09-15-2016 | On August 11, 2015, during operator investigations inside the reactor containment building, a through wall leak was discovered on the 24 Fan Cooler Unit (FCU) motor cooler service water ( SW) return line. The leak was in a 2 inch copper-nickel pipe near a brazed joint upstream of containment penetration SS. The leak was located within the ASME Section XI Code ISI Class 3 boundary and estimated to be approximately 2 gpm.
Since the pipe flaw was through wall and was located within the ASME Section XI boundary, it exceeds the flaw allowable limits provided per IWC-3000.
The weld leak was evaluated and determined to meet the structural requirements of ASME Code Case N-513-3.
The condition was determined to have no impact on SW cooling safety function or adverse impact on piping structural integrity. The pipe is considered a closed loop system inside containment and required to meet containment integrity.
An engineering evaluation was performed to determine the potential air leakage out of containment based on the observed SW leakage into containment.
This evaluation concluded that the leaking defect could result in post-LOCA air leakage out of containment in excess of that allowed by Technical Specification 3.6.1 (Containment) which requires leakage rates to comply with 10 CFR 50, Appendix J.
The direct cause was corrosion. The apparent cause was the length of time to implement a modification to replace the FCU motor cooler copper-nickel piping identified in 2009 per the SW mitigation strategy.
An engineered clamp was installed over the pipe defect. The pipe and affected elbow were replaced in accordance with the requirements of ASME Section XI Code during the spring refueling outage in 2016. A modification to replace piping will be processed for funding. The event had no significant effect on public health and safety. |
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LER-2015-001, Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for ContainmentIndian Point 2 |
Event date: |
08-11-2015 |
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Report date: |
09-15-2016 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(v), Loss of Safety Function |
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2472015001R01 - NRC Website |
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Category:Letter
MONTHYEARML24011A1982024-01-12012 January 2024 ISFSI, Notice of Organization Change for Site Vice President ML23342A1082024-01-0909 January 2024 Independent Spent Fuel Storage Installation Security Inspection Plan ML23353A1742023-12-19019 December 2023 ISFSI, Emergency Plan, Revision 23-04 L-23-019, Proof of Financial Protection 10 CFR 140.152023-12-18018 December 2023 Proof of Financial Protection 10 CFR 140.15 ML23339A0442023-12-0505 December 2023 Issuance of Amendment No. 68, 301 and 277 Regarding Changes to Implement the Independent Spent Fuel Storage Installation Physical Security Plan ML23326A1322023-12-0505 December 2023 Issuance of Amendment No. 67, 300 & 276 to Implement the Independent Spent Fuel Storage Installation Only Emergency Plan ML23338A2262023-12-0404 December 2023 Signed Amendment No. 27 to Indemnity Agreement No. B-19 ML23356A0212023-12-0101 December 2023 American Nuclear Insurers, Secondary Financial Protection (SFP) Program ML23242A2772023-11-30030 November 2023 NRC Letter Issuance - IP LAR for Units 2 and 3 Renewed Facility Licenses and PDTS to Reflect Permanent Removal of Spent Fuel from SFPs ML23338A0482023-11-30030 November 2023 ISFSI, Report of Changes to Physical Security, Training and Qualification, Safeguards Contingency Plan, and ISFSI Security Program, Revision 28 ML22339A1572023-11-27027 November 2023 Letter - Indian Point - Ea/Fonsi Request for Exemptions from Certain Emergency Planning Requirements for 10 CFR 50.47 and 10 CFR Part 50, Appendix E IR 05000003/20230032023-11-21021 November 2023 NRC Inspection Report Nos. 05000003/2023003, 05000247/2023003, 05000286/2023003, and 07200051/2023003 ML23100A1172023-11-17017 November 2023 NRC Response - Indian Point Energy Center Generating Units 1, 2, and 3 Letter with Enclosures Regarding Changes to Remove the Cyber Security Plan License Condition ML23050A0032023-11-17017 November 2023 Letter - Issuance Indian Point Unit 2 License Amendment Request to Modify Tech Specs for Staffing Requirements Following Spent Fuel Transfer to Dry Storage ML23100A1252023-11-17017 November 2023 Letter and Enclosure 1 - Issuance Indian Point Energy Center Units 1, 2, and 3 Exemption for Offsite Primary and Secondary Liability Insurance Indemnity Agreement ML23100A1432023-11-16016 November 2023 Letter - Issuance Indian Point Energy Center Generating Units 1, 2, and 3 Exemption Concerning Onsite Property Damage Insurance (Docket Nos. 50-003, 50-247, 50-286) ML23064A0002023-11-13013 