fire Pump Exceeded 7-day Limit.Cause Not Stated. Diesel Pump Wear Rings Replaced1982-10-0707 October 1982 Supplemental LER 82-022/03L-1:on 820816,maint Outage for 1/2B Diesel Fire Pump Exceeded 7-day Limit.Cause Not Stated. Diesel Pump Wear Rings Replaced ML20150E1741978-11-20020 November 1978 /03L-0 on 781026:dual Position Indication Was Received for Supression Chamber to Drywell Vacuum Breaker, Valve 1-1601-33E.Caused by Position Indication Problem ML20062E6521978-11-15015 November 1978 /03L-0 on 781025:smoke Detectors Were Removed from Svc in Cable Spreading Room,Elec Equip Room & Control Room for Installation of New Fire Detection/Suppression Sys ML20062D5871978-10-25025 October 1978 /03L-1 on 780420:during Routine Hydraulic Snubber Surveillance Inspec,Snubber Mark 149 Was Found Inoper Due to Empty Fluid Reservoir & Mark 144 Was Found W/Missing Cotter Pin,Due to Component Failure ML20062D5161978-10-19019 October 1978 /03L-0 on 780920:A RHR Room Watertight Door Found Open.Caused by Contractor Personnel Ignorance. Personnel Admonished to Heed Procedures at All Times ML20084Q0021976-12-30030 December 1976 LER 017/03L-0:on 761203,Grinnell Corp Snubber 4755 on RCIC Steam Supply Piping Found to Have Empty Oil Reservoir. Caused by Leakage Through Reservoir End Gap Gaskets.Snubber Repaired & Reservoir Refilled w/oil.W/761230 Forwarding Ltr 05000265/LER-1976-012, Updated LER 76-012/03L-1 Correcting Event Type,Category & Rept type.W/761001 Forwarding Ltr1976-10-0101 October 1976 Updated LER 76-012/03L-1 Correcting Event Type,Category & Rept type.W/761001 Forwarding Ltr ML20084P4791976-08-25025 August 1976 LER 023/03L-0:on 760727,diesel Generator 1/2 Out of Svc for Monthly Insp for 55 Minutes Longer than Tech Spec Limit of 1.5 H.Caused by Maint Personnel Not Being Aware of Time Limit.Procedure to Be Changed ML20084Q0281976-05-27027 May 1976 LER 017/03L-0:on 760427,while Performing Low Reactor Water Level Functional Test,Level Indicating Switch LIS-1-263-58A Tripped,Exceeding Tech Specs.Caused by Instrument Drift. Switch recalibr.W/760527 Forwarding Ltr ML20084Q0511976-04-30030 April 1976 L-0:on 760427,while Performing MSIV Surveillance, Duel Indication Received for Valves AO 1-203-1B & AO 1-203-1D.Caused by Switches Being Out of Alignment.Minor Air Leak repaired.W/760430 Forwarding Ltr 05000254/LER-1976-002, Updated LER 76-002/03L Re Excessive Leakage from Double Gasketed Seal X-4.Initially Reported on 760202.Caused by Equipment Failure & Insufficient Compression.Hatch Bolts Tightened1976-03-0303 March 1976 Updated LER 76-002/03L Re Excessive Leakage from Double Gasketed Seal X-4.Initially Reported on 760202.Caused by Equipment Failure & Insufficient Compression.Hatch Bolts Tightened 1993-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
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. Commenw::cith Edison CO Ouad Cities Nuclear Power Station
, Gy 22710 206 Avenue North Cordova, Illinors 61242-9740 Te6ephone 309!654 2241 i RLB-93-ll3 August 19, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Reference:
Quad Cities Nuclear Power Station Docket Number 50-254, DPR-29, Unit One Enclosed is Licensee Event Report (LER) 93-10, Revision 00, for Quad Cities Nuclear Power Station.
This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10, Part 50.73(a)(2)(v)(D). The licensee shall report any event or condition that alone could have prevented the fulfillment i of the safety function of structures or systems that are needed to mitigate ,
the consequences of an accident.