November 2023 NRC Issuance for Approval-Indian Point EC Units 1, 2 and 3 Emergency Plan and Emergency Action Level Scheme Amendments L-23-012, Master Decommissioning Trust Agreement Changes for Indian Point Nuclear Generating Units 1, 2 and 3, Pilgrim Nuclear Power Station, Palisades Nuclear Plant and the Non-Qualified Trust for Big Rock Point2023-11-13013 November 2023 Master Decommissioning Trust Agreement Changes for Indian Point Nuclear Generating Units 1, 2 and 3, Pilgrim Nuclear Power Station, Palisades Nuclear Plant and the Non-Qualified Trust for Big Rock Point ML23306A0992023-11-0202 November 2023 and Indian Point Energy Center, Notification of Changes in Schedule in Accordance with 10 CFR 50.82(a)(7) ML23063A1432023-11-0101 November 2023 Letter - Issuance Holtec Request for Indian Point Energy Center Generating Units 1, 2, and 3 Exemptions from Certain Emergency Planning Requirements of 10 CFR 50.47 and Part 50 ML23292A0262023-10-19019 October 2023 LTR-23-0211-RI Thomas Congdon, Executive Deputy, Department of Public Service, Chair, Indian Point Decommissioning Oversight Board, Letter Independent Spent Fuel Storage Installation Inspection and Office of the Inspector General Report-RI ML23289A1582023-10-16016 October 2023 Decommissioning International - Registration of Spent Fuel Casks and Notification of Permanent Removal of All Indian Point Unit 3 Spent Fuel Assemblies from the Spent Fuel Pit ML23270A0082023-09-27027 September 2023 Registration of Spent Fuel Casks ML23237A5712023-09-22022 September 2023 09-22-2023 Letter to Dwaine Perry, Chief, Ramapo Munsee Nation, from Chair Hanson, Responds to Letter Regarding Opposition of the Release and Dumping of Radioactive Waste from Indian Point Nuclear Power Plant Into the Hudson River ML23242A2182023-09-12012 September 2023 IPEC NRC Response to the Town of New Windsor, Ny Board Certified Motion Letter Regarding Treated Water Release from IP Site (Dockets 50-003, 50-247, 50-286) ML23250A0812023-09-0707 September 2023 Registration of Spent Fuel Casks ML23255A0142023-08-31031 August 2023 LTR-23-0211 Thomas Congdon, Executive Deputy, Department of Public Service, Chair, Indian Point Decommissioning Oversight Board, Letter Independent Spent Fuel Storage Installation Inspection and Office of the Inspector General Report IR 05000003/20230022023-08-22022 August 2023 NRC Inspection Report 05000003/2023002, 05000247/2023002, 05000286/2023002, and 07200051/2023002 ML23227A1852023-08-15015 August 2023 Request for a Revised Approval Date Regarding the Indian Point Energy Center Permanently Defueled Emergency Plan and Emergency Action Level Scheme ML23222A1442023-08-10010 August 2023 Registration of Spent Fuel Casks ML23208A1642023-07-26026 July 2023 Village of Croton-on-Hudson New York Letter Dated 7-26-23 Re Holtec Wastewater ML23200A0422023-07-19019 July 2023 Registration of Spent Fuel Casks ML23235A0602023-07-17017 July 2023 LTR-23-0194 Dwaine Perry, Chief, Ramapo Munsee Nation, Ltr Opposition of the Release and Dumping of Radioactive Waste from Indian Point Nuclear Power Plant Into the Hudson River ML23194A0442023-07-11011 July 2023 Clarification for Indian Point Energy Center License Amendment Request, Independent Spent Fuel Storage Installation Physical Security Plan ML23192A1002023-07-11011 July 2023 Response to Request for Additional Information Regarding License Amendment Request to Revise the Emergency Plan and Emergency Action Level Scheme ML23171B0432023-06-23023 June 2023 Letter - Indian Point Energy Center - Request for Additional Information for Independent Spent Fuel Storage Installation Facility-Only Emergency Plan License Amendment ML23118A0972023-06-0606 June 2023 06-06-23 Letter to the Honorable Michael V. Lawler, Et Al., from Chair Hanson Regarding Holtec'S Announcement to Expedite Plans to Release Over 500,000 Gallons of Radioactive Wastewater from Indian Point Energy Center Into the Hudson River ML23144A3512023-05-25025 May 2023 Clementina Bartolotta of Pearl River, New York Email Against Treated Water Release from Indian Point Site ML23144A3522023-05-25025 May 2023 Loredana Bidmead of New York E-Mail Against Treated Water Release from Indian Point Site ML23144A3412023-05-25025 May 2023 Dianne Schirripa of Rockland County, New York Email Against Treated Water Release from Indian Point Site ML23144A3472023-05-25025 May 2023 David Mart of Blauvelt, New York Email Against Treated Water Release from Indian Point Site ML23144A3402023-05-25025 May 2023 Melvin Israel of New York Email Against Treated Water Release from Indian Point Site ML23144A3542023-05-25025 May 2023 Terri Thal of New City, New York Email Against Treated Water Release from Indian Point Site ML23144A3532023-05-25025 May 2023 John Shaw of New York Email Against Treated Water Release from Indian Point Site 2024-01-09
[Table view] Category:Licensee Event Report (LER)
MONTHYEARNL-18-039, LER 2018-001-00 for Indian Point, Unit 2 Re Penetration Indications Discovered During Reactor Pressure Vessel Head Inspection2018-05-21021 May 2018 LER 2018-001-00 for Indian Point, Unit 2 Re Penetration Indications Discovered During Reactor Pressure Vessel Head Inspection 05000286/LER-2017-0042017-12-20020 December 2017 Reactor Trip Due to Main Generator Loss of Field, LER 17-004-00 for Indian Point Unit 3, Regarding Reactor Trip Due to Main Generator Loss of Field ML17252A8662017-09-0909 September 2017 Letter Regarding a 04/26/1977 Occurrence Concerning Failure of Number 22 Main Steam Line Isolation Valve to Close to a Manual Signal Initiated by the Control Room Operator - Indian Point Unit No. 2 05000247/LER-2015-0012017-08-29029 August 2017 Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment, LER 15-001-02 for Indian Point, Unit 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment 05000286/LER-2017-0032017-08-29029 August 2017 Condensate Storage Tank Declared Inoperable Per Technical Specification, LER 17-003-00 for Indian Point, Unit 3, Regarding Condensate Storage Tank Declared Inoperable Per Technical Specification NL-17-107, LER 15-001-02 for Indian Point, Unit 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed Leakage Rate fo2017-08-29029 August 2017 LER 15-001-02 for Indian Point, Unit 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed Leakage Rate for 05000247/LER-2017-0032017-08-23023 August 2017 Technical Specification Violation of Section 3.3.1 RPS Instrumentation, LER 17-003-00 for Indian Point Unit 2, Regarding Technical Specification Violation of Section 3.3.1 RPS Instrumentation 05000247/LER-2017-0012017-08-22022 August 2017 Manual Reactor Trip Due to Decreasing Steam Generator Levels Caused By Main Boiler Feedwater Pump Turbine Low Pressure Governor Valves Failed Closed, LER 17-001-00 for Indian Point, Unit 2 Regarding Manual Reactor Trip Due to Decreasing Steam Generator Levels Caused By Main Boiler Feedwater Pump Turbine Low Pressure Governor Valves Failed Closed 05000247/LER-2017-0022017-08-22022 August 2017 Auxiliary Feedwater Flow Indication Inoperable for Longer Than the Allowed Technical Specification Completion Time Due to Failure of Complete Restoration Following Calibration, LER 17-002-00 for Indian Point, Unit 2 Regarding Auxiliary Feedwater Flow Indication Inoperable for Longer Than the Allowed Technical Specification Completion Time Due to Failure of Complete Restoration Following Calibration 05000286/LER-2017-0022017-08-0909 August 2017 Manual Isolation of Chemical and Volume Control System Normal Letdown to Stop a Valve Leak Resulted in an Exceedance of Technical Specification 3.4.9 Condition A Limit for Pressurizer Level, LER 17-002-00 for Indian Point, Unit 3 re Manual Isolation of Chemical and Volume Control System Normal letdown to Stop a Valve Leak Resulted in an Exceedance of Technical Specification 3.4.9 Condition A Limit for Pressurizer Level 05000286/LER-2017-0012017-07-13013 July 2017 Single Flow Barrier Access Point Found Unbolted, LER 17-001-00 for Indian Point, Unit 3 Regarding Single Flow Barrier Access Point Found Unbolted 05000247/LER-2016-0102017-02-28028 February 2017 Safety System Functional Failure Due to an Inoperable Containment Caused by a Through Wall Defect in a Service Water Supply Pipe Elbow to the 24, Fan Cooler Unit, LER 16-010-01 for Indian Point 2 Regarding Safety System Functional Failure Due to an Inoperable Containment Caused by a Through Wall Defect in a Service Water Supply Pipe Elbow to the 24 Fan Cooler Unit 05000247/LER-2016-0022017-02-28028 February 2017 Automatic Actuation of Emergency Diesel Generators (EDGs) Due to 480 VAC Bus Undervoltage Condition and Loss of Residual Heat Removal (RHR) While in Cold Shutdown, LER 16-002-01 for Indian Point, Unit 2 Regarding Automatic Actuation of Emergency Diesel Generators (EDGs) Due to 480 VAC Bus Undervoltage Condition and Loss of Residual Heat Removal (RHR) While in Cold Shutdown NL-16-108, LER 15-001-01 for Indian Point 2 Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed Leakage Rate for Conta2016-09-29029 September 2016 LER 15-001-01 for Indian Point 2 Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed Leakage Rate for Contai 05000286/LER-2015-0052016-09-14014 September 2016 Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by the Trip of 345kV Main Generator Output Breaker 3 due to a Failure of South Ring Bus 345kV Breaker 5, LER 15-005-01 for Indian Point 3 RE: Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by the Trip of 345kV Main Generator output Breaker 3 due to a Failure of South Ring Bus 345kV Breaker 5 05000286/LER-2015-0042016-09-14014 September 2016 Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by a Failure of