Respectfully, COMMONWEALTH EDIS0N COMPANY QUA, CITIES NUCLEAR POWER STATION b
. L. Bax Station Manager RLB/TB/p1m Enclosure cc: J. Schrage T. Taylor INP0 Records Center NRC Region III C400: 4 STMGR(11393.RLB 9308240039 930819 [ g \
FDR ADOCK 05000254 L \
g PDR R2
e l
LICENSEE EVENT REPORT (LER) Form Rev. 2.0 F6cdny 54ame (1) Docket Number (2) Page (3)
Quad Cities Unit One 0 p p p p p p p 1 Mp p Title (4)
U l HPCIInop Due To IST Flow in Required Action Range During QCOS 2300-5 Event Date (5) LER Number (6) Report Date (73 Other Facilitsea involved (8)
Month Day Year Year Sequential Revision Month Day Year Facilay DocLet Number (s)
Number Number Names .
o P P P P I I I 0 [7 2 p 9 l3 9 p -
O p p -
O p 0 p i p 9 p 0 p p p p l l l OPEJLATING THIS REPORT 15 $UhMrITED PURSU ANT TO THE R WUIRDtENTS OF 10CFR MODE (9) (Check one or more of the following) (1i) 3 20.402(b) 20.40$(c) 50.73(a)(2)(ev) 73.71(b) power 20.405(a)(1)G) 50.36(c)(1) T50.73(a)(2)(v) -73.71(c)
LEVEL 20.405(a)(1)0i) 50.36(c)(2) 50.73(a)(2)(vii) Other (Specify 9 20.405(a)(1)Gii) 50.73(a)(2)0) 50.73(a)(2)(viii)(A) in Abstract (10) 0 l0l below and in 20.405(a)(1)0v) 50.73(a)(2)Si) 50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50.73(a)(2)Gii) 50.73(a)(2)(x) Text)
LICENSEE CONT ACT FOR THis LER (11) .
NAME TELEPHONE NUMBER AREA CODE Nick Radloff, HPCI System Engineer. Ext. 2942 3 p p 6 p p l-p p pp COMPLETE ONE LINE FOR EACH COMPONENT F AILURE DESCRihED IN THIS REPORT (13)
CAUSE SYSTDi COMPONENT M AN UF ACTURER REPORTABLE CAUSE SYSTEM COMPONENT M AN UF ACTURER REJaORTAbil TO NPRDS TO NPRDS i
D 813 I I I I I i N l l l l l l l I I I I I i I I I I I I I SUPPLEMEN"I AL REPOKI EXPECTED (14) Expected Month Day Year i Submission l
]YES (If yes, complete EXPECTED SUBMISSION DATE) 70 Date (15) l l l ;
i ABSTRACT (lamat to 1400 spacca,i.e., approximately fifteen amgle-space typewnnen Ames) (16) l l
ABSTRACT:
i At 2122 hours0.0246 days <br />0.589 hours <br />0.00351 weeks <br />8.07421e-4 months <br /> on July 20, 1993, Unit One was in the Startup mode at 9 percent of rated !
core thermal power. At this time, the NSO was performing the IST portion of IP-193, HPCI Periodic and Quarterly Pump Operability Test. During this test, the HPCI pump achieved approximately 4890 gpm at 1255 psig and 3700 rpm's. The IST acceptable range for the pump is between 5123-5559 gpm at 1255 psig pump discharge pressure and 3800 rpm's. Because the flow rate fell in the IST required action range, the Shift Engineer declared HPCI inoperable and initiated QCOS 2300-2, HPCI Outage Report.
l The cause of this event was due to a new procedure. A contributing factor to this event was the 1-2358 FT, HPCI flow transmitter.
Corrective actions will include revising the surveillance procedure to ensure the MSC is at the HSS during IST testing of the HPCI system and calibrating the HPCI square root convertor every cycle.
This report is being submitted to comply with 10CFR50(a)(2)(v)(D).