the 31 Main Transformer, LER 15-004-01 for Indian Point Unit No. 3 Regarding Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by a Failure of the 31 Main Transformer 05000286/LER-2015-0072016-09-0606 September 2016 Manual Reactor Trip Due to Decreasing Steam Generator Water Levels Caused by a Miss- Wired Circuit Board in the Main Feedwater Pump Speed Control System, LER 2015-007-01 for Indian Point, Unit 3 Regarding Manual Reactor Trip Due to Decreasing Steam Generator Water Level Caused by a Miss-Wired Circuit Board in the Main Feedwater Pump Speed Control System 05000286/LER-2015-0062016-08-0808 August 2016 Technical SpecificatiOn Prohibited Condition Due to Two Pressurizer Code Safety Valves Discovered Outside their As-Found Lift Setpoint Test Acceptance Criteria, LER 15-006-01 for Indian Point Unit No. 3 Regarding Technical Specification Prohibited Condition Due to Two Pressurizer Code Safety Valves Discovered Outside Their As-Found Lift Setpoint Test Acceptance Criteria 05000286/LER-2014-0042016-08-0101 August 2016 Automatic Reactor Trip as a Result of Meeting the Trip Logic for Over Temperature Delta Temperature during Reactor Protection System Pressurizer Pressure Calibration, LER 14-004-01 for Indian Point Unit 3, Regarding Automatic Reactor Trip as a Result of Meeting the Trip Logic for Over Temperature Delta Temperature During Reactor Protection System Pressurizer Pressure Calibration 05000247/LER-2016-0042016-05-31031 May 2016 Unanalyzed Condition due to Degraded Reactor Baffle-Former Bolts, LER 16-004-00 for Indian Point 2 re Unanalyzed Condition Due to Degraded Reactor Baffle-Former Bolts 05000247/LER-2016-0052016-05-25025 May 2016 Technical Specification (TS) Prohibited Condition Due to a Surveillance Requirement Never Performed for Testing the Trip of the Main Boiler Feedwater Pumps, LER 16-005-00 for Indian Point, Unit 2, Regarding Technical Specification (TS) Prohibited Condition Due to a Surveillance Requirement Never Performed for Testing the Trip of the Main Boiler Feedwater Pumps 05000247/LER-2016-0012016-05-0202 May 2016 Technical Specification Prohibited Condition Caused by One Main Steam Safety Valve Outside Its As-Found Lift Set Point Test Acceptance Criteria, LER 16-001-00 for Indian Point 2 RE: Technical Specification Prohibited Condition Caused by One Main Steam Safety Valve Outside Its As-Found Lift Set Point Test Acceptance Criteria 05000247/LER-2015-0042016-02-18018 February 2016 Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe, LER 15-004-00 for Indian Point 2 Regarding Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe 05000286/LER-2015-0082016-02-11011 February 2016 Automatic Reactor Trip Due to a Turbine-Generator Trip as a Result of a Fault on 345 kV Feeder W96 Tower Lines Caused by Pre-Existing Degraded Insulator, LER 15-008-00 for Indian Point, Unit 3, Regarding Automatic Reactor Trip Due to a Turbine-Generator Trip as a Result of a Fault on 345 kV Feeder W96 Tower Lines Caused by Bird Streaming 05000247/LER-2015-0032016-02-0303 February 2016 Manual Reactor Trip Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to a Power Supply Failure, LER 15-003-00 for Indian Point, Unit 2, Regarding Manual Reactor Trip Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to a Power Supply Failure NL-15-124, LER 15-001-00 for Indian Point 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed Leakage Rate for Cont2015-10-0909 October 2015 LER 15-001-00 for Indian Point 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size That Results in Exceeding the Allowed Leakage Rate for Conta NL-13-166, Report on Inoperable Gross Failed Fuel Detector2013-12-20020 December 2013 Report on Inoperable Gross Failed Fuel Detector NL-13-038, Event Report for Discovery of a Condition That Prevented Immediate Protective Actions to Avoid Exposures to Radiation from Byproduct Material2013-02-19019 February 2013 Event Report for Discovery of a Condition That Prevented Immediate Protective Actions to Avoid Exposures to Radiation from Byproduct Material NL-12-060, Submittal of Report on Inoperable Gross Failed Fuel Detector2012-04-26026 April 2012 Submittal of Report on Inoperable Gross Failed Fuel Detector ML1101906402010-11-0909 November 2010 Event Notification Report; Subject: Power Reactor Indian Point Unit 2 NL-09-108, Submittal of Report on Inoperable Core Exit Thermocouples2009-08-10010 August 2009 Submittal of Report on Inoperable Core Exit Thermocouples ML0509600412004-12-17017 December 2004 Final Precursor Analysis - IP-2 Grid Loop ML0509600512004-12-17017 December 2004 Final Precursor Analysis - IP-3 Grid Loop NL-03-136, LER 03-03-00 for Indian Point Unit 3 Regarding Automatic Turbine Trip/Reactor Trip Due to Fault in 345kV Generator Output Breaker 32003-08-21021 August 2003 LER 03-03-00 for Indian Point Unit 3 Regarding