LER254\93\010.%TF
LICENSEE EVENT REPORT (LER) TEXT CONTINUATIO95 Form Rev. 2.0 F AC11JTY N AMF 0) DOCKEI NUMBER (2) LDL NUMBER (b) PAGE (3) ;
Year sequentia! Revision Number Number ,
quad Cities Unit One O p p p p p p p 9 p 0 p p -
O p 2 pF p l6 TEXT Energy Industry identificauon System (Ells) codes are identified m the text as [XXJ PLANT AND SYSTEM IDENTIFICATION:
General Electric - Boiling Water Reactor - 2511 MWt rated core thermal power.
EVENT IDENTIFICATION:
A. CONDITIONS PRIOR TO EVENT:
Unit: One Event Date: July 20, 1993 Event Time: 2122 hours0.0246 days <br />0.589 hours <br />0.00351 weeks <br />8.07421e-4 months <br /> Reactor Mode: Startup (3) Mode Name: Startup Power Level: 9%
This report was initiated by Licensee Report 254\93-010.
STARTUP (3) - In this position, the reactor protection scram trips, initiated by condenser low vacuum and main steamline isolation valve closure are bypassed, the low 4 pressure main steamline isolation valve closure trip is bypassed and the reactor l protection system is energized, with IRM and APRM neutron monitoring system trips and j control rod withdrawal interlocks in service.
B. DESCRIPTION OF EVENT: l At 2122 hours0.0246 days <br />0.589 hours <br />0.00351 weeks <br />8.07421e-4 months <br /> on July 20, 1993, Unit One was in the Startup mode at 9 percent of i rated core thermal power. At this time, the Unit One Nuclear Station Operator (NS0) was performing the In-Service Testing (IST) portion of Interim Procedure (IP) 193, High Pressure Coolant Injection (HPCI)[BJ] Periodic and Quarterly Pump Operability Test. During this test, the HPCI pump [P] achieved approximately 4890 gallons per minute (gpm) at 1255 pounds per square inch gage (psig) and 3700 revolutions per l minute (rpm). The IST acceptable range for the pump is between 5123-5559 gpm at 1255 ;
psig pump discharge pressure and 3800 rpm's. Because the flow rate fell in the IST !
required action range, the Shift Engineer declared HPCI inoperable and initiated QCOS '
2300-2, HPCI Outage Report. I The IST testing portion of the surveillance requires measuring pump flow at a j constant pump speed and differential pressure across the pump. The results are compared against baseline data to detect any changes in system performance.
l At 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on July 20, 1993, the NRC was notified of the event via the Emergency Notification System in order to comply with the requirements of 10CFR50.72(b)(2)(iii)(D).
Instrument Maintenance (IM) personnel were notified due to possible drift in the flow control loop. Nuclear Work Request (NWR) #Q08740 was initiated to calibrate the flow control loop.
LER254\93\010.%TF I
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i i
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev. 2.0 i FACILTTY NAML(1) DOCKET SUMitLR (2) LER NUMBEJt (6) PAGE (3) ;
Year Sequenual Revision Number Number .
Quad Cities Umt one 0 p p p p p p p 9 p -
0 p p 0 p 3 pF p l6 1Erl Energy irrJustry idenuficauon System (Lil5) codes are idenufied in the text as (XX) i
- At 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> on July 21, 1993, IM personnel had completed their calibration of the
- flow control loop. They discovered air was trapped in the high side instrument line of the flow transmitter [ FIT] which could affect the flow transmitter output signal.
The transmitter was found to be within acceptable tolerances. The flow controller and square root convertor were also found to be within acceptable tolerances.
At 2140 hours0.0248 days <br />0.594 hours <br />0.00354 weeks <br />8.1427e-4 months <br />, IP 193 was performed again. The IST pump data was 5170 gpm at 1255 psig pump discharge pressure, thus falling into the acceptable range. Discussions L ensued and was determined the system would be tested again for repeatability.
4 At 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> on July 22, 1993, the Nuclear Station Operator (NS0) noticed the 1-2340-1 FIC, HPCI flow controller [FIC], indicating approximately 190 gpm in normal
! standby lineup. IM personnel were contacted.