Automatic Turbine Trip/Reactor Trip Due to Fault in 345kV Generator Output Breaker 3 ML0209104352002-03-19019 March 2002 LER 98-001-01 for Indian Point Unit 3 Re Potential Failure or Inadvertent Operation of Fire Protection Systems, Caused by Personnel Error in Design ML17252A8951979-05-25025 May 1979 Letter Reporting a 05/18/1973 Occurrence of a Pressure Transient within the Reactor Coolant System Due to the Closure of Certain Air Operated Valves in the Reactor Coolant Letdown System - Indian Point Unit 2 ML17252A8461974-02-19019 February 1974 Letter Regarding Performance of a Surveillance Test PT-M2 Reactor Coolant Temperature Analog Channel Functional Test - Delta T Overtemperature and T Overpower - Indian Point Unit No. 2 ML17252A8481974-02-19019 February 1974 Letter Regarding a February 1, 1974 Occurrence Where Both Door of the 80 Foot Elevation Personnel Air Lock to the Containment Building Were Inadvertently Open at the Same Time for a Period of About Thirty Seconds - Indian Point Unit. 2 ML17252A8471974-02-0808 February 1974 Letter Regarding an Occurrence on 1/25/1974 at the Indian Point Unit No. 2 Reactor Was Brought Critical in Preparation for Placing the Plant Back in Service Following Completion of Repairs Associated with No. 22 Steam Generator Feedwater Li ML17252A8491974-02-0606 February 1974 Letter Regarding an Occurrence Where Both Doors of the 80 Foot Elevation Personnel Air Lock to the Containment Building Were Inadvertently Opened at the Same Time for About Thirty Seconds - Indian Point Unit 2 ML17252A8501974-02-0505 February 1974 Letter Regarding an Occurrence Where a Slight Reactor Coolant System Pressure Transient Was Experienced in the Course of Placing a Reactor Coolant Pump in Service - Indian Point Unit No. 2 ML17252A8511974-02-0101 February 1974 Letter Regarding an Inspection of All Bergen-Paterson Hydraulic Shock and Sway Arrestors (Snubbers) Located in the Vapor Containment Was Performed and Two Did Not Meet the Established Criterion for Operability - Indian Point Unit No. 2 ML17252A8521974-01-31031 January 1974 Letter Regarding an Occurrence Where the Reactor Was Brought Critical Preparatory to Placing the Plant Back in Service Following Completion of Repairs Associated with the 11/13/1973 Feedwater Line Break Incident - Indian Point Unit No. 2 ML17252A8591974-01-28028 January 1974 Letter Regarding an Occurrence 01/23/1974 Where a Slight Reactor Coolant System Pressure Transient Above the Technical Specifications Limit Was Experienced in the Course of Placing a Reactor Coolant Pump in Service - Indian Point Unit No. 2 ML17252A8721974-01-18018 January 1974 Letter Regarding Analysis of Results of Monthly Periodic Surveillance Test PT-M11 (Steam Line Pressure Analog Channel Function Test) Indicated That One of the Low Steam Line Pressure Bistables Associated with High Steam - Indian Point Unit ML17252A8761973-12-28028 December 1973 Letter Regarding 12/17/1973 Analysis of the Results of Periodic Tests and Calibration Checks Relating to Pressurizer Level Indicated a Setpoint Drift - Indian Point Unit 2 ML17252A8771973-12-18018 December 1973 Letter Regarding a 12/17/1973 Analysis of Results of Periodic Tests and Calibration Checks Relating to Pressurizer Level Indicated a Setting for One of the Bistables Was Above the Technical Spec. Limit - Indian Point Unit 2 ML17252A8791973-12-0303 December 1973 Letter Regarding a 11/18/1973 Occurrence Relating to the Discovery of the Erroneous Setting for 1 of the Bistables Associated with Low Pressurizer Safety Injection Required by the Technical Specifications - Indian Point Unit No. 2 ML17252A8781973-11-30030 November 1973 Letter Providing Supplemental Information Concerning the 11/13/1973 Incident at Indian Point Unit No. 2 ML17252A8821973-11-19019 November 1973 Letter Concerning a 11/16/1973 Occurrence Regarding Periodic Tests and Calibration Checks Indicating the Setting for 1 of the Bistable Device Was Below the Technical Specification Requirements - Indian Point Unit 2 2018-05-21
[Table view] |
Note: The Energy Industry Identification System Codes are identified within the brackets fl.
DESCRIPTION OF EVENT
On August 11, 2015, at approximately 16:45 hours, during operator investigations inside the reactor containment building {NH}, a through wall leak was discovered on the 24 Fan Cooler Unit (FCU) {FCU} motor cooler service water (SW) {BI} return line. The leak was in a 2 inch 90-10 Copper-Nickel pipe {PSP}, line #495-SWN-NF near a brazed joint upstream of containment penetration SS at elevation 76 feet. The condition was recorded in the Indian Point Energy Center (IPEC) Corrective Action Program. (CAP) in Condition Report CR-IP2-2015-03550. NDE by UT was performed to characterize the flaw and the results evaluated using the structural margins provided in ASME Code Case N-513-3.
The leak was located within the ASME Section XI Code, Class 3 boundary and estimated to be approximately 2 gpm. Since the pipe flaw was through wall and was located within the ASME Section XI boundary, it exceeded the flaw allowable limits provided per IWC- 3000. Since the leaking defect was determined to be within the structural limits of the ASME Code Case N-513-3, the condition was determined to have no adverse impact on SW cooling safety function or on the structural integrity of the system. There was no visual indication of weld or base metal degradation at the affected pipe section, and there is no evidence of leakage at any other location on this weld or elsewhere on the piping adjacent to it. The leakage, if not contained, would have eventually drained into the containment sump. The impact of the pipe flaw was evaluated for containment free volume in-leakage and the leak is not expected to exceed the limit. The pipe is considered a closed loop system inside containment and required to meet containment integrity. An engineering evaluation was performed to determine the potential air leakage out of containment based on observed SW leakage into containment. This evaluation concluded that the leaking defect could result in post-LOCA air leakage out of containment in excess of that allowed by Technical Specification (TS) Surveillance Requirement (SR) 3.6.1.1 (Containment) which requires leakage rates to comply with 10 CFR 50, Appendix J.
The leak in 2 inch line #495-SWN-NF at the affected location is downstream of 24 FCU motor cooler which can be supplied with SW via either 18 inch line #408 (4-5-6 SW Header) or 18 inch line #409 (1-2-3 SW Header). At the time of discovery, the SW System (SWS) was aligned with the 4-5-6 SW Header as the Essential Header for Modes 1-4 Operations per Technical Specification (TS) 3.7.8 (Service Water System). The SWS is designed to supply cooling water from the Hudson River to various heat loads in both the primary and secondary portions of the plant. The design ensures a continuous flow of cooling water to those systems and components necessary for plant safety during normal operation and under abnormal or accident conditions. The SWS consists of two separate, 100% capacity, safety related cooling water headers. Each header is supplied by 3 pumps each having its own strainer, with SWS heat loads designated as either essential or non-essential. The essential SWS heat loads are those which must be supplied with cooling water immediately in the event of a Loss of Cooling Accident (LOCA) and/or Loss of Offsite Power (LOOP). The essential SWS heat loads can be cooled by any two of the three SW pumps on the essential header. Either of the two SWS headers can be aligned to supply the essential heat loads or the non-essential SWS heat loads. The design pressure and temperature of the SWS is 150 psig and 160 degrees F.
The function of line #495 is to return the SW that was used to cool the 24 FCU motor out of containment and discharge it to the discharge canal.
FACILITY NAME (1) DOCKET (2) LER NUMBER (6) PAGE (3)
Cause of Event
The direct cause was corrosion. Corrosion of the copper-nickel piping resulted in a through wall pipe defect and leakage of SW into the reactor containment. The leak was estimated to be approximately 2 gpm. Based on the UT wall thickness measurements the leak occurred at a degraded area approximately 0.5 inch long in both the axial and circumferential directions. Based on the Code Case N-513-3 evaluation, the allowable flaw length in the axial and circumferential direction was calculated to be 1.47 inches and 1.10 inches respectively. Using a calculated corrosion rate of 4.7 mil (0.0047 inches) per year based on measured conditions, the predicted flaw length by the next refueling outage in the spring of 2016 is estimated to be approximately 0.51 inches in both the axial and in the circumferential directions, which are within the allowable flaw lengths. Based on these results, the affected piping is structurally acceptable consistent with the requirements of ASME code Case N-513-3. The specific corrosion type was most likely pitting corrosion or flow-assisted erosion-corrosion.
The apparent cause was the length of time to implement a modification to replace the FCU motor cooler copper-nickel piping identified in 2009 per the SW mitigation strategy. The Site Integrated Planning Database (SIPD)-1049 was not appropriately funded.
Corrective Actions
The following corrective actions have been or will be performed under Entergy's Corrective Action Program to address the cause and prevent recurrence:
- A leak-limiting engineered clam-shell type clamp was applied to the pipe flaw until a code repair could be completed.
- The clamp was monitored daily by a special operator log for any signs of increased .
leakage until a code repair could be completed.
- UT monitoring was performed every 90 days until the pipe was repaired.
- The pipe and affected elbow was replaced in accordance with the requirements of ASME Section XI Code during the spring refueling outage in 2016.
- The removed pipe/elbow was sent out to a vendor (LPI) for a metallurgical analysis to determine/confirm the specific cause.
- SIPD-1049 will be processed for funding for the project to replace the SW piping supply and return from the FCU motor coolers with upgraded materials.
FACILITY NAME (1) DOCKET (2) LER NUMBER (6) PAGE (3)
Event Analysis
The event is reportable under 10 CFR 50.73 (a) (2) (i) (B) and 10 CFR 50.73 (a) (2)(v). The licensee shall report any operation or condition which was prohibited by the plant's TS. This condition meets the reporting criteria because TS 3.6.1 Containment Operability was not met. Because the FCUs are utilized to maintain normal containment temperature within accident analysis input limits and for accident mitigation, SW flow is not isolated following a DBA. SW piping supply and discharge for the FCUs is considered to be a closed system in containment or an extension of the containment boundary. Consequently, defects discovered within this piping may adversely affect containment integrity, and the ability to control release of radioactive materials.
The isolation valve for the faulted FCU SW piping was operable but the line was not isolated therefore the applicable TS not entered.