IM's found the flow transmitter zero had shifted. After extensive troubleshooting, it .
was determined after the flow transmitter housing was removed for calibration, the HPCI Room Cooler fan blew air on the balance bar of the tranistter causing an e incorrect calibration of the transmitter. The ir flow was blocked so it would not be i directed on the flow transmitter balance bar. IM personnel calibrated the flow transmitter again.
At 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, HPCI was run again. The system engineer and IM personnel were in the !
control room to observe the flow controller's response. A General Electric (GE) field engineer was down in the HPCI room to observe the governor controls. The IST .
data was 4450 gpm at 1250 psig pump discharge pressure and 3690 rpm's. During the test, the GE field engineer noticed that the HPCI Motor Speed Changer (MSC) [SC]was at the electrical High Speed Stop (HSS), but had not reached the mechanical HSS. He immediately reported this to the system engineer and Operating. The system engineer i and Operating discussed the finding and had the field engineer manually raise the MSC !
approximately 3/8 of a turn to the mechanical HSS using the MSC handwheel stem. The pump flow increased to 5270 gpm. The MSC was cycled a couple of times using the MSC control switch from the control room. The NSO held the control switch in the slow i raise position approximately 15 seconds after the electrical HSS light indication .
pick.ed up. The flow consistantly returned to approximately 5270 gpm. HPCI was i i shutdown.
Discussions ensued and it was determined that during the startup of the turbine, the !
procedure directs the NSO to increase the turbine speed by taking the MSC to the HSS ;
observing the light indication. Although the MSC was at the electrical HSS, its ,
possible the MSC was not at its mechanical HSS. It was decided to adjust the MSC and i MGU HSS limit settings to provide a more accurate indication to the NSO when the MSC
- was at the mechanical HSS. NWR #Q08761 was initiated to adjust the HPCI limit switch
, controls. It was also determined the MSC electrical HSS limit switches would not have affected operability of the system and that if the MSC was at the mechanical HSS during the first test run, it would have passed the IST requirements.
At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> on July 23, 1993, Electrical Maintenance (EM) personnel had finishec adjusting the HPCI governor controls and Operating prepared to run HPCI again.
l LER254i93\010.%7F v
i LICENSEE EVENT REPORT (IIR) TEXT CONTINU ATION Form Rev. 2.0 FACILITY N AME (1) DOCKET NUMBER GJ LER NUMBER (6) PAGE 0)
Year $cquennal Revision ;
Number Numtwr l Quad Ciues Urut One O p p p p p p p 9 p 0 $ p -
0 p 4 pF p p TLXT Ermrgy Industry idenuficauon system (L115) codes a-c idenufied in the text as [XXJ During the surveillance, the pump achieved 5620 gpm flow at 1255 psig pump discharge pressure and 4020 rpm's. The rest of the surveillance was completed successfully.
It was decided to run HPCI again to ensure consistant data for IST requirements. l At 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />, HPCI was run again with the same results as before. Because the HPCI controls were adjusted, new IST baseline data was established. The rest of the surveillance was completed successfully. The SE declared HPCI operable and
, terminated the outage report. l C. APPARENT CAUSE OF EVENT: ,
This report is being submitted to comply with 10CFR50.73(a)(2)(v)(D) which requires ;
~
the licensee report any event or condition that alone could have prevented the fulfillment of the safety function of systems that are needed to mitigate the consequences of an accident. i The cause of this event was due to a new procedure. IP-193 tests the HPCI system ,
using the MSC control switch in " Slow Raise" to manually startup the turbine and bring it up to operating speed. The procedure steps directs the Operator to keep raising the MSC until the HSS light indication is received in the control room. The !
slow raise of the MSC allows the MSC to pickup the limit switches quick enough to f stop short of the mechanical HSS, thus not allowing the system to achieve full .