Initial operability determined the leak was within the Code Case Limits, that the inventory loss was not significant with no impact on other safety related structures, systems and components. Initially TS 5.5.14 requirements was not evaluated but subsequently it was determined the 10 CFR 50, Appendix J requirements were more stringent. The SW pipe flaw leakage was evaluated for containment in-leakage for potential flooding and out leakage for containment integrity per TS 5.5.14 and 10 CFR 50, Appendix J. TS 5.5.14.e requires that SW in-leakage into containment be limited to less than 0.36 gpm per FCU. Prior testing provided measured leakage that was less than the TS limit. Containment out leakage is required to be in accordance with TS Surveillance Requirement (SR) 3.6.1.1 whose leakage rate requirements comply with 10 CFR 50, Appendix J, Option B. The current total Appendix J leakage is 51,616.35 cc/min, therefore the total air leakage through the pipe defect must be limited to no more than 77,677.65 cc/min. A calculation based on a more limiting value of 70,000 cc/min of containment air leakage through the defect at 47 psig containment pressure and 7.41 psig of pipe internal pressure during LOCA conditions was determined to be equivalent to approximately 0.024 gpm of SW leakage out of the defect under current operating pressure (approximately 14.47 psig pipe internal pressure). Since TS 3.6.1 requires the containment to be operable in Modes 1-4 and TS SR 3.6.1.1 requires leakage rate requirements comply with 10 CFR 50, Appendix J, Option B and the estimated pipe flaw leak rate (2 gpm) exceeded the calculated equivalent containment air outleakage, TS 3.6.1 was not met. The application of an engineered clamp on the pipe flaw affected pipe section is structurally acceptable while degraded and the pipe considered operable.
The condition was also a safety system functional failure reportable under 10 CFR 50.73(a)(2)(v). The licensee shall report any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (C) Control the release of radioactive material. This condition meets the reporting criteria because TS 3.6.1 Containment Operability was not met. Because the FCUs are utilized to maintain normal containment temperature within accident analysis input limits and for accident mitigation, SW flow is not isolated following a Design Basis Accident (DBA). SW piping supply and discharge for the FCUs is considered to be a closed system in containment or an extension of the containment boundary. Defects discovered within this piping may adversely affect containment integrity, and the ability to control release of radioactive materials. As a result of revised reportability guidance provided by Entergy fleet experience, the inoperability of single train systems (e.g., containment barrier) are to be considered as a safety system functional failure (SSFF). This event was not at the time considered a SSFF therefore an event notification under 10CFR50.72(b)(3)(v) was not provided.
Past Similar Events
A review was performed of the past three years of Licensee Event Reports (LERs) for events reporting a TS violation due to inoperable SW piping caused by leaks and one LER was identified. This LER is a result of an extent of condition review. LER-2013-004 reported pin hole leaks in Code Class 3 SW piping elbows for series 300 stainless steel. The pin hole leaks were due to pitting corrosion. The cause of the event reported in LER-2013-004 was not the same as this event as the piping material was different (copper-nickel vs stainless steel), was in an elbow and the cause was failure to follow procedure EN-DC-336 (Plant Health Committee).
Safety Significance
This event had no effect on the health and safety of the public. There were no actual safety consequences for the event because there were no accidents or events during the degraded condition.
There were no significant potential safety consequences of this event. The leakage from the affected SW pipe was within the capability of the SW system to provide adequate SW flow to SW loads. The degraded piping was on the discharge of the FCU motor therefore any failure would not prevent the SW cooling function. Current analysis for SW pipe failures are postulated to be limited to small through-wall leakage flaws as SW is defined as a moderate energy fluid system. The SW leak would eventually drain to the containment sump. The containment sumps have pumps with sufficient capacity to remove excessive leakage.
The impact of the pipe flaw was evaluated for containment free volume in-leakage per the limits of TRM 3.4.D. The leak did not and is not expected to exceed the TRM 3.4.D limit. The pipe leak was just upstream of outboard containment isolation valve SWN-71- 4A.
SW effluent is monitored by radiation monitors R-46 and R-56 prior to discharge. If radiation is detected, each FCU heat exchanger can be individually sampled to determine the leaking unit. The SW for the 24 FCU can be isolated to prevent radioactive effluent releases. The Containment Spray System and Containment Fan Cooler System are Engineered Safety Feature systems designed to ensure that the heat removal capability required during the post-accident period can be attained. The CSS and the Containment FCU System provide redundant methods to limit and maintain post accident conditions to less than the containment design value. Five FCUs alone, or 3 FCUs and 1 CSP, or no FCUs and 2 CSPs possess this capability. The configuration with one CS train and two FCU trains is the configuration available following the loss of any safeguards power train (e.g., diesel failure). Accident analysis assumptions regarding containment air cooling and iodine removal are met, by one CS train and any two FCU trains (i.e., at least three FCUs). The Containment FCU System consisting of five 20 percent capacity FCUs and the CSS consisting of two 50% trains are divided into trains based on the safeguards power train which supports them. During the period of time the FCU SW pipe leak was being addressed there was minimum safeguards capability available. FCU 24 is associated with Fan Cooler Train 2A/3A which consists of the 24' FCU and the 23 FCU. An evaluation of the leak concluded that it did not result in any structural, flooding, or spraying condition that would adversely impact the capability of SSCs to perform their safety function.