- operating speed. Because the MSC was not at its mechanical HSS, turbine speed was !
reduced enough to create a low flow condition. j
't Investigation into this event revealed other contributing factors affecting the flow !
controller's indication. The 1-2358 FT, HPCI flow transmitter had some air trapped in the instrument line. The drift in the transmitter caused the flow controller reading to be approximately 120 gpm lower than actual flow. This alone would not ,
have been able to cause a failure with the surveillance test due to the drift still ;
being within allowable tolerances. l I
After the flow transmitter was calibrated, the drift in the flow controller in standby mode was due to an inaccurate calibration of the flow transmitter created from the air turbulence within the HPCI room. The flow transmitter balance bar was in the direct flow path of the HPCI room cooler fan causing an inaccurate calibration.
D. SAFETY ANALYSIS OF EVENT:
The safety of the plant and personnel was not affected in this event. Per Technical Specification 3.5.C.2, if the HPCI subsystem is inoperable, reactor operation is allowed for fourteen days provided all active components of the Automatic Pressure Relief (APR) subsystems, the Core Spray (CS) subsystems, and Low Pressure Coolant Injection (LPCI) mode of Residual Heat Removal (RHR) system are operable. These systems were operable throughout this event.
LER254\9h010.WPF
e LICENSEE EVENT REFORT (LER) TEXT CONrINUATION Form Rev. 2.o FACILITY NAME(1) DOCKET N UMBER (2) LEJL NUMBER (6) PAGE (3)
Year Sequennal Revision Nmder Nurder Qind Cities Unit One O p p p p p p p 9 p -
O p p -
O p 5 pF p l6 TEXT Energy industry idenuficeuon system (Ells) codes are idenufied in the text as [XXj HPCI would still have fulfilled its intended safety function. During an auto-initiation signal, the MSC controls the startup ramp of the turbine. 1he MSC will run from the LSS to the mechanical HSS in " Fast Raise" mode and will remain at the mechanical HSS. The MSC HSS limit switch indicating light does not affect the operation of the MSC.
E. CORRECTIVE ACTIONS:
The immediate corrective actions consisted of declaring HPCI inoperable and initiating the HPCI system outage report and NWR #Q08740.
The surveillance procedure will be revised to ensure the MSC is at the HSS during IST testing of the HPCI system (NTS# 2541809301001).
After troubleshooting the flow control loop, IM personnel calibrated the flow transmitter, flow controller, and square root convertor. IM personnel will incorporate procedural guidance in their flow transmitter calibration procedures to ensure no fans or any other air moving devices are operating during instrument calibrations where the air turbulence can affect the instrument calibration (NTS# 2541809301002).
The HPCI square root convertor will be cal'brated once a cycle to ensure no drift occurs in the instrument (NTS# 2541809301003).
EM personnel readjusted the mechanical and electrical MSC HSS to allow the system to operate more closely to its designed flowrate and speed.
F. PREVIOUS EVENTS:
A search of previous License Event Reports (LER) and Deviation Reports (DVR) over the last five years has identified multiple LER's involving problems with IST testing, however, there were no similar events identifying MSC HSS control problems. Some of the LER's involving IST t; sting are listed below:
D-4-1-90-110 HPCI inoperable due to high flow during IST portion of QCOS 2300-5 D-4-2-91-043 HPCI pump operability IST data fell into required action range due to unknown causes D-4-1-91-132 RCIC inoperable due to high pump flow D-4-2-91-024 2C RHR pump declared inoperable for high flow due to procedural deficiencies D-4-2-90-041 2D RHR pump declared inoperable due to incorrect reference value LER254\93\010.WPF
e a
LICENSEE EVENT REPORT (LER) TEXT COffrINUATION Form Rev. 2.0 FACILITY NAME (1) DOCK 13 NUMhEJt (2) LUt NUMBut t6) PAGE (3)
Year Sequenual Revision Number Noneer
@od Citie: Unit one O p pp p p p l4 9 p -
O p p -
O p 6 pF p p TEXT Emergy Induary kiemaficeuon System (Uli) codes are idenufied in the text as {XXj A Nuclear Plant Reliability Data System (NPRDS) search was not conducted due to no -
failed component was identified during this event.
G. CMPONENT FAILURE:
There was no failed component identified during this event.
I e
LER254\93\010.%TF ,