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05000286/LER-2015-001, Safety System Functional Failure Due to Inoperable Refueling Water Storage Tank Level Alarms Due to Freezing of the Level Instrument Sensing Lines Caused by a Failed Strip Heater | Safety System Functional Failure Due to Inoperable Refueling Water Storage Tank Level Alarms Due to Freezing of the Level Instrument Sensing Lines Caused by a Failed Strip Heater | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000286/LER-2015-001 | Safety System Functional Failure Due to Inoperable Refueling Water Storage Tank Level Alarms Due to Freezing of the Level Instrument Sensing Lines Caused by a Failed Strip Heater | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000247/LER-2015-001 | Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment LER 15-001-02 for Indian Point, Unit 2, Regarding Technical Specification (TS) Prohibited Condition Due to an Inoperable Containment Caused by a Service Water Pipe Leak with a Flaw Size that Results in Exceeding the Allowed Leakage Rate for Containment | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2015-002 | Safety System Functional Failure Due to Fuses for Residual Heat Removal Heat Exchanger Outlet Valves That Would Not Remain Operable Under Degraded Voltage Conditions | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000286/LER-2015-002 | Technical Specification Prohibited Condition Caused by Four Main Steam Safety Valves .Outside Their As-Found Lift Set Point Test Acceptance Criteria | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2015-003 | Manual Reactor Trip Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to a Power Supply Failure LER 15-003-00 for Indian Point, Unit 2, Regarding Manual Reactor Trip Due to Indications of Multiple Dropped Control Rods Caused by Loss of Control Rod Power Due to a Power Supply Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000286/LER-2015-003 | Buchanan, N.Y. 10511-0249 Tel (914) 254-6700 Lawrence Coyle Site Vice President NL-15-065 June 8, 2015 U.S. Nuclear Regulatory Commission Document Control Desk 11545 Rockville Pike, TWFN-2 Fl Rockville, MD 20852-2738 SUBJECT: Licensee Event Report # 2015-003-00, "Technical Specification Prohibited Condition Caused by Failure to Meet Containment Fan Cooler Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance Test Configuration" Indian Point Unit No. 3 Docket No. 50-286 DPR-64 Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2015-003-00. The attached LER identifies an event where containment fan cooler unit service water flow rates did not meet test criteria as a result of improper test configuration, which is reportable under 10 CFR 50.73(a)(2)(i)(B) as a Technical Specification Prohibited Condition during past operation. This condition was recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2015-01063 and CR-IP3-2015-02448. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. Robert Walpole, Manager, Regulatory Assurance at (914) 254-6710. Sincerely, fild-#44‘xe LC/cbr cc: Mr. Daniel H. Dorman, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Ms. Bridget Frymire, New York State Public Service Commission NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (01-2014) LICENSEE EVENT REPORT (LER) APPROVED BY OMB NO. 3150-0104 EXPIRES: 01/31/2017 Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollectssesource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME: INDIAN POINT 3 2. DOCKET NUMBER 05000-286 3. PAGE 1 OF 5 4.TITLE:Technical Specification Prohibited Condition Caused by Failure to Meet Containment Fan Cooler Unit Service Water (SW) Flow Rate Due to Improper SW Surveillance Test Configuration | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2015-004 | Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe LER 15-004-00 for Indian Point 2 Regarding Safety System Functional Failure Due to an Inoperable Containment Caused by a Flawed Elbow on the 21 Fan Cooler Unit Service Water Motor Cooling Return Pipe | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2015-004 | Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by a Failure of the 31 Main Transformer LER 15-004-01 for Indian Point Unit No. 3 Regarding Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by a Failure of the 31 Main Transformer | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2015-005 | Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by the Trip of 345kV Main Generator Output Breaker 3 due to a Failure of South Ring Bus 345kV Breaker 5 LER 15-005-01 for Indian Point 3 RE: Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by the Trip of 345kV Main Generator output Breaker 3 due to a Failure of South Ring Bus 345kV Breaker 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2015-006 | Technical SpecificatiOn Prohibited Condition Due to Two Pressurizer Code Safety Valves Discovered Outside their As-Found Lift Setpoint Test Acceptance Criteria LER 15-006-01 for Indian Point Unit No. 3 Regarding Technical Specification Prohibited Condition Due to Two Pressurizer Code Safety Valves Discovered Outside Their As-Found Lift Setpoint Test Acceptance Criteria | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000286/LER-2015-007 | Manual Reactor Trip Due to Decreasing Steam Generator Water Levels Caused by a Miss- Wired Circuit Board in the Main Feedwater Pump Speed Control System LER 2015-007-01 for Indian Point, Unit 3 Regarding Manual Reactor Trip Due to Decreasing Steam Generator Water Level Caused by a Miss-Wired Circuit Board in the Main Feedwater Pump Speed Control System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | 05000286/LER-2015-008 | Automatic Reactor Trip Due to a Turbine-Generator Trip as a Result of a Fault on 345 kV Feeder W96 Tower Lines Caused by Pre-Existing Degraded Insulator LER 15-008-00 for Indian Point, Unit 3, Regarding Automatic Reactor Trip Due to a Turbine-Generator Trip as a Result of a Fault on 345 kV Feeder W96 Tower Lines Caused by Bird Streaming | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
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